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  Evaporator_2, Page 31 of 34  Not logged in ELOG logo
ID Date Authordown Target Material Target Oven W.O# Source Status Subject
  283   Friday, March 18, 2016, 17:13 Aurelia LaxdalTa41790-1LP-SISIn progressTa#47 LP-SIS (with new center block) conditioning

Aurelia Laxdal wrote:

Anders Mjos wrote:

Laura Lambert wrote:

Aurelia Laxdal wrote:

Started Ta#47 heating at Evap2 using the autoramp program. The TGHT current is setup to go to 300A (for now) and the TBHT to 230A (final value).

 Monday, March 14, 2016, 09:20

One thermocouple was not welded on correctly and is not working. 

Cooling evap2 back down, to remove target and re-weld thermocouple.

Once thermocouple replaced, will ramp back up and continue with tests/ conditioning of target.


 

 Monday, March 14, 2016, 13:12: Stopped turbo pump

 After EVAP2 was vented the thermocouple problem was fixed: it was the wire at on connector inside the box not making proper contact. The lid of the heat shield was also replaced since the one initially mounted had no holes, so one couldn't see the center block. Restarted pumping down at 4:30pm. Just started again the autoramp program: TGHT set to 300A (for the time being) and TBHT to 230A. Temperature measurements will resume tomorrow morning.

 Raised the TGHT at 620A. The TBHT was already set at 230A. The temperature is at 1902 deg C. As per John's instructions the target will condition at these setpoints over the week-end.

  284   Monday, March 21, 2016, 18:57 Aurelia LaxdalTa41790-1LP-SISIn progressTa#47 LP-SIS (with new center block) conditioning

Aurelia Laxdal wrote:

Aurelia Laxdal wrote:

Anders Mjos wrote:

Laura Lambert wrote:

Aurelia Laxdal wrote:

Started Ta#47 heating at Evap2 using the autoramp program. The TGHT current is setup to go to 300A (for now) and the TBHT to 230A (final value).

 Monday, March 14, 2016, 09:20

One thermocouple was not welded on correctly and is not working. 

Cooling evap2 back down, to remove target and re-weld thermocouple.

Once thermocouple replaced, will ramp back up and continue with tests/ conditioning of target.


 

 Monday, March 14, 2016, 13:12: Stopped turbo pump

 After EVAP2 was vented the thermocouple problem was fixed: it was the wire at on connector inside the box not making proper contact. The lid of the heat shield was also replaced since the one initially mounted had no holes, so one couldn't see the center block. Restarted pumping down at 4:30pm. Just started again the autoramp program: TGHT set to 300A (for the time being) and TBHT to 230A. Temperature measurements will resume tomorrow morning.

 Raised the TGHT at 620A. The TBHT was already set at 230A. The temperature is at 1902 deg C. As per John's instructions the target will condition at these setpoints over the week-end.

Today, lowered the TGHT from 620A (at 1894 deg C) to 300A.  TBHT is still at 230A.

  285   Tuesday, March 22, 2016, 11:31 Aurelia LaxdalTa41790-1LP-SISIn progressTa#47 LP-SIS (with new center block) conditioning

Aurelia Laxdal wrote:

Aurelia Laxdal wrote:

Aurelia Laxdal wrote:

Anders Mjos wrote:

Laura Lambert wrote:

Aurelia Laxdal wrote:

Started Ta#47 heating at Evap2 using the autoramp program. The TGHT current is setup to go to 300A (for now) and the TBHT to 230A (final value).

 Monday, March 14, 2016, 09:20

One thermocouple was not welded on correctly and is not working. 

Cooling evap2 back down, to remove target and re-weld thermocouple.

Once thermocouple replaced, will ramp back up and continue with tests/ conditioning of target.


 

 Monday, March 14, 2016, 13:12: Stopped turbo pump

 After EVAP2 was vented the thermocouple problem was fixed: it was the wire at on connector inside the box not making proper contact. The lid of the heat shield was also replaced since the one initially mounted had no holes, so one couldn't see the center block. Restarted pumping down at 4:30pm. Just started again the autoramp program: TGHT set to 300A (for the time being) and TBHT to 230A. Temperature measurements will resume tomorrow morning.

