Logbooks Lab Maintenance Evaporator_1 Evaporator_2 Laser cutter Target Production Test-Stand RH-ISAC RH-Cyclotron RH-Meson Hall RH-Beamlines RH-ARIEL
  RH-ISAC, Page 1 of 135  Not logged in ELOG logo
New entries since:Wed Dec 31 16:00:00 1969
Entry  Tuesday, January 14, 2025, 10:00, David Wang, South Hot-Cell, Standard Operation, TM3, UCx#47, after operation electrical check, Tm3 UCx 47 TM3_UCX_47_after_operation_electrical_check.pdf

TM3 UCx#47 after operation electrical check  is done at SHC. The result is normal. See attachment.

Entry  Monday, January 13, 2025, 10:36, Frank Song, ITE, Standard Operation, TM3, UCx#47, module disconnection TM3_with_spent_target_UCx#47_disconnection_in_ITE_2025-01-13.pdf

 TM3 with spent target UCx#47 was disconnected in ITE and will be moved to SHC.

Entry  Monday, January 13, 2025, 10:02, Travis Cave, Spent Target Vault, Standard Operation, , UC#46, Spent Target Move Target_Index_2025-01-13.pdf
UC#46 was placed in pail# 301 in spot 1B and was 26.3mSv/hr when removed from the SHC. See attached PDF for vault 
details.
Entry  Thursday, January 09, 2025, 11:46, David Wang, Safe Module Parking, Standard Operation, TM4, No target, SMP is under vacuum for TM4 storage during shut down.  

 SMP:MP1 is started with SMP BV1 is opened. SMP is under vacuum for TM4 storage during shut down.

Entry  Thursday, January 09, 2025, 11:08, David Wang, Facilities, Maintenance, , , ITH:MP1 is deteriorating by watching on ITH:CG1 and CG2 readings 

ITH:MP1 is deteriorating by watching on ITH:CG1 and CG2 readings and investigation in pit. A fault 17644 has been issued. this pump will be replaced in March when general fielding in vacuum pit is reasonable for the job.

Entry  Wednesday, January 08, 2025, 07:37, chad fisher, South Hot-Cell, Standard Operation, TM4, UCx#46, UCx#46 removal TM4_UCx46_07012024.jpegTM4_UCx46_2_07012024.jpeg

UCx#46 removed from TM4 and placed into a pail back-filled with argon. Nothing visually unusual; no issues.

Entry  Tuesday, January 07, 2025, 12:05, David Wang, ITE, Standard Operation, TM3, UCx #47, ITE primary and secondary vacuum vessel leak check for 2025 shut down 

ITE primary and secondary vacuum vessel leak check for 2025 shut down have been done. No leak.  The TM3 waterlines helium pressure test will be done at TCS when module is there.

Entry  Monday, January 06, 2025, 08:38, Frank Song, ITW, Standard Operation, TM4, UCx#46, module disconnection TM4_with_UCx#46_disconnection_in_ITW_2025-01-02.pdf

 TM4 WITH UCx#46 was disconnected in 2025-01-02 in ITW. Forms attached.

Entry  Friday, January 03, 2025, 12:34, Frank Song, 5 Shielding Blocks, Maintenance, , UCx#47, shielding blocks moving 

 Five shielding blocks are moved from ITE to storage area ( one of them is sitting on B2 as limit of room) for target stations maintenance in 2025 winter shut down .

Entry  Friday, January 03, 2025, 10:41, David Wang, ITW, Standard Operation, TM4, UCX46, ITW primary and secondary vacuum vessel leak check for 2025 shut down ITW_primary_and_secondary_vacuum_leak_check_2025.pdf

ITW primary and secondary vacuum vessel leak check for  2025 shut down has been done. Also,TM4 internal water line helium pressure test has been finished.  Both results are normal. There are two small old leak on EXit 1 and Exit2 module top plate  o-ring under 1Xe-8 atm.cc/sec which we knoew in past years test. resin spray on leak  area reduce the leak ratee below 5Xe-9 atm.cc/sec. No concern on these small leak.   See attachment  for detail results.

Entry  Friday, January 03, 2025, 09:59, Adam Newsome, Facilities, Standard Operation, , , Safety Walkaround complete - ISAC Hot Cells, Target Hall 

A safety walkaround was completed for the ISAC Hot Cells and Target Hall Areas.

The resulting spreadsheet can be found on DocuShare as Document-242733.

Main deficiencies identified:

  • Hot Cells:
    • NHC right manipulator gripper stuck (known, repair planned)
  • Target Hall:
    • 50% of overhead light bulbs burnt out (David Wang contacted Electrical Services to rectify)
    • One RH camera for target pit not working (Travis Cave notified)

Action has been taken on all deficiencies.

Entry  Wednesday, December 18, 2024, 14:17, Adam Newsome, Pail Handling Tool, Maintenance, , , Pail Handling Tool - Inspection ISAC_Pail_Handling_Tool_Inspection_Record_-_2024.pdf

An informal inspection of the main Pail Handling Tool was performed today as the final one for the year. Note that the main formal annual inspection was performed June 18, 2024 for this year.

The attachment to this e-log serves as a record of all inspections for this tool throughout 2024.

The spare tool was not inspected as it was not in service this year.

Entry  Wednesday, December 18, 2024, 12:18, Adam Newsome, Spent Target Vault, Standard Operation, , , Five Pails Transferred from Main Vault to Mini Vault MiniVault_2024-12-18.pdf

Five pails were transferred from main vault to mini vault. Note that there was already one pail in the mini vault, so at present there are six pails staged for packaging into F-308s.

Nb#10, Pail 295, Tray 4A
C#4, Pail 277, Tray 4C
Ta#64, Pail 273, Tray 5C
Ta#62 with wire scanner, Pail 256, Tray 7A
TiC#5, Pail 279, Tray 3A

The target index has been updated accordingly (see attached but note that the summary does not reflect the sixth pail).

Entry  Monday, December 09, 2024, 13:10, Frank Song, 5 Shielding Blocks, Standard Operation, TM3, UCx#47, shielding blocks transfer 

 5 Shielding Blocks have been transferred from ITW to ITE. MAA is secured after moving.

Entry  Thursday, December 05, 2024, 12:00, Adam Newsome, Spent Target Vault, Standard Operation, , Ta#68, Spent target move - Ta#68 in Pail 300 Storage_Vault_Contents_2024-12-05.pdf

Ta#68 spent target was moved in Pail 300 to storage vault location 5A. The dose rate measured at the South Hot Cell was 429 mSv/h at 1m. The target index spreadsheet has been updated and the current vault configuration is attached to this e-log. At this time, the storage vault is getting quite full - it is planned to remove five pails in January 2025.

Entry  Thursday, December 05, 2024, 11:43, Aaron Tam, South Hot-Cell, Standard Operation, , Ta#68, Pail loading - Ta#68 & Others into Pail#300 Pail_Landing.jpgLoaded_Pail.jpgParasitic_Lid_that_was_missed.jpgLocation_of_all_parasitic_type_targets_and_fasteners.jpgParastics_and_Target_stuff_that_went_inside_this_pail.jpg

December 5, 2024 - Aaron Tam w/ help from Chad, Peter and Adam at the Crane  

Hot Cell Prep:

  • Tools organized, working space cleared, spot for clean tool to sit placed, Air tool is open and spinning clockwise for tightening 

Loading:

  • Ta#68 was loaded into pail# 300
  • PEEK seal parasitic assemblies loaded (PEEK seals were removed in ID: 2724)
  • Farran had some old samples that also went in (More details to come when Farran sends the info)

Lid/latching:

  • This went smoothly

Bail attachment:

  • Some difficulty in attaching the Lifting Bail, but went on smoothly with the help of Chad

Notes:

  • One of the PEEK seal parasitic Target assembly lids was missed in the loading. This will have to be loaded next time. 
  • All parasitic type targets remain in the yellow container shown in photos below. 
Entry  Wednesday, December 04, 2024, 14:30, Aaron Tam, South Hot-Cell, Standard Operation, , Ta#68, Ta#68 PIE 32x

 Abstract:
This target has seen some irregular beam patterns 
Possibility that the beam hit the walls of the target tube or even the cooling fins
This PIE we want to investigate how the irregular beam physically affected the target 

Related ELOGS: 
ID: 2728
ID: 2698

PIE was performed by Aaron Tam, Directed by Aurelia Laxdal, Observed by Lucas Backes, Special help from Chad Fisher 

External views:

  • Windows are clear of any irregularities 
  • More pictures of this can be found in RH-ISAC E-log 2728

Internal Views:

  • Heatshield internal
    • Some discolouration from heat and soot deposits.
    • This seems to be fairly clean to normal amounts - not concerning 
  • Target tube
    • tube is bent with the middle higher than the sides
    • Target tube was not removed 9/64ths allen wrench could not be located for this operation 
  • Target tube Exit
    • Heatshield windows were punctured to reveal the target tube entraces/exits
    • Entrance is waterline side (ITE)
  • Extraction electrode parts were removed from the back off the target
    • These parts look normal
    • some of the extraction electrode would not pull out due to tight fitting parts and the investigation stopped here.

Conclusion: Target physical condition is normal as far as we could investigate 

Entry  Wednesday, December 04, 2024, 10:40, Adam Newsome, South Hot-Cell, Standard Operation, TM2, , TM2 move - SHC to silo 

TM2 was remotely moved from the South Hot Cell to SW Silo. Reading at SHC = 89.8 mSv/h. The move was smooth.

Entry  Wednesday, December 04, 2024, 09:00, David Wang, Facilities, Standard Operation, TM2, , all water lines on TM2 have been purged. 

all water lines on TM2 have been purged. Refilled them(except HS ) with 60psi nitrogen for module silo storage before next year using. 

Entry  Wednesday, December 04, 2024, 08:05, Frank Song, ITE, Standard Operation, TM3, UCx#47, Module Connection TM3_with_new_target_UCx#47_connection_in_ITE_2024-12-03.pdf

TM3 with new target UCx#47 was connected in ITE right after be moved from TCS. 

Entry  Tuesday, December 03, 2024, 15:53, Aaron Tam, South Hot-Cell, Standard Operation, TM2, Ta#68, Ta#68 Removal 22x

  Note: Ta#68 had a difficult install. See E-log ID# 2698 for more info 

First look:

  • Containment box cover looks the same as previous (See:ID: 2697)
  • Target shows large amount of soot-like deposits (See photos for locations)
  • Deposits seem to have been left on parts of the service tray as well ie.: Multipin connector 

Removal:

  • Removal was smooth
  • Water-line bracket fixing bolts seemed loose even before I put a tool to them 

Eyes of sides:

  • Better photos of where deposits are 
  • Everything else seems normal 
Entry  Tuesday, December 03, 2024, 12:28, Adam Newsome, South Hot-Cell, Standard Operation, TM2, , TM3 move - TCS to ITE 

TM3 was moved with UCx#47 from TCS to ITE. The move was smooth.

Entry  Tuesday, December 03, 2024, 10:51, Adam Newsome, South Hot-Cell, Standard Operation, TM2, , TM2 move - ITE to SHC 

TM2 was moved from ITE to SHC with Ta#68 target. During the move, a railing was lightly bumped by the corner of the module - no obvious damage or issues have been observed. Otherwise, the move was smooth.

Entry  Tuesday, December 03, 2024, 10:10, Frank Song, ITE, Standard Operation, TM2, Ta#68, module disconnection TM2_with_spent_target_TA#68_disconnection_in_ITE_2024-12-03.pdf

TM2 with spent target TA#68 was disconnected  in ITE and is being moved to SHC. All water lines are purged for module storage.

Entry  Thursday, November 28, 2024, 16:13, Aaron Tam, South Hot-Cell, Standard Operation, , TiC#9 Parasitics, TiC#9 Parasitics Leak Check and removal from hotcell Leak_Test.jpgDissassembly.jpgSeal_Seat.jpgPEEK_seal.jpgPEEK_Seal_Closer_look.jpg

 November 27th, 2024 - Aaron Tam with Farran & David 

Parasitic Assembly Leak Check (Aaron, Farran, David)

-Note that the furthest upstream (right of the target) parasitic top cap screws had been loosened and retightened in error when attempting to remove it off TiC#9

-This puts this data point into question 

-Leak check starting from upstream to down stream 

-First parasitic had no leak 

-Second parasitic had some leak 

-Third parasitic was not pumping down at all

-First parasitic checked on test hose again with same success

Parasitic Dis-assembly (Aaron) 

-First parasitic had good tension in all 3 screws

-second parasitic had 2 screws with a perceptible breaking-loose of the screws, but one was imperceptible 

-Third parasitic had lower (than first parasitic), but okay tension in all 3 screws 

In an attempt to move the PEEK seal into a safe spot with tweezers, this one was accidentally sprung across the hotcell in the direction of the tool port 

A lengthy attempt to find it was conducted, but no PEEK seal was recovered 

This may effect our ability to do work during hot cell entries coming up. 

PEEK Seal extraction (Aaron, Farran) 

-A labeled bag was inserted into the hotcell via the tool port and onto an existing tray in the Hotcell

-PEEK seal placed inside bag, placed back on tray, and moved back to the tool port for extraction

-With tool port open, the draft was able to push the bag across the lift table. Changing the cross section exposed to the draft works to keep the bag from moving

-Farran used picker to extract the bag into the tool port where he wiped and placed into separate bag.

-This process was repeated for the second PEEK seal 

-Bags were wiped and swiped, put in another bag, swiped and brought over to Hot cell Service area Lab 

 

 

 

Entry  Tuesday, November 26, 2024, 14:52, Aaron Tam, South Hot-Cell, Standard Operation, TM3, UCx#47 , UC#47 LP-SIS w/ gas Install 6x

 November 26, 2024 - Aaron Tam 

Handover from TPO and inspection

  • Completed
  • Some modification to the center Inner-Outer conductor had to be made (hole enlarged as tab was slightly short)

Target Insertion:

  • Successful 

Target Mounting:

  • Upon fully seating UC#47 on service tray locating pins, the gas line VCR gasket came off 
    • Operator doesn't have line-of-sight to this area, so there has to be healthy clearance (Foreshadowing) 
    • Gas line VCR gasket reinstalled using manipulators  
  • 2nd seating of UC#47 on service tray locating pins, the gas line VCR gasket came off again
    • Some alignment interference with the gas line coupling is the cause of the gasket falling off during placement (photo attached)
    • Gas line on service tray was loosened, raised to highest position and fastened (Photo attached)
    • Failed to re-install VCR gasket (Plastic separated from gasket material)
  • Target removed from Hot cell to reinstall gaskets and make modifications to the gas-line coupling
    • Gas line coil plastically deformed to give less of a spring action so the coupling can stay down under friction until it is time to couple
    • Target carefully inserted into hot cell without disturbing spring/friction of gas-line coupling. 
      • This had to be repeated several times. Once for the waterline gaskets coming off, and a few other times to insert the target/tray without disturbing sprung coupling
  • Target mounted without issue after the above steps successfully 

Gas and Water Services:

  • VCR connections coupled 
  • Leak test passed
    • leak test faster today because module had been left in silo for a long time to dry out. 
  • Gas line no-longer needed, so was not checked

Electrical Services:

  • Conductor bolts installed
  • All bolts (including mounting bolts) checked for fit with mirror
  • Coil conductor bolts torqued to at least 130inch-lbs 
  • Electrical test completed 

Containment box panel reinstalled 

Cleared area around module for craning out. 

 

Entry  Tuesday, November 26, 2024, 13:54, Adam Newsome, Conditioning Station, Standard Operation, TM3, , TM3 move - SHC to TCS 

TM3 was moved from SHC to TCS with UCx#47. The move was smooth.

Entry  Tuesday, November 26, 2024, 13:03, Frank Song, South Hot-Cell, Standard Operation, TM3, UCx#47, electrical check/leak check TM3_with_new_target_UCx#47_electrical_check_on_SHC_2024-11-26.pdf

An electrical check and leak check had been done after new target UCx47 was installed on TM3 in SHC. see attachment pls.

Entry  Monday, November 25, 2024, 09:56, Adam Newsome, South Hot-Cell, Standard Operation, TM3, , TM3 move - silo to SHC 

TM3 was moved from silo to SHC with no target. Move successful.

Entry  Thursday, November 21, 2024, 14:11, Frank Song, 5 Shielding Blocks, Standard Operation, TM4, UCx#46, shielding blocks transfer 

 Shielding blocks have been moved from ITE to ITW and MAA is secured.

Entry  Monday, November 18, 2024, 12:18, Aaron Tam, South Hot-Cell, Repair, , , SHC West Manipulator Repair  

 November 14, 2024 - Aaron Tam w/ Chad Fisher 

Following ID: 2716   
"Nov. 8, 2024 - Aaron Tam 
Tong cable snapped when attempting to remove multipin connector bracket"

Repair went as follows:

  • weighted clip attached to tong return side to tension/keep tapes on pulleys
  • Manipulator was pinned from both sides (Pinning from master side first makes it easier to position slave side)
  • clamps were used to suspend all tapes and cables near the relay bracket 
  • extension tube limit clamps were moved to the top to stop it from dropping when Z motion tapes disconnected
  • Z motion tapes/tension adjusting screws taken off master carriage and suspended with equalizing weight ~10+ lbs)
  • Extension tube limit clamps and extension tube lowered give space to expose multiplier later 
  • Wrist joint and handle removed as a unit 
  • extension tube to multiplier screws taken out
  • Extension tube raised to expose multiplier - using extension tube to wrist joint positioning clamp to keep it in place 
  • Old cable removed
  • new cable installed

installation in reverse with spare master handle 

Notes:

Spare master wrist joint was missing gears that connect wrist drums 

  • this had to be disassembled and installed with gears from old wrist joint

Handle ratcheting pawl spring was not oriented properly, so this had to be disassembled and reinstalled properly (in the process one spring was lost Part#: A-5800)
 

 

 

 

Entry  Tuesday, November 12, 2024, 12:30, Frank Song, ITW, Standard Operation, TM4, UCx#46, Module Connection TM4_with_new_target_UCx#46_connection_in_ITW_2024-11-12.pdf

 TM4 with new target UCx#46 was moved from TCS to ITW and has been re-connected right after. see attachment pls.

Entry  Friday, November 08, 2024, 10:54, Aaron Tam, South Hot-Cell, Standard Operation, , TiC#9, TiC#9 Pail Loading into Pail#299 

 Nov. 8, 2024 - Aaron Tam 

Tong cable snapped when attempting to remove multipin connector bracket 

Assistance from Chad required for the rest of procedure 

Tic#9 was loaded into Pail#299 

  • Along with fixing and conductor bolts (no other material was loaded)

 

Entry  Friday, November 08, 2024, 10:44, Aaron Tam, South Hot-Cell, Standard Operation, TM4, UCx#46, UCx#46 Install and Parasitic Target Status  Left_side_Array_Parasitic_with_floppy_spacer.jfifRight_side_Window_Parasitic.jfifLid_Parasitics_order.jfif

November 6, 2024 - Aaron Tam 

UCx#46 Target handover from TPO 

Target insertion: successful 

Parasitic Install: All Parasitic targets left off target

  • Left side In-beam array type parasitic install attempt #1 
    • Parasitic assembly is too thin/studs too tall for the socket nut to fasten onto target. Stud protrudes through the length of socket section, not allowing tool to insert 
    • previously a 3/4 spacer was used to give space for thermal couple to enter 
    • Install of 3/4 spacer was difficult because it does not hold its shape when handled (pivots around 1/2 ad 1/4 portions) 
    • With spacer installed, parasitic assembly is too thick for socket nuts to fasten onto studs. 
      • It may have been possible to back out studs to use, but left off in the interest of time UCx is exposed. 
  • Right side In-beam window type parasitic install
    • Similarly to Left side, studs were too short for install, studs could be backed out, but was left off in the interest of time UCx exposed
  • PEEK seal parasitic targets were left off as per schedule, and will be leak checked at another date (after tong cable has been repaired) 
    • Order of PEEK seal locations preserved and follows order as seen with target installed (Photo attached)

Target install: successful 

Leak Check: Successful 

Electrical Check: Successful 

  • Initially failed due to wiring diagram being different between production wiring diagram and electrical test sheet

Containment box panel closed 

 

 

Entry  Friday, November 08, 2024, 10:39, Travis Cave, Spent Target Vault, Standard Operation, , TiC#9, Spent Target Move Target_Index_2024-11-08.pdf

 TiC#9 was placed in Pail 299 in spot 8A of the vault and was 92.1mSv/hr when removed from the south hot cell. See attached pdf for full vault details.

