Logbooks Lab Maintenance Evaporator_1 Evaporator_2 Laser cutter Target Production Test-Stand RH-ISAC RH-Cyclotron RH-Meson Hall RH-Beamlines RH-ARIEL
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Entry  Friday, December 20, 2024, 09:37, Dave Neilson, , , , , , , , Winter holiday shutdown 

Friday, December 20, 2024, 09:37    turned off all 4 turbopumps. winding down prior to evacuating.

Friday, December 20, 2024, 11:43 Purged and closed all water cooling lines.

Friday, December 20, 2024, 15:54   removed target and installed Uline.

 roughing down test stand 

Friday, December 20, 2024, 16:17    valves closed and roughing pump off. 

Friday, December 20, 2024, 16:17   shut down test stand computer for holiday break 

Entry  Tuesday, January 07, 2025, 17:06, Dave Neilson, , LP-FEBIAD, , , 44692-4, 42972-10, In progress, FEBIAD development 

 Tuesday, January 07, 2025, 16:00 -  Target assembly installed in test stand. electrical connections assessed:

Prior to installation:  oven and cathode isolated from heatshield. no shorts

After installation:  Oven and Cathode 35kΩ from HVC. 

Tuesday, January 07, 2025, 16:05  -  pumping down to rough vacuum

Tuesday, January 07, 2025, 16:45  TP1B on.      TP1A on.  Pumping down

 

Prior to proceeding, ensure that ALL water cooling is turned on, as it was all drained and empty for the past 2 weeks.

 

Tuesday, January 07, 2025, 17:10   Beam line TP1 and TP2 on. 

Wednesday, January 08, 2025, 09:01    chamber pressure at 1.0E-6 T,  beamline pressure at 3.7E-7 T

 Wednesday, January 08, 2025, 10:32 - water cooling all on. no effect on vacuum pressure. 

Wednesday, January 08, 2025, 10:33    - Increased argon pressure in the gas line has no effect on vacuum pressure. it is registered on the pressure gauge at feedthrough.- 

  - However, roughing pump doesn't seem to be venting the argon gas line. I disconnected the copper line to the venting valve to confirm pump activity. - no activity detectable. 

- removed pump from assembly. switching on by itself shows no evidence of pump functionality. When on, pump is heating to very hot temperatures. I've emailed Edi at vacuum group to investigate further.

Wednesday, January 08, 2025, 15:02   - Vacuum group says that the pump is dead. We can replace it if we'd like, but i've created a temporary solution by connecting the argon venting valve to the backing pumps. For the sake of being careful (although this may be overly cautious), we must avoid opening this venting valve without first isolating the connection from the turbo pumps via closing TSG:PV1

 

Wednesday, January 08, 2025, 15:04  ramping up COIL to ensure conditioning against outgassing later.  vacuum appears to be stabilizing below 2e-6 T

Wednesday, January 08, 2025, 16:32   vacuum recovered, beginning to heat at 1A/30s up to 580A/230A    TGHT/TBHT

Wednesday, January 08, 2025, 22:32   with COIL on, the vacuum pressure increased to ~2.2E-6 T before beginning to recover, leaving on to encourage vacuum recovery.

 

Thursday, January 09, 2025, 08:27 Vacuum at 1.0E-6 T.  COIL off.

Thursday, January 09, 2025, 10:15   Argon gas line at 0.5 bar.a

Thursday, January 09, 2025, 10:56   increasing BIAS/EE/EZL  to 30/1.5/13 kV 

Thursday, January 09, 2025, 11:19    turning on optics elements. TMS:Q2 is timed out and possibly unalive. - must be investigated

Thursday, January 09, 2025, 12:38  HV at 30kV. monitoring for spark activity 

Thursday, January 09, 2025, 12:53  over 15 minutes, there was just one possible spark.  I see also that TPS:Q2 (quadrupole prior to FC0) seems to be half-down. i can't seem to get it to stop timing out and recharge. must investigate further

after investigating further and attempting to reset/reconfigure. I tried power cycling the canbus controller as well. In the end, controls group determined that this controller needed to be replaced.

