Logbooks Lab Maintenance Evaporator_1 Evaporator_2 Laser cutter Target Production Test-Stand RH-ISAC RH-Cyclotron RH-Meson Hall RH-Beamlines RH-ARIEL
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New entries since:Wed Dec 31 16:00:00 1969
Entry  Monday, November 17, 2014, 11:38, Travis Cave, Conditioning Station, Standard Operation, TM3, no target, module move 

TM#3 with no target has been moved from the conditioning station to the north west silo.

Entry  Wednesday, September 30, 2015, 08:50, Travis Cave, South Hot-Cell, Maintenance, TM3, no target, Module moved 

TM#3 is in the south hot cell it was moved from the north west silo.

Entry  Wednesday, September 30, 2015, 11:14, Travis Cave, South Hot-Cell, Repair, TM3, no target, Electrical Check TM3_elecchk_notgt_shc.PDF

TM#3 electrical check at the south hot cell, no target, all value are done at 1000Volts. See the attached PDF for the results.

Entry  Tuesday, October 06, 2015, 21:12, Aurelia Laxdal, South Hot-Cell, Repair, TM3, , TM3 service cap inspection in target hall Pic1.jpg

David Wang and I did the service cap inspection in target hall: see WP I2015-10-06-10.<br>

Signs of sparking were seen underneath 3 insulators: E ("Cavity"), A ("Oven+") and B ("Oven -") at the pair water lines coming out of the  feed-through and going to the HV chase. Specifically one water line of E is very close to the feed-through insulator (2-3mm gap) and here the sparking sings are more prominent: see picture.

Entry  Thursday, October 08, 2015, 14:08, David Wang, South Hot-Cell, Standard Operation, TM3, Dummy target febiad., TM3 has been moved from SHC to NW silo 

Bill and I moved TM3 from SHC to NW silo with a dummy febiad target installed on it. The move is smooth.

Entry  Thursday, November 05, 2015, 09:57, Travis Cave, Conditioning Station, Maintenance, TM3, no target, Module moved 

TM#3 has been moved from the north west silo to the conditioning station.

Entry  Friday, November 06, 2015, 14:36, Anders Mjos, Conditioning Station, Development, TM3, FEBIAD test target, Testing TM3 

Friday, November 06, 2015, 14:35: Roughing

Turbos was started around 4pm. Later it was found that the manual valve for the two turbo pumps on the service cap was closed. The valve was open and pumping resumed. The roughing vacuum was high and increased into Saturday morning. The vacuum system was switched off on Saturday.


Purged MP1 using the purging function. Performance recovered. Started rouging.

Monday, November 09, 2015, 09:18: Started TP1S

Monday, November 09, 2015, 09:22: Started TP1 and TP2

Monday, November 09, 2015, 09:33: All 3 turbos at speed


Leak found on F/T for multipin connector

Tuesday, November 10, 2015, 09:53: stopped turbos

Entry  Friday, November 06, 2015, 14:44, Anders Mjos, Conditioning Station, Repair, TM3, , O-rings replaced on service cap 

O-rings were replaced on the service cap by Anders, Maico, Aurelia and Keith under work permit  I2015-11-05-5    


 

 One of the wires for the steerers had come loose and was reattached by Maico. Photo on DocuShare

 

 

 

 

 

 

 

 

 

 

 

 

 

 

 

 

Entry  Monday, November 09, 2015, 16:47, Anders Mjos, Conditioning Station, Maintenance, TM3, FEBIAD Test Target, Leak check of Service Cap 

Service cap leak checked this afternoon. Found multiple leaks of 10E-8 to 10E-7 range. Connected to the backing line with IG1 at ~4E-6 T, CG1A around 40 mT. Got responses around large round flange on top, rectangular side panels, water f/t on GND and water f/t on HV. Will resume leak checking tomorrow to attempt to pinpoint sources of leak more accurately.

Entry  Tuesday, November 10, 2015, 10:23, Anders Mjos, Conditioning Station, Maintenance, TM3, , Air to vacuum leak on service cap TM3_Service_Cap_Leak.pdf

Conducted a more thorough leak check this morning with Edi. He found a leak on the base of the  blue F/T insulator for the multi-pin connector (see attachment). I discovered that all the bolts could rotate freely in the threads as they were too small. The bolts were replaced. The leak rate was reduced but still significant. The o-ring will likely need to be replaced.

Tuesday, November 10, 2015, 17:00: Could not find new o-ring. Cleaned groove and o-ring and applied o-ring grease. Re-attached F/T.

    Reply  Tuesday, November 10, 2015, 16:53, Anders Mjos, Conditioning Station, Development, TM3, FEBIAD test target, Testing TM3 2015-11-13_TCS_TM3_FEBIAD_Test_Target.docx

Tuesday, November 10, 2015, 16:53: Roughing

Tuesday, November 10, 2015, 18:24: TP1S started

Tuesday, November 10, 2015, 18:30: TP1 and TP2 started

Tuesday, November 10, 2015, 18:41: All 3 turbos at speed.