Entry  Wednesday, November 06, 2024, 16:33, David Wang, South Hot-Cell, Standard Operation, TM4, UCX46, TM4 with UCx46 electrical and leak check at SHC TM4_UCx46_electrical_check.pdf

TM4 with UCx46 electrical and leak check at SHC is done. Everything is good.

Entry  Wednesday, November 06, 2024, 08:29, Aaron Tam, South Hot-Cell, Standard Operation, TM4, TiC#9, Target and Parasitic assemblies removal from TiC#9 17x

November 5, 2024 - Aaron Tam

TiC#9 HP-SIS removed from TM4

  • Top left fixing bolt shows signs of heating on it (Comparison photos attached Bolt_profile.jfif  & Bolt_Tops.jfif)
  • Location and orientation of darker bolt (Darker_bolt.jfif)

Parasitic Targets Removed

  • Left target has residue left from ablation 

See photos attached for detail 

Entry  Tuesday, November 05, 2024, 11:04, Frank Song, South Hot-Cell, Standard Operation, , TiC#9 , electrical check with the spent target Electric_Check_of_TM4_with_spent_TiC#9.pdf

 David made electrical check right after TM4 is moved from ITW to SHC. see attachment pls.

Entry  Tuesday, November 05, 2024, 09:49, Frank Song, ITW, Standard Operation, TM4, TiC#9 , module disconnection TM4_with_spent_target_TiC#9_disconnection_in_ITW_20241029.pdf

 TM4 with spent target TiC#9 was disconnected in 29-10-2024 and it is being moved from ITW to SHC.

Entry  Thursday, October 24, 2024, 10:42, Travis Cave, Spent Target Vault, Standard Operation, , SiC#44, Target repacked moved to the mini vault. Mini_Vault_Index_2024-10-24.pdf

 On October 22 2024 the spent SIC#44 returned from CNL was repacked in a new pail it was in pail 275 and repacked into pail 298 it was 2.34mSv/hr when removed from the south hot cell.

It was placed in the very back of the mini vault. 

Entry  Thursday, October 24, 2024, 10:37, David Wang, Conditioning Station, Standard Operation, , , TCS water system functionnal test.  

TCS water system has been started for functional test. System parameters including  pressure, all temperature sensors, flow rate sensors, resistivity are ok. I will watch on chiller CP1/2/3 in rest of the week and make sure chiller CP1/2/ 3 auto stage in/out work fine.

Entry  Tuesday, October 15, 2024, 13:44, Travis Cave, Spent Target Vault, Standard Operation, , TiC#8 and Ta#67, Spent Target Move Target_Index_2024-10-15.pdf

 On Friday October 11th TiC#8 and Ta#67 were place in the spent target vault in Tray 8. See attached PDF for details. 

Entry  Tuesday, October 15, 2024, 12:57, Frank Song, ITW/ITE, Standard Operation, , , shielding blocks transfer 

 5 shielding blocks are transferred from ITW to ITE, Target Area is secured again after moving.

Entry  Friday, October 11, 2024, 15:59, Aaron Tam, Facilities, Repair, , , ISAC B2 North Hot Cell Phone Fixed 

 Resolution comment / Commentaire de résolution:

     Fixed issue by changing patch cord that was connected to the switch from patch panel.

Emile V

Entry  Thursday, October 10, 2024, 12:20, Adam Newsome, Facilities, Standard Operation, , , Safety Walkaround complete - ISAC Hot Cells, Target Hall 

A safety walkaround was completed for the ISAC Hot Cells and Target Hall Areas.

The resulting spreadsheet can be found on DocuShare as Document-242733.

Main deficiencies identified:

  • Hot Cells:
    • Phone not working at North hot cell operator station
  • Target Hall:
    • Uncertain if NHC and SHC ventilation pressure gauges have recently been inspected

Action has been taken on all deficiencies.

Entry  Thursday, October 10, 2024, 10:54, Aaron Tam, South Hot-Cell, Standard Operation, , TiC#9, TiC#9 PIE  32x

 Post Irradiation Examination

October 9, 2024 - Aaron Tam 

Goal: Training (First PIE by Aaron), Characterize any anomalies 

Notes:

  • Overall the target looks exceedingly clean with only some discolouration on the copper behind the target tube, and multipin cable insulation. 
Target loosely reassembled
Awaiting pail loading, and move to vault 
Entry  Thursday, October 10, 2024, 10:24, Aaron Tam, South Hot-Cell, Standard Operation, TM2, Ta#67, Ta#67 PIE  35x

 Post Irradiation Examination

October 9, 2024 - Aaron Tam w/ Chad Fisher, Aurelia Laxdal, and Lucas Backes 

PIE conducted by Chad with direction from Aurelia. Aaron and Lucas observing/documenting 

Goal: Thin foil target material is somewhat novel, and we should characterize the differences if there are any. 

Photos of the pre-examined target can be seen on ELOG 2697  on Tuesday October 1, 2024, when the target was removed from TM2

Notes:

  • Right most inner/outer target conductor bolts was sitting proud and had threads showing, photo attached
  • Some Black deposit was found on the inside of the heatshield directly below the extraction tube, and loose in powder form inside the heatshield. 
  • Target tube seems to have more of a crystalline texture than previous examinations.
  • When Target tube was being removed, one of the target electrode conductors broke off
  • some dimple texture was found on the target tube windows and this was further explored by prying a channel through the length of one side of the tube to get a better look

Target pieces were placed loosely back within the heatshield, and the lid loosely placed back on.

Awaiting pail loading, and move to storage vault

 

Entry  Wednesday, October 09, 2024, 14:04, Frank Song, ITE, Standard Operation, TM2, Ta#68, Module Connection TM2_with_new_target_Ta#68_connection_in_ITE.pdf

 TM2 with new target Ta#68 installed is connected in ITE. Pls see form attached.

Entry  Tuesday, October 08, 2024, 11:46, David Wang, ITE, Standard Operation, TM2, Ta#68., Tm2 has been moved form SHC to ITE. 

Tm2 has been moved form SHC to ITE. The move is smooth.

Entry  Tuesday, October 08, 2024, 11:45, David Wang, South Hot-Cell, Standard Operation, TM2, , Tm2 electrical check with Ta#68 installed at SHC.  TM2_Ta#68_electrical_check.pdf

ABCD was dead shorted to 60kv bias during the first time measurement after target installation. Target was removed and reinstalled again with new VCR seals by Ferran.  during target removal process, short disappeared when Aaron remove bolts on CD tube heaters terminal.  leak check and electrical check result are good after second time target installation. 

Entry  Tuesday, October 08, 2024, 11:20, Aaron Tam, South Hot-Cell, Standard Operation, TM2, Ta#68, Ta#68 install onto TM2, w/ Troubleshooting  17x

October 7, 2024 - Aaron Tam 

Ta#68 HP-SIS checks performed at B1 lab, moved to anteroom, and inserted into SHC via tool port w/ Aaron Schmidt. 

Ta#68 fixed to source tray with 4 mounting bolts in order of: Right manip. holding, Top left, Right manip. removed, Bottom right, Top right, bottom left. w/ Aaron Schmidt and Brady Borrmann

  • Motion was smooth, no resistance when positioning onto pins

VCR fittings done up with ample force, leak check passed

Conductor bolts installed in order of: 2 Target electrode conductors (Checked washers), 3 target Inner and outer conductors.

All bolts checked for full contact with mirror and binos. 

Electrical check failed: Dead short (look for David's ELOG for more detail when available) 

Troubleshooting while David is checking resistance: w/ Ferran

  • Intermittent success with heavy manipulation of water lines
    • Loosening off Waterline bracket-to-source-tray 
    • Loosening off Bracket to water line bolts 5/32 hex's 
    • Rotating bracket towards operator (effectively raising waterlines in the back upwards) seems to yield more intermittent success, but never passing megger @ 250V 
    • Tube was inadvertently dented when handling the tube in a wrenching motion with manip tong. counterclockwise
  • Target removed while David is still on the multimeter (calling for any sign of success)
    • Starting to remove Target in order of: Tightening back waterline-to-bracket 5/32 hex screws, loosening off waterline bracket, loosening off VCR nuts, 2 Target electrode conductor bolts, 3 Target inner and outer conductor bolts, Fixing bolts Top left (dropped below source tray), Bottom right...
      • (At this time David called with some success with electrical check)
    • Reversing course to verify fault has passed, target was reassembled, only finger loose on the VCR nuts.
    • Faults no longer present
    • Target removed
      •  As target was being pulled off source tray locating pins, a piece of ceramic fell onto the source tray just behind window waterlines.

Target taken out of Hotcell by Ferran. New VCR gaskets installed. Target reinserted 

Target installed no issues. Used fixing bolt used to replace dropped one. 

Leak check passed, Electrical check passed

  • Notably don't have a photo of reinstalled target or source tray before 2nd install attempt. 

Containment cover reinstalled 

Ceramic piece moved into Pail #285 (suspect this is a very hot piece)

TM2 ready for move to ITE

Entry  Tuesday, October 01, 2024, 12:40, Aaron Tam, South Hot-Cell, Standard Operation, TM2, Ta#67, Target Ta#67 Removed from TM2  9x

 October 1, 2024 - Aaron Tam 

Ta#67 LP-SIS removed from TM2

Ta#67 is sitting in SHC awaiting PIE 

TM2 Containment Box Cover has not been reinstalled 

Photos of target removal and module attached 

Entry  Tuesday, October 01, 2024, 10:55, David Wang, South Hot-Cell, Standard Operation, TM2, , TM2 has been moved from ITE to SHC. 

TM2 has been moved from ITE to SHC. Peter did the move with Travis on help.  The move is smooth.

Entry  Tuesday, October 01, 2024, 09:16, Frank Song, ITE, Standard Operation, TM2, Ta#67, module disconnection TM2_with_spent_target_Ta#67_disconnection_in_ITE_2024-10-01.pdf

 TM2 with spent target Ta#67 was disconnected in ITE. see attachment pls.

Entry  Friday, September 27, 2024, 07:29, David Wang, Conditioning Station, Repair, , , TCS water system resistivity analyzer has been repaired. 

TCS water system resistivity analyzer has been repaired. Two diodes and one capacitor on PS board were broken. They were replaced. Installed analyzer back and tested it in system. it works fine. Operator closed e-fault, removed force on TS5, and enabled alarm on TS5 and TC1.

Entry  Wednesday, September 25, 2024, 09:12, David Wang, South Hot-Cell, Maintenance, TM3, , Tm3 has been moved from SHC to silo. 

Tm3 has been moved  from SHC to silo. the move is smooth.

Entry  Wednesday, September 25, 2024, 07:25, David Wang, Cooling, Maintenance, , , HALCW O2 level sensor maintenance.  

HALCW O2 level sensor annual maintenance is done. sensor membrane has been changed and electrolyte has been refilled. gauge is calibrated. It works normal after the job.

Entry  Tuesday, September 24, 2024, 09:37, Frank Song, ITE/ITW, Standard Operation, , , shielding blocks transfer 

 5 shielding blocks have been moved from ITE to ITW.

Entry  Monday, September 23, 2024, 16:06, Aaron Tam, South Hot-Cell, Repair, TM3, , Insulator Addition to Water block c02c089c-d2f0-4ddb-9f06-3dd8b8d05afa.jfif0fd6eb03-7d82-48af-8ef7-99fd481bf1aa.jfif14247104-53dc-4b00-852d-3a860c4baeb8.jfif

 September 23, 2024 - C. Fisher 

  • Containment box removed
  • Insulator installed
  • New window line VCR seals installed
  • Dropped bolt from TiC#8 removed
  • Containment box reinstalled

September 23, 2024 - A. Tam

  • Containment box cover reinstalled 

Photos attached 

Entry  Monday, September 23, 2024, 11:35, David Wang, ITW, Standard Operation, TM4, TiC #9., vacuum leak check on TM4 service cap in ITW.  

vacuum leak check on TM4 service cap in ITW was done this morning.   leak detector leak rate 0.0XE-9 atm.cc/sec. No leak on TM4 service cap module top.

Entry  Monday, September 23, 2024, 11:31, David Wang, South Hot-Cell, Development, TM3, , 10 pins lectrical check result after insulator is installed on water cap C.  

10 pins lectrical check result after insulator is installed on water cap C.

pin 14 to 60kv bias has 20 Kohm @250V Megga check. The rest check on ohmmeter and megga @250 are either OLor over 25Mohm which are good.

Entry  Monday, September 23, 2024, 11:26, David Wang, South Hot-Cell, Standard Operation, TM3, , TM3 window line has been leak checked.  

TM3 window line has been leak checked after containment box removal and installation for insulator installation on water cup C.   No leak.

Entry  Wednesday, September 18, 2024, 13:47, David Wang, South Hot-Cell, Standard Operation, TM3, TiC#8, Tm3 has been moved from silo to SHC. 

Tm3 has been moved  from silo to SHC. The move is smooth.

Entry  Wednesday, September 18, 2024, 13:40, Aaron Tam, South Hot-Cell, Standard Operation, TM3, TiC#8, Target removal  13x

 TiC#8 HP FEBIAD removed from TM3

Target sitting in SHC

1 Coil Conductor bolt fell under source tray 

Photo Dump uploaded

Entry  Tuesday, September 17, 2024, 13:42, Frank Song, ITW, Standard Operation, TM4, TiC#9 , Module Connection TM4_with_TiC#9_connection_in_ITW_2024-09-17.pdf

 TM4 with target TiC#9 is connected in ITW. See attachment.

Entry  Tuesday, September 17, 2024, 11:16, David Wang, ITW, Standard Operation, TM4, TiC#9, TM4 has been moved from TCS to ITW. 

TM4 has been moved from TCS to ITW. The move is smooth.

Entry  Monday, September 16, 2024, 08:48, chad fisher, Manipulator Maintenance, Maintenance, , , CRL Technicain Manipulator Maitenance Trip Triumf_Document_2024-09-20_102936.pdf

Over the course of September 9th - September 13, 2024 a CRL manipulator technician carried out the following manipulator maintenance:

NHC operator side arm #9763 (right side installed position) - Inspection and re-tensioning of tong cable prior to re-installation (was a little too tight). Operational.

E-HD clean spare #8015 - repaired stuck manual 'Z' motion - removed one rouge 5-40 screw that had been dropped inside remote end during 'Z' motion cable run through in 2017, found that related 5-40 screws from the cable end clamp were not tight and therefore proud and also jamming. Complete tape replacement and tensioning. This manipulator is fully back to operational status other then needing some screw for the air restriction on the remote end.

E-HD "dirty" spare #7985 - inspection and evaluation of parts on the operator side require to return to operational status. Wrist and handle reassembled (all parts of wrist and handle accounted for) Ball and socket joint at and of motion lock replaced (parts were on hand already) as well as tape motion lock assembly (parts on hand already). This arm may be missing a relay or two. Remote side still bagged with unrecorded issue (suspect it is only a broken tong cable) this will be put in the maintenance schedule for earl 2025.

NHC operator side "spare" arm #9351 - Damaged 'Z' motion tape replaced. Tensioning. Operational once 'Y' motion linear actuator re-installed.

Meson hall warm cell manipulators evaluated/inspected - No issue found

Entry  Monday, September 16, 2024, 08:23, chad fisher, North Hot-Cell, Repair, , , Model N Remote end #9352 reapir 

On Friday, September 6, 2024 Model 'N' remote arm #9352 was removed from the NHC right side installed position to investigate  an ongoing issue with the tong motion circuit (no motion on the remote side when handle on operator side operated).

Inspection revealed that the tong cable on this arm have hopped its cable drum and rapped around the shaft of the cable drum. As well, the tong cable had hopped a lower pulley and was jammed between the pulley and casting of the pulley housing. These issues were corrected and arm#9352 was reinstalled onto the right hand position. This repair resolved an ongoing tong motion system stemming from November 2023 described below.

initial tong motion problem from November 2023 when the tong system jammed, operator side arm #9763, remote arm #9342.

Remote arm #9342 was removed and replaced with arm #9352 as it was suspected there was a hopped cable on #9342. Upon removal it was confirmed the tong cable on remote arm #9342 had indeed hopped the pulley. After installation of the "spare" remote arm #9352 that hAd not been installed since previous servicing and should have been completely operational, it was found the tong system still did not work properly.

Upon thorough inspection of operator arm # 9763 it was found that the tong cable was prematurely reaching the end of its travel on its drum causing the inability to activate the circuit. The tong cable was reset on its drum as per manufacture's specs with one full cable rap on the drum and one full pretension wrap of the tong drum spring.

Although this resolved part of the problem and allowed a full squeeze of the operator handle it did not result in transfer of motion through the system to the remote end.

Further investigation continued, separating the operator side arm from the seal tube and testing the seal tube and operator side arm independently. Both systems worked fine independently, pointing to a potential problem between the seal tube and spring loaded coupler on the remote arm.

Remote arm #9352 was removed and couplers visually inspected and end of seal tube on the hot side was inspected and found that the pin in the end of the shaft on the tong circuit was not installed symmetrically which could cause uneven pressure on the spring loaded coupler of the remote arm. This pin was adjusted and all pins on the hot side of the seal tube were dimpled and loctite applied as a precautionary measure.

This still did not remedy the tong motion problem. These led to the September 6, 2024 removal and repair of remote arm #9352. This arm had previously been serviced by a CRL technician in December of 2017 and had not been installed or used since and should have been in operational status. It is still not clear why it was not.

 

 

Entry  Thursday, September 12, 2024, 14:12, Adam Newsome, Waste Package/Ship, Development, , SiC#44, Failed waste emplacement at CNL: Flask #22, Pail 275 (SiC#44) Report_on_Inspection_of_Pail_275_on_2024-10-03.pdf

On 2024-09-12, CNL reported difficulty with lowering Pail 275 from F-308 flask #22 into their tile hole. The four other pails associated with this shipment were successfully emplaced. It is suspected that the issue was related to a kink in the lowering cable, causing a jam during lowering. This was observed approximately 1 year ago.

Discussions with CNL to learn more about the root case are ongoing, and this e-log will be updated when more information is learned. It is expected that this flask will be shipped back to TRIUMF and the pail will need to be repacked.

 

Update 2024-09-12: email from A. Swan at CNL: "4 of the 5 flask were emplaced successfully with F308 #22 SiC#44 having an unsuccessful pull test and left within the flask."
This is the extent of the information they have provided and is not sufficiently helpful to determine what the issue is.

 

Updated 2024-10-03: an investigation was performed (work permit C2024-09-26-10). It was determined that the root cause of the issue is attributed to an assembly error - the cable was incorrectly routed through the holder part. See attached report for full details.

 

Entry  Wednesday, September 11, 2024, 13:38, Adam Newsome, North Hot-Cell, Repair, , , Spare Manipulator - Y-axis motion not functioning 

Update 2024-09-12: C. Fisher confirms this is actually normal behaviour. The Y-axis motion is inhibited when X and Z are in a certain configuration, which was true when the manipulator was mounted on the wall in storage position. Non-issue. A note about this has been made in the operator manual.

