Friday, April 07, 2017, 09:53, Travis Cave, Conditioning Station, Maintenance, TM1, no target, Electrical Check and TM1 other checks
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Results of an electrical check on TM#1 with no target attached to it.
I use this e-log entry for TM1 notes as well 1. TM1 IG1 is a dual filament gauge . Its filament is very close to grid now. It shorted one time during the pumping down. It still works fine so far . But, we may need to change it if we use this module in TS again.
TCS 1G1 and 1G1S are pumped to 5Xe-6 torr. IG2 stayed at 2.5XE-5 torr. Since no target is installed on module , I capped top of HS water line. Maybe, the small o-ring seal in cap is too old, I found a big leak on this seal when i use LD check it. That is the reason IG2 stayed too high. Still, Leak check and helium presuure test are fulfilled on TM1. Leak detector BLR 5XE-7 atm.cc/sec, BP 0.0XE-4 torr9. Back up pressure is 51 mtorr which is high because of leak on HS line cap seal so LD BLR is high. At this level, Ta+-, Tube +-, MSP, EE are good. Other air to vacuum seal are good as well at this leak rate. I will check and change small o-ring seal in HS cap. The TM1 is functional basically. |
Thursday, April 06, 2017, 15:16, Anders Mjos, Conditioning Station, Maintenance, , , Installation of new break out box to accommodate both ITM:MP2 and TCS:MP1
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Installation by Marshall. Dave M from controls adjusted circuitry to get TCS:MP1 to start.
Work is being done in preparation for the Module Move Ventilation SAS project |
Thursday, April 06, 2017, 15:11, Grant Minor, Crane, Maintenance, , , Target Hall Crane 20 ton hoist - Report by Gordon Crane 5-Apr-2017
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-------- Forwarded Message --------
Hi Curtis
Further to the emergency service call at the Isac Target Hall on Thursday March 23rd, we advise as follows:
It was reported that the hoist was making an unusual noise and that there was a strong brake odour during operation.
The lift was completed using the auxiliary hoist.
A man-lift was arranged and Senior Service Technician Tom Kauss attended site the next morning to troubleshoot.
He determined that one of two hoist brakes (walkway side) had a strong odour and on closer examination it appeared that the
brake lining material was breaking down and particulate lining material was getting caught between the lining and the discs.
These lining fragments were rubbing and burning off during the hoist operation.
The end cover of the brake had an accumulation of brake lining fragments
The lining was not overly worn, but appears to be becoming friable, perhaps with age or exposure to radiation.
The brake was cleaned with compressed air to remove the friable material and thoroughly tested.
A test load of approximately 10 tons was lifted and the hoist handled the load without issue
The brake fragment issue did not recur while we on site and the hoist was recommissioned for use.
To guard against the likely recurrence of this condition on this critical application crane, and as both brakes have seen identical conditions in operation,
we recommend that both brake assemblies be replaced.
The brake assembly would include the brake coil, friction discs, steel brake discs and the brake springs
TRIUMF does not have a spare brake on hand, therefore one of the removed brakes could be rebuilt and kept on hand.
Two (2) each XL-60009637 Complete Brake Assemblies $ 5,706.00 Each
One (1) only XL-60009674 Brake Repair Kit $ 2,435.00
For Rebuild
One (1) only XL-52272125 Brake Spring Kit $ 59.72 For Rebuild
Installation & Testing of New Brakes estimated at: $ 1,250.00 Lot
We have one brake in stock in our Vancouver Service Depot. A second brake is available Ex-Ontario
FOB Site
Applicable Taxes Extra
Quote Valid for 30 days, subject to prior sale.
We are available next week to perform this work on site.
Please let us know if you have any questions or if you would like us to proceed.
Best Regards
Aidan
------------------
Aidan C. Gordon
General Manager
aidan@gordoncrane.com
Gordon Crane & Hoist Inc.
