Thursday, May 07, 2015, 16:23, Isaac Earle, 100KW Beam Dump, Development, RH Clamp Installed with Used Seal
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The remote handling 4" marman flange clamp was reinstalled today with a used seal. It is "Clamp B" as tested in Document-114623. The purpose of installing the clamp now is to prepare for the upcoming remote handling test of the vacuum joint and one of the water blocks.
During installation it was found that it will be necessary to manipulate both the BD flange and the EHDT beam pipe flange to have the seal mated on both of them. Clamp installation will therefore be a 2 or 3 person job when done remotely. The BD can be moved upstream by pushing on the back of the clamp mounting collar. The EHDT beam pipe can be moved downstream by threading a pole tool into the collar just upstream of the vacuum flange.
If the clamp becomes stiff during early travel it means that the flanges aren't seated in the jaws properly and the position of the clamp or flanges must be adjusted. Do not back off the clamp drive nut or lift the clamp in this case. This procedure was followed during today's installation. |
Friday, April 17, 2015, 14:37, Isaac Earle, 100KW Beam Dump, Development, RH Clamp Delivered to Beamlines Group
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A 4" Remote Handling Marman Flange Clamp was delivered to Doug Preddy today to be used to clamp the EHDT beam pipe section to the beam dump during beam pipe installation.
The clamp is one of the two manufactured in 2014, Identified with marker "B" |
Friday, December 22, 2017, 12:42, Jason Kapalka, T-Hall Crane, Standard Operation, Powered down ARIEL Target Hall Crane
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Powered down ARIEL Target Hall Crane today by switching off main power switch on B1 level in preparation for site-wide BC Hydro power outage on Dec. 27-29. |
Friday, February 18, 2022, 09:26, Adam Newsome, T-Hall Crane, Maintenance, Potential grease leak observed
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Naimat Khan noticed after using the crane that some grease dropped onto a spreader bar, and believes it is a leak from the main hoist (see attached photo). The hoist should be inspected.
Edit: Dan McDonald notes that this has been observed since the crane was installed and is likely due to excess grease dropping out. Perhaps not a major concern. |
Monday, January 25, 2016, 13:20, Allon Messenberg, T-Hall Crane, Maintenance, Possible oil leak  
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Two small (approx. 5 cm across) puddles of green fluid were discovered on the floor, directly below the crane trolley. The hook block was lowered and inspected. No fluid found on hook block.
The plant group (Neil Wong) was notified and asked to schedule an inspection when the maintenance crew is on site to inspect the ISAC target hall crane.
The crane bridge and trolley were moved to another position on Friday evening and parked over the weekend. The floor directly below the crane trolley was inspected on Monday morning. Three very small (1-3cm diameter) puddles of green fluid were found. |
Friday, January 20, 2023, 14:48, Adam Newsome, T-Hall Crane, Standard Operation, Pendant/Receiver Communication Issue (Repeated)
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An issue was observed in which the pendant did not work to control the crane. This is the second time in recent memory this has happened. See e-log 55 for details. The same sequence of steps outlined in e-log 55 was followed, and the pendant control was re-established. It is still unclear what the root cause of this issue is, but it is suspected that the crane pendant loses communication with the receiver for some reason, and even though communication can be re-established, the reset button on the crane control console does not clear the fault message, and the system must be power-cycled in order to fully reset. This is just speculation based on what is observed. Further investigation required. |
Wednesday, August 24, 2022, 13:47, Adam Newsome, T-Hall Crane, Standard Operation, Pendant/Receiver Communication Issue
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In preparing to troubleshoot the issue described in e-log #54, the crane was power cycled, and the pendant battery removed, to get to a "fresh start" state. Prior to this, the crane functioned normally aside from the incorrect E/W direction control on the North Aux Hoist.
Upon powering the crane back on, the pendant did not work to control the crane in any mode. The HMI had a fault present which read "305. Radio Control Receiver in Fault (3700RC)". This was accompanied by a red light in the safety control relay status summary screen, for "Radio Control Converter Communication Fault With Receiver (3714CONV)".