 

It was observed today that for the spare manipulator (Model N, Serial 9351), the Y-axis motion was not functioning. X motion and Z motion are functioning as expected. Note that the Y-axis linear actuator was recently replaced and successfully tested and has not been used since the replacement (see e-log 2422).

The following information was determined from troubleshooting:

  • X motion functioning correctly
  • Z motion functioning correctly
  • Y motion selection functioning correctly - the indicator light on the operator control box lights up to confirm Y is selected, and the relay on the main control board which selects the Y axis toggles, as expected
  • Y motion motor contactors do not function as expected when toggling in either direction. Note that these contactors are shared in common with the other two motion axes, so they are functioning correctly and presumably the motor controller itself is as well, since the other axes work.
  • Most likely, because of the above reasons, there is an issue with the inhibit signal that is specific to the Y axis. The inhibit signal which runs from the main control board to the motor control board is shared in common with all motion axes (same for the two direction select signals). It is suspected (not yet confirmed), that the microcontroller is not outputting the inhibit signal as it should be. This is not due to a limit switch related issue because the Y axis does not have limits. Troubleshooting this has been difficult because the schematics do not show the full extent of the circuitry.

Further troubleshooting steps:

  1. Check inhibit signal functionality - is it working for Y axis?
  2. Check direction control signal functionality - are they working for Y axis?
  3. Swap motor select wires to "trick" the microcontroller into thinking it is running a different motor, to further isolate the issue.
  4. If required, swap the entire main control board with another manipulator's, to see if the issue is related to the circuitry which is not described in the schematics.

At the time, this issue is not deemed critical because this is a spare unit.

 

Entry  Wednesday, September 11, 2024, 07:59, David Wang, Conditioning Station, Standard Operation, TM4, TiC#9, TM4 has been moved from SHC to TCS. 

TM4 has been moved from SHC to TCS. The move is smooth.

Entry  Tuesday, September 10, 2024, 12:41, Frank Song, South Hot-Cell, Standard Operation, TM4, TiC#9 , electrical check/leak check TM4_with_TiC#9_Surface_electric(leak)_cheak_on_SHC_2024-09-10.pdf

 TM4 with new target TiC#9 Surface installed in SHC was leak/electric checked before moving to TCS. See attached pic pls.

Entry  Tuesday, September 10, 2024, 12:41, Aaron Tam, South Hot-Cell, Standard Operation, TM4, TiC#9, Target TiC#9 HP-SIS installed onto TM4 089c5872-091d-484b-9b9c-dda8444b217b.jfif566cae27-5562-4934-b23a-5c99af810900.jfifcc853ae8-5896-46f3-9f21-f6ede8c82626.jfifffdf443c-2656-499a-9d0a-01ddef2f954a.jfif

September 9, 2024 - Aaron Tam 

  • Water from waterline found puddled on source-tray and containment box. 
  • Water was wiped up as much as possible, but likely still in containment box 
  • leaving to dry overnight
  • Target inserted into Hotcell with nuts for the parasitic target. 4/4 socket nuts installed on upstream flange, and 3/4 installed on downstream flange

September 10, 2024 - Aaron Tam

  • TiC#9 HP-SIS installed onto TM4 
  • Leak check passed after retightening VCR joint
  • Target Electrode Conductor screws torqued to 130 inch-lbs 
  • Electrical test passed 
  • Containment box cover reinstalled

Photos attached

Entry  Friday, September 06, 2024, 14:28, Aaron Tam, South Hot-Cell, Standard Operation, , Ta#68(Spare), Ta#68(Spare) removed from TM4 and into Anteroom  

September 5, 2024 -AT

  • Plastic and clean target tray added to SHC 
  • TM4 moved to SHC 
  • TM4 containment box cover removed

September 6, 2024 - AT

  • Ta#68(Spare) removed from TM4 onto clean tray 
    • top left mounting bolt fell under source tray in containment box - unretrievable
  • Ta#68(Spare) moved out of SHC via toolport door 
    • SHC lift table was lower than tool port tunnel by 2". Target-on-Tray slipped back onto lift table when trying to drag it up to the tool port. Target bounced out of one locating pin, but stayed within boundaries of the tray 
    • Water also leaked out from the VCR fitting and on to the SHC lift table, and toolport. 
  • Target-on-tray slid into a clean plastic bag, and then into a plastic box. 

 September 9, 2024 - AT

  • Ta#68(Spare) taken out of plastic bag and water drained from waterlines
    • Target was rotated in every direction several times until no more water poured out from the VCR joints
  • Ta#68(Spare) put back in box without the bag (to promote evaporation) 

 

Entry  Friday, September 06, 2024, 10:01, David Wang, South Hot-Cell, Standard Operation, TM4, Ta#67 back up. , TM4 has been moved from SMP to SHC. 

TM4 has been moved from SMP to SHC. The move is smooth.

Entry  Thursday, September 05, 2024, 12:50, Adam Newsome, Crane, Maintenance, , , Overhead crane: up/down hoist delayed start issue 

D. Wang reports that recently the overhead crane has been exhibiting a delayed start (approx. 1 min) when operating in local mode. This issue applies to the main hoist's up/down functionality only and does not seem to apply to other motion axes. T. Kauss briefly investigated but did not find any obvious cause.

This issue will be monitored and investigated over the following weeks and this log will be updated as more information becomes available.

Suggested troubleshooting steps:

  • Isolate the issue to local or remote mode to confirm this suspicion (it appears to be present in both local and remote mode)
  • With help from someone locally operating the crane, confirm at the receiver in the control room whether signals are coming through for up/down commands immediately, or whether the receipt of signals itself is delayed. At the same time, confirm whether the PLC input card is receiving the command signals from the receiver immediately or in a delayed manner. (it appears that the command signals are being received by the VFDs - the issue seems to be on the output side)
  • Time the delay, and repeat to confirm if the timing is consistent every time as reported by D. Wang (it appears timing is inconsistent. After a weekend of no use, it was approximately 2 minutes. After a few hours of no use, it was around 10 seconds).
  • Check if delay is present across various crane positions in the target hall (completed by D. Wang - result: yes)
  • Inspect controls hardware in the cabinet in the control room, as well as the remote IO on top of the crane, for obvious issues (checked cabinet but not remote IO - nothing obvious)
  • Go online with the PLC and test up/down commands to see if the program indicates any obvious issues (note: this may not actually help - seems to be an electrical issue isolated to the VFD-related electronics)
  • Mechanical inspection of the motor (not likely an issue)
  • Disconnect motor, repeat test of trying to command up/down motion and see if the motor itself had any effect on the delay

Update, 2024-09-09 [DW]:  Confirmed both local and remote mode have the same problem on delayed main hoist functional issue after crane was switched on. The delay time is 1 minutes 40 seconds to 2 minutes. It happens mostly when first time the crane was switched on. But if the crane was not used in the rest of day after first time switching on , the problem showed again 5 to 6 hours after in same day.

Update, 2024-09-09 [AN]: Checked again around 11:30am... tested running both hoists A and B in remote mode. Upon first attempt to lower hoist, no motion occurred. Hoist A VFD exhibited fault code 51, and Hoist B exhibited fault code 52. Both hoists appeared to receive the command from the PLC to attempt to move. Both hoists (initially) had their "ready" status as ON. When attempting to move, however, hoist B's ready status dropped out. Note also that the delay observed between the failed attempt to start, and when motion was actually possible, was only approximately 10-20 seconds. Perhaps this correlates to the fact the crane was recently operated this morning. It is suspected that the charging circuit for hoist B's DC bus voltage is faulty.
Tomorrow, another test will be performed by checking A and B independently to see if one can run but the other cannot.

 

Update, 2024-09-10 [AN]: Tested the crane using only Hoist A: working upon first power-up of the day. Tested using only Hoist B: not working, fault 52 re-appears. We are certain the issue lies with Hoist B. Furthermore, upon observing the motor contactors and status LEDs when attempting to energize the motor, the following is observed:

  • For Hoist A (normal, working operation) - on power up K1 toggles on (in). When pressing down button, K7 toggles (in). The hoist begins to move.
  • For Hoist B (non-functioning), on power up K1 toggles on (in). When pressing down button, K7 does NOT toggle. K1 toggles OFF (it should not) then comes back, then triggers the fault.

Upon further inspection it was noted that for K1 for Hoist B, there appears to be a snubber (XEB2202) wired in across the A1 and A2 terminals of the contactor. The fact that a time-dependent circuit is involved matches earlier theories about a charge-timing related issue. Suggested action: attempt to remove the snubber and test again to determine if the issue persists.

 

Update, 2024-09-11 [AN]: Under work permit I2024-09-10--3, the following was tested and observed:

  • Run Hoist B to confirm it is not working (expected behaviour) - confirmed
  • Power off crane, remove the snubber from Hoist B's contactor K1
  • Power on crane, attempt to run Hoist B - the hoist did not run
  • It was noticed also that Hoist A did in fact have a snubber installed as well - it was hidden. The snubber for Hoist B's capacitance was measured and confirmed to match what it should be, so it is suspected that it is working fine.
  • This indicates that the snubber is not the issue. The snubber was reinstalled and the system returned back to normal state. Tested - working.

At this time the root cause remains unknown, but the snubber has been eliminated from the possibilities.

It appears that the issue can be isolated to the fact that contactor K1 momentary toggles off when attempting to operate the hoist. This short blip would explain the fault code related to insufficient line voltage. The drawings indicate the only way that K1 can turn off is if the 48 VAC supply from the transformer drops out momentarily, or if an unnamed relay located (presumably) in the VFD momentary toggles.

Further troubleshooting steps could include:

  • Probe for 48VAC at A2 terminal of K1 and attempt to operate the hoist - see if it drops off briefly. If so, the issue is either the transformer or the relay contact in the VFD. Perform continuity check across the relay contact, repeat attempt to operate hoist, and determine if it is the relay contact causing the issue. This test will significantly isolate the issue.
  • Check inside Hoist B's VFD circuitry and measure the DC bus voltage during attempted operation, and compare to Hoist A. There may be an issue with the charging circuit inside the inverter.

 

Update, 2024-09-13 [AN]: Under work permit I2024-09-10--3, the following was tested and observed:

  • Probe the A2 terminal of K1 for Hoist B with respect to the transformer's 0V output upon initial power-up of the system: ~53VAC measured (should be 48VAC but 53 is acceptable)... this confirms that the appropriate relay coil voltage is present upon power-on, as expected because it is observed that the relay toggles upon power-up.
  • Continue probing A2 while attempting to jog Hoist B down, with min-hold set on the multimeter to check for voltage drops: the voltage measured was approximately 24VAC during one attempt and 36VAC during another. This implies that K1's coil voltage does in fact drop out instantaneously, resulting in K1 very briefly disengaging which causes the observed VFD vault. The fact that the measured min voltage is different can be attributed to the mulitmeter's sampling rate, catching the voltage during its decline towards 0.
  • Because of the aforementioned test results, it is confirmed that there is an issue associated with K1's coil voltage briefly dropping out when attempting to run the hoist. There are only two reasons this could happen: 1) the transformer power output of 48VAC actually drops, or 2) the relay contact in series with this (located inside the VFD) opens up as a result of a VFD fault. The latter is more likely.
  • Upon investigating the VFD further, it was determined that another fault code was present prior to the above mentioned code 52. This fault code happened very briefly at the same time as K1 toggling, but was then covered up by code 52. This fault code is 2, which states that there's an overvoltage condition - the DC bus voltage has exceeded 911 VDC (135% of device maximum nominal voltage of 500V). This can be attributed to a supply voltage surge in which it is raised 35% above its nominal value.
  • Note: line-to-line voltages were measured at the input to K1 after the "warm up period" and the issue was resolved, when the hoist was sitting idle. These were measured to be almost exactly 480VAC. This represents a reference condition.
  • What seems to be happening is that when the hoist motion attempts to start, there is a line voltage surge for some reason (back-emf?) which causes this fault condition for a temporary instant, but then when the voltage dissipates the fault instantly clears. This explains why contactor K1 very briefly flickers during motion attempt - the fault is only briefly present. But then, fault code 52 takes over and remains present (because of the line voltage disruption).
  • Still, the root case of this issue is unknown. It is not confirmed whether there is actually a voltage surge or not (to be measured next week), and why it seems to only happen for the first ~2 minutes of the day.
    It could be attributed to one of the following reasons:
    • Coil voltage rectifying diode partial failure inside K1... the diode may need time to "warm up"
    • Brake solenoid partial failure for Hoist B (causing additional friction which leads to overvoltage condition for the motor)... the brake may need time to "warm up"
    • Charging capacitor issue in DC bus voltage charge circuit inside the VFD

Suggested troubleshooting steps:

  • Probe line-to-line voltage at input terminals to K1 during attempt to operate Hoist B in max-hold mode: check for surge, record values
  • Probe DC bus voltage during the same condition, record value
  • Determine if the above indicate a true overvoltage condition, and determine why this may be

 

Update, 2024-09-16 [AN]: Under work permit I2024-09-10--3, the following was tested and observed:

  • Probe L1-L2, L2-L3, and L1-L3 line voltages on input side of contactor K1 for Hoist B with max hold set on multimeter to confirm whether there is a surge when attempting to move the hoist - no surge was observed. 480VAC constant was measured in each case.
  • There may be another issue causing the DC bus overvoltage condition (an issue with the motor or an issue with the drive itself)

Suggested troubleshooting steps:

  • Probe DC bus voltage during the faulted condition, record value
  • Disconnect the motor from the drive and check motor winding resistances before and after the "warm up" period to see if there is a change, and also compared to Hoist A
  • With the motor disconnected, attempt to run the drive - determine if fault code 2 shows up or if the drive appears to be working.. this may eliminate the motor from the list of potential issues

 

 Update, 2024-09-16 [AN]: Under work permit I2024-09-16--3, the following was tested and observed:

  • Probed DC bus voltage on Hoist B's VFD prior to attempting to move hoist, and during the attempt to move it. In both cases it remained a constant 690 VDC. No temporary spike was observed. This is also lower than the threshold that the VFD's manual stated the fault would typically occur at (~911 V) so it casts doubt on whether this is the root cause of the problem.
  • Probed DC bus voltage for Hoist A's VFD, for comparison - same measurement.

Suggested troubleshooting steps:

  • Disconnect the motor from the drive and check motor winding resistances before and after the "warm up" period to see if there is a change, and also compared to Hoist A
  • With the motor disconnected, attempt to run the drive - determine if fault code 2 shows up or if the drive appears to be working.. this may eliminate the motor from the list of potential issues
  • Swap VFDs between Hoist A and B to determine if the problem tracks the drive
  • Swap K1 between Hoist A and B

 

Update, 2024-09-16 [AN]: Under work permit I2024-09-16--3, the following was tested and observed:

  • Measured motor winding resistance between every combination of lines for both Hoist A and B (for comparison). Note: this was done mid-day, prior to any use of the crane for the day. In each case, the resistance was measured to be 2.2 Ohms. There is no difference between the A and B. This is not likely the root cause of the issue.

Suggested troubleshooting steps:

  • With the motor disconnected, attempt to run the drive - determine if fault code 2 shows up or if the drive appears to be working.. this may eliminate the motor from the list of potential issues
  • Swap VFDs between Hoist A and B to determine if the problem tracks the drive
  • Swap K1 between Hoist A and B

 

Update after email discussion with Kone service tech, 2024-09-23 [AN]:

The Kone service tech said "This is a obsolete inverter and there is not a direct replacement available or parts for repair .  It is recommended to replace inverter with a conversion panel. The conversion panel consists of new, correctly sized components including D2V inverter, to have the same functionality as original panel. All components mounted and prewired to a back panel that fits directly inside the existing enclosure. All inputs and outputs are terminated at a terminal strip. Interconnecting wiring diagrams are also provided for ease of installation. The lead time for a conversion panel is approximately 10-12 weeks after receipt of a Purchase order."

A quote will be obtained from Kone for the replacement.

Update after K7 swapping between hoist A and B with Jason, Mike, Julie, 2024-10-09 [DW]:

Contactor K7 was swapped between hoist A and B. On hoist B we saw F52 fault and K7 did not engage in properly. On hoist A we saw F51 fault which is "stop limit has be tripped" and K7 also did not engage in properly. After 2 minute wait, both hoist A and B are back to normal. The plan for tomorrow: switch to A hoist and test. right after, switch to B and test. 
UPDATE FOR PAST THREE DAYS TESTS AND PROGRESS.  DAVID WANG 2024-10-12
2024-10-09 noon. Left crane with power on for 1 hour. switched off power on crane for rest of day to Thursday morning test.
2024-10-10 morning. Set to A hoist only. Switched on main power and tested hoist A down. It was normal, no delay. Right away switched to hoist B and tested hoist B down . It was normal, no delay. Switched to A and B and tested hoist up and down. It was normal, no delay.

2024-10-10 noon.  Replaced spark quenchers on hoist B K1 and K7. Tested crane after replacement. Everything works fine. Used crane to lift up F308 around 1:30. Then switched off crane for next morning test.

2024-10-11 morning. Set to A and B. Tested crane hoist down twice 2-3 seconds each time with 3 second between. No fault. Hoist worked fine.  3 second after, tested hoist up and found  K7s were not on on both A and B. 10 seconds after tested hoist up again and it worked. Then tested all crane movements. Everything was normal. Crane was used for spent target moves to 2:30pm . Then switched off.

2024-10-12 morning: Set to A and B.  Right after power on, tested hoist up for 5 seconds. wait 3 seconds, tested hoist down for 5 seconds. Repeated same up and down test within 3 seconds.  No fault. the hoist A and B works fine. Tested N-S,E-W movement. all good.  at the last, tested hoist up and down 10 seconds each. Hoist A and B are still good. The plan for next morning test: Leave crane power off to Tuesday morning and test hoist A+B(48 hours power off). Also plan to replace spark quenchers on hoist A /K1 and K7 if any delay is found on Tuesday morning test. 
2024-10-15 morning: Set to A and B. tested hoist up and down one click on each. I saw K7 momentarily "on" then drop off symptom as before. I saw F51 on A and F52 on B. Switched to A right away and tested. A works fine. Then switched to B and tested. B works fine. The total test time from A+B to B then to A is about 30 seconds. Then i switched back to A+B for checking. everything works fine as anticipated.

2024-10-16  A-K7 snubber was replaced yesterday after morning test . Tested hoist A+B this morning after 24 hours crane power off. Hoist A+B works fine on both up and down. 

2024-10-17 Tested A+B hoist this morning after 22 hours crane power off. Hoist A+B works fine on both up and down.

2024-10-18 Tested A+B hoist this morning after 24 hours crane power off. Hoist A+B works fine on both up and down.

2024-10-21 Tested A+B hoist this morning after 72 hours crane power off. The delay issue on hoist B appeared. Hoist A is fine. B/K7 was momentarily on then dropped off. By the same time B/K1 was momentarily dropped off then on with F52 code.

2024-10-22 Tested A+B hoist from target hall this morning after 22 hours crane power off.  hoist A+B  works fine on both up and down.

2024-10-22 noon.  Swapped  hoist A/K1 and B/K1. Crane power off at 9:30am after flask/pail repacking job.

2024-10-24. Tested A+B hoist this morning after 46 hours crane power off. Hoist A+B works fine on both up and down. Crane will be left as power off for 48 hours for next test.

2024-11-21. In the past month ,I tested crane multiple times. 24 hours power off test results are good always. 48 hours or longer power off test results are not consistent. Hoist B had 15 to20 seconds delay on early checks after last e -log. But in recent  6 days power off check and 3 days power off check, the hoist B has no delay. The next step: 1, keep on multiple days power off check. 2, replace Hoist B K1 (line+auxiliary) contactors with new parts.

2024-11-25. tested hoist A+B this morning after 4 days crane power off. No delay. everything works fine. Replacement contactors for K1 have been requested. Line contactor is in 5 weeks back order status from Digikey so we will replace Hoist B K1 next year in January mostly.