 Thursday, January 09, 2025, 14:34   all optics set.  setting COIL CATHODE to 40A 120V.   CATHODE is leaking 0 current. (0.000 mA readback).  

Thursday, January 09, 2025, 14:37   reading 2.91e-8A at FC0 . found Argon peak at 40 exactly. MB1 current 96.4561 A

Thursday, January 09, 2025, 14:42 using COIL CATHODE scan program to optimize. (data file measure_id=9106)  A local maximum was identified at 140V with 40A coil current. However, a short seems to show up when the cathode voltage reaches ~130V. it lets through only ~10mA at 130 and then will release up to at least 100mA at 140V.

As time passes, the sustained voltage drops over time, given a current limit of 100mA. it dropped to ~50V. On subsequent increases of the power supply, current begins leaking through at ~65V. 

Given this, I will continue (while monitoring the cathode power supply) with a cathode coil of 50V 90A.

Thursday, January 09, 2025, 15:28  FC0 = 2.21 e-8 A.    FC6 at 3.21e-10A   RPM taken for all 4.

Thursday, January 09, 2025, 16:04   mass scan complete  -  2025_01_09-16_01 FEBIAD no retainer 1.txt CATHODE voltage was stable at 50V throughout.

 Thursday, January 09, 2025, 16:07  decreasing BIAS/EE/EZL to 0, 0, 0

 Friday, January 10, 2025, 09:09    ramping BIAS/EE/EZL  to 30/1.5/13 kV 

Friday, January 10, 2025, 11:51 Increasing COIL and CATHODE to 90A and 50V (was able to ramp cathode up to 100V before seeing current loss)

Friday, January 10, 2025, 11:53   FC0 = 1.7e-8 A.    FC6 = 4.9e-10 A    wire scans taken.

Friday, January 10, 2025, 12:00     Beginning mass scan with COIL CATHODE at 90A 50V   - 2025_01_10-12_28 FEBIAD no retainer 2.txt

Friday, January 10, 2025, 12:28   decreasing BIAS/EE/EZL to 0, 0, 0

 Friday, January 10, 2025, 13:15   gas inflow OFF (at rough vacuum pressure). Ramping up again BIAS/EE/EZL  to 30/1.5/13 kV 

Friday, January 10, 2025, 14:27   FC0 = 1.22e-8A.   FC6 = 2.93e-12A  (at 40) .   mass scan taken  = 2025_01_10-14_18 FEBIAD no retainer 3 argon off.txt     wire scans taken.

Friday, January 10, 2025, 14:28   TGHT TBHT cooling to 0A 0A at 1A/30s
 

 

Monday, January 13, 2025, 11:00   testing cathode isolation on cold target by ramping up cathode voltage until breakdown.   At 120V, CATHODE current is 2.4mA. (125V, 8.5mA), at 130V, current limiting and dropping voltage.

 Monday, January 13, 2025, 11:10   power supplies off. Winding down turbo pumps for chamber evac

Monday, January 13, 2025, 13:07   venting 

 

 

Entry  Thursday, January 23, 2025, 17:12, Dave Neilson, , , , , , , , CATHODE ANODE current leak testing 

Recent tests have shown that CATHODE voltage breaks down at ~130V, continually leaking current and progressively dropping voltage, making febiad CATHODE testing impossible.

 

Thursday, January 23, 2025, 15:18    disconnected cathode wire from TBHT feed through, simply suspended in cage.

 

voltages are held for ~1min prior to increase. current will be reported after 1min and stable.