If the crane was placed in remote mode, the safety control relay status summary all turned green, and the reset button could be pressed, enabling remote mode. This means the issue was specific to the pendant/receiver communication specifically.
The receiver (in the cabinet in the control room) was inspected and the power status LED was on, the RF LED was off (which means there is no issue, OK), and the "OK to receive signal" LED was on - this indicates that the receiver was functioning as expected.
To further troubleshoot the issue - the crane was powered off, the receiver's antenna was disconnected and reconnected, and the multipin connector for the receiver was disconnected and reconnected. The system was powered back on, and the reset button was pressed. The fault message and the safety relay issue were cleared, and the pendant functioned again as normally expected (aside from the persistent issue from e-log #54).
It is unclear exactly what the issue was and how it was resolved, but could have been related to either a loose connector, or power cycling and resetting the system. |
Tuesday, December 20, 2022, 10:03, Adam Newsome, T-Hall Crane, Standard Operation, Overhead crane powered off for the holidays
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[edit 2023-01-03] The crane was powered back on this morning - there do not appear to be any faults on the HMI and it seems that the crane was unaffected by the power outage.
The ARIEL target hall overhead crane was powered off for the holidays. In the new year, throw the main disconnect in the crane control room to power back on. |
Tuesday, April 15, 2025, 10:35, Riley Sykes, Hot Cell 1, Repair, North Roxtec Hinge and door.
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Repairs were done on the North door that would not close. Due to the weight on the hinge pintle and gudgeon repairs were only possible with a Hydraulic power pack and ram to lift the door into position. Door is held closed with single Stainless bolt as top bolt hole would no longer line up. If the door is needed to swing open, recommendation is to use Hydraulic power pack to take some of the weight to facilitate ease. See attached bolt hole photo for misalignment reference. |
Friday, July 03, 2020, 15:43, Adam Newsome, T-Hall Crane, Repair, North Aux Hoist: West Travel Motion Failure
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An issue was observed in which the North Aux hoist failed to travel West when commanded to, but the East motion was functioning. The North Aux hoist Trolley was stuck in a position up against the East wall.
Present during troubleshooting: Adam N, Maico D, Tom K, Allon M, Travis C
After troubleshooting, it was determined that:
- There were no fault messages on the HMI display relating to this issue
- The HMI indicated "Bridge Not in North Limit and/or Auxiliary Trolley North Not in East or West Limit" - the Bridge was not in the north limit as described, and this message implies the PLC thought the North Aux hoist was somewhere along the middle of its travel
- The West run signal was reaching the remote receiver from the crane pendant
- The West and East run signals were correctly reaching their respective input pins on the VFD (DI1, DI2)... upon swapping wires and commanding it to run East, the West direction still did not function
- The VFD was displaying the correct output frequency information on its display when commanded to run East, but not west
- The limit switch was not related to this issue
Upon swapping out the VFD with the working one from the South Aux hoist, the North Aux hoist Trolley was able to move both East and West, as normal. It was therefore determined that the VFD had failed and must be replaced.
Current state of system as of July 3, 2020:
- The North Aux hoist is fully functioning (contains VFD from South one)
- The South Aux hoist is disabled (no VFD, breakers shut off)
- The North Aux hoist limit switch flag has been temporarily bypassed to allow for crane work in the target hall (not a safety issue - extended bumpers are installed and the regular bridge limit switches are functioning normally... this is only to allow the bridge to run its full length of travel when the North Aux hoist is at its fully East position)
Next steps:
- Adam Newsome requested quote for replacement drive (Delta Electronics TDN007E1100WM0) - will advise when replacement arrives
- Install replacement drive into South Aux hoist upon arrival (note: check EMC level modification)
- Verify entire system functioning as normal
- Reinstall North Aux hoist limit switch flag
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Tuesday, March 15, 2022, 10:03, Adam Newsome, T-Hall Crane, Repair, North Aux Hoist VFD Replaced
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The North Aux Hoist VFD which had failed (e-log 50) was replaced today by Tom Kauss and Adam Newsome on Work Permit A2022-03-15-1.