 Raised the TGHT at 620A. The TBHT was already set at 230A. The temperature is at 1902 deg C. As per John's instructions the target will condition at these setpoints over the week-end.

Today, lowered the TGHT from 620A (at 1894 deg C) to 300A.  TBHT is still at 230A.

 Cooling down the target.

 

  332   Saturday, October 15, 2016, 12:42 Aurelia LaxdalTa41790-5LP-SISIn progressTemperature measurements for Ta#50

Laura Lambert wrote:

Thursday, October 13, 2016, 18:04

Target loaded into evap2

No heat shields.

Both endcaps inserted and expanded.

Rh foil inserted [when inserting, the Ta rod used to expand the Rh foil inside the ionizer tube snapped off inside the container - this piece was able to be shaken out and is no longer inside]

Chamber pumped down.

HS water valves opened, no leaks detected
 
Tapped up manually to 35A
 
Vacuum stable, IGP1 = 5e-7 Torr
 
Initiating auto-ramp.
 
OMEGA slope = 0.98

TBHT will be ramped up to 230A at 1.0A/min.

TGHT will be ramped up to 300A at 2.0A/min.

Final desired temperature = 1900C


Friday, October 14, 2016, 13:28

TGHT and TBHT had reached 300A/ 230A respectively.

Power bump ~10min ago caused evap2 to trip off.

Tapped back up manually to 35A.

Re-initiating auto ramp now.


 

Friday October 14: the target was ramp up to 300A/230A after Laura started it. Then, I cooled down at 6pm before leaving TRIUMF. <br>

Saturday October 15: restated the auto-ramp for Ta#50 in EVAP2. It's currently set to go to 300A/230A.

  333   Sunday, October 16, 2016, 17:55 Aurelia LaxdalTa41790-5LP-SISIn progressTemperature measurements for Ta#50

Aurelia Laxdal wrote:

Laura Lambert wrote:

Thursday, October 13, 2016, 18:04

Target loaded into evap2

No heat shields.

Both endcaps inserted and expanded.

Rh foil inserted [when inserting, the Ta rod used to expand the Rh foil inside the ionizer tube snapped off inside the container - this piece was able to be shaken out and is no longer inside]

Chamber pumped down.

HS water valves opened, no leaks detected
 
Tapped up manually to 35A
 
Vacuum stable, IGP1 = 5e-7 Torr
 
Initiating auto-ramp.
 
OMEGA slope = 0.98

TBHT will be ramped up to 230A at 1.0A/min.

TGHT will be ramped up to 300A at 2.0A/min.

Final desired temperature = 1900C


Friday, October 14, 2016, 13:28

TGHT and TBHT had reached 300A/ 230A respectively.

Power bump ~10min ago caused evap2 to trip off.

Tapped back up manually to 35A.

Re-initiating auto ramp now.


 

Friday October 14: the target was ramp up to 300A/230A after Laura started it. Then, I cooled down at 6pm before leaving TRIUMF. <br>

Saturday October 15: restated the auto-ramp for Ta#50 in EVAP2. It's currently set to go to 300A/230A.

 Sunday October 16: the target temperature measurements up to 620A/230A were performed today not on October 15 (yesterday, it was cooled down before reaching 300A/230A). Currently the target is cooling down, to be ready tomorrow morning for the Test Stand. 

  666   Thursday, July 25, 2024, 15:46 Angelina Chennp-Ta TARGET BOATIn progressCarbonization of Heat Stabilized np-Ta Fibres Disk (1st Attempt)

 Thursday, July 25, 2024, 15:18

Target container consists of two np-Ta fibres disk samples. Both disks are made from heat stabilized np-Ta fibres (150 C for 17 hours) and were pressed at 8 tons / 300 MPa.

Sample 1 was made from np-Ta fibres spun using Dope solution #1. Sample 1 disk has an average thickness of 0.727 mm and a diameter of 17.113 mm. Mass of the green sample 1 disk is 0.1957 g. 