Celebrating 34 years of Excellence (1983-2017)
www.gordoncrane.com
Toll Free 1-866-HOIST-IT
(1-866-464-7848)
Tel: (604) 324-2441
105-8475 Ontario St
Vancouver BC V5X 3E8
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Thursday, April 06, 2017, 12:33, David Wang, Conditioning Station, Repair, TM1, , TM1 rust inpsection and removal
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TM1 inside service cap surface and shielding plug surface are visually inspected yesterday. No rust has been found. I cleaned all rust on top of TM1 today. Rust on TM1 silo top plate are cleaned as well. |
Wednesday, April 05, 2017, 14:13, David Wang, Conditioning Station, Maintenance, TM1, , TM1 and TCS vacuum system are connected together
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I started two turbo-pumps on TM1 and one small TP on TCS. They are work fine. |
Wednesday, April 05, 2017, 11:57, David Wang, ITE, Maintenance, , , ITE target module flange o-ring repalcement
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ITE target module tank flange o-ring was replaced yesterday before TM4 moving. ITE: IG1S reading looks fine so far. |
Wednesday, April 05, 2017, 09:46, Travis Cave, Conditioning Station, Standard Operation, TM1, no target, module moved
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TM#1 has been moved from the North West silo to the conditioning station. |
Tuesday, April 04, 2017, 14:40, David Wang, ITE, Standard Operation, TM4, , TM4 has been connected in ITE
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all turbo-pumps are started. Everything looks fine so far. |
Tuesday, April 04, 2017, 14:39, David Wang, Crane, Standard Operation, , , Crane check main hoist on jogging with shielding plug lifted.
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Today, I checked TH crane main hoist when shielding plug is installed into ITE pit. I did some jogging actions on main hoist during the operation. Everything looks fine. No burning smell, no strange noise. An outside crane expert suggest that jogging is the worst working situation for crane. We have to use jogging actions during our crane operation. But, we could try to use less jogging when operate the crane. |
Tuesday, April 04, 2017, 10:24, David Wang, Conditioning Station, Standard Operation, TM4, , Stopped TCS pumps this morning
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Argon vented TCS and TM4 after pumps are stopped. |
Tuesday, April 04, 2017, 10:23, David Wang, Conditioning Station, Standard Operation, TM4, , Helium pressure leak check on TM4 Ta(-) water lines
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This morning, The helium pressure leak check on TM4 Ta(-) is done after TM4 finished conditioning yesterday. LD base LR:8.0XE-9 atm.cc/sec, base pressure: 0.0XE-4 torr. Applied 70 psi helium to TM4 TA(-) water line. The LR slowly climbed to 2.2XE-7 atm.cc/sec, and stopped there. Waited for 5 minutes and change at 2.2 X E-7 atm.cc/sec. |
Tuesday, April 04, 2017, 09:29, Travis Cave, ITE, Standard Operation, TM4, UC#19, module moved
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TM#4 with UC#19 has been moved from the conditioning station to the east target station. |
Thursday, March 30, 2017, 11:21, David Wang, Conditioning Station, Repair, TM4, , Leak check on TM4 Ta(-) water lines in service cap
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Leak check on TM4 Ta(-) water lines in service cap is done. LD base LR after 50minutes pumping down:0.0xE-9 atm.cc/sec. base pressure: 0.0XE-4 torr. I sprayed lots helium on welding stems on Ta(-) line in service cap including stems in blue nylon insulator and stems to service tray. no any response has been foun on LD. The Ta(-) line in service cap is leak free.
Totally panel open and leak check time is about 12minutes. Argon vented TCS before leak check this morning. |
Wednesday, March 29, 2017, 14:11, David Wang, Conditioning Station, Standard Operation, TM4, , small leak on TM4 Ta(-) water line.
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A small leak has been found on TM4 Ta(-) which is marked as "B" on terminal blocks. The LD base Leak rate is 1.2XE-8 atm.cc/sec. 70psi helium has been applied to Ta(-) water line for 3minutes. The leak rate went up to 2.5xE-6 atm.cc/sec and stabilized there. Anders found a helium response on RGA helium reading during the same time. This confirms the leak is real. Other lines are leak checked today also. They are good still. All TM4 water lines were leak checked in ITE in 2017 January. They were all good at 0.0 X E-9 atm.cc/sec. See attachment e-log. |
Wednesday, March 29, 2017, 11:42, Anders Mjos, Conditioning Station, Standard Operation, TM4, UC#19, Conditioning UC#19
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Wednesday, March 29, 2017, 11:37: RGA on
Wednesday, March 29, 2017, 13:51: Water package on
Thursday, March 30, 2017, 08:50: Restarted chiller. OP3 fault on both VFDs.
Thursday, March 30, 2017, 10:18: Roughing
Thursday, March 30, 2017, 16:02: Configured EE to conditioning mode. All power supplies for SIS operation was checked to be working earlier.