100V - 0.000mA

120V - 0.000mA

130V - 0.000mA

140V - 0.000mA

150V - 0.000mA

170V - 0.000mA

200V - 0.000mA

- the Cathode wire and power supply have no leak problem

 

Thursday, January 23, 2025, 15:42

Reattached the CATHODE line to TBHT feedthrough. Removed the 100||100kΩ resistor pair that connects TBHT to HVC.

Same process as before:

100V - 0.000mA

120V - 0.000mA

125V - 0.000mA

130V - 0.000mA

135V - 0.000mA

140V - current limit ---> dropped to 52V

-- The TBHT resistor pair is not the problem

 

venting chamber to investigate lines.

 

Thursday, January 23, 2025, 17:05

removed piece of broken ceramic that held the coil terminal

still current leaking, but it's not as immediate or as shorted. more resistive.

__V__mA__

30    0

35    2.4

40    6.1 

45   12.2

50   19.5

55   32

60   gradually ramped up to limited

 

Thursday, January 23, 2025, 17:10

Disconnected COIL terminal.  Behaviour still similarly bad. Doesn't seem to have improved.

 

Disconnected all TBHT and TGHT feedthroughs. ALL are now isolated from ground (AS BEFORE). TBHT + and - are isolated from all others, TGHT + and - are isolated from all others but 100R apart due to resistor at feedthroughs (as expected).

Increasing CATHODE voltage on TBHT+ feedthrough to test isolation.

V ____ mA

120  ___ 0

135 ____ 0

150 ____ 0

200 ____ 0

- The TBHT+ terminal does not leak directly to ground

 

Connecting CATHODE cable to TBHT(-) feedthrough to test

V___mA

130 __ 0

150 __ 0

200 __ 0

- the TBHT- terminal does not leak directly to ground.

 

Connecting CATHODE to TGHT+ feedthrough , and disconnected the 100R between - and +

V ___ mA

100 __ 0

150 __ 0

200 __ 0

- the TGHT + terminal does not leak directly to ground

 

Connecting CATHODE to TGHT-  feedthrough:

V __ mA

125 __ 0

150 __ 0

200 __ 0

- the TGHT- terminal does not leak directly to ground.

 

connected cathode cable to TBHT+ cable.

V __ mA

30 __ 0

40 __ 0

50 __ 12

60 __ 35

70  -> 60__ 80 current limited

 

Disconnected 100R path between TBHT and TGHT power supply

CATHODE cable still on TBHT+ cable

V __ mA

150 __ 0

200 __ 0

TBHT is not the problem

 

reconnected 100 path from TBHT to TGHT.  REMOVED varistors that connect TGHT to ground

V __ mA

100 __ 0

200 __ 0

These are likely the issue.

 

Reconnected varistors to confirm

SHORTED at 50 V -- 10mA, 65V gives 80mA, current limited.

 

Removed varistors.  WIll have to acquire appropriately specced ones

Entry  Friday, February 28, 2025, 17:16, Dave Neilson, , LP-SIS, , , 45447-17, 42972-2, In progress, UCx heat shield conditioning 

Friday, February 28, 2025, 15:54 : installed target assembly in test stand

Friday, February 28, 2025, 15:54  roughing

Friday, February 28, 2025, 17:16 Turbo pumps on

Monday, March 03, 2025, 15:00 Ramping TGHT/TBHT to 580/230A at 1A/30s

 Tuesday, March 04, 2025, 13:46  increasing BIAS/EE/EZL  to 30/2.5/13  kV 

Tuesday, March 04, 2025, 14:00  Optics on. SIS tune confirmed

Tuesday, March 04, 2025, 14:30   Mass scan complete - no end caps - no beam

Tuesday, March 04, 2025, 17:35 Current integrators appear to be down. Investigating further. 