Sample 2 was made from np-Ta fibres spun using Dope solution #6. Sample 2 disk has an average thickness of 0.688 mm and a diameter of 17.123 mm. Mass of the heat stabilized fibres used to make the green sample 2 disk is 0.1860 g. Mass loss from pressing the heat stabilized fibres was virtually zero. Therefore, although the mass of the green sample 2 disk was not measured, it can be extrapolated to be 0.1860 g. 

Target container was wrapped with Ta foil. Each sample disk was wrapped in graphite foil and placed inside the target container horizontally near the center. 

Omega slope was initially set to 0.980. After reviewing previous logbook on np-Ti (e-log ID#633), changed the Omega slope to 0.990. 

Chamber is currently being pumped down. The current reading (as of 15:40) is 4.70e-05 Torr. 

Two heating schedules will be tested. Heating schedule 1 entails heating both sample disks at ~1000 C until the pressure reaches below 1.00e-06 Torr. Once heating schedule 1 is completed, sample 1 will be removed. Heating schedule 2 entails heating sample 2 to ~1800 C until the pressure reaches below 1.00e-06 Torr. TGHT is estimated to be approximately 440A/7.6V to reach 1875 C (348A/5.8V to hold temperature at 1600 C). Refer to e-log ID#605. 


 

  55   Friday, January 11, 2013, 15:16 Anders Mjos   MaintenanceReplace terminal insulator

John Wong wrote:

Friday, January 11, 2013, 10:59

The insulator that holds the terminals was broken when a target container was installed.  The insulator had seen so much heat shine from the Cu heat-shield gaps, see attachment.  Tightening the bolts on the target container might further put more force on the insulator and eventually broke it.

To prevent this to happen again.  The Cu-heat shield gaps have covered with Ta-foil to prevent any shine from the target  container onto the insulator.  Also, a torque wrench will be used to tighten the bolts on the terminals.  At this point, we don't know the max torque the insulator can tolerate.  Some measurements were done on the target resistant (ohm) as a function of torque (in pounds).  The best torque to tighten the terminal bolts is 150 lbs


 

The insulators were installed with torques as indicated in the attached PDF ITD0052. A torque test was performed on the broken insulator before installation. No damage was seen on torques of up to 60 in lbs for the 1/4-20 bolts, however for torques in excess of 50 in lbs the insulator material seems to "give".

  60   Wednesday, March 06, 2013, 10:41 Anders MjosEmpty38481-4HP-FEBIADDoneCTL thermal test

Wednesday, March 06, 2013

The Cool Transfer Line (CTL) test target is installed for thermal tests. Drawing number is ITD0431 REV A.

Thermocouple channels are as follows:

T1: Cu block on CTL
T2: Heat Shield above CTL
T3: Heat Shield cooling water Supply
T4: Heat Shield cooling water Return

Cooling water is in Evap2 supplied to the cooling line that goes directly to the area on the Heat Shield above the CTL.

Test results attached.
 

  62   Monday, March 11, 2013, 12:23 Anders MjosEmpty38481-4HP-FEBIADDoneCTL thermal test 2

 

Anders Mjos wrote:

Wednesday, March 06, 2013

The Cool Transfer Line (CTL) test target is installed for thermal tests. Drawing number is ITD0431 REV A.

Thermocouple channels are as follows:

T1: Cu block on CTL
T2: Heat Shield above CTL
T3: Heat Shield cooling water Supply
T4: Heat Shield cooling water Return

Cooling water is in Evap2 supplied to the cooling line that goes directly to the area on the Heat Shield above the CTL.
 

 

Monday, March 11, 2013

The CTL test target was installed again for a second thermal test. CTL block fastened to HS with 1 in lbs. A small piece of Ta-foil of 0.001" thickness was used between the CTL Cu-block and the Ta transfer line to reduce the heat transfer..

Thermocouples were re-attached to CTL and Heat Shield (see above for channels #s).

See attached graph (PDF) for details.