2024-12-02. Tested hoist A+B this morning after 4 days crane power off. No delay. everything works fine. It looks like  no delay status is stable now by watching on past 40days morning check result. Daily and multiple days check on hoist B  will be kept on.

2025-01-02. Tested hoist A+B this morning. The last time of crane using in 2024 should be 18th Dec. No delay . Crane works fine.

Entry  Tuesday, September 03, 2024, 11:40, David Wang, ITW, Standard Operation, TM3, TiC#8, TM3 has been moved from ITW to S-W silo. 

TM3 has been moved from ITW to S-W silo. The move is smooth.

Entry  Tuesday, August 27, 2024, 13:30, Frank Song, ITW, Maintenance, TM3, TiC#8, module disconnection TM3_with_TiC#8_disconnection_in_ITW_2024-08-27.pdf

 TM3 is disconnected and all water lines are purged/refilled with 50psi Nitrogen. Pls see pics attached with.

Entry  Monday, August 26, 2024, 09:57, Travis Cave, Spent Target Vault, Standard Operation, , Nb#10, Spent Target Move Target_Index_2024-08-26.pdf

 Nb#10 was placed in pail#295 and moved from the south hot cell to the spent target vault, spot 4A, it was 230uSv/hr when removed from the SHC. See attached PDF for vault details.

Entry  Wednesday, August 21, 2024, 10:53, Travis Cave, Spent Target Vault, Standard Operation, , TiC#7, Spent Target Move Target_Index_2024-08-21.pdf

 TIC#7 was placed in pail #294 and then moved from the south hot cell to the spent target vault spot 4B. It was 82.3mSv/hr when removed from the SHC. See attached PDF for details.

Entry  Tuesday, August 20, 2024, 11:53, Carla Babcock, South Hot-Cell, Standard Operation, , Nb#10, Nb#10 PIE 

Nb#10 never worked online - repeller had no effect on the beam and one of the RF wires was touching HVC. Max 60pA was seen on the source cup. See notes here ITW-TM2-Nb#10/#11-LP-IGLIS  (Web view)

Target was handled roughly after use - kicked around in NHC for a long time, then loaded into a pail (multipin had to be dettached for this) then moved to SHC, unloaded from pail, then plates covering the RF electrodes had to be pried off. Lots of knocking and shaking.

Theory was that the repeller wire was disconnected. But found it not obviously broken, had good continuity from the ring tongue to the end of the wire pulled out of the multipin, even after all the abuse. Same for the RF (from the end of the electrode to the end of the wire pulled out of the multipin). Did find some of the multipin wires were flaky - if moved around they showed intermittent shorts to HVC. But not clear if this is from the rough handling afterwards or not. The problem was not in the module since NB#11 ran immediately afterwards with no issues. Most likely culprit seems to be the insulation beads on the wires. Should look for more robust insulation solutions. On the other hand, the connections of the wires to the electrodes seems very good.

Still not sure why no effect of the repeller was seen. Could be a intermittent break/short, though this seems unlikely. Maybe the connection in the multipin was not good? I did not get a chance to inspect that.

Entry  Tuesday, August 20, 2024, 11:36, Carla Babcock, South Hot-Cell, Standard Operation, , TiC#7, TiC#7 PIE 

TiC#7 failed after two weeks of operations - measurements in the electrical room indicated that the negative side of the CHT was broken (35kOhms to the rest of the target). This was likely due to a large number of proton trips during this target run. At every trip I could see the CHT voltage getting higher and more unstable. This cahnge in voltage was reflected in the unstable anode current and fluctuating RIB beam intensity, as a direct result of the fluctuating power on the CHT. The break was confirmed in PIE, loosening the screws caused the target container to come off without the cathode. Otherwise nothing unusual was seen. The anode wire connections seem very robust, dragging the target around with the multipin disconnected, flipping it up and down, etc and the anode wire stayed attached. Though we saw lots of outgassing on this target, things looked the normal level of dirty. There was no buildup between PE and EE.

Entry  Monday, August 19, 2024, 15:29, Frank Song, ITW/ITE, Standard Operation, TM2, Ta#67, shielding blocks transfer 

 5 shielding blocks have been transferred from ITW to ITE, MAA has been secured after moving.

Entry  Monday, August 19, 2024, 09:32, David Wang, Conditioning Station, Standard Operation, TM4, Ta#68 , TM4 has been moved from SHC to TCS. 

TM4 has been moved from SHC to TCS. The move is successful.

Entry  Friday, August 16, 2024, 15:32, Aaron Tam, South Hot-Cell, Standard Operation, TM4, Ta#68 LP-SIS, Target Ta#68 loaded onto TM4  Ta-68_Installed.jfif

 Target Ta#68 loaded onto TM4 

-leak check passed

-Target electrode conductor screws torqued to 130 in-lbs

-electrical check passed

Containment box cover re-installed 

photo attached 

Entry  Friday, August 16, 2024, 15:28, Aaron Tam, South Hot-Cell, Standard Operation, TM4, TiC#7 HP-FEBIAD , TiC#7 Target Removed from TM4 TiC-7_normal_exposure.jfifTiC-7_ettr.jfifTiC-7_Panel.jfifTiC-7_extraction_electrode.jfif

 TiC#7 Target Removed from TM4. - Photos attached 

TiC#7 Currently sitting in SHC waiting for disposal 

Entry  Friday, August 16, 2024, 13:29, Frank Song, South Hot-Cell, Standard Operation, TM4, Ta#68, electrical check/leak check TM4_with_Ta#68_electric_and_leak_check_on_SHC_2028-08-16.pdf

 New target Ta#68 is installed on TM4 and be leak/electric checked. Pls see attachment.

Entry  Friday, August 16, 2024, 09:50, David Wang, South Hot-Cell, Standard Operation, TM4, TiC #7 febiad., TM4 has been moved from SMP to SHC. 

TM4 has been moved from  SMP to SHC. The move is smooth.

 

Entry  Friday, August 16, 2024, 08:47, Travis Cave, Spent Target Vault, Standard Operation, , SiC#46, Spent Target Move Target_Index_2024-08-16.pdf

 SiC#46 (pail 293) was placed in the vault (spot 3B) on Wednesday the 14th of August. It was 111 mSv/hr when removed from the south hot cell. See attached PDF for details.

Entry  Wednesday, August 14, 2024, 11:29, Aaron Tam, Waste Package/Ship, Standard Operation, , SiC#46, Target Disposal and visual check  SiC46.jfif

 SiC#46 loaded into pail 293 successfully along with other hotcell waste 

Upon visual inspection of the target, a spark-sign was spotted on the perimeter of the extraction electrode. Metallic looking material also found built up between the extraction electrode and the backing plate of the target 

Photo attached 

Entry  Tuesday, August 13, 2024, 14:23, David Wang, ITE, Standard Operation, TM3, Ta#67., TM2 with Ta#target has been moved from SHC to ITE. 

TM2 with Ta#target has been moved from SHC to ITE. the move is smooth.

Entry  Tuesday, August 13, 2024, 14:18, Frank Song, ITE, Standard Operation, TM2, Ta#67, Module Connection TM2_with_Ta#67_connection_in_ITE_20240813.pdf

 TM2 with new target Ta#67 was connected in ITE, all TP are running at their full speed now.

Entry  Tuesday, August 13, 2024, 08:39, Frank Song, South Hot-Cell, Standard Operation, TM2, Ta#67, electrical check/leak check TM2_with_Ta@67_electric_and_leak_check_on_SHC.pdf

 TM2 with new target Ta#67 had been electric/leak checked before moving to ITE. See attachment pls.

Entry  Monday, August 12, 2024, 15:55, Aaron Tam, South Hot-Cell, Standard Operation, TM2, Ta#67 LP-SIS, Target Loading 

 Ta#67 Target loaded onto TM2

Leak check passed

Electrical test passed after loosening off target electrode conductor screws, and torqueing by feel 

 

Entry  Sunday, August 11, 2024, 11:25, Carla Babcock, South Hot-Cell, Repair, TM3, TiC#8, short on multipin wires to TBHT discovered 

With the new TiC#8 target installed on TM3, there was a ~7kOhm connection between TGHT/TBHT (A/B/C/D) and HV common. The standard electrical check on the module showed standard values, so it was assumed the problem was inside the target.

Started removing bolts/water connections one by one to see if any of them had an effect on the measurement. Found that disconnecting the multipin on the target from the mating connector on the source tray resolved the issue. Determined that the only way this could happen is if a spark cut through the insulation covering the multipin wires. Because of the way they are routed, they can touch the water lines and they are definitely touching waterline C, TBHT-. We do not typically check continuity of multipins to all water lines, just to HVC, so did not see this in the standard electrical check. Measurements verified that pin 2-4 was touching water line C, creating a short from TGHT/TBHT to HV common when the multipin connector is attached, since the pins are shorted to HVC inside the connector when they are not used.

Issue was solved by removing the target into the ante room, removing connector 1 all together since it was not used, and removing the grounding on the other pins, leaving only pin 2-2 connected for the anode.

In future we will change the IGLIS wiring so pin 2-4 is not used, and redesign the cable routing so it cannot touch the blocks. For the immediate term, we will add to the electrical check a check of each pin to TBHT/TGHT/COIL.

Entry  Friday, August 09, 2024, 19:01, David Wang, ITW, Standard Operation, TM3, TiC#8., TM3 has been connected in ITW. TM3_TiC#8_connection_in_ITW_checklist.pdf

TM3 has been connected in ITW. See attachment for checklist.

Entry  Friday, August 09, 2024, 18:20, David Wang, ITW, Standard Operation, TM3, TiC#8, TM3 has been moved from SHC to ITW. 

With TiC # 8 installed, TM3 has been moved from SHc to ITW. The move is smooth.

Entry  Friday, August 09, 2024, 18:18, David Wang, ITW, Standard Operation, TM4, TiC#7, Tm4 has been moved from ITW to SMP. 

Tm4 has been moved from ITW to SMP. the move is successful.

Entry  Friday, August 09, 2024, 16:15, Frank Song, South Hot-Cell, Repair, TM3, TiC#8, electrical check/leak check electrical_and_leak_check_of_TM3_with_new_target_TiC#8_replaced_at_SHC_20240809.pdf

 TM3 with replaced target TiC#8 has been checked on SHC before moving to ITW. Pls see attachment

Entry  Friday, August 09, 2024, 08:11, Frank Song, ITW, Standard Operation, TM4, TiC#7, module disconnection TM4_with_spent_TiC#7_disconnection_in_ITW_20240809.pdf

 TM4 with spent target TiC#7 (dead) was disconnected in ITW and ready to move to TCS.

Entry  Thursday, August 08, 2024, 13:58, David Wang, South Hot-Cell, Standard Operation, TM3, SiC #46, TM3 SiC#46 electrical check at SHC with target on (After operation) TM3_Sic_46_after_run_E_check.pdf

ABCD is short to 60KV bias. Othjer are ok.  see attachment.

Found afterwards that this short was due to sparking through the multipin wire insulation where the wires pass behind the TBHT block "C". See fault 17265.

Entry  Thursday, August 08, 2024, 11:41, David Wang, South Hot-Cell, Standard Operation, TM3, SiC #46, Tm3 was moved from ITE to TCS this Tuesaday, then to SHC this morning. 

Tm3 was moved from ITE to TCS this Tuesday, then to SHC  this morning. Both moves are successful.

Entry  Tuesday, August 06, 2024, 09:16, Frank Song, ITE, Standard Operation, TM3, SiC#46, module disconnection TM3_with_SiC#46_disconnection_in_ITE_2024-08-0106.pdf

 TM3 with spent target SiC#46 was disconnected in ITE and ready to move to TCS soon.

Entry  Wednesday, July 24, 2024, 10:10, Frank Song, ITE/ITW/Storage Area, Standard Operation, , , shielding blocks transfer 

 5 shielding blocks have been transferred from ITE to ITW. MAA is secured again after moving.

Entry  Thursday, July 18, 2024, 11:22, Travis Cave, Spent Target Vault, Standard Operation, , UC#45, Spent Target Move Target_Index_2024-07-18.pdf

 The UC#45 target was moved from the south hot cell to the spent target vault. It was place in Pail#292 spot 1A of the vault, was 19.5mSv/hr. Also this pail contains the target material of UC#44. See attached PDF for more details.

Entry  Wednesday, July 17, 2024, 15:06, Adam Newsome, Facilities, Standard Operation, , , Safety Walkaround Complete - SHC/NHC Area 

A safety walkaround for July 2024 was completed for the B2 level by A. Newsome. No deficiencies to report.

Results can be found in the master spreadsheet

Entry  Tuesday, July 16, 2024, 13:14, Frank Song, ITW, Standard Operation, TM4, TiC#7, Module Connection TM4_with_new_target_TiC#7_connection_in_ITW_2024-07-16.pdfMicrosoftTeams-image_(65).png

 TM4 with TiC#7 was connected in ITW, all TPs are running at full speed.

Entry  Tuesday, July 16, 2024, 11:15, David Wang, ITW, Standard Operation, TM4, TiC #7 febiad. , TM4 has been moved from TCS to ITW.  

TM4 has been moved from TCS to ITW.  the move is smooth.

Entry  Tuesday, July 16, 2024, 11:15, David Wang, ITW, Standard Operation, TM4, TiC #7 febiad. , TM4 has been moved from TCS to ITW.  

TM4 has been moved from TCS to ITW.  the move is smooth.

Entry  Friday, July 12, 2024, 08:51, Riley Sykes, Safe Module Parking, Maintenance, , , SMP chain guard 

 SS washers were added to all slotted holes on SMP chainguard cover plate

Entry  Wednesday, July 10, 2024, 10:44, Riley Sykes, South Hot-Cell, Maintenance, , , Spring idler install Image.jfifImage_(2).jfif

 New spring idlers were installed onto rotational chain drive for SHC roof. Operation ran smoothly in both directions to full limit. Chain was noted to have adequate slack when not on driven side. Periodic checks to confirm operation will continue in the following months to guarantee proper operation.

Entry  Wednesday, July 10, 2024, 09:55, Adam Newsome, Safe Module Parking, Maintenance, , , Annual electrical and mechanical inspection of Safe Module Parking  PXL_20240710_160636341.jpgPXL_20240710_160506424.jpg

An annual electrical and mechanical inspection was performed on the SMP today by Adam Newsome, Travis Cave, Riley Sykes, Maico Dalla Valle, and Jason Zhang as per Work Permit  I2024-07-10-1. The following items were checked:

  • Check condition of wiring for physical/radiation/UV damage
    • OK, no signs of significant damage
  • Check for cable tray debris or damage
    • There were multiple items in the cable tray which do not belong there - misc. pieces of wood and metal... these items were not disposed of but should be in the near future
  • Check inside control panel: components and wiring, labeling
    • Labeling intact, components in good condition
    • Misc. random wires pulled to check... OK
  • Verify camera views
    • This was not inspected in detail as it is something that would be done prior to remote operation
  • Check connectors for damage
    • All connectors OK
  • Check pendant for damage and verify labeling intact
    • Pendant OK
  • Lid open/close test
    • Lid was opened and close multiple times - smooth operation, no concern
    • Lid close logic was checked - OK
  • Vessel rotation and limit switch check
    • Both CW and CCW limits were checked, functioning
    • No concern on rotation - chain drive, rotary limit switch, and cable reel all functioning normally
  • Lubricate chains
    • Not done - should be done next year
  • Inspect tensioners
    • Done - OK
  • Tighten fasteners
    • Not all fasteners were checked - washers will be replaced soon so this was not deemed necessary
    • Approximately 50 washers are missing for socket head screws in slotted parts. Not safety critical but they should be replaced soon.
  • Visual inspection
    • All OK

Overall the inspection was successful.

Entry  Tuesday, July 09, 2024, 16:14, Carla Babcock, ITE, Repair, , , Attempts to reduce ITE:EL trips from HV sparks 8x

ITE:EL has been tripping off due to HV sparks. Usually this also trips ITE:Q1/2. These are sitting in side-by-side racks.

The working theory is that HV sparks are returning to ground through the EL and quads, tripping them off. Possibly this is the result of a changed low impedance ground path. How this change happened could be either something we did during shutdown or the changes we made in TM3, no clear evidence yet.

The goal of these changes is to stop the EL and quads from tripping, assuming the sparks are travelling through the ground.

 

Possible routes through ground to the EL power supply:

  1. Through controls. EL is controlled by a canbus card. Preliminary investigations by Mike Rowe make it look like the canbus reads the PSU max voltage (60kV), then the staton bit trips, then after a while of trying to talk to the power supply, the statdrv is turned off. It is not clear why the power supply is turning itself off, since it doesn't seem to have a trip or protection circuit inside. To be further investigated.
  2. Through the AC ground.
  3. Through the shield on the output voltage conductor that runs to the pit.
  4. Through the EL wire and conductor itself.

 

Current attempts to mitigate the tripping:

  • Add an isolation step to the AC power, in case it is coming through AC ground (option #2).
  • Add ferrites on the controls lines (option #1, this was done earlier and no effect has been seen).
  • Add transient voltage suppresors on the Vmon, Imon, Vprog and Iprog control cables (option #1).
  • Replace grounding cable with a grounding strip where the grounding wire used to be on ITE:EL. The ground wire was a braid, so probably not too bad, so not sure if this will help.
  • Improve the connection between the two grounding bars in the racks. The grounding bar for th EL supply is well connected to the copper ground strip from ITE, but only connected through a small cable to the grounding bar for the quads. A copper foil sheet was added between them and the previously used wire was disconnected on the quad side bar..

 

Entry  Monday, July 08, 2024, 10:40, David Wang, Conditioning Station, Standard Operation, TM4, TiC#7, TM4 has been moved from SHC to TCS. 

TM4 has been moved from SHC to TCS. The move is successfully.

Entry  Friday, July 05, 2024, 14:13, Adam Newsome, Waste Package/Ship, Standard Operation, , , F-308 flask loading - five flasks loaded  Target_Index_2024-07-05.xlsm

Today (2024-07-05), five flasks were loaded in preparation for shipment with the following targets: SiC#43 (Pail 272), SiC#44 (Pail 275), Ta#63 (Pail 266), UC#40 (Pail 278), UC#38 (Pail 274).

The crimped lifting loop has been applied to each pail. The locks have not yet been applied to the flasks at the time of writing this log, but will be done next week.

The mini-storage vault is now EMPTY. Because some of the pails had contamination (200 - 1500 CPM), it is highly recommended that the mini-storage vault be cleaned or at least swiped for contamination.

The target index spreadsheet has been updated (attached).

Entry  Friday, July 05, 2024, 12:50, David Wang, South Hot-Cell, Standard Operation, TM4, TiC#7, TM4 and TiC#7 target electrical check and HS leak check at SHC after target installation . 

TM4 and TiC#7 target electrical check and HS leak check at SHC after target installation have been done.  all results are good. I will attach the checklist when printer is back to work.

TM4 HS line was helium pressure tested at TCS this morning. No leak. Also i leak checked TM4 top all air to  vacuum seals at TCS. Everything is good.

TiC #7 is a febiad target.TM4 top has been configured for febiad target. checked pin 2-2 to bias, target ,and chassis at 250V. they are all OL.  

 

Entry  Thursday, July 04, 2024, 13:23, David Wang, South Hot-Cell, Standard Operation, TM4, UCx#45, electrical check on TM4 UCx#45 target at SHC after operation.  Tm4_UCx_46_at_SHC_after_operatiom.pdf

electrical check  on TM4 UCx#45 target at SHC after operation is done.   see attachment.

Entry  Thursday, July 04, 2024, 11:45, Frank Song, ITW, Standard Operation, TM4, UCx#45, module disconnection TM4_with_Spent_Target_UCx#45_disconnection_in_ITW_2024-07-04.pdf

TM4 with spent target UCx#45 was disconnected in ITW and moved to SHC.