Tuesday, March 04, 2025, 17:35    at 30kV, there was sparking once approximately every 5 minutes. over time, the voltage was decreased and at 26kV the spark frequency decreased to one every 20-30 minutes. This sparking appeared to be from BIAS to EZL based on the strip tool data. It was also silent, so likely inside the test stand chamber.  Two sparks over the HV time appeared to spike the TGHT current as well, although there was no disruption to TGHT operation

Tuesday, March 04, 2025, 17:38  HV BIAS / EE / EZL ramped down to zero

Tuesday, March 04, 2025, 17:38  ramping down TGHT/TBHT to zero at -1A/30s

Thursday, March 06, 2025, 09:45 Increasing BIAS / EE / EZL to 30/2.5/13kV to see if sparking persists while cold.

Thursday, March 06, 2025, 16:11 no sparks seen, even at 30kV

Thursday, March 06, 2025, 16:14  HV ramped down.

Thursday, March 06, 2025, 16:14   ramping back up TGHT TBHT to 580 230 at 1A/30s to reevaluate sparking

Friday, March 07, 2025, 09:06   ramped up HV/EE/EZL to 20/2.5/13 kV to continue HV conditioning. will be bumping up HV throughout the day depending on spark frequency

Friday, March 07, 2025, 23:30  ramped down HV/EE/EZL to zero, at end of day HV BIAS was at approximately 22kV after a 90 minute period of no sparking.

Saturday, March 08, 2025, 17:08    increasing HV/EE/EZL 20/2.5/13 kV  to resume HV conditioning.

Saturday, March 08, 2025, 23:59   At 30kV, no sparks seen for 30 min. Conditioning appears to have been effective. Suspicion is that the sparking is likely due to test stand infrequent use during improvements, etc.

Sunday, March 10, 2025, 00:07 decreasing HV/EE/EZL to zero.

Sunday, March 09, 2025, 00:13  cooling TGHT TBHT to 0A 0A at 1A/30s 

Tuesday, March 11, 2025, 09:44  winding down turbo pumps

 

Entry  Tuesday, March 11, 2025, 14:36, Brady Borrmann, , , , , 44691-8, 44378-2, In progress, Mass Marker Test Target 

Tuesday, March 11, 2025, 14:36 Roughing. Target installed.

Tuesday, March 11, 2025, 15:06 TP1B turned on.

Tuesday, March 11, 2025, 15:10 TP1A turned on. 

Tuesday, March 11, 2025, 15:18 IG1 Turned on 6.25e-05T 

Tuesday, March 11, 2025, 16:39 Turned water on. Started autoramping TGHT/TBHT to 580/230A at 1A/30s

Wednesday, March 12, 2025, 11:03  slowly ramping BIAS/EE/EZL to 30/2.5/13 kV 

Wednesday, March 12, 2025, 14:00 no beam seen out. It seems that FC0 is working though. Investigation needed

Wednesday, March 12, 2025, 16:00 decreased HV to 0 to investigate. See report (to be released and attached) for more information

Friday, March 14, 2025, 09:20 :  increasing TGHT TBHT to 100A at 1A/30s, then to 580/230A at 1.7A/10s. 

Friday, March 14, 2025, 11:31 increasing BIAS/EE/EZL to 30/2.5/13 kV 

 Friday, March 14, 2025, 12:57    it appears that everything is stable. FC0 = 3.6e-10 A (VQSX).  beginning mass scan.  mass scan saved as '2025-03-14-13-30 MM a 0A.txt'

Friday, March 14, 2025, 14:12 mass separator focused at mass 115 to visualize indium.

Friday, March 14, 2025, 14:12  increasing MM current, following mass peak.

__ Current __ FC6 output __

    0A        1.9e-11

    1A        2e-11

    2A        2.22-11

    3A        4.6e-11

    4A        5.9e-10

    5A        3.6e-9

    6A        8.6e-9

 Friday, March 14, 2025, 14:39  conducting mass scan.   '2025-03-14-15-20 MM b 6A.txt'   after the scan, it was noticed that the mm current had failed at some point during the scan.