  64   Wednesday, March 13, 2013, 16:08 Anders MjosEmpty38481-4HP-FEBIADDoneThermal test

Wednesday, March 13, 2013 

Thermocouple channels (see attached PDF for photos)
T1 - Left target leg at tube
T2 - Between cooling fins close to tube, left side
T3 - Supply water HS
T4 - Return water HS


Friday, March 22, 2013

Test not conducted. Target removed.

  65   Thursday, March 14, 2013, 12:27 Anders MjosEmpty38481-4HP-FEBIADDoneCTL thermal test 3 (w/o CTL block)

Thursday, March 12, 2013 

The CTL was removed and target heated to 580A / 300A

T1: Left target leg close to tube
T2: Heat Shield above CTL
T3: Heat Shield cooling water Supply
T4: Heat Shield cooling water Return


Thursday, March 13, 2013  

The target was cooled down 


Results attached as PDF and Excel

  68   Friday, April 19, 2013, 15:27 Anders MjosEmpty38481-4HP-FEBIADDoneCTL test

Target installed with 4 T/C

The target assembly is ITD0300 with the CTL Cu cooling block slightly modified.

Ch1 - CTL cooling block T/C feedtrough
Ch2 - Heat shield below left gripper arm - T/C feedthrough
Ch3 - Heat shield below left gripper arm - 9 pin connector
Ch4 - Target left side leg on tube - 9 pin connector

Friday, April 19, 2013, 15:23: Roughing

Friday, April 19, 2013, 15:41: Started turbo


Monday, April 22, 2013, 09:43: Opened water supply. Vacuum stable at 2.8E-7 T (IGP1)

  70   Tuesday, April 23, 2013, 10:11 Anders MjosEmpty38481-4HP-FEBIADDoneCTL test

 

John Wong wrote:

 

Anders Mjos wrote:

Target installed with 4 T/C

The target assembly is ITD0300 with the CTL Cu cooling block slightly modified.

Ch1 - CTL cooling block T/C feedtrough
Ch2 - Heat shield below left gripper arm - T/C feedthrough
Ch3 - Heat shield below left gripper arm - 9 pin connector
Ch4 - Target left side leg on tube - 9 pin connector

Friday, April 19, 2013, 15:23: Roughing

Friday, April 19, 2013, 15:41: Started turbo


Monday, April 22, 2013, 09:43: Opened water supply. Vacuum stable at 2.8E-7 T (IGP1)

 

Monday, April 22, 2013, 18:48

Ramping TGHT/TBHT to 850A/300A at 1A/min.


 

 

Tuesd ay, April 23, 2013, 10:07

TBHT / TGHT: 820A / 300A

TGHT:RDCUR: 816.6A
TBHT:RDCRU: 303.5A

Local P/S displays
TGHT: 821A / 11.05V
TBHT: 307A / 4.37V

Tuesday, April 23, 2013, 10:45: Ramping down TBHT to 0A @ 5A/min

Tuesday, April 23, 2013, 12:49: Ramping down TGHT to 0A @ 5A/min

Tuesday, April 23, 2013, 15:52: Swithced off TGHT and TBHT P/S. TGHT P/S showed 30A read back value, while local value was 0A


 Wednesday, April 24, 2013, 09:53: Turbo stopped

Wednesday, April 24, 2013, 12:00: Target removed 


The ionizer tube was found to have deformed as seen in the attached photo.

  71   Tuesday, April 30, 2013, 11:20 Anders MjosEmpty38481-5HP-FEBIADDoneCTL thermal test

 CTL block on T/C F/T Ch 1
Supply on Ch 3
HS Return on Ch 4

Tuesday, April 30, 2013, 11:20: Roughing

Tuesday, April 30, 2013, 11:45: Turbo started


Wednesday, May 01, 2013, 08:43: Cooling water opened. Vacuum stable at 5.1E-7 T (IGP1)

Wednesday, May 01, 2013, 08:48: Ramping TGHT and TBHT to 850A and 300A at 1A/60s


Thursday, May 02, 2013, 09:10: TGHT reached voltage limit (12V) at ~780A yesterday at ~10pm. Increased limit to 12.5V and continued auto ramping. CTL block temp ~80C

