ID |
Date |
Author |
Category |
Type |
Module |
Target/Number |
Subject |
2646
|
Tuesday, August 06, 2024, 09:16 |
Frank Song | ITE | Standard Operation | TM3 | SiC#46 | module disconnection |
TM3 with spent target SiC#46 was disconnected in ITE and ready to move to TCS soon. |
Attachment 1: TM3_with_SiC#46_disconnection_in_ITE_2024-08-0106.pdf
|
|
2649
|
Friday, August 09, 2024, 08:11 |
Frank Song | ITW | Standard Operation | TM4 | TiC#7 | module disconnection |
TM4 with spent target TiC#7 (dead) was disconnected in ITW and ready to move to TCS. |
Attachment 1: TM4_with_spent_TiC#7_disconnection_in_ITW_20240809.pdf
|
|
2671
|
Tuesday, August 27, 2024, 13:30 |
Frank Song | ITW | Maintenance | TM3 | TiC#8 | module disconnection |
TM3 is disconnected and all water lines are purged/refilled with 50psi Nitrogen. Pls see pics attached with. |
Attachment 1: TM3_with_TiC#8_disconnection_in_ITW_2024-08-27.pdf
|
|
2695
|
Tuesday, October 01, 2024, 09:16 |
Frank Song | ITE | Standard Operation | TM2 | Ta#67 | module disconnection |
TM2 with spent target Ta#67 was disconnected in ITE. see attachment pls. |
Attachment 1: TM2_with_spent_target_Ta#67_disconnection_in_ITE_2024-10-01.pdf
|
|
2710
|
Tuesday, November 05, 2024, 09:49 |
Frank Song | ITW | Standard Operation | TM4 | TiC#9 | module disconnection |
TM4 with spent target TiC#9 was disconnected in 29-10-2024 and it is being moved from ITW to SHC. |
Attachment 1: TM4_with_spent_target_TiC#9_disconnection_in_ITW_20241029.pdf
|
|
2725
|
Tuesday, December 03, 2024, 10:10 |
Frank Song | ITE | Standard Operation | TM2 | Ta#68 | module disconnection |
TM2 with spent target TA#68 was disconnected in ITE and is being moved to SHC. All water lines are purged for module storage. |
Attachment 1: TM2_with_spent_target_TA#68_disconnection_in_ITE_2024-12-03.pdf
|
|
2741
|
Monday, January 06, 2025, 08:38 |
Frank Song | ITW | Standard Operation | TM4 | UCx#46 | module disconnection |
TM4 WITH UCx#46 was disconnected in 2025-01-02 in ITW. Forms attached. |
Attachment 1: TM4_with_UCx#46_disconnection_in_ITW_2025-01-02.pdf
|
|
2747
|
Monday, January 13, 2025, 10:36 |
Frank Song | ITE | Standard Operation | TM3 | UCx#47 | module disconnection |
TM3 with spent target UCx#47 was disconnected in ITE and will be moved to SHC. |
Attachment 1: TM3_with_spent_target_UCx#47_disconnection_in_ITE_2025-01-13.pdf
|
|
638
|
Friday, April 04, 2014, 14:59 |
Keith C Ng | ITE | Maintenance | | | measurement of new beam tube section |
R. Kuramoto and A. Laxdal measured the distance from the 2A tunnel to the tank flange of ITE. The new fabricated beam pipe with bellows was used to gauge the distance to the tank flange; The flange face of the beam tube was butted up to the tank flange and the beam tube was marked at the plane of the wall. A metal rod was used to gauge the distance to the tank face using the same method.