 TM4 move from ITW to SHC is smooth.

Entry  Thursday, July 04, 2024, 01:20, Carla Babcock, ITE, Development, TM3, SiC#46, TM3 conditioning with protons 

Initial Summary:

TM3 sparking behaviour in ITE has been very disruptive both with and without protons. Protons are at 60uA, target heater at 540A. Max voltage achieved so far is 51kV, limited by time and a current limit on the BIAS supply.

The ITE:EL trips off every couple of minutes. Just needs to be restarted. Mike investigated and found that the trip is happening inside the power supply, then a moment later the canbus is defining the supply off when it cant get it to respond. Trip frequency decreased over time but still disruptive.

All the waterflow signals, including ones controlled in the cyclotron system, were tripping off regularly. These have all been forced, then we implemented a 5s delay in the ISAC waterflow interlocks. This seems to have solved the issue.

The ITE:BIAS supply has also been limited at 500uA instead of 5mA. Probably something hardcoded into the canbus - this was fixed by Keiko and the hardcode limit was set to 20%(?) of 5mA.

 

TM3 has been very sparky, even at low voltages. I can't understand why. A new ground path would be explicable but the excessive sparking is difficult to understand.

Possible avenues:

  1. make sure the module outer surface is connected through a copper sheet to the sheet on the wall.
  2. check that special ground still grounds all the gnd power supplies in the electrical room - this I checked but some of the grounds are connected through wires instead of sheets, this can be improved.
  3. try running the module with only HV hooked up and nothing else.
  4. try running TM3 in ITW.
  5. Search work permits and shutdown jobs for any changes made to the system that could affect this.
  6. hope there is a software solution for the EL problem, or start moving towards PLC control - no software solution because the canbus card is only reacting to the power supply refusing to turn on, so it seems the issue originates in the PSU. Moving to PLC is possible but may not help and increases the risk of frying the PLC module.
  7. Add a spark gap or limiting resistor to the EL somewhere. Resistor only helpful if the EL itself is sparking. Difficult to find a spot for the spark gap.
  8. Get a bipolar supply that can sink the current of a spark and replace the EL supply. - Tomislav doesn't seem to think this is viable.
  9. Add protection on the controls cables.

 

Spark recording:

60uA/50kV/540A July 3 02:30 - 05:30 : average of 50 sparks per hour. data file https://isacwserv.triumf.ca/onlylocal/isacdata/ITE_TM3_SiC46_HVConditioning_2_20240704

60uA/32kV/540A July 3 19:15 - July 3 21:45 : average of 8.4 sparks per hour. data file https://isacwserv.triumf.ca/onlylocal/isacdata/ITE_TM3_SiC46_HPSIS_HVConditioning_20240704

50uA/42.8kV/540A July 4 8pm - July 5 2pm : average of 20 sparks per hour, or if you cut out the last two hour that were very sparky, 14 sparks per hour. data file http://isacwserv.triumf.ca/onlylocal/isacdata/TM3commissioning_July4_52024.dat

50uA/42.8kV/540A July 8 00:00 - July 8 18:00 : average of 3.4 sparks per hour. data file http://isacwserv.triumf.ca/onlylocal/isacdata/TM3commissioning_July82024.dat

50uA/42.8kV/540A July 10 10am - 3pm : 3.6 sparks per hour

50uA/53kV/540A July 17 5am - 10am : 4 sparks per hour

45uA/53kV/540A July 20 8pm - July 21 6:30am : 24 sparks in 11 hrs, avg 2.2 sparks per hour.

 

 

EL trip recording (first 2 entries from the archiver, verify with ops elog):

50uA.42.8kV/540A July 4 23:00 - July 5 16:00 : 9 trips, average 0.5 trips per hour

50uA/42.8kV/540A July 6 12:00 - July 7 03:00 : 6 trips with 2.5hrs off, average 0.5 trips per hour

50uA/42.8kV/540A July 7 05:00 - July 8 18:00 : no trips in past 30hrs. Last trip July 7 at 3am.

50uA/42.8kV/540A July 10 3pm - still no EL trips

50uA/53kV/540A July 16 8pm - July 17 10am : 3 trips in 6 hrs. Note cable in EL circuit got burned so EL is running at only ~4kV

45uA/53kV/540A July 17 3pm - July 18 9:30am : 7 trips in 18hrs

45uA/53kV/540A July20 14:00 - July 21 6:30 : 5 trips in ~17hrs

 

2024-11-15 EDIT, Alexander Shkuratoff:

I was not involved in this run, but I have gone through all the Elogs for TM3 up to this point and summarized all the data dumps at the bottom, so I may as well do it here.

[   ] ITE_TM3_SiC46_HPSIS_HVConditioning_20240704 2024-07-04 01:42 4.8M
[   ] ITE_TM3_SiC46_HVConditioning_Vac_20240704 2024-07-04 01:59 5.3M
[   ] ITE_TM3_SiC46_HVConditioning_2_20240704 2024-07-04 05:31 1.1M
[   ] TM3commissioning_July32024.dat 2024-07-04 17:04 11M
[   ] TM3commissioning_July4_52024.dat 2024-07-05 14:18 12M
[   ] TM3commissioning_July82024.dat 2024-07-08 18:03 13M

 Additionally, there is no Elog entry for August 18, 2024 for which TM3 commissioning continued in ITW, but I have found the following StripTool data:

[   ] TM3commissioning_Aug182024.dat 2024-08-18 05:37 14M  
[   ] TM3commissioning_Aug182024_2.dat 2024-08-19 06:16 14M  

 

Entry  Wednesday, July 03, 2024, 14:01, David Wang, Conditioning Station, Standard Operation, TM2, , Tm2 has been moved from TCS to SW silo. 

Tm2 has been moved from TCS to SW silo. the move is smooth.

Entry  Tuesday, July 02, 2024, 11:38, Frank Song, ITE/ITW/Storage Area, Standard Operation, , , shielding blocks transfer 

 5 shielding blocks have been moved from ITW to ITE, MAA area has been secured.

Entry  Thursday, June 27, 2024, 09:49, David Wang, North Hot-Cell, Standard Operation, , Nb#10, Nb#10target has been remotely transferred from NHC to SHC.  

Nb#10target has been remotely  transferred from NHC to SHC. 

Entry  Wednesday, June 26, 2024, 13:49, David Wang, Conditioning Station, Standard Operation, TM2, , Tm2 has been moved from SW silo to TCS. 

Tm2 has been successfully moved from SW silo to TCS.

Entry  Tuesday, June 25, 2024, 12:49, Frank Song, ITE, Standard Operation, TM3, SiC#46, Module Connection TM3_with_SiC#46_connection_in_ITE_2024-06-25.pdf

 TM3 with new target SiC#46 was connected in ITE.

Entry  Tuesday, June 25, 2024, 11:59, David Wang, ITE, Standard Operation, TM3, SiC #46, Tm3 has been moved from TCS to ITE. 

Tm3 has been moved from TCS to ITE. the move is smooth.

Entry  Tuesday, June 25, 2024, 11:59, David Wang, ITE, Standard Operation, TM3, SiC #46, Tm3 has been moved from TCS to ITE. 

Tm3 has been moved from TCS to ITE. the move is smooth.

Entry  Monday, June 24, 2024, 14:37, Carla Babcock, South Hot-Cell, Development, TM3, UCx#44, Inspection of TM3 and UCx#44 after no-protons run MicrosoftTeams-image_(61).pngMicrosoftTeams-image_(62).pngMicrosoftTeams-image_(60).pngMicrosoftTeams-image_(63).png

TM3 and UCx#44 ran in ITE but issues with the cyclotron prevented proton beam delivery. Nonetheless, the target was heated and provided stable beam to TITAN as well as for tuning and some tests.

Results of inspection of TM3 module after run:

The module looked pretty good. There were no marks on the polished surface of the containment box, next to the water blocks, that were visible. But we didn't remove the box, only looked with the camera and it was visible by turning the module. So some things may have been hidden. There were some black marks on the door, near the bolts that hold in the handle (see attachment). This seems a very unlikely spot for sparking as the fields should be considerably lower than at the target handles, lower down. Maybe the spots are from oil left on the door that had a chemical reaction? There is one very faint matching spot on the top of the copper trident connector, but it doesn't look much like a spark mark. The other two marks have no corresponding mark on the source tray. There were no marks on the ground electrode, or anywhere else on the source tray. There was a scuff on one of the trapezoidal insulators, but it could have happened during installation.

 

Results of inspection of the target after run:

The FEBIAD target developed the same cathode short we have seen on almost every FEBIAD we run online - a high resistance short from cathode to HVC that prevents voltage on the cathode. This time the short remained after cooling the target, and David measured 208kOhms with the ohmmeter on the module top (11kOhms with the megger). We used a multimeter in the hot cell to test after the target had been dismounted and we found no short. So it must be related to either the position of the target (upright vs face down) or time (a conductive trace on an insulator oxidizes and becomes non-conductive again) or some pressure/shaking during the de-installation.

There weren't many marks on the target - a faint mark near where the faint mark on the copper trident was observed, some marks on the EE which had no counterparts on the ground electrode. See pictures.

Entry  Wednesday, June 19, 2024, 14:16, David Wang, South Hot-Cell, Standard Operation, TM3, SiC #46, Tm3 electrical check with SiC#46 target at SHC TM3_with_SiC_46#_target_electrical_check_at_SHC.pdf

Tm3 electrical check with SiC#46 target  and HS line helium spray check at SHC. were done. everything is good. see attachment.

Entry  Wednesday, June 19, 2024, 14:11, David Wang, South Hot-Cell, Standard Operation, TM3, , TM3 has been moved from SHC to TCS. 

TM3 has been moved  from SHC to TCS.The move is smooth.

Entry  Wednesday, June 19, 2024, 08:10, David Wang, Waste Package/Ship, Development, , , 5 gallon spent target pail, spent target lifting long pole and hook assembly load test 

 5 gallon spent target pail, lifting long pole and hook assembly load test was done by Rupan, Keyur ,and David.  Load in pail 101 lbs, test time 10 minutes. No deform on pail( pail OD 29.8mm is not changed before and after test.  The test passed. Also 50 lbs load test on empty tray transit frame was done. The frame is good on test.  Rupan will have a test report on this job.

Entry  Tuesday, June 18, 2024, 15:16, Adam Newsome, Crane, Maintenance, , , Pail Handling Tool - Annual Inspection PXL_20240618_213742257.jpgPXL_20240618_213455575.jpgPXL_20240618_213626154.jpg

The pail handling tool which is used to move 5 gallon pails around the target hall was inspected by A. Newsome. The main tool was checked, but not the spare as it is currently in a disassembled and unusable state. The tool appears to be in good, working condition. The following items were checked.

  • Inspect structural integrity of long tube - check for bending, warpage, dents, cracks, rust/corrosion
  • Inspect structural integrity of hook assembly - check for bending, warpage, dents, cracks, rust/corrosion
  • Inspect fasteners - check all fasteners installed as per drawings, fasteners are tight (note: one fastener on crane interface subassembly was loose - all fasteners in these subassembly were tightened as a precautionary measure)
  • Inspect crane interface assembly - check for damage and wear where the tool connects to the crane
  • Check alignment - verify the tool connects to the crane and hangs vertically with no major misalignment (this step was not done - alignment is regularly checked during operations, and there was no concern as the tube was straight)

 Note: these tools are being inspected monthly by D. Wang and F. Song.

Photos can be found in G:\remote handling\Facilities and Projects\ISAC\Pail Handling Tool\Inspections\June 2024

IMPORTANT: the maximum load capacity and lifter tag for the tool are not present. There is a plan in place to affix these two labels in the very near future.

Entry  Tuesday, June 18, 2024, 15:04, Adam Newsome, Spent Target Vault, Maintenance, , , Annual Inspection of Main and Mini Storage Vaults  PXL_20240618_213819000.jpgPXL_20240618_213905146.jpg

The annual inspection of the main storage vault will be skipped this year since extensive inspection and testing was performed during the re-alignment job in May (see this e-log for details: e-log 2584). This included successful testing of the emergency close mechanism.

The mini storage vault was informally inspected by Adam Newsome on 2024-06-18. The following was checked:

  • Cabling and cable management
  • Connectors (note: the strain relief for the remote control input cable was loose - it was tightened)
  • Controls box - external connectors and wiring
  • Limit switches - wiring, mounting
  • Motor visual check
  • Drive wheels visual check
  • Drive track visual check (note: the track had small pieces of metal shavings on it which were wiped off)
  • Bearings visual check
  • Miscellaneous fasteners visual check

Photos can be found in G:\remote handling\Facilities and Projects\ISAC\Mini Storage Vault\Inspections

The inspection was generally successful. No areas of concern. Regular inspection will resume next year.

Entry  Tuesday, June 18, 2024, 11:59, David Wang, South Hot-Cell, Standard Operation, TM3, , Tm3 electrical check without target. TM3_without_target_2024_june_18.pdf

Tm3 electrical check without target is done. Everything is good including 2 x 5 pin connectors( all OL at 250 V to 60 KV and each other)  see attachment.

Entry  Monday, June 17, 2024, 17:24, Carla Babcock, ITE, Development, TM3, UCx#44, Status of gas system prototype in ITE schematic_pumpinggaslines_detailed.png

A new gas system for FEBIAD operation was installed in ITE to enable us to use a calibrated leak which is attached to the target heat shield. This will allow us to control the quantity and purity of the gas going into the system, and to switch quickly between gasese and pressures.

The schematic of the system is attached. The use of the ballast container is likely not needed - it was originally included in case we want to run the system at pressures greater than 1 ATM. The roughing pump inlet limit is 1ATM, so it was envisaged to used the ballast container to reduce the pressure to that level or below before opening the system to the pump. But since it has been difficult to commission the system over 1ATM and this opens the door to several concerns about gas leakage, it was deemed better to keep operation below 1 ATM. This tank will likely be removed.

The storage tank was implemented because we are not sure if irradiated gases will be pulled out of the target lines when we pump on them, and so this was devised as a way to test that. The alternative is to have the exhaust of this pump go directly into nuclear ventilation by way of a plastic tube leaving the faraday cage, however this solution is also quite some work to implement. So the consensus was to start with the storage tank and sample it several times to understand what sorts of radioactivity we are dealing with, then make a decision about future operations.

This system has been tested offline using the development target UCx#44 and appears to work well. Unfortunately there were no protons available for this beam time so the gas sampling part of the system was not tested.

The operation of the rest of the system worked reasonably well. Beam disappeared when pumping out the lines and reappeared when re-opening the gas bottle. It seems that the storage container can be used to pump out the lines about 7 times before it gets up to around atmosphere, as was estimated based on volume. The pump can get the lines down to about 250mTorr as read by the pressure gauge DG2 on the module top, given about 30mins of pumping.

We did have some issue with the gauges, HV sparks destroyed both controllers and so we were unable to monitor pressures as we would have liked. It is possible one gauge itself is broken as well, to be investigated.

It may be that the gas leak we used was too small, but the idea of changing the pressure on the module by changing the needle valve didn't seem to work. This is not sure since we didn't have a reading on the pressure, but watching the ion beam as you turn the gas back on seemed quite binary. You would see no change until you had the needle valve fully open. This may be different with a larger leak, since this leak required about 1ATM in the lines to see anything. It is still not clear why this behaviour was different than the tests at the test stand, in which 0.5ATM of upstream pressure produced about 2nA of beam.

This system is considered a prototype and is not turned over to ops for operation. Further commissioning is required.

Entry  Monday, June 17, 2024, 07:36, David Wang, ITE, Repair, , , IG1S elbow oring seal and a blabk off cap oring seal beside the elbow were replaced on ITE entrance module top.. 

IG1S elbow o ring seal and a blank off cap o-ring seal beside the elbow were replaced on ITE entrance module top last Friday. IG1s has a higher than normal reading so i leak checked entrance module top last Thursday and found leaks to 5x E-8 atm.cc/sec leak on one of (or both of )these two o-rings seals. they are too close to identify exactly on which one was leaking so both o rings were replaced.  other air to vacuum seal on entrance module are leak free. 

Entry  Friday, June 14, 2024, 16:04, Carla Babcock, ITW, Repair, TM4, UC#45, Replaced and reinstalled electronics in ITW cage 

ITW has been behaving badly at higher voltages recently, even without protons on. I conditioned it up to 50kV with heaters off in the TCS and it was fine. But when I tried to do the same with heaters on in the station, it was quite sparky and it kept tripping the TGHT/TBHT. I went to 49kV where it was unstable, then lowered to 48kV where it looked fine for 30mins. But even operating at 40kV, it tripped the heaters several times. The TBHT voltage came back lower than before on the last trip, so I am getting worried about it.

I decided to make sure all the electronic spark protection was ok in the faraday cage. There is a resistor/gmov combination across the terminals of each TGHT/TBHT in which Tomislav replaced the gmovs for me because his tester did not work at those low voltages, so we couldnt see if they were broken. The electronics diagram called for 18V gmovs, the replacements are 22V because that's all we have.

We also tested and re-installed the capacitor-gdt-resistor combinations that John installed last year from TGHT/TBHT bubars to HV common. I originally removed them because we couldn't bias a FEBIAD with them on - this still has to be investigated. The measured values are 0.148uF, 90kOhms and a breakdown voltage on the gdt of 410-450V.

Hopefully this prevents sparking the power supplies off.

 

Sunday, June 16, 2024, 07:03 : power supplies have not tripped off since electronics repair. See data/TM4sparkingbehaviour_June152024.dat for sparking frequency over ~10hrs of protons (5-14uA). >14 sparks during this time (14 captured by PLC when voltage dropped, many more current peaks).

Entry  Friday, June 14, 2024, 11:56, David Wang, ITE, Standard Operation, TM3, UCx#44, Tm3 has been moved form ITE to SHC. 

Tm3 has been moved form ITE to SHC. the move is smooth.

Entry  Friday, June 14, 2024, 11:55, David Wang, South Hot-Cell, Standard Operation, TM3, UCx#44, TM3 UCx#44 after operation electrical check at SHC  TM3_UCX#44_after_operation_electrical_check.pdf

TM3 UCx#44 after operation electrical check at SHC . see attachment.

Carla: Looks like the short on the cathode observed while trying to operate the FEBIAD in cathode-bias mode is still there. Will do investigations in the hot cell during disassembly.

Entry  Friday, June 14, 2024, 11:18, Frank Song, ITE, Standard Operation, TM3, UCx#44, module disconnection TM3_with_UCx#44_disconnection_in_ITE_2024-06-14.pdf

 TM3 with target UCx#44 was disconnected in ITE. 

Entry  Thursday, June 13, 2024, 11:44, David Wang, Conditioning Station, Repair, TM2, , Replaced several o ring seals on TM2 service cap. 

  couple of E-8 to low E-7 atm.cc/sec leak were found on TM2 service cap top air to vacuum  o rings.  Replaced these leak o ring seals including o ring on IG1 and steerer service panel,o rings on MSP, EE, D blue nylon and copper feed through, and o ring on a round blank off beside MSP terminal on second row. 

2024-july-03 update: TM2 was leak checked again at TCS. no air to vacuum leak on module top. i helium pressure tested(60psi) all water cooling lines (except HS) . They are leak free.

Entry  Wednesday, June 12, 2024, 10:18, David Wang, Conditioning Station, Standard Operation, TM2, , TM2 is moved from TCS to silo this morning 

TM2 is moved from TCS to silo this morning. The move is smooth.

Entry  Monday, June 10, 2024, 11:02, Frank Song, ITW, Standard Operation, TM4, UCx#45, shielding blocks transfer 

 5 shielding blocks have been transferred from ITE to ITW. 

Doc # 181007

 

Entry  Wednesday, June 05, 2024, 11:32, David Wang, Conditioning Station, Standard Operation, , , TCS water system filters have been changed.  

