M9sol Logbooks Solenoid Daily log
  Solenoid logbook, Page 3 of 15  ELOG logo
Entry  Fri Jul 10 01:10:59 2009, Doug Preddy, Quench Recovery, switch to parallel warm return 
 
Entry  Thu Jun 2 01:38:25 2005, Doug Preddy, Quench Recovery, strip tool plot 02-06-05-12.57.26 AM.jpg
This is a strip tool  plot of the cooldown
Entry  Thu Nov 25 07:21:37 2004, Doug Preddy, Quench Recovery, started power lead flow 
Curtis switched to series mode last night at 7:00.
Startedflow to power leads at 7:00 this morning.
Entry  Wed Jul 28 00:04:30 2004, Doug Preddy, Quench Recovery, started flow to solenoid 
Solenoid temps were: C1 & C12 about 30K. C6 &C7 about 11K. Started flow to 
solenoid in parallel cold return. Jumpered out the vacuum gauge for the 
solenoid vacuum.
Entry  Tue Nov 23 09:30:15 2004, Doug Preddy, Quench Recovery, started flow to solenoid 
Started flow to solenoid in parallel warm return.
Entry  Thu Jun 2 01:26:30 2005, Doug Preddy, Quench Recovery, started flow to solenoid Capture6-2-05-1.13.33 AM.jpg
See attached file for a screen grab of temps.
Entry  Thu Nov 3 09:27:16 2005, Doug Preddy, Quench Recovery, started flow to solenoid 
started flow to solenoid in parallel cold return.
Entry  Wed May 5 09:59:10 2004, Doug Preddy, Quench Recovery, started flow to power leads 
Started flow to power leads.
TIC121 into auto mode
Entry  Fri Oct 22 09:15:06 2004, Doug Preddy, Start Up, started flow to power leads 
Started flow to power leads HIC142 at 0.8. 
Entry  Thu Apr 1 11:57:55 2010, Doug Preddy, Start Up, started flow to power leads 

Solenoid cold. Buffer tank pressure ~3psi, so Kevin will add a bottle of helium. Started flow to power leads at 11:45

Entry  Mon Jun 7 09:24:47 2010, Doug Preddy, Quench Recovery, started flow to power leads 
 
Entry  Fri Sep 26 09:50:18 2008, Doug Preddy, Quench Recovery, started flow in parallel cold return mode 
 
Entry  Fri Sep 14 12:44:52 2007, Doug Preddy, Start Up, started compressor 
running purifier over weekend
Entry  Thu Nov 8 09:28:53 2007, Doug Preddy, Quench Recovery, started compressor 
And started flow to coldbox,solenoid in parallel warm return.


Tuesday evening theree was a 2 hour power outage 19:00- 21:00. No call 
made to M9 operator.
Wednesday tried to recover vacuum. Started cool down Thursday morning.
Entry  Thu Jul 20 13:21:57 2006, Willy Andersson, Quench Recovery, started // warm return flow. 
TIC121 was down to 27K
warm return valves were wide open
opened supply valves CV143 and CV146.
TIC121 went up to about 37K
Mu1 return temperature went down to about same temp as TIC121 so set Mu1 to 
cold return. Open CV145 then close CV151. Mu2 return was still > TIC121 so 
kept it in warm return mode. Adjust turbines as required.
After about 20 minutes Mu2 return temp dropped down to about equal to Mu1 
return temp of about 38K. Then set Mu2 to cold return. Open CV147 then 
close CV143. TIC 121 drops to 30 K. Even though Mu1 and Mu2 return temps 
greater than TIC121 I will keep it in //cold return mode to see if the core 
solenoid temperatures will start to fall. To maximize the use of the 
cooling from T2 outlet temperature CV155 is tweaked open to its maximum 
stable opening. This helps cool the lower heat exchangers. If this works 
then cr_c1 and cr_c12 should start to tick downwards. If they keep rising 
then have to switch back to //warm return.
Entry  Wed Jun 1 08:23:19 2005, Doug Preddy, Start Up, start up notes 
The solenoid was pumped out Monday and yesterday after the quads just 
downstream of the solenoid were put back in place. The quad just 
downstream of the solenoid was remove to replace two coils on it. 
The cold box vacuum had tripped off some time in the last little while. 
Started it pumping on Monday also. The compressor was started Tuesday 
afternoon and flow was started to the solenoid. The purifier was 
regenerated and put on line in it's total buffer tank flow mode. The cold 
box was pressurized and the turbines were briefly spun up to check the 
operation of the new turbine speed indicator. It seems to be working 
properly. 
Flow to the turbines was started this morning and all went well. The speed 
indicator works properly. 
M9BIG1 started ot 6.6 x 10-6 before flow was started. One hour later it 
reads 4.8 x 10-6
Entry  Thu Jul 29 13:25:29 2004, Doug Preddy, Quench Recovery, start flow to power leads 
 
Entry  Fri Jul 10 00:34:03 2009, Doug Preddy, Quench Recovery, solewnoid quench due to power bump 

Solenoid quench due to power bump caused by an airplane crash in Richmond at ~ 22:00. Compressor off. Water pump off. Restarted compressor at ~ 11:30. Cooling solenoid in parallel cold return mode by 12:15.

Entry  Thu May 13 07:39:55 2010, Doug Preddy, Quench Recovery, solenoid quench last night 

Solenoid quenched on power lead temps last evening. I am recovering it in parallel cold return mode. C12~60K C1~50K.

Entry  Thu Aug 10 20:26:09 2006, Willy Andersson, Quench Recovery, solenoid energized 
Powerleads seem stable.
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