Thursday, March 30, 2017, 16:06: BIAS / EL 10 / 5 kV and 0.02 / 0.04 mA
Thursday, March 30, 2017, 16:10: BIAS / EL210 / 10 kV and 0.03 / 0.06 mA
Thursday, March 30, 2017, 16:11: IG1 at 7.8E-7 T, IG2 at 2.3E-6 T
Thursday, March 30, 2017, 16:21: No sparking. Ramping down for the day
Friday, March 31, 2017, 08:32: BIAS / EL 20 / 10 kV and 0.03 / 0.06 mA
Friday, March 31, 2017, 08:32: IG1 at 4.2E-7 T, IG2 at 1.4E-6 T
Friday, March 31, 2017, 08:45: BIAS / EL 25 / 12.5 kV and 0.04 / 0.08 mA. Some minor vacuum responses around 24 kV
Friday, March 31, 2017, 10:03: BIAS current was limiting at 26 kV after EPICS restart. Updated limit
Friday, March 31, 2017, 10:10: BIAS / EL 30 / 15 kV and 0.04 / 0.09 mA. Vacuum and current responses when increasing BIAS.
Friday, March 31, 2017, 10:54: BIAS / EL 35 / 17.5 kV and 0.05 / 0.10 mA.
Friday, March 31, 2017, 11:24: BIAS / EL 40/ 20 kV and 0.05 / 0.11 mA.
Friday, March 31, 2017, 11:43: BIAS / EL 45/ 22.5 kV and 0.06 / 0.13 mA.
Friday, March 31, 2017, 13:47: No sparks for ~90 min. Ramping down HV
Friday, March 31, 2017, 13:58: Starting auto-ramping heaters to 100 / 100 A at 1 A/min. Good/bad vacuum at 3E-6 and 5E-6 T on IG2. EE to 1500 V
Friday, March 31, 2017, 14:03: BIAS / EL / EE at 30 / 15 / 1.5 kV and 0.04 / 0.09 / 1.5 mA
Saturday, April 01, 2017, 10:58: Continue auto-ramping to 440 A / 200 A.
Saturday, April 01, 2017, 17:17: IG1 / IG2 to 1.7E-6 and 3.6E-6 T at 440 A. Reduced manually to 430 A to limit outgassing.
Saturday, April 01, 2017, 18:03: Discovered TP2 had tripped off. Likely causing "increased outgassing" above.
Saturday, April 01, 2017, 18:12: TP2 back at speed.
Saturday, April 01, 2017, 23:25 : TP2 fault from spark. Restarting. Ramping down heaters.
Sunday, April 02, 2017, 06:45: Found source to be tripped on water flow TGHT at around 1:15 am. Vacuum and water flow otherwise ok. Set source to 0. To be investigated Monday.
Monday, April 03, 2017, 11:05: The paddle wheel on the TGHT line was not turning this morning. After running water through a bypass an reconnecting to the module, flow was restored, but it appeared to be at a relatively low rate.
Monday, April 03, 2017, 12:00: BIAS / EL / EE at 30 / 15 / 1.5 kV and 0.03 / 0.09 / 1.5 mA
Monday, April 03, 2017, 12:18: Tested TGHT / TBHT to 20 / 10 A.
Monday, April 03, 2017, 12:18: Increased EE to 2 kV and 2.0 mA |
Tuesday, March 28, 2017, 10:44, chad fisher, South Hot-Cell, Standard Operation, TM4, UCx#19, UCx#19 Installed
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UCx#19 has been installed onto TM4. High current fasteners torqued to 130 in lbs. Has been leak and electrical checked and is ready to leave hot cell. |
Tuesday, March 28, 2017, 10:30, Travis Cave, South Hot-Cell, Standard Operation, TM4, UC#19, Electrical Check
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Electrical check done on TM#4 with UC#19. See attached PDF for results. |
Tuesday, March 28, 2017, 09:18, Travis Cave, South Hot-Cell, Standard Operation, TM4, no target, module moved
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TM#4 has been moved from the conditioning station to the south hot cell. |
Monday, March 27, 2017, 13:40, Travis Cave, South Hot-Cell, Standard Operation, TM2, no target, Electrical Check
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Did the start of the running year electrical checks of both TM#2 and TM#4 with no target attached to either module. TM#2 was in the south hot cell and TM#4 is in the conditioning station under vacuum. |
Monday, March 27, 2017, 12:55, David Wang, Spent Target Vault, Repair, , , S/W silo rust clean up
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Rust on S/W silo and cover plate stored at silo area are cleaned up. |
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