Friday, March 14, 2025, 15:27   conducting mass scan with 0A mm current.  saved as 2025-03-14-15-55 MM c 0A.txt

Friday, March 14, 2025, 15:55 ramping down HV

Friday, March 14, 2025, 15:56 ramping down TGHT TBHT to 0 (1A/30s) to assess and correct mm OL issue

Tuesday, March 18, 2025, 14:49 After bringing down vacuum to open test stand, the mass marker connection has been investigated. Two multipin connections have become disconnected, seems to be at a soldered junction.

Tuesday, March 18, 2025, 14:51    MM has been moved to different pins for operation. multipin will be fixed at a later date. Now test stand has been vacuumed down and TGHT TBHT brought to 580 230 for measurement.

Tuesday, March 18, 2025, 14:51 MM temperatures:

MM current    _____    temperature:

0A ___ 195.8°C

1A ___ 198.1

2A ___ 223.7°C

3A ___ 282.1°C

4A ___ 370.1­­­°C

5A ___ 486.4°C

6A ___ 631.6°C

 

Tuesday, March 18, 2025, 16:17 cooling TGHT TBHT at -1A/30s to 0A

Wednesday, March 19, 2025, 16:30 :  Mass marker replaced - new ceramic oven and sleeve, new reservoir with Indium - 0.102g.  Same transfer tube and target assembly

Wednesday, March 19, 2025, 16:45:  Install complete, roughing vacuum

Wednesday, March 19, 2025, 17:07  Turbopumps on

Thursday, March 20, 2025, 10:00 :  Water cooling on. Increasing TGHT TBHT to 580 230 at 1A/30s.

Thursday, March 20, 2025, 12:00 :  at ~200A 200A, increased heating rate to 1A/10s

Thursday, March 20, 2025, 13:45 increasing HV BIAS/EE/EZL to 30/2.5/13 kV 

Thursday, March 20, 2025, 14:32   at HV now, stable. Beginning mass scan.    

 Thursday, March 20, 2025, 15:15  magnet positioned at mass 115

__ Current __ FC6 output __

    0A        1.17e-11

    1A        1.23e-11

    2A        2.60e-11

    3A        9.2e-11

    4A        2.8e-10

    5A        5.5e-10

    6A        1.4e-9

Thursday, March 20, 2025, 15:57  running mass scan - 2025-03-20_16-26 mm e 6A

 Thursday, March 20, 2025, 17:00 run mass scan - 2025-03-20_16-58 mm f 0A.txt
 
Thursday, March 20, 2025, 17:29  mm has cooled more, repeating mass scan.  2025-03-20_17-51 mm g 0A.txt
 
Thursday, March 20, 2025, 17:58  BIAS/EE/EZL down to 0V .  left hot for mm temperature evaluation tomorrow

Friday, March 21, 2025, 11:08   Temperature testing

Current ___ Temperature

0A     184.5

1A     187.2

2A     208.3

3A     268.7

4A     374.1

5A     419.2

6A     495.8

 Friday, March 21, 2025, 12:09   cooling TGHT TBHT at 1.7A/10s to make Faraday cage accessible for controls work

                           decreased cooling rate to 1A/20s for final 100A. at 14:00, test stand was opened for controls work.

Wednesday, March 26, 2025, 10:08   Turbo pumps switched off for venting and changing the mass marker reservoir

Wednesday, March 26, 2025, 18:01  Chamber opened, MMR replaced with MMR3, roughed, now turbopumps on.