The hoist's motions were all tested - it is functioning normally again. |
Wednesday, September 09, 2020, 10:51, Adam Newsome, T-Hall Crane, Repair, North Aux Hoist Replacement (followup on E-Log 44)
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See E-Log 44 for details on North Aux Hoist failure.
A replacement VFD was ordered by Adam Newsome and installed by Tom Kauss.
Adam and Tom replaced the VFD in the South Aux hoist (which had been relocated to the North Aux hoist). The original braking resistor was used. No functionality changes to the system.
Both Aux hoists were tested: E/W travel, up/down travel. Each hoist is functioning correctly. E/W speeds were compared between the two hoists and found to be the same (~14 Hz for slow speed, ~95 Hz for fast speed).
The replacement job is complete and the issue outlined in E-Log 44 is resolved, although the original cause for failure has not been determined.
Current state of system as of Sept 9, 2020:
- The North Aux hoist is fully functioning (contains original VFD from South one)
- The South Aux hoist is fully functioning (contains newly replaced VFD with original braking resistor)
- The North Aux hoist limit switch flag has been temporarily bypassed to allow for crane work in the target hall (not a safety issue - extended bumpers are installed and the regular bridge limit switches are functioning normally... this is only to allow the bridge to run its full length of travel when the North Aux hoist is at its fully East position)
Next steps:
- Reinstall North Aux hoist limit switch flag (TBD when Target Hall installation work is done)
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Tuesday, August 23, 2022, 10:32, Adam Newsome, T-Hall Crane, Maintenance, North Aux Hoist - reverse motion axes on E/W
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Update 2022-10-06: During routine inspection of the crane, Tom Kauss investigated the direction swap issue. It was determined that there was likely an issue with the initial installation of the new VFD back in March 2022, and that it was unnoticed (directional control wires crossed). The issue has been resolved by Tom Kauss and is no longer a concern.
It was observed during operation today (Aug. 23, 2022) that the motion axes were reversed for East/West travel on the North Aux Hoist. i.e. when pressing the joystick on the local pendant in the East direction, the hoist traveled West, and vice-versa. This behaviour was not noticed (or at least not reported) before. It could potentially be related to the recent replacement which was done in March 2022 (https://elog.triumf.ca/TIS/RH-ARIEL/52), although the motion was checked after replacement. It is possible that an oversight was made in the testing at that time though.
The controls should be checked and the issue should be rectified as soon as possible. The Aux Hoist controls are not run through the PLC, but rather handled directly within the hoist's control box. It is recommended to go online with the PLC and check if there is any hint as to why this is occurring, before making any modifications. If no info can be gained, it is recommended to try swapping the VFDs for East and West motion, and check if that rectifies the issue. It is possible that the VFDs are programmed specifically for their direction output, and they simply need to be swapped.
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Tuesday, February 01, 2022, 08:29, Adam Newsome, T-Hall Crane, Repair, North Aux Hoist - West Motion Failure
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An issue was observed in which the North Aux hoist failed to travel West when commanded to, but the East motion was functioning. The up/down motion was also functioning. The North Aux Hoist Trolley failed during regular usage, seemingly randomly, when it was about 70% towards the West end of travel. Note that the West motion VFD inside the North Aux Hoist is the one previously taken from the South Aux Hoist (the same issue with the North Aux Hoist was observed last year, and the VFD was swapped, and a new one was installed in the South Aux Hoist).
A replacement VFD (Delta TDN007E1100WM0) will be ordered and installed, and this e-log will be updated.