Thursday, May 02, 2013, 10:08: TGHT voltage limit changed to 13V. TGHT:RDCUR goes to ~810A with TGHT:RDVOL at 12.5V. CTL block temp ~80C

Thursday, May 02, 2013, 11:33: TGHT manually stepped to 850A RDCUR at 846A, RDVOL at 13.1V. CTL block temp ~84C

Thursday, May 02, 2013, 15:13: Ramping down TGHT and TBHT to 580A and 280A at 2A/min and 1A/min


Friday, May 03, 2013, 08:30:  TGHT and TBHT at 580A and 280A. CTL block temp ~60C 

Friday, May 03, 2013, 08:37: Ramping down TGHT and TBHT to 0 at 2/min and 1A/min

Friday, May 03, 2013, 11:04: T/C logger removed


Monday, May 06, 2013, 09:37: Turbo stopped.

Monday, May 06, 2013, 10:26: Venting

  92   Tuesday, October 29, 2013, 15:50 Anders Mjos   In progressCopper bars on TGHT and TBHT

 Tuesday, October 29, 2013, 15:50: Pumping down

Wednesday, October 30, 2013, 09:32: Turbo started

Wednesday, October 30, 2013, 14:50: The Cu-bars were heated to 600A and 300A for TGHT and TBHT respectively.

Wednesday, October 30, 2013, 15:17: PS off. Turbo off.

Results can be found on DocuShare and in the attached plot.

  93   Friday, November 01, 2013, 17:20 Anders Mjos   ProblemsBacking pump needs new filter

The source of the poor vacuum in the backing line seems to be related to a dirty filter. We will try to find a replacement filter next week.

The problem seem to have started September 17th, when backing preassure CG1A went from 40 mTorr to 130 mTorr. CG1B remained around 30 mTorr.

  94   Monday, November 04, 2013, 14:02 Anders Mjos   MaintenanceBacking pump replaced

 

Anders Mjos wrote:

The source of the poor vacuum in the backing line seems to be related to a dirty filter. We will try to find a replacement filter next week.

The problem seem to have started September 17th, when backing preassure CG1A went from 40 mTorr to 130 mTorr. CG1B remained around 30 mTorr.

With the help of Anthony Ip from vacuum group, the problem was diagnosed to be the roughing pump itself. The pump was replaced and pumping improved. The chamber can now be evacuated and turbo ready to start in less than 10 minutes.

The filter is not stocked by vacuum group and could not be replaced.

Last week parts of the roughing line was cleaned by Rick. The PVC roughing line has been replaced with a SST bellows. The SST bellows is KF25 and should be replaced by a KF40 bellows in the long run.

  96   Thursday, November 07, 2013, 09:38 Anders Mjos   Problems resolvedHeat Shield cooling line twisted

See attached photo.

The Heat Shield has been taken to the Machine Shop for repair.

Friday, November 08, 2013

 The Heat Shield cooling line has been repaired and the lid re-installed in the evaporator. Photo attached.

Friday, November 08, 2013, 10:58 : Roughing Started

Friday, November 08, 2013, 11:05: Turbo started 

Friday, November 08, 2013, 11:15: Turbo at speed Vacuum at (IGP1) 5.7E-5 T 

  120   Friday, March 07, 2014, 10:34 Anders Mjos   Problems resolvedTGHT2 water flow signal

There was no signal going from the coils to the PLC. After manipulating the connection points on the coil a signal could again be established. Frequency is ~ 40Hz.

  161   Friday, October 03, 2014, 13:02 Anders MjosEmpty  MaintenanceBroken insulators

John Wong wrote:

 Thursday, October 02, 2014, 11:22

It was found that after the last process, Evap#2 has broken insulators - the cylinder insulator that supports the target centre legs and the block insulator that supports the terminals.  

Informed Anders/Rick.


 

 Friday, October 03, 2014

  • Insulators replaced. Torque 55 in lbs on all fasteners.
  • Cleaned TGHT terminals with scotch-brite and methanol.
  •  New (clean) heat shield prepared WO-39230-2.
  • Re-installed right side heat shield alignment pin (previously removed to allow line of sight to the target).
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