Thursday, March 27, 2025, 12:38 TGHT TBHT brought up to 580 230 at 1A/30s for 100A and then 1.7A/10s for the rest. now increasing  HV BIAS/EE/EZL to 30/2.5/13 kV 

 Thursday, March 27, 2025, 13:58    at high voltage, beginning mass scan.   (h)

Thursday, March 27, 2025, 14:37    Magnet at 115, measuring beam output with increases of MM current

current ___ FC6 output

0A    8.2e-11

1A    8.2e-11

2A    8.6e-11

3A    1e-10

4A    1.88e-10

5A    5e-10

6A    8.7e-10

Thursday, March 27, 2025, 15:26 beginning mass scan at MM 6A. --- MM Current failed at the beginning of the mass scan. data still collected - indium peak lower than expected due to gradual cooling. mass scan saved (i) 2025-03-27_15-32 mm i 6A-0A.txt

Thursday, March 27, 2025, 15:33   cooled 0A mass scan beginning - (j) 2025-03-27_16-13 mm j 0A.txt

Thursday, March 27, 2025, 16:32  decreasing HV to 0

Friday, March 28, 2025, 09:13  spinning down turbo pumps to vent system. Must *begin* to repair/replace the multipin connection. - will affix twisted pair to two appropriate channels for IGLIS AC

Tuesday, April 08, 2025, 12:26   spinning down turbo pumps 

 Wednesday, April 09, 2025, 15:36  Twisted pair wire shielded, routed and crimped for iglis and high(er) current purposes. multipin channels 8 and 9.

                 roughing.

 Wednesday, April 09, 2025, 16:26   turbo pumps on

Thursday, April 10, 2025, 09:43    beginning heating - TGHT TBHT to 580 230 at 1A/30s

Thursday, April 10, 2025, 10:41     at 100A100A. increasing ramp rate to 1.7A/30s

Thursday, April 10, 2025, 11:39 increasing HV BIAS/EE/EZL to 30/2.5/13 kV 

Thursday, April 10, 2025, 13:12   -  mass scan - 0A mm. - -  2025-04-10_13-46 mm k 0A.txt
Thursday, April 10, 2025, 13:50     magnet on 115 u - turning on MMR current.

current ___ FC6 output

0A    1.56e-11

1A    1.5e-11

2A    1.81e-11

3A    2.1e-11

4A    3.1e-11

5A    5.2e-11

6A    1.75e-10

7A    1.08e-9

8A    5.3e-9

 

 Thursday, April 10, 2025, 14:49   mass scan at 8A. Frequent sparking, ~1/min but doesn't appear to be affecting anything. no affect on optics or power supplies.  appears to be inside TS chamber as well.   mass scan saved (l 8A) 2025-04-10_15-04 mm l 8A.txt

Thursday, April 10, 2025, 14:50   MMR current decreased to 6A. waiting to cool to begin mass scan. sparks have stopped .

Thursday, April 10, 2025, 15:08  beginning mass scan.  (m 6A)  saved. 2025-04-10_15-34 mm m 8A.txt

Thursday, April 10, 2025, 15:34  MMR current 0A. repeat mass scan after cooled. (n 0A) saved.  2025-04-10_16-10 mm n 0A.txt

Thursday, April 10, 2025, 16:02 voltages to 0 for temperature testing

Current ___ Temperature

0A    205     

1A     205.5 

2A     227    

3A     268    

4A     327    

5A     391    

6A     462      

7A     546

8A      645.6

Thursday, April 10, 2025, 16:51    cooling TGHT TBHT at 1A/30s

 

 Friday, April 11, 2025, 09:00  spinning down turbo pumps to vent chamber. must replace source cup (p2n style --> old style)

Friday, April 11, 2025, 09:56  opened VV1 to begin venting the chamber. 

Friday, April 11, 2025, 15:39    P2N source cup removed, old source cup installed for repeat test. roughing chamber now.