From the inside of the tunnel wall:
- To tank flange: 45 5/16"
- To ITE vacuum tank face: 49"
See attached PDF. |
Attachment 1: wall_to_flange_length.pdf
|
|
968
|
Tuesday, June 30, 2015, 09:47 |
chad fisher | South Hot-Cell | Repair | | | manipulator repair |
The right hand manipulator has been repaired. It took 43 minutes and I received ~ 0.56 mSv |
1579
|
Monday, July 10, 2017, 09:09 |
Dan McDonald | North Hot-Cell | Repair | | | manipulator cart repair |
A hydraulic leak was found on the manipulator install and repair cart, upon further investigation the cause was a faulty cylinder. Once the cylinder was removed and disassembled the inner bore was found to be scored beyond repair. Another point of interest was that the rod was painted to the point that when retracted it compromised the rod seal causing the cylinder to leak. attached are photos outlining the issues. new cylinders are being sourced and will be installed upon arrival. We have found that there is interaction between the tops of the cylinders and the bed of the cart when fully retracted and compressed, this might require some modifications to ensure proper operation in the future.
|
Attachment 1: IMG_2955.JPG
|
|
2442
|
Friday, May 19, 2023, 09:39 |
Frank Song | South Hot-Cell | Standard Operation | TM2 | TiC#6 | leak/electrical check |
TM2 with TiC#6 was checked on SHC, see pic attached pls. |
Attachment 1: TM2_with_TiC#6_leak_and_eletrical_check.png
|
|
967
|
Monday, June 29, 2015, 10:51 |
David Wang | Conditioning Station | Repair | TM2 | | leak on TM2 side panel |
There is an air to vacuum leak on TM2 service cap side panel which we moved out during the TM2 wiring job. The CS pumps are stopped now. The CS will be vented soon. The seal on this panel has to been changed.
2016-06-30. The o-ring seal on this panel(PNG1 and steerers) is replaced and leak checked. No leak now. |
972
|
Tuesday, June 30, 2015, 15:53 |
David Wang | Conditioning Station | Development | TM2 | | leak on TM2 at CS |
I leak checked TM2 at CS this afternoon which including air to vacuum check on service cap and helium pressure test on water lines. There is a small leak on water line R ,U (COIL1) during the helium pressure test.. Below 20 psi helium, there is no leak on it. But , once the helium pressure is increased over 20 psi, it showed up on Leak Detector. At 60 psi helium, the leak rate is 9.4xE-9 atm.cc/sec. For detail information, See attachment. All other water lines and air to vacuum seals are good. |
Attachment 1: TM2_leak_check_2015-06-30.pdf
|
|
Attachment 2: leak_check_2015-06-30_007.JPG
|
|
Attachment 3: leak_check_2015-06-30_009.JPG
|
|
107
|
Friday, May 18, 2012, 08:37 |
David Wang | South Hot-Cell | Standard Operation | TM4 | sic 27 | leak check on heat shield circuit |
Chad and I leak checked the heat shield circuit after sic 27 target installed. It took 20minutes to pump down the circuit to the leak detector bottom scales. The leak detector is calibrated today,and all the vacuum lines and connections are leak checked by spraying helium. Chad sprayed helium to each vc fittings for 2 seconds. There is no any response on leak detector . The test repeated one time and the result is same. Chad flushed helium around the target for 10 second .This time leak detector also have no respone. The heat shield circuit is leak tight at this stage . We will move TM4 to conditioning station and pressure helium test the circuit. |
139
|
Wednesday, July 04, 2012, 13:18 |
David Wang | Conditioning Station | Standard Operation | TM4 | uo#3 | leak check on heat shield circuit |
Chad and I leak checked the heat shield circuit after uc#3target installed. It took 5minutes to pump down the circuit to the leak detector bottom scales. All the vacuum lines and connections are leak checked by spraying helium. Chad sprayed helium to each vcr fittings for 2 seconds. There is no any response on leak detector . The test repeated one time and the result is same. The heat shield circuit is leak tight at this stage . We will move TM4 to conditioning station and pressure helium test the circuit.