Thursday, November 12, 2015, 08:30: Purged backing pump using purging function. Vacuum in backing line recovered to previous value. 


Module connected for HV testing. No target heating possible. All F/Ts tied together to HV common. EZL connected.

Friday, November 13, 2015, 11:20: Started water package

Friday, November 13, 2015, 11:52: 1kV on BIAS and 1 kV on EL

Friday, November 13, 2015, 12:54: BIAS/EL 10 / 5 kV

Friday, November 13, 2015, 12:59: BIAS/EL 15 / 7.5 kV

Friday, November 13, 2015, 13:04: BIAS/EL 20 / 10 kV

Friday, November 13, 2015, 13:08 : BIAS/EL 22 / 11 kV. Some sparks.

Friday, November 13, 2015, 13:17: Sparking at 22.5 kV. Had to return to 20 kV to recover. Back at 22.5

Friday, November 13, 2015, 13:21 : BIAS/EL 24 / 12 kV. 

 Friday, November 13, 2015, 13:27: Heavy spakring around 24.5 kV. Had to return to 20 kV to recover.

Friday, November 13, 2015, 13:31: Attempted to increase voltage again. Sparking started around 23 kV. Had to lower to 20 kV.

Friday, November 13, 2015, 13:36: 9 sparks for the last 5 min.

Friday, November 13, 2015, 13:45: Spark rate reduced, but multiple sparks encountered again at 20.5 kV. Reduced back to 20 kV

Friday, November 13, 2015, 13:50: Increased sparking at 20 kV. Had to lower to 18 kV

Friday, November 13, 2015, 14:07: Back at 20 kV

Friday, November 13, 2015, 14:13: BIAS and EL off


Monday, November 16, 2015, 08:18: Fault on chiller. Reset chiller unit on the roof.

    Reply  Thursday, November 12, 2015, 10:18, Anders Mjos, Conditioning Station, Maintenance, TM3, , Air to vacuum leak on service cap 

Anders Mjos wrote:

Conducted a more thorough leak check this morning with Edi. He found a leak on the base of the  blue F/T insulator for the multi-pin connector (see attachment). I discovered that all the bolts could rotate freely in the threads as they were too small. The bolts were replaced. The leak rate was reduced but still significant. The o-ring will likely need to be replaced.

Tuesday, November 10, 2015, 17:00: Could not find new o-ring. Cleaned groove and o-ring and applied o-ring grease. Re-attached F/T.

Tuesday

Steerer wire had disconnected again. See DocuShare for photos.


Thursday, November 12, 2015

Leak checked the fixed F/T and the panel for steeerers. No leaks found.

Entry  Thursday, November 12, 2015, 13:25, Anders Mjos, Conditioning Station, Standard Operation, TM3, FEBIAD Test Target, Electrical check and leak check TM3_iwth_FEBIAD_in_TCS_Electrical_Check.pdf

Target to Anode and target to Common showed ~ 500 kOhm values. No leaks above 3E-9 atm-cc/s seen. See attached.  

Entry  Monday, November 16, 2015, 10:09, Anders Mjos, Conditioning Station, Standard Operation, TM3, FEBIAD Test Target, Electrical check after HV conditioning 2015-11-16_TM3_Electrical_Test.pdf

 Problem found between ANODE (F) and chassis 90 kOhm. See attachment for details.

Entry  Monday, November 16, 2015, 10:37, David Wang, Conditioning Station, Repair, TM3, , TM3 has been disconnected at TCS. 

I stopped the TM3 and TCS vacuum pumps and water system. The TM3 is disconnected and vented. It will be moved to silo this afternoon.

Entry  Monday, November 16, 2015, 13:59, Travis Cave, Conditioning Station, Maintenance, TM3, no target, Module moved 

TM#3 has been moved back to the NW silo.

Entry  Monday, May 09, 2016, 08:43, David Wang, Conditioning Station, Repair, TM3, , I reinstalled all the side panel on TM3 service cap. 

They were moved for TM3 inspection job last week. All the bolts on the panel are hand tight only now since they will be removed out for camera installation during next stage inspection.

Entry  Tuesday, May 31, 2016, 09:45, Travis Cave, South Hot-Cell, Standard Operation, TM3, no target, module moved 

TM#3 has been moved from the NE Silo to the south hot cell.

Entry  Thursday, June 02, 2016, 08:44, Travis Cave, South Hot-Cell, Standard Operation, TM3, no target, Electrical Check TM3_elec_chk_no_tgt.PDF

Electrical check of TM#3 no target at the south hot cell. see attached for results.

Entry  Thursday, June 02, 2016, 11:59, David Wang, South Hot-Cell, Repair, TM3, , 5K mega test on TM3 5K_mega_check_on_TM3.pdf

I did a 5KV mega test on TM3.  Only5Mohm @5kV between coli line PQ and chassis(ground). It confirmed the close gap between P,Q and GE. Other lines are ok. See attachment.

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