Monday, November 20, 2023, 12:28, Eric Lahe, South Hot-Cell, Maintenance, , , Light Bulb Replacement - South Hot Cell roof lights
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3 light bulbs replaced in the ISAC South Hot Cell - North West light, South west light, and South East light bulbs. Northeast light currently still working.
The South East light is not working after bulb replacement. This bulb was tested using the wires from the Northeast light station and the bulb is working properly. Electrical services is being contacted to troubleshoot the cable issues. |
Tuesday, June 23, 2015, 10:55, chad fisher, South Hot-Cell, Repair, , , Left Manipulator Repair
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The master wrist/tong cable has been replaced on the left manipulator. Everything appears to function well so far. |
Tuesday, November 24, 2015, 14:02, chad fisher, South Hot-Cell, Repair, , , Left Manip repair
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electronics package on left manip died completely yesterday (it has been going for a while).
Disconnected entire package and replaced with package from "spare" manipulator.
everything is back up and working. |
Wednesday, May 10, 2017, 13:42, Anders Mjos, Conditioning Station, Repair, , , Leaky gauge at TCS:TS2 (e-fault: 9609)
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Neil Wong will fix this leak tomorrow Friday. See attached schematics for location. |
Thursday, October 26, 2017, 09:56, Anders Mjos, ITE, Repair, TM4, SiC#37, Leak on multi pin connector feedthrough
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On maintenance day Tuesday, the roughing of the target station could not go below 1.5 Torr. A brief troubleshooting on Tuesday was unsuccessful in determining the cause. Leak checking continued on Wednesday by David and Anders. A leak was finally found on the multi pin connector feedthrough due to the seal between the connector and flange on top of the nylon insulator. Upon re-tightening the connector, the leak could be stopped and the module pumped down to allow starting of turbo pumps. |
Thursday, August 15, 2013, 16:35, Anders Mjos, ITE, Repair, TM4, SiC#29, Leak found on Coil 1
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By pressurizing the water lines with 70 psi helium David and I detected a major leak on the Coil 1 circuit. The response maxed out on the leak rate on the leak detector and we could also see a pressure increase on the leak detector. ISAC controls reported a change in vacuum at the same time (link).
The Heat Shield and Coil 2 circuit was checked before we moved to Coil 1. No response was detected on these two circuits. We would like to check the remaining circuits as well, but this cannot be done today due to the large amount of helium still present. The remaining circuits will have to be checked tomorrow morning.
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Friday, October 28, 2011, 14:42, Bevan Moss, South Hot-Cell, Maintenance, TM4, , Leak check on service cap feed through
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After Chad and Davids leak check results from the containment box it was decided to perform a leak check on the feed through stem in the service cap. This is a known point of failure on TM1 and the same design flaw is likely in TM4. Once the service cap was open a visual inspection was performed and some oxidization of the copper line on the tube heater (+) circuit was observed (see attached pictures). The leak check was performed with the cart at a base pressure of 0.0 x 10^-4 Torr and base leak rate of 0.0 10 x 10^-9 atm cc/sec. A total of 4 joints were checked and no response was found. The service cap was then flooded with helium and once again no response was found. It was decided to give the module a clean bill of health, make note of the baseline test from the conditioning station, and continue to monitor the circuit. |
Thursday, March 30, 2017, 11:21, David Wang, Conditioning Station, Repair, TM4, , Leak check on TM4 Ta(-) water lines in service cap
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Leak check on TM4 Ta(-) water lines in service cap is done. LD base LR after 50minutes pumping down:0.0xE-9 atm.cc/sec. base pressure: 0.0XE-4 torr. I sprayed lots helium on welding stems on Ta(-) line in service cap including stems in blue nylon insulator and stems to service tray. no any response has been foun on LD. The Ta(-) line in service cap is leak free.
Totally panel open and leak check time is about 12minutes. Argon vented TCS before leak check this morning. |
Thursday, October 19, 2017, 10:11, David Wang, Conditioning Station, Standard Operation, TM4, , Leak check on TM4 HS line at SHC and TCS.
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Chad and I leak checked TM4 HS line after new target is installed yesterday. No leak has been found. Also, I helium pressurized the HS line at TCS this morning. TM4 HS line is good on this test. The TM4 gas line configuration on TM4 top is leak check as well. No problem. |
Wednesday, May 17, 2017, 08:31, David Wang, South Hot-Cell, Standard Operation, TM4, , Leak check on TM4 HS line at SHC
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Chad and I finished leak check on HS line with UCx target installed on it. Base Leak rate:0.0X 10^-9 atm.cc/sec, Base pressure 0.0X 10 ^-4 torr. Sprayed helium to VCR joints. No leak has been found . The line will be pressurized with helium at TCS.
