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  RH-ISAC, Page 47 of 141  Not logged in ELOG logo
IDdown Date Author Category Type Module Target/Number Subject
  1900   Tuesday, March 26, 2019, 11:17 Travis CaveSouth Hot-CellStandard OperationTM2no targetElectrical Checks of TM#2 during the source tray change.

 The four electrical check done on TM#2 during the source tray change.

Attachment 1: Elecrictal_Check_TM#2_Old_source_Tray_Jan_11_2019.pdf
Elecrictal_Check_TM#2_Old_source_Tray_Jan_11_2019.pdf
Attachment 2: Electrical_Check_TM#2_No_Source_Tray_Feb_25_2019.pdf
Electrical_Check_TM#2_No_Source_Tray_Feb_25_2019.pdf
Attachment 3: Electrical_Check_TM#_New_source_Tray_Mar_22_2019.pdf
Electrical_Check_TM#_New_source_Tray_Mar_22_2019.pdf
Attachment 4: Electrical_Check_TM#2_new_source_tray_Mar_25_2019.pdf
Electrical_Check_TM#2_new_source_tray_Mar_25_2019.pdf
  1899   Tuesday, March 26, 2019, 11:10 Travis CaveConditioning StationStandard OperationTM2Dummy TargetElectrical Check

 Electrical Check of TM#2 with the dummy target attached.

Attachment 1: Electrical_Check_TM2_Dummy__Target_CS_Mar-26-2019.pdf
Electrical_Check_TM2_Dummy__Target_CS_Mar-26-2019.pdf
  1898   Tuesday, March 26, 2019, 09:32 Travis CaveConditioning StationStandard OperationTM2Dummy TargetModule move

 TM#2 with a new source tray and the dummy target has been moved from the south hot cell to the conditioning station.

  1897   Monday, March 25, 2019, 10:11 Aaron SchmidtSouth Hot-CellRepairTM2 LP-FEBIAD Test Target (empty)

Link to previous target information: https://elog.triumf.ca/TIS/RH-ISAC/1039

Monday, March 25, 2019, 10:00: Target electrical checks (See Attachment 1)

Tested for TM2 

Attachment 1: TM2_-_FEBIAD_target_-_Electrical_Test.pdf
TM2_-_FEBIAD_target_-_Electrical_Test.pdf
  1896   Thursday, March 21, 2019, 09:56 chad fisherSouth Hot-CellRepairTM2 Tray insertion

This morning new water block fasteners and gas line capture nut fasteners were inserted into the hot cell. Window waterline blank off was removed from TM2, surfaces inspected and given a polish with Veltex (30 seconds, 70 psi) as there was a small bit of c seal residue. Transfer try with new source tray has been latched to the module.

Attachment 1: 20190321_091833.jpg
20190321_091833.jpg
Attachment 2: 20190321_094625.jpg
20190321_094625.jpg
  1895   Wednesday, March 20, 2019, 11:19 Travis CaveSouth Hot-CellStandard OperationTM2no targetModule move

 TM#2 has been moved from the conditioning station to the south hot cell.

  1894   Monday, March 18, 2019, 07:25 David WangConditioning StationMaintenanceTM3 TCS vacuum pumps have been stopped.

 The TCS will be vented soon for TM2 move.

  1893   Monday, March 18, 2019, 07:23 David WangConditioning StationRepairTM2 TM2 window line helium test

New seals with a blank off cap are installed on TM2 window line water block.   The seals are checked at TCS with 70 psi helium for 5 minutes with LD at 0.0xE-9atm/cc.sec. No response on LD during test. Seals are good.

  1892   Friday, March 15, 2019, 08:51 Travis CaveConditioning StationStandard OperationTM2no targetModule move

 TM#2 has been moved from the south hot cell to the conditioning station.

  1891   Thursday, March 14, 2019, 10:25 chad fisherSouth Hot-CellRepairTM2 Water Block Polishing status

Phase 2 (intermediate) and Phase 3 (Final) polishing is complete on all water blocks on TM2 (minus ground electrode circuit which has only had a cursory cleaning). Phase 2 with 2000 grit wet sand paper and isopropynol for 1 minute with tool at 75 psi, Phase 3 with Veltex polishing cloth for 1 minute with tool at 75 psi.