 Friday, April 11, 2025, 16:05   turbo pumps on

Monday, April 14, 2025, 09:43  Water cooling on. TGHT TBHT ramping up at 1A/30s to 580A/230A

Monday, April 14, 2025, 12:57 increasing HV BIAS/EE/EZL to 30/2.5/13 kV 

 Monday, April 14, 2025, 15:27   FC0 signal very low. running mass scan - (o - 0A MMR),  2025-04-14_15-42 mm o 0A.txt
Monday, April 14, 2025, 15:45   magnet set to 115u
increasing mmr current.

current ___ FC6 output

0A     2.4e-12

1A     4e-12     

2A     3.9e-12  

3A     4.8e-12

4A     3e-12 

5A    4e-12  

6A    4e-12

7A    4e-12

8A   4e-12

Monday, April 14, 2025, 16:06     no indium out was seen here due to increase of mmr current.

running mass scan again at 8A

MMR power supply tripped after 20u, had to reset power supply trip, quickly ramped down HV, reset, ramped back up.

mass scan running at 8A MMR.   appears that no beam is coming from this target...    spark occured halfway through the run that tripped the MMR power supply as well as the beam line vac gauge IG6 -> leads to interlock trip on many optics. Restored as quickly as possible. however, beam was far past 115, where indium had been expected    saved as  2025-04-14_16-42 mm p 8A.txt
 

 Monday, April 14, 2025, 16:44   dropping HV to 0V and cooling TGHT TBHT to 0A/0A for target examination

Monday, April 14, 2025, 16:53   This trip has caused some sort of communication issue with the TGHT, This caused TGHT to be 'stuck' at 580A. I had to eventually cut power to the supply and have power cycled it. have not been able to restore power to it remotely

Fixed TGHT. Was able reset it locally after opening the cage.

Tuesday, April 15, 2025, 08:06   Turbo pumps off to vent, remove target and examine. 

Tuesday, April 15, 2025, 08:43   VV1 open 

Tuesday, April 15, 2025, 11:22   Target opened, taken apart, examined. Appears that the MMR transfer line had become dislodged from the target block, preventing transfer. Fixed this, reassembled, put back in TS.

Tuesday, April 15, 2025, 11:23  roughing.

Tuesday, April 15, 2025, 12:00  turbo pumps on.

Tuesday, April 15, 2025, 13:23  water cooling on. no effect on vacuum

Wednesday, April 16, 2025, 09:37 ramping TGHT TBHT 

Wednesday, April 16, 2025, 12:46  increasing HV BIAS/EE/EZL to 30/2.5/13 kV

Wednesday, April 16, 2025, 14:47 HV BIAS /EZL has been sparking occasionally, so increase has been slow

Wednesday, April 16, 2025, 15:05   mass scanning - 0A MMR. 

Wednesday, April 16, 2025, 15:07    spark external to TS (audible) tripped IG1 and shut down all power supplies. error thrown by TGHT as before.. cannot reset remotely. must discuss this error with controls.

Wednesday, April 16, 2025, 15:17  reset all and ramped up quick. running mass scan. 0A MMR  (q 0A) 2025-04-16_15-42 mm q 0A.txt

Wednesday, April 16, 2025, 15:43 heating MMR

current ___ FC6 output

0   4.4e-12

1   3e-12

2   4e-12

3   5e-12

4   6e-12

5   8e-12

6   4.8e-11

7   1.5e-10

8   9.1e-10

Wednesday, April 16, 2025, 16:31 mass scan 8A (r)   2025-04-16_16-31 mm r 8A.txt

Wednesday, April 16, 2025, 16:32 dropping HV to check temperatures

Current ___ temperature   (note. takes ~ 6 min to cool from max to min)

0A   197

1A   206

2A   218

3A   220

4A   300

5A   395

6A   500

7A   608

8A   735

Wednesday, April 16, 2025, 17:01  cooling TGHT TBHT at 1A/10s

Thursday, April 17, 2025, 08:37  turbo pumps off, spinning down 

Thursday, April 17, 2025, 11:15  venting

Entry  Thursday, April 17, 2025, 16:11, Dave Neilson, C#5, , , , , 45235 - 5, , LPSIS C#5 conditioning 

Thursday, April 17, 2025, 15:46  target installed. now roughing

Thursday, April 17, 2025, 17:12 Turbo pumps on.

ELOG V2.9.2-2455