Edit 2022-03-15: the replacement VFD has been installed and the system is operational. See e-log 52. |
Thursday, January 06, 2022, 10:46, Adam Newsome, T-Hall Crane, Development, Modification of South Limits
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Edit: as of May 30, 2022, the modification has been reversed, and the crane is functioning normally as per the manufacturer's limits.
Modifications have been made to the crane to allow for the South Aux Hoist to reach closer to the South wall during the ARIEL Hot Cell installation period. These modifications are temporary, and were considered to be a safer and simpler alternative to the modification proposed by the hot cell contractor workers, which involved installing a sort of come-along on the wall and pulling the hoist closer to obtain the desired reach. The following modifications were made:
- Removal of the bumpers on the south side (T. Kauss). There are no bumpers on the South side of the crane’s bridge currently.
- Modification of the PLC program to reduce the software limit by approximately 4 inches (A. Newsome). The previous soft limit was set at 0.36 m and it was reduced to 0.26 m (~3.9 inch reduction).
These changes have been tested – the crane stops in the expected position. However, it is very close to the wall now. If you are using the crane anywhere near the South wall: exercise extreme caution. The crane automatically slows down when approaching the South wall, and there is plenty of time for the operator to react and further slow the motion by only holding the joystick down at about 20% speed. I strongly recommend operating at about 20% speed when close to the wall (on top of the automatic speed reduction I mentioned).
- These changes are based on Work Permit A2022-01-06-1
- Changes have been noted in the crane’s logbook
See attached screenshot of PLC program indicating that the new limit has been reached.
Contact me (Adam Newsome) for more detailed information.
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Friday, December 05, 2014, 10:43, Isaac Earle, 100KW Beam Dump, Development, Lower Lead Shield Drain Line Installed  
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A 1/8" SS tube was routed from the Swagelok fitting on the front of the lower lead shield to the service stand water catch tray as shown in the attached photos.
The tube was routed to fit in the cut-out and chamfered corner gaps of block TSH0387 in the de-rated EHDT shielding assembly TSH0293. |
Friday, March 20, 2015, 11:45, Isaac Earle, 100KW Beam Dump, Development, Lower Half of BD EHDT Shielding Installed    
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The lower half of the beam dump EHDT shielding was installed yesterday by Plant Group. After installation of the service stand plug, the position of the south and east faces of the plug were checked with the laser tracker w.r.t. EHAT MB4. The south face was within approximately 2mm of nominal, and the east face was approximately 6mm east of nominal position. It was decided that this positioning was acceptable. The modified 6 foot block (TSH0387) was then installed with approximately 4mm clearance from the plug according to TSH0293.
Beamlines Group may now proceed with installation of the EHDT section of beam pipe.
Photos and results of the laser tracker measurements are attached.
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Tuesday, November 23, 2021, 11:01, Adam Newsome, T-Hall Crane, Repair, Load Cell - Not Functioning
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The load cell which is located on the crane itself to display the load to operators was reported not working during the week of November 15. It is planned to investigate on Nov. 25 and this e-log will be updated with the status.
Edit (2022-02-02): the load cell is functioning again. No changes were made. |
Wednesday, August 02, 2023, 09:13, chad fisher, Hot Cell 1, Repair, Leak Rate Testing
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On August 1, 2023 HC1 was pumped down to -1200 Pa (gauge) and then valved off to test the leak rate after turntables had been sealed with backer rod in the gaps.
The sealing with backer rod allowed the cell to reach the test pressure of 1000 Pa. The cell pressure equalized within 30-40 seconds which is an improvement but still not sufficient to meet the goals we have set.
Next step is to pump down to -500 Pa and use smoke generator and perform thorough investigation to identify any leaks. |
Wednesday, February 15, 2017, 11:57, chad fisher, T-Hall Crane, Development, Jason's Remote Crane Test Boxes
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On Tuesday, February 14th I finished modifying Jason's boxes for the remote crane tests by adding shelves to mount cameras... Apart from given the edges a quick sanding (so no one gets slivers)...which I will try and do tomorrow. |
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