Attachment 1: Blocks_final_polished.jpg
Blocks_final_polished.jpg
  1890   Tuesday, March 12, 2019, 09:13 chad fisherSouth Hot-CellRepairTM2 Water Block Polishing status

Stage 1 polish has been achieved on all single seal water blocks using the single pad tool run at 75 psi, 2 3 minute cycles per block using red scotch brite.

Attachment 1: Blocks_Stage_1_Polish.jpg
Blocks_Stage_1_Polish.jpg
  1889   Monday, March 11, 2019, 14:34 chad fisherSouth Hot-CellRepairTM2 Water Block Polishing status

Stage 1 polishing (water scale and at least 99% of visual indium removed) has been achieved on all 2 seal water blocks that will be used (Ground electrode has not been polished). Process required 3-4 3minute cycles of the tool using scotch brite pads with the tool running at approximately 75 psi.

  1888   Friday, March 08, 2019, 14:10 chad fisherSouth Hot-CellRepairTM2 Water block polishing

After trials with 2000 grid wet paper I have moved up to "red" scotch brite. This seems to have worked the best so far although it took two minutes to remove the ring that the other materials could not remove (see picture).

I have moved to next circuit. Currently at 3 minutes and 30 seconds with scotch brite but significant ring remains.

Attachment 1: B_after_SB_(2).jpg
B_after_SB_(2).jpg
  1887   Thursday, March 07, 2019, 13:59 chad fisherSouth Hot-CellRepairTM2 Polishing

Polishing of the water block sealing surfaces has commenced. First attempt was on block B with low nap brown polishing pad (the least aggressive pad prepared) and isopropyl for 30 seconds. This cleaned a little but did not remove the "ring" which I believe is water scale. I will step up to 2000 grit wet sand paper and iso next.

  1886   Thursday, March 07, 2019, 12:20 chad fisherSouth Hot-CellRepairTM2 Pre-polishing pictures

Pictures of the water blocks before polishing can be found on docushare, collection 24400

  1885   Thursday, March 07, 2019, 12:02 chad fisherSouth Hot-CellRepairTM2 Box Off water block jig on

The containment box has been removed from TM2 and the water block jig installed in preparation for water block polishing.

Attachment 1: 20190307_113548.jpg
20190307_113548.jpg
  1884   Thursday, March 07, 2019, 09:12 David WangConditioning StationStandard OperationTM2 TM2 move from TCS to SHC.

TM2 has been moved from TCS to SHC. The move is smooth.

  1883   Tuesday, March 05, 2019, 14:29 chad fisherSouth Hot-CellRepair  Tray Transfer Fixture Repair Complete

Repair of the tray transfer fixture is complete (minus testing).

A distorted ball nut lock plate was replaced and thread loc added. to the ball nut/plate assembly. Testing will take place tomorrow once the thread lock has a chance to cure.

Attachment 1: 20190305_130312.jpg
20190305_130312.jpg
Attachment 2: 20190305_132303.jpg
20190305_132303.jpg
Attachment 3: 20190305_133800.jpg
20190305_133800.jpg
Attachment 4: 20190305_141346.jpg
20190305_141346.jpg
  1882   Tuesday, March 05, 2019, 09:38 chad fisherSouth Hot-CellRepair  Transfer Fixture Repair

Transfer fixture has been remotely disassembled to the point where the ball nut lock plate assembly can be inserted into the tool port and the plate replaced by hand in the tool port without having to enter the hot cell. Straight head screws will be replaced with SHCS to facilitate easier re-assembly and future disassembly.

Attachment 1: 20190305_092228.jpg
20190305_092228.jpg
Attachment 2: 20190305_092231.jpg
20190305_092231.jpg
Attachment 3: 20190305_092326.jpg
20190305_092326.jpg
Attachment 4: 20190305_092558.jpg
20190305_092558.jpg
  1881   Tuesday, March 05, 2019, 07:20 David WangConditioning StationRepairTM2 TM2 HV test at TCS

Spark between HV cover vertical mesh plate and HS 60KV  bias connecting clamp 90degree angle at 55 KV on TM2 top. HV cover is removed to test above  55KV. The spark triggered TH and SHC ventilation secondary alarm.

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