Helium pressure test on TM4 HS line is done at TCS. BLR 0.0XE-9 atm.cc/sec. 70psi helium , 2 minutes. No response. The line is leak free. |
Tuesday, June 27, 2017, 10:26, David Wang, South Hot-Cell, Standard Operation, TM4, Ta#52, Leak check on TM4 HS line at SHC
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LD base LR:0.0Xe-9 atm.cc/sec. No leak has been found during the check. The HS line will be helium pressurized at TCS this week.
Helium pressurized the HS line at TCS. 70 psi 2 minutes, 0.0 x E-9 atm.cc/sec. No leak. |
Friday, October 25, 2013, 06:58, David Wang, South Hot-Cell, Standard Operation, TM4, , Leak check on TM4 target heat shield
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Maico and I leak checked HS circuit after Chad installed the target. The circuit was a little bit difficult o pump down because of residue water moister inside. But once the moisture was pumped out, the pumping down was smooth and fast. The base leak rate 0.0xE-9 atm.cc/sec, base pressure 0.0xE-4 torr. Maico checked helium flow before the leak test. Then,He sprayed helium to all 3 VCR fiitings on target with 2 seconds on each one, He also flushed 10 seconds helium around the target. There were no any response during all these test time on leak detector.He checked the helium flow again after the test and confirmed the helium flow. The HS circuit is leak tight. |
Thursday, December 05, 2013, 14:55, David Wang, South Hot-Cell, Standard Operation, TM4, , Leak check on TM4 target heat shield
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Chad and I leak checked TM4 heat shied water circuit at SHC. The pumping down was very good.Base leak rate 0.0xe-9 atm.cc/sec. BP 0.0xe-4torr. Sprayed helum twice on both VCR fittings.There is no response on leak detector. The circuit is leak tight. |
Thursday, May 02, 2024, 15:23, David Wang, South Hot-Cell, Development, TM3, , Leak check on TM3 new containment box window line VCR fittings.
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After new containment box installation on TM3, Chad and I did a helium spray leak check on two VCR fittings on front side water lines. they are leak free.
Helium pressurize window water line to 70 psi for 3minutes. No response on leak detector which is 0.0xe-9 atm.cc/sec. |
Thursday, July 24, 2014, 18:21, Grant Minor, South Hot-Cell, Repair, TM2, No target / no source tray, Leak check on TM2 ionizer tube cooling lines C and D - module side
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Target Ionizer tube cooling lines "C" and "D" in Target Module 2 were both leak checked at the Hot Cell. The lines were both blanked-off.
Bill Paley was present with David Wang in the Target Hall, operating the leak detector. Grant Minor and Anders Mjos were present with Chad Fisher at the Hot Cell.
The "D" circuit was already blanked off with a copper blank containing silver brazed stainless steel inserts and indium plated inconel c-seals.
The "C" circuit was already blanked off with an aluminum blank and rubber o-rings.
The cooling lines are indicated in the attached screencapture from ITA6021 Rev .14, and are also labelled in the attached photo.
The "D" circuit was checked first, starting at around 12pm.
1. The helium flow was tested by blowing dust on the work table.
2. The base leak rate on the Varian leak detector was confirmed in the "D" circuit to be stable at 10^-9 atm cc / sec and the pressure was 10^-4 Torr.
3. Each soldered joint on the "D" circuit was sprayed with a 2-second blast of helium - no response at the Varian.
4. The joint between the module-half of the water block and the copper blank-off was sprayed with a 2-second burst - no response.
5. A general area flood of helium sprayed for 10 seconds was applied all around both the "D" and "C" blocks - no response.
It was concluded that the "D" circuit had passed this leak check. The "C" circuit was checked next. The detector was changed to the "C" circuit and the circuit was pumped down. At around 2pm the leak check resumed.
6. The base leak rate on the Varian leak detector was confirmed in the "C" circuit to be stable at 10^-9 atm cc / sec and the pressure was 10^-4 Torr.
7. The solder joint area on the "C" circuit was sprayed with an 8-second burst of helium - no response.
8. The joint between the two halves of the water blocks was sprayed with a 6-second helium burst - no response.
It was concluded that the "C" circuit had passed this leak check.