TCS water system  five filters were changed yesterday by plant group Dan.T. Service labels on filters are updated.  No water leak after job.

Entry  Wednesday, June 05, 2024, 11:25, David Wang, Conditioning Station, Standard Operation, , , refilled TCS:TK2 to 27.4 inches.  

refilled TCS:TK2 to 27.4 inches to compensate water lost during THC filters change.

Entry  Tuesday, June 04, 2024, 11:44, Carla Babcock, South Hot-Cell, Development, , empty LP FEBIAD, investigation of cathode short on empty LP FEBIAD MicrosoftTeams-image_(58).png

On May 30 Aaron, Chad and I removed the empty LP FEBIAD target from the SHC into the anteroom to attempt to find out the source of the cathode short observed online. The behaviour online was that a connection of several hundred ohms was preventing the cathode from being biased. The resistance was still enough to allow us to run in anode mode, which is what we did. I am not sure where the cathode short came from but there was significant sparking on this module when ops conditioned it (destroyed the gmov of the COIL power supply and the electronics for anode/cathode switching) and we have seen this cause cathode shorts before. The shorted behaviour did not go away when the target was cooled down, so I assume it was permanent damage to one of the insulators. This would be either the support insulator, the trident insulator, the gas line insulator or one of the tube retainer insulators.

Since the target didn't see protons, we decided to take it out of the hot cell and disassemble it to find which insulator was broken. Unfortunately, it appeared totally fine outside of the hot cell, no shorts could be found. We disassembled it anyway to look for issues but all we saw was a heat mark on the copper plates covering the coil, underneat the target (see attachment). We even shook the target quite a bit, and didn't produce a short.

Maybe there was a trace created on one insulator by the sparking, which oxidized when exposed to air and became insulating again? We didn't see anything obvious on the insulators, but I'm not sure if we would expect to.

No conclusions from this work.

Entry  Thursday, May 30, 2024, 11:08, David Wang, Conditioning Station, Standard Operation, TM2, , TM2 was moved from silo to TCS yesterday morning. 

TM2 was moved from silo to TCS yesterday morning. The move is smooth.    TCS vacuum system was started after. TCS and TM2 pumping down is ok so far.

Entry  Tuesday, May 28, 2024, 13:49, Frank Song, ITW, Standard Operation, TM4, UCx#45, Module Connection TM4_with_UCx#45_connection_in_ITW_20240528.pdf

 TM4 with new target UCx#45 was connected in ITW this morning. pls see attachment uploaded with.

Entry  Tuesday, May 28, 2024, 10:13, David Wang, ITW, Standard Operation, TM4, UCx#45, Tm4 has been moved from TCS to ITW.  

Tm4 has been moved from TCS to ITW.  the move is smooth.

Entry  Tuesday, May 28, 2024, 07:45, David Wang, Conditioning Station, Standard Operation, TM4, UCx#45, TCS was argon vented this morning between 6:00 and 7:30am.  

TCS was argon vented this morning between 6:00 and 7:30am for TM4 moving to ITW.

Entry  Friday, May 24, 2024, 08:10, chad fisher, South Hot-Cell, Standard Operation, TM4, UCx#45, UCx#45 Installation 

On Wednesday, May 22, 2024 UCx#45 was installed on TM4 in the SHC. Installation was normal other then minor issue with the multipin connector drive screw not engaging and/or driving properly. This was remedied by loosening the left guide bolt slightly (1/2 turn). After loosening the multipin drove in and seated correctly (verified by camera). High current fasteners torqued to 130 in lbs.

Entry  Thursday, May 23, 2024, 11:10, David Wang, MAA, Standard Operation, , , BL2A MAA ASU test. 

MCR Travis Curucz and I finished BL2A MAA ASU test per document 154779. everything works fine. Travis kept  the test document.

Entry  Thursday, May 23, 2024, 10:59, Frank Song, ITE, Standard Operation, TM3, UCx#44, shielding blocks transfer 

 the five shielding blocks have been moved from storage area to ITE and is ready for beam delivery.

submitted WP# I2024-05-22--1

actived  WP # I2024-05-23-4

Entry  Wednesday, May 22, 2024, 12:43, David Wang, South Hot-Cell, Standard Operation, TM4, UCx#45, electrical check and leak check were done on TM4 UCx#45 target at SHC. Scanned_from_a_Xerox_Multifunction_Printer.pdf

electrical check and leak check were done on TM4 UCx#45 target at SHC.  everything is ok. See attachment

helium pressure test on TM4 HS line at TCS is done.   No leak.

Entry  Wednesday, May 22, 2024, 12:32, David Wang, South Hot-Cell, Standard Operation, TM4, UCx#45, TM4 has been moved from SHC to TCS. 

TM4 has been moved from SHC to TCS. the move is smooth.

Entry  Tuesday, May 21, 2024, 11:46, David Wang, ITW, Standard Operation, TM4, LP febiad empty. , Tm4 has been moved from ITW to SHC. 

Tm4 has been moved from ITW to SHC. the move is smooth.

Entry  Tuesday, May 21, 2024, 09:50, David Wang, ITW, Standard Operation, TM4, Lp Febiad empty, Tm4 has been disconnected in ITW. TM4_with_Lp-Febiad_empty_target_disconnection_in_ITW_2024-05-21.pdf

Tm4 has been disconnected in ITW per document 141576. Checklist is done.  HS line is purged.

Entry  Wednesday, May 15, 2024, 10:06, Travis Cave, Spent Target Vault, Standard Operation, , UC#38,40 Ta#62,63 SiC#44, Targets moved to the mini vault. Mini_Vault_Index_2024-05-15.pdfTarget_Index_2024-05-15.pdf

 Targets UC#38,40 Ta#62,63 SiC#44 have been moved from the spent target vault to the mini vault in preparation for F-308 loading. See attached PDFs for details.

Entry  Tuesday, May 14, 2024, 15:27, Carla Babcock, ITE, Development, TM3, UCx#44, TM3 conditioning and testing in ITE Screenshot_from_2024-05-14_10-47-22.png

Tuesday, May 14, 2024, 10:26 :

Ramping up bias/EE/EL on ITE - will see if the HV cage in the pit can hold 60kV or not.

At around 50kV the bias read current starts to get jumpy. Doesn't look like its an issue for the voltage, but definitely instability increases.

Screenshot_from_2024-05-14_10-47-22.png

Occasional sparks seem to increase the EL current significantly...

David heard some sparks in the target hall. Looks like from heat shield feed through to the top of the cage. Several sparks heard in the TH also changed the einzel lens draw current significantly. These feethroughs are not far from each other so could be related.

Apparently the sparking also tripped off all the optics and heaters in ITW, by changing the state of the water flow interlock. Interesting and not seen ever before. Will test again with the cage off, rather than risk tripping ITW again.

Tried ramping up the voltage on just the EE. Seems the limit is 7kV - at that level it gets sparky and unstable. Should be investigated (should hold 10kV) but not critical for module function.

 

Wednesday, May 15, 2024, 10:05 :

HV cover was removed this morning and the MAA was locked out.

Started ramping things up, was very easy until around 58kV. At 59.5kV a spark tripped off the EL. Canbus controller had to be power cycled to fix it. Bias current is much more stable in this configuration.

Ramped up again while listening from the TH to see if it was sparking outside. Went slowly to 60kV (left EL at 29kV) and didn't see any outside sparks in the first 10 mins, couple sparks in vacuum. But after 15 mins a spark seems to have fried the EL canbus card. We were not in the TH so not sure if it was on the outside or not.

After 2 hours a spark tripped off both ITE and ITW. Looks like it makes a water interlock go bad momentarily, but after the trip the interlocks seem fine.

 

Tuesday, May 28, 2024, 16:41

Running TM3 at any voltage in ITE produces fairly destructive sparks. There are not many but so far they have tripped off all optics in ITW, the water flow interlocks (later forced on to prevent this), the EL (generally comes back but killed the canbus card once), destroyed two vacuum gauge controllers, and may have contributed to the cathode short on ITE-TM3-UC44-LP-FEBIAD.

The conditioning process seems to go as planned, but the occassional inevitable spark still trips things, which is making it difficult to run stable.

Will continue with regular HV conditioning to see if this helps. Control over the current limit on the ITE:BIAS supply would also help, but seems a complicated thing to add according to Roberto.

 

TM3 sat fine at 53kV overnight and at 58kV for several hours. The EZL trips off maybe once every 2-3hrs or so, which is not ideal but liveable. This was with the TGHT and CHT power supplies forced, so not sure if we would know if they would have tripped...

 

CONCLUSIONS:

  1. TM3 has been commissioned for beam delivery after one week of delivery of UF to TITAN using a FEBIAD ion source in anode bias mode. Cathode mode was also used, so all functionality of the target except IGLIS current/voltage delivery through the mutlipin has been tested successfully.
  2. TM3 still requires commissioning at high voltage with protons to be considered fully commissioned, this will be done July 2 2024 due to problems with the cyclotron.

 

Entry  Monday, May 13, 2024, 09:28, David Wang, ITE, Standard Operation, TM4, UCx#44, ITE water signal annual interlock check. 

ITE water signal annual interlock check is done. Ed helped me on this check. Everything works normal.

Entry  Friday, May 10, 2024, 09:04, David Wang, ITE, Standard Operation, TM3, UCx#44, Tm3 has been connected in ITE.  Scanned_from_a_Xerox_Multifunction_Printer.pdf

Tm3 has been connected in ITE.  see attachment.

Entry  Thursday, May 09, 2024, 13:52, Riley Sykes, Waste Package/Ship, Standard Operation, , , F308 Service/Inspection 

 F308 Inspection and service complete on #06, #08, #13, #15, #16, #19, #20, #21, #22.

All in good condition with new gasket material installed on #20.

Prepped for move to ISAC B3 for storage.

Entry  Wednesday, May 08, 2024, 14:01, Frank Song, ITW, Maintenance, , , Annual clean up for ITW Faraday cage  

The ITW Faraday Cage has been cleaned, this is part of Winter Shut Down job happens in ISAC-1 Electric maintenance room annually.

Entry  Wednesday, May 08, 2024, 12:37, David Wang, ITE, Standard Operation, TM3, UCx#44, Tm3 has been moved form TCS to ITE 

The move is smooth and successful.

Entry  Wednesday, May 08, 2024, 12:36, David Wang, Conditioning Station, Standard Operation, TM3, UCx#44, TCS was argon vented this morning between 7:00 to 8:30 am. 

TCS was argon vented this morning between 7:00 to 8:30 am before module was moved to ITE.

Entry  Tuesday, May 07, 2024, 12:39, Eric Lahe, Spent Target Vault, Repair, , , ISAC Storage Vault Re-alignment Testing_and_updates_to_storage_vault_2024-05-01.pdf

 

ISAC Storage Vault Door Re-alignment (April-May 2024) 

Issue

  • Rollers gouging and marking on roller supports, testing shows door shifts at least 185 thou on structural beam when fully open vs. fully closed
  • door misaligned: 1/4" laterally, slight rotation (~1/16" difference across closed door gap).

 

Repair

  • Moved left structural beam (facing front of door) inward 1/4" at post.
  • Loosened drive system to shift door over via crane to average laterally (1/8" shift) towards center,
  • Attempted to fix door rotation with crane, door would not settle down perfectly flush, but got slight improvement 
  • Adjusted limit switches for fully open and closed (due to the adjustments made previously, needed to realign limit switches) - adjusted flag for final close back by ~1/4"; adjusted limit switch at back of vault forward ~1/4" 

 

Verification 

  • Unloaded vault door actuation tested multiple times with no issues, door returned to same position every cycle, no interferences during travel
  • Vault Door actuation tested with trays 4 and 6 engaged, no issues
  • All pails accessible when open
  • Tested open and closed limit switches: the open limit switches are working properly; the closing soft and hard limit switches are slightly close together, causing the door to just "bump" the vault when closing, The scale of this is OK for current operation, will be adjusted when the ISAC Target Hall Controls Overhaul is done
  • Tested and reset Emergency override mechanism - works properly

 

Outstanding Tasks

  • Will paint marks on structural supports to track if problem reoccurs - update ELog when complete 

 

System State: Operational

See attached file for details

 

 

Entry  Tuesday, May 07, 2024, 09:47, David Wang, ITE/ITW, Maintenance, TM2, , Broken TM2:TP2 has been replaced.  

Broken TM2:TP2 has been replaced otday by a new TV-1001 nav pump supplied by vacuum group. replaced pump seris number:201281. new pump series number:IT23431008. TPs replacement history sheet will be updated by Frank. I will put comment on this e fault and let operator to close it.

Entry  Friday, May 03, 2024, 12:20, Travis Cave, Spent Target Vault, Standard Operation, , Ta#66, Target repacked Target_Index_2024-05-03.pdf

 The Ta#66 target was repacked after the parasitic target was removed it was place in a new pail (#290) and place back in spot 5B of the vault. See attached PDF for further details.

Entry  Thursday, May 02, 2024, 18:48, Carla Babcock, ITW, Standard Operation, , , ITW cage setup 

ITW gas lines pumped down to 2e-3Torr on leak detector with leak rate in the low e-7 atm-cc/s. Gas bottles opened at 3psi and labels in epics changed to reflect correct setup. switch box set to cathode mode, checked that anode wire was at HV common.

note ballast is removed from ITW now to be used in ITE so that line is blanked off.

Entry  Thursday, May 02, 2024, 15:23, David Wang, South Hot-Cell, Development, TM3, , Leak check on TM3 new containment box window line VCR fittings.  

After new containment box installation on TM3, Chad and I did a helium spray leak check on two VCR fittings on front side water lines. they are leak free.

Helium pressurize window water line to 70 psi for 3minutes. No response on leak detector which is 0.0xe-9 atm.cc/sec.

Entry  Thursday, May 02, 2024, 14:58, David Wang, South Hot-Cell, Standard Operation, TM3, UCx#44, TM3 with UCx#44 electrical check and leak check. Scanned_from_a_Xerox_Multifunction_Printer_(11).pdf

TM3 with UCx#44 electrical check and leak check are good. see attachment.

HS line 70 psi helium pressure test at TCS: no leak at 0.0xe-9 torr.

Entry  Thursday, May 02, 2024, 14:54, David Wang, Conditioning Station, Standard Operation, TM3, UCx#44, TM3 has been moved from SHC to TCS. 

TM3 has been moved  from SHC to TCS by David and Frank. The move is smooth.

Entry  Thursday, May 02, 2024, 09:00, David Wang, ITW, Standard Operation, TM4, , Annual ITW water signal interlock check has been done.  

Annual ITW water signal interlock check has been done. Renee helped me on it. Everything works fine.

Entry  Wednesday, May 01, 2024, 14:51, David Wang, South Hot-Cell, Standard Operation, TM3, , Tm3 has been moved form TCS to SHC. 

Travis and I moved TM3 from TCS to SHC this afternoon. The move is smooth.

Entry  Wednesday, May 01, 2024, 09:50, David Wang, ITW, Standard Operation, TM4, , TM4 has been connected to ITW. Scanned_from_a_Xerox_Multifunction_Printer_(10).pdf

TM4 has been connected to ITW. see attachment.

Entry  Tuesday, April 30, 2024, 09:20, David Wang, ITW, Development, TM4, , A new SST gas line is using for ITW febiad gas staion in pit. 

A new SST gas line with swagelock tube fittings and VCR fit is using for ITW febiad gas staion in pit. Gas line is leak checked on bench. No leak . it is installed on TM4 in ITW now,

Entry  Tuesday, April 30, 2024, 08:00, Frank Song, South Hot-Cell, Standard Operation, TM4, Lp-Febiad empty, electrical check/leak check TM4_with_Lp-Febiad_empty_target_checking_on_SHC_2024-04-29.pdf

 David Wang made E/L checking before module moving to ITW. read attachment pls.

Entry  Monday, April 29, 2024, 14:21, David Wang, ITE/ITW, Standard Operation, TM4, , TM4 has been moved from SHC to ITW. 

TM4 has been moved from SHC to ITW. Peter did the move. Travis helped on him.   The move is successful.

Entry  Saturday, April 27, 2024, 09:35, Carla Babcock; Alexander Shkuratoff, Conditioning Station, Development, TM3, , TM3 source and service tray testing 

Saturday, April 27, 2024, 09:35 :

Started ramping up HV, EE and EL together. First small spark at 20.5kV on bias, no reaction in other devices.

Note both BIAS and EL are off in their readbacks. See table below

BIAS set pt BIAS readback BIAS actual EL set pt EL readback EL actual
24 24.4 24.5 14 13.42 14
30 30.52 31 16 15.34 16
35 35.6 36 19 18.2 19
40 40.65 41.5 20 19.16 20
45 45.8 46.5 22 21 22
50 50.8 51.5 25 23.9 25
55 55.9 57 27 25.84 27
60 60.95 62.5 30 28.7  
62  63  64.5      
66 67.1 68.5      
67 68  69.5      
69 70.1 71.5      
70 71.1 ??      
70.5 71.7 73      

Saturday, April 27, 2024, 10:23 :

Spark on HV only at 25.5, couple sparks from here to 33, then at 33 starts real conditioning.

EL is reacting to some of the sparks, not sure if this is just electrical noise or not.

Saturday, April 27, 2024, 18:14 :

lots of trips above 60kV on the set pt. tripping off turbos and gauges. IG2 needed the controller reset.

 

RESULT: Got to 64.5 (actual) 62 (set point) with quite a bit of sparking over 60kV. Will go the rest of the way to 73 in the next days. Data dumped as isac/data/TM3_HVtests_Apr272024.dat

 

Sunday, April 28, 2024, 11:23 :

Ramped back up to 60kV reasonably easily, couple sparks and turbo trips.

Went up to 64kV (set point) with a lot of difficulty. Data dumped as isac/data/TM3_HVtests_Apr282024.dat

 

Monday, April 29, 2024, 14:58 :

Ramped up to set pt 62 easily, went down to 500V then 100V steps after that.

Went to set pt of 67 and left it there for ~40mins. Not perfectly stable but not too bad.

 

Tuesday, April 30, 2024, 17:12 :

After rebooting the TCS PLC to fix all the non-responsive devices, everything is working fine again.

Ramped easily to 60kV in 1kV steps.

Still got to 67 without too much trouble. Behaving pretty well...

At 70.2 (set pt, 71.3 readback) the water and vacuum gauge both tripped off and cannot be restarted. I am not sure what the real power supply reading is here but in the past it has been 70.5 set pt = 73 real value, which is as high as the power supply goes.

Stopping here since I'm not sure the water is circulating... the off pump says it is and the on pump says its not... left it at 70.2 for 40mins, still sparking going on (20:28 to 21:10)

Data dumped as isac/data/TM3_HVtests_Apr302024.dat

 

Sunday, May 05, 2024, 10:50 :

Containment box and target installed.

HV conditioning starting at 47kV.

Spark at 58kV knocked out IG1. Continuing with IG2 and IG1S.

Went up to set point of 63, readback 64. Will continue on Monday.

Data dumped: isac/data/TM3_HVtests_May52024.dat

 

Monday, May 06, 2024, 09:37 :

Ramping system back up.

First sparks at 50kv while raising the EL voltage (not sure if they are related).

AS: Voltage quickly up to 63 kV from 49 kV. Very smooth, no sparks or instabilities. Ramped at around 250 V steps every 10-20 seconds. First signs of instability at ~62.75 kV and definitely at 63 kV. I guess this is where it was conditioned to last. Let sit at 63 kV for a while while doing something else. It sparked once and turned off a turbo after half an hour. Starting ramping again.

AS: Spark at 65.75 kV killed IG1. Carla manually reset at 69 kV. Still working. A spark at 70.25 kV took out IG1 again.

AS: Maximum voltage reached at about 16:45. Setpoint 70.5 kV, readback 71.7 kV, PS itself ~73 kV. Carla reset IG1.