|
|
80
|
Tuesday, April 03, 2012, 12:11 |
David Wang | Conditioning Station | Development | | | leak check on conditioning station vacuum system |
I did a leak check on conditioning station vacuum system today.The vacuum system had been roughed over night . This morning before the leak check,the convectron gauge reading on emittance box is 20m torr which is reasonable. I hooked the leak detector to system (without turbo pump on) . The leak detector showed base LR 6.3xE-8 atm.cc/sec. At this base LR, I found 2 leaks up to low E -6range on that cross tube flange to small turbo pump, and the cross tube flange to vessel. I found some of the bolts on the flanges could be tightened more ½ to ¾ turn without difficulty. I checked all the fasteners on the box, cross tube, and turbo pump, tightened some of them. By doing it, the base leak rate dropped to 3.0x E-8 atm,cc/sec, base pressure still 0.0XE-4 torr. I sprayed helium again, the response I found before now disappeared. I waited for about 1hour, and let the leak detector base leak rate dropped to 1.3 xE-8 atm.cc/sec, and base pressure still at 0.0xE-4 torr. At the same time, i only use leak detector as back up pump for whole sysytem and shut off the valve to the scroll pump.By doing this , the leak detector is much stable on the base leak rate. With the help of Bevan, i sprayed the helium to all the vacuum equipments again.This time,no any tiny response has been found on leak detector.The leak rate stayed at 1.2x E-8atm.cc/sec, and no change on pressure also. I checked helium bubble several times during the spray. The conditioning station vacuum system is leak tight. |
89
|
Thursday, April 19, 2012, 09:48 |
David Wang | South Hot-Cell | Standard Operation | TM1 | LP SIS Nb 6 | leak check heat shield circuit |
Chad and I did a leak check on TM1 Nb5 target heat shield circuit. The leak detector was connected to heat shield circuit.The pumping down of the circuit is very smooth.Base leak rate is 0.0xE-9atm.cc/sec,and the base pressure is 0.0xE-4 torr. Chad checked the helium flow downstairs .He sprayed helium to both up and down VCR joints 2seconds each time. There is no any response on leak detector(30 seconds waiting time). Both joints did the same test twice, no response . Finally, he flushed helium around the target for 10 seconds,and i didnt see any response on leak detector either.The heat shield circuit on TM1 Nb5 target is leak tight at this stage. |
119
|
Wednesday, June 06, 2012, 14:33 |
David Wang | South Hot-Cell | Standard Operation | TM1 | Ta38 | leak check heat shield circuit |
Chad and I did a leak check on heat shield circuit after target is installed on TM1.The leak detector pumping down is smooth. The base leak rate is 0.0xE-9 atm.cc/sec. The base pressure is 0.0xE-4torr. Chad checked helium flow downstairs and sprayed helium to each joints for 2 seconds.The first joints is good and there is no any response on leak detector.we double checked it again and got the same result. On the second joint, Chad sprayed helium 2second. After 15 second of spraying,the leak detector got a response which climbed to 3.2xE-8 atm.cc/sec max,and back to 2.5 XE-8 atm.cc/sec. Chad tried to tighten the fitting. During his tight, the leak rate response to 7.5x E-8 atm.cc/sec momentarily. After the tightening ,the leak rate back to 0.0x E-9atm.cc/sec whic is the base.So we sprayed the helium to the joint again.This time ,there is no any response on leak detector. We checked this joint again and got the same result which is no response. Finally, Chad flush the helium around the target for 10 second ,and during 45 sec observation time there is no any response on leak detector. I would say the heat shield circuit is leak tight so far. I will do a helium pressure test on it once the TM1 is moved the CS. |
181
|
Tuesday, September 18, 2012, 13:41 |
David Wang | South Hot-Cell | Standard Operation | TM1 | Nb#7 | leak check heat shield circuit |
Chad and i did a leak check on TM1 heat shield circuit with new Nb#7 target installed. It took about 5 mins pump down the circuit to leak rate 0.0x E-9atm.cc/sec and 0.0x E-4 torr on leak detector.
All vacuum lines and joints which connected to the leak detector had been helium sprayed and they are leak tight. Chad sprayed helium on each VCR joints for 2 seconds every time. During 45sec waiting time, there is no any response on leak detector. Chad repeated same test again for double checking and we got same result. Chad finally flushed the helium around the target heat shield for 10 seconds.we waited for 45minute and found no response on the leak detector. The heat shield circuit is leak tight at this stage. I will do a helium pressure test on this circuit when TM1 is in CS and under vacuum.
|