The electrical continuity of the "C" and "D" circuits were confirmed in the Target Hall at the service cap, and in the module at the Hot Cell, to double check that the correct lines has been pumped and leak checked - this was OK.
The ionizer tube heater lines appear to be leak tight at the Hot Cell.
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Thursday, August 02, 2018, 07:57, David Wang, Conditioning Station, Standard Operation, , , Leak check on TM2 UCx #23 @ TCS and SHC.
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I did a helium pressure test on TM2 HS line at TCS. At 70psi helium, the leak rate is 2.5 xE-7 atm.cc/sec. I think this is the number that close to result before which is 1.7xE-9 atm.cc/sec. WE know there is a small leak on this water block seal. Chad and I did helium spray check yesterday at SHC. It was good at bottom scale. No much worry on this low E-7 range leak. |
Thursday, November 09, 2017, 09:34, David Wang, Conditioning Station, Standard Operation, TM2, Ta#55, Leak check on TM2 HS line at SHC and TCS.
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The TM2 HS line was leak checked at SHC yesterday . 0.9xE-9 atm.cc/sec.Helium sprayed by Chad, NO leak. It was helium pressurized at TCS this morning. Leak rat:2.5 XE-7 atm.c/sec. The result is same as last time check. No concern. |
Tuesday, December 02, 2014, 13:33, David Wang, South Hot-Cell, Development, TM2, , Leak check on TM2 tube heater +(D) at SHC
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Chad and I leak checked TM2 tube heater+(D) circuit at SHC with water bypass loop and new seals installed on the water block. The LD base LR 0.0xE-9 atm.cc/sec,base pressure0.0xE-4 torr. Chad sprayed helium on the leak check area in SHC for 5 seconds. No any response has been found on LD during 1minutes waiting time. The test was repeated again and the result is same. NO LEAK at this stage! After the TM2 is moved to CS , The D line will be pressured with 80 psi helium for helium pressure leak test before any hot water is circuited through it. |
Wednesday, June 26, 2013, 11:03, David Wang, South Hot-Cell, Standard Operation, TM1, , Leak check on TM1 UCx target heat shield
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Chad and I leak checked the TM1 UCx target heat shield at SHC. No leak has been found so far. |
Wednesday, March 02, 2016, 10:04, David Wang, ITW, Standard Operation, TM2, , Leak check on ITW and TM2.
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Dan and I leak checked TM2 and ITW primary vacuum vessel. It was found a 1X E-7 atm.cc/sec leak on top T flange seal between TM2 and dump module in first time check. But it is not a repeatable leak. I checked the same spot and around area two more times with increased helium volume.It did not show up again. The first response could be a helium drift to dry scroll pump. I will check it again later. The primar vacuum vessel on ITW and TM2 are leak free.
Dan and I found a small leak on ITW dump module top flange seal. The leak detector got a response to 7xE-9 atm.cc/sec when I spray the helium to west side of dump module top flange. We tested again, and got same result. The o-ring which seals ITW dump module top flange is deteriorating. It need to be replaced at a proper time. This is the only air to vacuum leak we confirm so far on primary and secondary vacuum vessel on TM2 and ITW. The module and station no other air to vacuum leak.
The TM2 water lines helium pressure tested started in ITW. The helium pressure 70psi. The result so far is: Window: good, GE: huge leak directly shoot over E-7 atm.cc/sec( need to be confirmed tomorrow), HS: good, EE: good, MSP: tiny leak which is response to 3-4xE-9 atm.cc/sec. Coil 1 : small leak which is response to 1.3XE-8 atm.cc/sec. Tomorrow, We will test the rest water lines on TM2which are TA+, TA-, Tube+, Tube-, and coil 2. And We will confirm the GE huge leak at the last.
Finished the helium pressure test on TM2 water line.70 psi helium, The result of the rests 5 circuits: coil 1: leak 7.2xE-8atm.cc/sec,Ta(+): small leak 1.7XE-8 atm.cc/sec, Ta(-) small leak 8.7xE-9atm.cc/sec,Tube(-) 1.5 x E-8 atm.cc/sec. Tube(+)small leak 3.7xE-8 atm.cc/sec. We repeated the helium pressure test on GE. There is a huge leak on TM2 GE circuit. The leak detector shoot up to E-7 atm.cc/sec right after the helium was applied.It went up to E-6 range in less than 1 minutes.
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