AS: 18:30, spent about 1.5 hours cumulatively at this maximum voltage. During this time it sparked about 15 times. Not long enough to tell if the spark frequency is decreasing. In the middle of this, Carla did something accidentally and caused the voltage to drop a bunch, so I manually set it to 0 V. She then reset TP1S, which was not staying on. Also, the EE and EL stayed at their respective voltages during this downtime (2 kV and 28.7 kV). I ramped the main BIAS voltage back up to the maximum voltage within 5 minutes and it was smooth all the way but sparked again at the maximum voltage. It seems conditioned up to or near the max voltage. Ramped down and turned off BIAS, EL, and EE.

AS: Dumped data to isac/data/TM3_HVtests_May62024_Alexander.dat

 

Tuesday, May 07, 2024, 10:02 :

Tested the EE - ramped up easily to 7kV, but then had issues maintaining the voltage. No vacuum response. Ramped down since we never use it that high anyway, though cable should be good for 10kV. More investigations later.

 

EDIT 2024-11-25, Alexander Shkuratoff:

Summary of StripTool data taken during this round of tests:

[   ] TM3_HVtests_Apr272024.dat 2024-04-27 18:56 12M
[   ] TM3_HVtests_Apr282024.dat 2024-04-28 13:16 1.4M
[   ] TM3_HVtests_Apr302024.dat 2024-04-30 21:11 9.0M
[   ] TM3_HVtests_May52024.dat 2024-05-05 13:06 5.0M
[   ] TM3_HVtests_May62024_Alexander.dat 2024-05-06 18:45 9.5M

 

Entry  Friday, April 26, 2024, 13:22, David Wang, South Hot-Cell, Standard Operation, TM4, , TM4 has been moved from SMP to SHC. 

TM4 has been moved from SMP to SHC. Adam and I did the move. the move is smooth.

Entry  Friday, April 26, 2024, 08:59, David Wang, Conditioning Station, Development, TM3, , TM3 helium pressure test and electrical check with new source tray at TCS. Scanned_from_a_Xerox_Multifunction_Printer_(9).pdf

TM3 helium pressure test and electrical check with new source tray at TCS were done yesterday. The results are excellent. See attachment

Entry  Friday, April 26, 2024, 08:56, David Wang, Conditioning Station, Development, TM3, , TM3 module top helium spray leak test.  

TM3 module top helium spray leak test was done yesterday.  No leak on TM3 module top @ LD base leak rate 0.0 x E-9 atm.cc/sec.

Entry  Wednesday, April 24, 2024, 10:15, David Wang, Conditioning Station, Standard Operation, TM3, , TM3 has been moved from SHC to TCS. 

TM3 has been moved  from SHC to TCS. The move is smooth.

Entry  Tuesday, April 23, 2024, 17:34, Carla Babcock, South Hot-Cell, Repair, TM3, , TM3 wire pulling 

Wires were pulled in TM3 and service cap was closed up again:

Einzel lens wire (30kV kapton), routed in the pumping duct and attached with #10 ring tongue to EZL feedthrough in service cap

4 steerer wires, routed in th pumping duct and attached with push on connectors to the 4 SHV feedthroughs on the module side panel. Coax grounding sheath is cut back by about 3cm.

Multipin cable bundle #1, routed through the left cable tube in the service tray then along the heat shield water lines (with PEEK zip ties) to feedthrough A.

Multipin cable bundle #2, routed through the right cable tube in the service tray then along the heat shield water lines (with PEEK zip ties) to feedthrough B. This bundle contains the EE wire as well, which was branched out after exiting the service tray and routed along the gas lines to the EE feedthough. It was attached with a smaller (size?) ring tongue to the EE feedthrough. Do not use this wire again, very fragile. Use the Accuglass 30kV wire instead.

 

The multipin wires touch the back of the water blocks in the source tray (same as in MT2/4, so far no issues with that) and they also touch the COIL lines in the service cap.

The EZL and steerer wires are routed along the floor of the service cap.

Due to the difficulty of the installation, there is no metal braid over the multipin bundles in the service cap.

Photos here : https://triumfoffice365-my.sharepoint.com/:f:/g/personal/cbabcock_triumf_ca/EslWNUST-UJKh1s8jjxWG6EBpLQEnWxgV4v-NvR4ZJjlOQ?e=Mw5vvI

Entry  Friday, April 19, 2024, 10:44, David Wang, South Hot-Cell, Development, TM3, , TM3 water lines helium spray leak check at SHC. Scanned_from_a_Xerox_Multifunction_Printer_(7).pdf

TM3 water lines helium spray leak check at SHC is done. No leak has been found on all lines. seeattachment

Entry  Wednesday, April 17, 2024, 11:58, David Wang, ITE/ITW, Maintenance, , , ITH:MP1S pump inside lubricant was changed today.  

ITH:MP1S pump inside lubricant was changed today. old lubricant is dirty with dark color. they are stored in sealed waste oil jug and stored in silo area. Pump has been installed back and started. It works fine.

Entry  Tuesday, April 16, 2024, 12:33, David Wang, Conditioning Station, Standard Operation, , , test TCS water system chillers stage in/out.  

Monday and Tuesday, I started TCS water system and enabled the TCS chillers auto stage in/out. I saw chiller 2 in/out three times at 17C and 21.8C without issue.   TCS water system works fine. The test is finished.

Entry  Thursday, April 11, 2024, 06:27, David Wang, South Hot-Cell, Development, TM3, , TM3 new source tray was transferred into SHC on this Tuesday.  

TM3 new source tray was transferred into SHC on this Tuesday. one hook arm of transfer jig is very close to optic tray tube when engaging the jig on transfer frame. tube side hook arm should go east side a little bit further to avoid the tube.  Also the HS tube top lines to  transfer frame beam bottom distance needs to be watched closely when hooking on the frame.Help from HC window is necessary. By watching on this details, Source tray are successfully moved into SHC with crane controlled locally in TH.Transfer frame was retrieved back to TH. It was cleaned, bagged and stored in TH.

Entry  Thursday, April 11, 2024, 06:07, David Wang, South Hot-Cell, Standard Operation, TM3, , Tm3 was moved from silo to SHC yesterday. 

Tm3 was moved from silo to SHC yesterday. the move is smooth.

Entry  Monday, April 08, 2024, 09:29, David Wang, Cooling, Standard Operation, , , HALCW system general inspection.  

water are supplied to both ITE and ITW. I did a general inspection on HALCW system. Two small leaks on 2" shut off valves are fixed. No other leak has been found so far. all water flow meters work fine. MP2 pump discharging pressure is ok which is just above 100 psi on local gauge reading. pump noise are low. pump body temperature is less than 45C which is good. 

Entry  Thursday, April 04, 2024, 13:10, David Wang, Cooling, Maintenance, , , high active water refurbishment, reinstallation, and test operation.  

both high active pumps ITC:MP1 and MP2 are refurbished by RH group Maico and Peter. Pumps have been installed back to system with new inlet/outlet flange gaskets. high active water surging tank is refilled with water and pumps were primed. I asked operator to switch on pumps separately. Both pumps work fine. They are quiet and pumps discharging pressure is a little bit better comparing to before refurbishment. Nitrogen gas is injecting into system. O2 level is decreasing and R is going up.

2024-04-09: Joel.S checked pumps phase current draw: MP1 16.8 to 17.1A on each phase. MP2 17.0 to 17.2 A on each phase. They are normal. Pump body temperature are below 45C which is fine. 

Entry  Wednesday, April 03, 2024, 10:48, chad fisher, South Hot-Cell, Maintenance, , , SE Manipulator wrist swap original_but_incorrect_cable_routing_E-HD_manipulators.JPG

On April 2, 2024 the wrist on the SE manipulator of the SHC (Serial # 7986) was swapped with a rebuild unit originally from SW position (serial # 8106). The "new" wrist was a wrist + tong assembled unit with the tong cable being routed if-front of the spacer A-14118 rather then behind as in all previous replacements (see attached pictures). This change was a result of a discussion with Central Research's senior repair technician who informed us that the original routing was incorrect from the factory. This can be seen when inspecting unit we have on-site that are still in the original configuration from the factory as about half are routed one way and half the other.

Entry  Thursday, March 28, 2024, 09:26, David Wang, South Hot-Cell, Standard Operation, TM3, , Tm3 has been moved from SHC to silo. 

Tm3 has been moved  from SHC to silo. The move is smooth.

Entry  Wednesday, March 27, 2024, 09:52, David Wang, ITE, Standard Operation, , , ITE entrance module top and module flange o-ing to tank have been leak checked. 

ITE entrance module top and module flange o-ing to tank have been leak checked. no leak at 0.0xe-9 atm.cc/sec. things are double checked.

Entry  Wednesday, March 27, 2024, 09:49, David Wang, South Hot-Cell, Standard Operation, TM3, , Tm3 has been moved to SHC from silo. 

Tm3 has been moved to SHC from silo. the move is smooth.

Entry  Monday, March 25, 2024, 10:55, David Wang, ITE, Standard Operation, , , ITE entrance module has been reconnected in ITE pit.  

ITE entrance module has been reconnected in ITE pit per document 190510.

Entry  Monday, March 25, 2024, 10:53, David Wang, ITE, Repair, , , ITE entrance module has been moved from TCS to ITE. 

ITE entrance module has been moved from TCS to ITE. The move is smooth.

Entry  Thursday, March 21, 2024, 11:35, Ferran Boix Pamies, ITE, Development, , , Wiring of new thermocouple PLC module 

 Thursday, March 21, 2024, 11:33 Three channels are available now for thermocouple readouts from the Target multipin. Wiring from the PLC modules to the connection terminal blocks and labeling done.

Entry  Friday, March 15, 2024, 10:04, Adam Newsome, South Hot-Cell, Standard Operation, TM3, , TM3 Move - SHC to NE Silo 

TM3 was moved from SHC to NE silo. Cable tray was recently installed.

Entry  Thursday, March 14, 2024, 14:54, David Wang, ITE, Maintenance, , , ITE entrance module has been moved from ITE pit to TCS.  

ITE entrance module has been moved from ITE pit to TCS. The move is smooth.ITE entrance module top tank flange and o ring slot are cleaned, and old o ring are replaced.

Entry  Wednesday, March 13, 2024, 11:12, Keith C Ng, Assembly/Bench Test, Repair, TM3, , optics tray for tm3 20240313_optics_tray_alignment_notes.pdf

Alignment notes attached for the optics tray for the refurbished tm3 with the new service and source tray.

 

*Note: Drive screw bracket sheared off during alignment check with source tray. The drive bracket was replaced. The optics tray was re checked. The front element was .015 to left and centered u/d. The rear element remained the same. The center element could not be checked to do the assembly.

Entry  Friday, February 23, 2024, 06:36, David Wang, ITE, Maintenance, , , ITE entrance module has been disconnected. 

ITE entrance module has been disconnected per document 190510. Its a preparation job for next month module moving out to SHC.

Entry  Friday, February 16, 2024, 11:48, David Wang, Cooling, Maintenance, , , high active water transferr to holding tank 

100 liters of high active water from HALCW system( mostly from s-tank and pipe lines closing to pumps) are transferred to holding tank in 2A tunnel. Transfer is smooth.  it is a preparation job for ITC:MP1/MP2 refurbishment.  water sample is passed to RPG for assay.

Entry  Friday, February 16, 2024, 10:57, Adam Newsome, Spent Target Vault, Standard Operation, , , F-308 flask loading - three flasks loaded Target_Index_2024-02-16.xlsm

Today (2024-02-16), three flasks were loaded in preparation for shipment with the following targets: UCx#39, UCx#41 and C#3.

Note: prior to shipping, the pails within these flasks will need to have a crimped lifting loop added to them.

The mini-storage vault is now EMPTY.

The target index spreadsheet has been updated.

Entry  Thursday, February 15, 2024, 17:40, Carla Babcock, ITE, Standard Operation, , , ITE annual HV testing 

ITE was set up for HV tests - this time the module plug was not in so the BIAS and EE had to be bypassed. NOTE: ITE:BIASPLC must also be bypassed for this to work. Currently it is located on the vacuum bypasses page, but may be changed to the optics page soon.

ITE was ramped to 60kV in steps of 1kV easily. It sat at 60 for about 1.5 hours with a current draw around 173uA. It was not entirely stable though, and appears to have sparked many times. None of them seemed very large, but hard to tell.

When ramping down, current dropped quickly with the first couple steps. Data saved as isac/data/ITE_HVtesting_shutdown2024

Entry  Thursday, February 15, 2024, 13:52, David Wang, ITW, Standard Operation, , , ITW entrance module and exit 1 module leak check after module move and tank flange orings replacement. 

 ITW entrance module and exit 1 module leak check on module service cap/top air to vacuum seals and module to tank flange  o-rings have been done. all seals and o rings are leak free to 0.0 xE-9atm.cc/sec except one leak ( to low E-6 atm.cc/sec) on ITW RV4 KF50 o-ring was found. It caused by a cross o ring surface scratch on KF 50 flange. the scratch was sanded and polished out. on second time leak check, it is leak free.

Entry  Wednesday, February 14, 2024, 11:34, Adam Newsome, Spent Target Vault, Standard Operation, , Misc., Three pails moved from main vault to mini vault Target_Index_2024-02-14.xlsm

In preparation for F-308 loading, three pails were moved from the main storage vault to the mini storage vault. The following pails were moved:

  • Pail 270 (C#3)
  • Pail 276 (UC#39)
  • Pail 231 (UC#41)

 

Target Index spreadsheet updated, attached.

Entry  Wednesday, February 14, 2024, 11:32, Adam Newsome, Spent Target Vault, Standard Operation, , UCx#43, Spent Target Move Target_Index_2024-02-14.xlsm

Spent target UCx#43 (pail 289) was moved from the South Hot Cell to the Storage Vault, placed in location 2A. Dose rate at 1m was approximately 22.6 mSv/hr.

Target index spreadsheet updated, attached.

Entry  Monday, February 12, 2024, 18:44, Carla Babcock, ITW, Maintenance, , , ITW annual HV testing Screenshot_from_2024-02-12_18-44-03.png

ITW was set up for HV testing - water is running and at a high resistivity due to injected N. Einzel lens is attached to ground. Everything else is as normal. The module plug is in so no vacuum bypasses were needed. Very easy to ramp to 60kV. Sat at 60 for about 1.5hrs with maybe 1 spark (hard to say from the strip tool data). Current draw was about 176uA. Data dumped as isac/data/ITW_HVtesting_shutdown2024

Entry  Friday, February 09, 2024, 12:52, Adam Newsome, Spent Target Vault, Standard Operation, , , F-308 flask loading - five flasks loaded Target_Index_2024-02-09.xlsm

Today (2024-02-09), five flasks were loaded in preparation for shipment with the following targets: SiC#41, SiC#42, Nb#9, UC#36, Ta#58.

Note: prior to shipping, the pails within these flasks will need to have a crimped lifting loop added to them.

The mini-storage vault is now EMPTY.

The target index spreadsheet has been updated.

Entry  Tuesday, February 06, 2024, 13:36, David Wang, ITW, Maintenance, , , ITW exit 1 module tank flange o ring has been replaced.  

ITW exit 1 module tank flange o ring has been replaced. the old o r-ing was completely flat in slot without elastic property.  tank flange, module flange, and o ring slot were clean by acetone and canister vacuumed. Raised up module 3 feet and pulled new o-ring over module top so new o ring could be  installed without moving module out. after new o ring installation, craned down module to flange and raised up module 2 feet again to confirm the o ring is properly sit in slot.

Entry  Tuesday, February 06, 2024, 13:28, David Wang, ITW, Maintenance, , , ITW exit 1 module has been disconnected and reconnected for o ring replacement 

ITW exit 1 module was disconnected  for Exit module flange o -ring replacement yesterday. After oring replacement, the module has been reconnected.

Entry  Friday, February 02, 2024, 07:48, David Wang, ITE, Standard Operation, TM4, , ITE primary and secondary vacuum vessel leak check.  

ITE primary and secondary vacuum vessel leak check has been done. SST bellow for 2A3M19  wire scanner on entrance module top has a big leak to E-5 atm.cc/sec on tiny helium spray. The bellow will be replaced in March by probe group. The LD base leak rate is affected by this big leak so i cant keep the LD scale at 0.0Xe-9 atm.cc/sec during the leak check. Other seal are leak free to 8XE-9 atm.cc/sec. I have no big concern on ITE vacuum seals status by the result.

Entry  Friday, January 26, 2024, 16:48, Carla Babcock, South Hot-Cell, Standard Operation, TM4, UC43, UCx#43 PIE 

UCx#43 PIE was done in the SHC. As expected based on electrical measurements, the target container was broken on the right side and came off easily. Despite all the black stuff seen on the containment box and source tray, the inside of the heat shield was very clean. Checked if the Re foil was curled in and didn't see anything. Looked fine other than the broken container.

Entry  Friday, January 26, 2024, 11:57, David Wang, Safe Module Parking, Standard Operation, TM4, , TM4 coil1, 2, and HS electrical check at SMP after module moving. 

TM4 coil1, 2 and HS are all OL at 250V at SMP after module move. This week, Chad and Carl fixed short issue on coil1, 2 and HS by insert dropped ultem ring back to position at SHC.

Entry  Friday, January 26, 2024, 11:53, David Wang, Safe Module Parking, Standard Operation, TM4, , Tm4 has been moved to SMP. 

TM4 has been moved to SMP. The move is smooth. I started SMP vacuum pump. The TM4 and SMP vessel is under vacuum now.

Entry  Friday, January 26, 2024, 08:30, David Wang, South Hot-Cell, Standard Operation, TM4, , window line VCR leak check after containment box removal/installation.  

Chad and I did window line VCRs leak check after containment box removal/installation.  The first  pair of  VCRs have leak. Chad changed VCRs. Both VCr fittings on window lines are completely leak free to 0.0 XE-9 atm.cc/sec now.

Entry  Thursday, January 25, 2024, 07:31, David Wang, Crane, Standard Operation, , , Inspection oftareg hall crane below hook attachment pins and plates ITA6550-01 

Tom Kauss inspected target hall crane below hook attachment pins and plates ITA6550-01 yesterday. He certified the use of these pins and plates for year 2024. The inspection of these pins and plates was in Target hall crane annual check list. It was issued as a calibration index by Isaac Earle in 2022-Feb-08.  After inspection, The inspection tag  was issued and attached to pin. Tom has an inspection record on this job.

Entry  Thursday, January 25, 2024, 07:27, David Wang, Crane, Standard Operation, , , Inspection of target module lifting frames ITA0494-1997-01 and ITA0494-1997-02 

Tom Gauss inspected  two target module lifting frames ITA0494-1997-01 and ITA0494-1997-02 yesterday. He certified the use of these two frames for 2024. Inspection tags have been issued and attached to frames. He has inspection record on them. 

Entry  Thursday, January 25, 2024, 07:24, David Wang, Crane, Standard Operation, , , targe hall annual crane inspection 

Tom Kauss finished TH crane annual inspection yesterday. The crane woks fine. Tom has this inspection record in his file. The crane inspection tag has been issued for 2024.

Entry  Wednesday, January 24, 2024, 08:34, chad fisher, South Hot-Cell, Repair, TM4, UCx#43, Plating and coating from UCx#43 failure IMG_2464.jpgIMG_2465.jpgIMG_2470.jpgIMG_2471.jpgIMG_2472.jpg

TM4 has seen significant coating of the main standoff insulators and various other components stemming from failure in UCx#43 target. See attached pictures showing coating on containment box, support frame, main standoff insulators, standoff insulators high voltage shield etc. Note tracking marks on main standoff insulators.

 

Wednesday, January 24, 2024, 12:54 Carla's edit:

Meggered all HV components relative to HV common and HV common relative to ground. Nothing out of the ordinary, HV common to gnd was 700MOhms at 1kV. Seems whatever got onto the insulators is non-conductive, or is not as bad as it seems.

Entry  Monday, January 22, 2024, 14:12, Frank Song, ITE, Standard Operation, TM4, UCx#43, module disconnection TM4_with_UCx43_disconnected_in_ITE_2024-01-22.pdf

 TM4 with spent target UCx#43 was disconnected in ITE and is ready moved to SHC. see attachment pls.

Entry  Monday, January 22, 2024, 10:16, David Wang, ITE, Standard Operation, TM4, UCx#, Tm4 waterlines helium pressure test and TM service cap helium leak check. 

Tm4 waterlines helium pressure test and TM service cap helium leak check was done last Friday. All water lines were pressurized with 70psi helium for 3 minutes each. The 3 minutes stable leak rate on all lines are less than 4.0 X E-9atm.cc/sec. some of lines had surging leak rate to 2xE-8 atm.cc/sec at the first 10 seconds of pressurization which should be a gas hammer result at the beginning. Based on the numbers, I would say all water lines are leak free still.  I did helium spray on TM4 service cap. There could be a small leak in high E-9 atm. cc/sec on ion gauge and steer service panel o-ring.  I will replace this o-ring when module is moved out of ITE. Other seals are leak free or less than 2.5X E-9 atm.cc/sec leak rate which are good. I am pretty confirm there is a small leak on ITE entrance module top. The leak rate and location will be confirmed when the rest of leak checks in ITE pit are done.

Entry  Monday, January 22, 2024, 09:56, David Wang, ITW, Standard Operation, , , Entrance module has been connected in ITW pit. 

Entrance module has been connected in ITW pit per document 190510 " entrance module disconnection and removal procedure".

 

Entry  Monday, January 22, 2024, 09:50, David Wang, ITW, Standard Operation, , , ITW entrance module has been moved from SHC to ITW. 

ITW entrance module has been moved from SHC to ITW. A slightly bump on module shielding block bottom side corner to tank vessel side when lowed module into tank. No big concern on this slight  bumping. Otherwise the move is perfect.

 

 

 

 

 

 

Entry  Wednesday, January 17, 2024, 20:09, Carla Babcock, South Hot-Cell, Standard Operation, , Ta#66, Ta#66 post irradiation inspection 20240109_100926(1).jpg20240109_101053.jpg20240109_102409.jpg

On Jan. 9 we did the PIE on Ta#66. Opened the heat shield and removed the EE. The inside of the heat shield was very black with lots of flakes falling off. The target itself looked overheated, and the container looked pretty bad for a Ta target. The outside of the EE looked perfect but after removing it there was a lot of black stuff on the side and we saw that the Re foil was curled up. Jens said during the runtime that he saw something that looked like a wire in the beam path, so maybe this was it.

Entry  Friday, January 12, 2024, 11:25, David Wang, South Hot-Cell, Standard Operation, TM2, Ta#66, Ta#66 post operation electrical check at SHC TM2_Ta66_post__oeration_electrical_check.pdf

Ta#66 post operation electrical check was done at SHC this Monday. See attachment.

Entry  Friday, January 12, 2024, 10:53, David Wang, South Hot-Cell, Standard Operation, , , ITW entrance module has been moved from ITW to SHC.  

ITW entrance module has been moved from ITW to SHC. The move is smooth.  I cleaned entrance module tank flange and o r-ing slot.  entrance module tank flange o ring  is replaced .

Entry  Thursday, January 11, 2024, 13:57, David Wang, ITW, Standard Operation, , , ITW entrance module has been disconnect. 

ITW entrance module has been disconnected per document190510. It will be moved to SHC for diagnostic group tomorrow.

Entry  Thursday, January 11, 2024, 13:54, David Wang, Conditioning Station, Development, TM3, , TM3 servic cap air to vacumm seals leak check. 

After Tm3 service tray and service cap installation, TM3 service cap air to vacuum seals leak check has been done at TCS. TCS:IG1 and IG1S are at low E-7 torr range.  leak detector base  0.0XE-9 atm.cc/sec,  base pressure0.0X E-4 torr.  I sprayed helium to all new air to vacuum seals on service cap. No leak on seals. The leak check has been repeated  2 times with same result.   

Entry  Wednesday, January 10, 2024, 16:51, Carla Babcock, ITE, Standard Operation, TM4, UCx#43, UCx#43 failure 

 To deliver stable beam to RadMol, started heating UCx#43 up again. Target was overheated during initial conditioning in Nov but then ran well for 4 weeks. During the run time, the TGHT voltage jumped around and this was reflected in the ion current, but yields seemed unaffected.

When re-heating it, the TGHT voltage was very unstable and once it got to 440A, it went into voltage limiting mode. We ramped down and it was still voltage limiting, but turning things off solved it. We ramped back up and it did about the same thing. TBHT voltage and current remained steady. Looks like a heat generated issue.

Measured the resistance in the lines from the electrical room. Resistance of the lines to ITE should be 1.19mOhms for TGHT and 1.95mOhms for TBHT. TBHT positive to negative had a resistance of 7.9mOhms from the electrical room today, and 5.7mOhms on module top when measured Nov. 8. This seems to track.

TGHT positive to negative was measured at 27.6mOhms today (and was jumping around), whereas it was 7.14m Ohms on Nov. 8.

10V @ 440A is 22.7mOhms, so it makes sense that it limited. Tried with increased voltage (up to limit of 16V) but this didn't help. Declared the target dead on Jan. 11.

 

David measured resistances on the module top and found (in mOhms):

A-B = 27 (TGHT)

A-C = 7.473

A-D = 6.380

B-C = 26.053

B-D = 25.569

C-D = 5.212 (TBHT)

 

So looks like the tube is broken on the B side.

Entry  Wednesday, January 10, 2024, 11:24, Travis Cave, Spent Target Vault, Standard Operation, , Ta#66, Spent Target Move Target_Index_2023-01-10.pdf

 The spent Ta#66 was moved from the south hot cell to the spent target vault, it was placed in pail#285 and placed in spot 5B of the vault. The target was 46.2mSv/hr when removed from the south hot cell. See the attached PDF for vault details.

Entry  Tuesday, January 09, 2024, 16:10, Adam Newsome, South Hot-Cell, Standard Operation, TM2, , TM2 Move - SHC to Silo 

TM2 was moved with no target attached from the South Hot Cell to a silo.

Entry  Monday, January 08, 2024, 14:47, Adam Newsome, South Hot-Cell, Standard Operation, TM2, , TM2 Move - ITW to SHC 

TM2 was moved from ITW to the South Hot Cell with Ta#66 target.

Entry  Wednesday, January 03, 2024, 14:03, David Wang, ITW, Standard Operation, TM2, Ta#66, ITW primary and secondary vacuum vessel leak check and TM2 water lines helium pressure test.  ITW_2024_shut_down_leak_check.pdf

ITW primary and secondary vacuum vessel leak check and TM2 water lines helium pressure test are done today. No major concern. see attachment for small air to vacuum leak we found.  TM2 water lines helium pressure test is fine.   HS and window line leak rate are 1.4Xe-8 atm.cc/sec. all other water lines are below 3.0XE-9atm.cc/sec.

Entry  Wednesday, January 03, 2024, 13:55, David Wang, ITW, Standard Operation, TM2, Ta#66, Disconnect TM2 in ITW. TM2_with_Ta#66_was_disconnected_in_ITW_2024-01-02.pdf

TM2 has been disconnected in ITW. All water lines are nitrogen purged. Filled 60 psi argon to all Tm2 water lines for module storage in winter shut down.

Entry  Tuesday, January 02, 2024, 16:01, Carla Babcock, Conditioning Station, Development, TM3, , TM3 service tray HV testing and conditioning Screenshot_from_2024-01-02_16-05-43.pngScreenshot_from_2024-02-08_17-57-50.png

Tuesday, January 02, 2024, 15:58 :

Started HV ramp up on TM3 service tray about 3pm today. Had to bypass TCS:BIAS interlocks to make it work - there are some flow restrictions on the water lines that are causing the flow interlock to periodically trigger. The water flow it not very important for this test as long as the water is moving. Turned out that it was also conveninent to have all the interlocks bypassed because sparks tripped off the IG1 gauge and this did not cause the HV bias supply to turn off. Should use same setup next time.

Some sparking around 35-44kV, tripped off turbos/IG1/IG1S 3 times and so decided to ramp down.

Tried again while standing outside TH door to hear if sparking is outside the vacuum. Went to 48kV very slowy with multiple trips of the turbos, mostly TP2. Lots of sparks but easy to ramp back up to previous high point, so likely just a painful conditioning process. Current draw 167uA at 48kV. No sparks audible outside door, and vacuum response looks too large to be electrical noise.

 

Continued on Wednesday January 03 - went up to 53kV in the same way as before, lots of TP2 trips making its current a bit unstable... data was dumped as TM3_servicetray_conditioning_jan32023. Tried limiting the current on the power supply to very near the drain current to see if that reduces the number of trips. Didn't notice a significant effect.

 

Thursday, January 04, 2024, 09:57 :

Restarting conditioning, starting at 180uA at 53kV. Got up to around 60kV with many trips of the turbos, and one restart of the IG1 controller needed. Added a grounding hook to the vacuum controller rack to see if that helps reduce the trips. (doesnt appear to have).

 

Friday, January 05, 2024, 09:51 :

Continuing conditioning. Starting by sitting at 50kV for 10mins. No sparks observed during this time.

Even though we got to 60kV last time, onset of conditioning started at 58.6kV with a trip at 58.9kV... got up to 70kV.

 

Got to 72kV on Monday January 08 2024.

 

On Monday Jan. 15, tried to improve the grounding on the vacuum services rack to reduce sparking through the turbo controllers. Added two welding cables from the vacuum rack ground busbar to the copper grounding strip on the ground. If the spark is travelling from the faraday cage to the rack through conduit or grounding cables, maybe this will help. If it is coming through the turbo cable then it likely won't. Tried to add grounding straps on the turbo controller chassis (there is a brass screw which I think is for this purpose) but couldn't get either of the screws out with any resonable force. They undo a bit then get stuck...

 

 Wednesday, January 17, 2024, 20:39:

David vented TM3 with N, then opened the service cap to install new insulators. We pumped back down and Alexander and I ramped back up today - instabilities started around 55kV and we were back to slow conditioning in the high 50s. Got up to a set point of 65kV. Ray did some work on the TCS bias supply and now neither the set point or readback is correct. The PSU was reading 51.5kV at set point 50kV and 60kV at set point 58kV. Will continue later...

 

Wednesday, January 31, 2024, 16:23

Ramped up again, some slight instabiities around 56kV but could still go up pretty quick until about 65kV. Since Ray's testing of the TCS:BIAS supply both the readback and the set point are off from the powersupply display. Ran out of time and ramped down at set point 70.5.

Set point Readback PSU reading
63 64 65.5
66.5 67.5? 68
69.5 70.6 71.5
70.5 71.7 73
     
     

 

Tuesday, February 06, 2024, 14:47

Testing again after venting the module with air. First tiny spark at 48, then some vacuum reactions starting at 49 but still no issues. Bit more reactive around 53.

Set point Read back PSU reading
53 53883 55
57 57924 59
 60  61 62
 64  65 66.5
     

 stopped at 69.4

 

Wednesday, February 07, 2024, 15:28 :

Ramped easily to 60kV set point and let it sit there. Didn't spark at all then after 100mins, sparked TP2 off. Otherwise first sparking happened at set point 67.

Found at limit at around 72.5 on the PSU front output, set point 70.6. think it comes from EPICS. Will have to test the power supply.... stopped there.

 

Thursday, February 08, 2024, 15:03 :

Long term testing. ramped back up, first spark at set point 65.

Let it sit for 2hrs 20mins. Something like 6 sparks during this time. Current also dropped significantly from 0.32A to 0.27A.

Screenshot_from_2024-02-08_17-57-50.png

EDIT 2024-11-25, Alexander Shkuratoff:

All the StripTool data related to the above tests are on the server as the following below. Those without "Alexander" in the name were dumped by Carla.

[   ] TM3_servicetray_conditioning_Jan32023 2024-01-03 17:29 807K
[   ] 20240103_TM3_Service_Tray_TCS_Alexander 2024-01-03 17:31 1.2M
[   ] 20240104_TM3_Service_Tray_TCS_Alexander 2024-01-04 16:58 238K
[TXT] 20240104_TM3_Service_Tray_TCS_Alexander_2.csv 2024-01-05 07:00 13M
[TXT] 20240104_TM3_Service_Tray_TCS_Alexander_1sec.csv 2024-01-05 12:21 81
[TXT] 20240105_TM3_Service_Tray_TCS_Alexander.csv 2024-01-05 16:51 13M
[TXT] 20240105_TM3_Service_Tray_TCS_Alexander_1sec.csv 2024-01-05 16:52 2.7M
[   ] TM3_servicetray_conditioning_Jan52023 2024-01-05 21:24 8.8M
[TXT] 20240108_TM3_Service_Tray_TCS_Alexander_1sec.csv 2024-01-08 16:56 4.7M
[TXT] 20240108_TM3_Service_Tray_TCS_Alexander.csv 2024-01-08 16:56 7.1M
[   ] TM3_servicetray_conditioning_Jan172024 2024-01-17 13:29 257K
[TXT] 20240117_TM3_Service_Tray_TCS_Alexander.csv 2024-01-17 20:11 4.0M
[   ] TM3_servicetray_conditioning_Jan312024 2024-01-31 17:24 2.2M
[TXT] 20240131TM3_Service_Tray_TCS_Alexander.csv 2024-01-31 17:55 4.5M
[TXT] 20240206_TM3_Service_Tray_TCS_Alexander.csv 2024-02-06 17:58 2.6M
[   ] TM3_servicetray_conditioning_Feb62024 2024-02-06 19:29 4.6M
[   ] TM3_servicetray_conditioning_Feb82024 2024-02-08 17:55 3.1M

 And the StripTool settings:

[   ] Alexander_TCS_HV_Conditioning.stp 2024-01-17 19:57 3.7K

 

Entry  Thursday, December 21, 2023, 09:37, Ferran Boix Pamies, ITE, Development, , , Rewiring of TC multiping wires 
Thursday, December 21, 2023, 09:36. ITE multipin wires 12-13-14-15 were rewired from the RF driver box to a TC datalogger inside the HV cage. A webcam was also installed to monitor the TC values during operation. This is only a temporary setup to be upgraded during shutdown.
Entry  Friday, December 15, 2023, 11:31, Adam Newsome, Spent Target Vault, Standard Operation, , Ta#58, Pail repack, transfer to mini-storage vault Target_Index_2023-12-15.pdf

Pail 211 which contained Ta#58 spent target was repackaged into Pail 286 in the South Hot Cell.

The dose rate at approx. 1 m was 4.16 mSv/h.

Pail 286 was transferred to the mini-storage vault and placed in the outermost location. The mini-storage vault is full at this time, in preparation for the next shipment.

Entry  Friday, December 15, 2023, 11:07, Adam Newsome, Conditioning Station, Standard Operation, TM3, , TM3 Move - SHC to TCS 

TM3 was moved from the SHC to the TCS (no target installed).

Entry  Wednesday, December 13, 2023, 11:42, Adam Newsome, South Hot-Cell, Standard Operation, TM3, , TM3 Move - TCS TO SHC 

TM3 has been moved from the target conditioning station to the south hot cell.

Entry  Wednesday, November 29, 2023, 12:45, Carla Babcock, ITE, Standard Operation, , , gas lines pumped down 

Pumped down the gas lines in ITE on Tuesday Nov. 28 2023 and opened the CF4 bottle valves. Missed the small section between the regulator and SV2 though, so will probably redo it.

Pumped down again on Dec. 12 2023. Was taking a long time so might not be as good as earlier. Maybe there is a leak in there...

Entry  Tuesday, November 28, 2023, 12:58, Adam Newsome, South Hot-Cell, Standard Operation, TM3, , TM3 Move - Silo to SHC 

TM3 was moved from the Silo to South Hot Cell.

Entry  Monday, November 27, 2023, 12:01, chad fisher, South Hot-Cell, Maintenance, , , Manipulator tong cable and wrist replacement 

Broken tong cable on SW manipulator (serial #8106) of SHC was replaced today.

Following ISAC Hot Cell entry procedure, Document 157554, SHC was entered and wrist and tong cable were replaced with a pre-run/assembled wrist, cable and tong. It is standard to try and pre-make/load a new cable into a spare tong assembly to reduce time spent in the HC. This marks the first time a wrist has been replaced. Rationale for replacing the wrist at this time is that internal spacer A-14118 which the ting cable rides over has had grooves worn into it. This is a result of regular wear and tear but could be causing premature wear on the tong cable. Replacement is a preventative measure. This is the original wrist and spacer from the original install in 1998. The wrist that was removed will be rebuilt and swapped out with the original one on the SE manipulator (serial #7986) at a later date.

 

Parts replaced today are: New - Bottom half of wrist joint (CRL-13950), New - Tong cable (CRL-14230) and used tong assembly (CRL-18062)

Procedure took about 40 minutes. Dose received was ~0.046 uSv

Entry  Thursday, November 23, 2023, 11:15, Adam Newsome, Crane, Repair, , , Target Hall Crane: CW/CCW rotation mechanism failure [tripped breaker] 

It is reported that the crane's hook rotation is not working currently. It was working yesterday (Nov 22). Investigation to follow, and this e-log will be updated.

Edit [2023-11-23]: the issue was a result of a tripped circuit breaker. Perhaps the motor became overloaded. It is advised to monitor the rotation mechanism over the new few operations, and rotate the hook CW and CCW prior to performing any critical operation to confirm it is working.

Entry  Wednesday, November 22, 2023, 12:24, Adam Newsome, Spent Target Vault, Standard Operation, , Ta#65, Spent Target Move 

The spent Ta#65 target was removed from the south hot cell and placed in the spent target vault. It was placed in pail #284 and placed in spot 2B. It was 41 mSv/hr at 1 m upon removal. Target index spreadsheet updated.

Entry  Monday, November 20, 2023, 12:28, Eric Lahe, South Hot-Cell, Maintenance, , , Light Bulb Replacement - South Hot Cell roof lights 

 3 light bulbs replaced in the ISAC South Hot Cell - North West light, South west light, and South East light bulbs. Northeast light currently still working.

 

The South East light is not working after bulb replacement. This bulb was tested using the wires from the Northeast light station and the bulb is working properly. Electrical services is being contacted to troubleshoot the cable issues. 

Entry  Friday, November 17, 2023, 11:28, Adam Newsome, Spent Target Vault, Maintenance, , , Storage vault: issue observed with door opening PXL_20231117_200245076.jpgPXL_20231124_210005281.jpg

During operation today, it was observed that the main vault door had issues opening.. typically when the door was around 80-90% opened, it would stop motion. Note that this issue has allegedly been present since early 2023. It appeared that the motor was still spinning but the clutch was slipping. This issue was consistent and observed multiple times when trays 2, 5, and 6 were engaged (note these are all on the same side of the vault). It was overcome by backing the door up slightly then trying again. The door close function worked with no issue.

It is suspected that there is a problem with the clutch or potentially a piece of debris on the track. [no longer true after 2023-11-17 inspection]

Edit [2023-11-17]: Maico Dalla Valle and Adam Newsome inspected the vault on 2023-11-17. It was very clear that the door, when opening, is rubbing up against the rails. Specifically, the side rollers located on each side of the vault (red housing). There are clear wear marks on each side. The skew is obvious because on one side, the wear marks begin immediately and stop halfway through travel, whereas the other side shows the reverse wear pattern. It is therefore suspected that the skew has become so significant that the friction is too high towards the end of travel which causes the clutch to slip. The travel rails were cleaned (significant grime buildup) and the offending side was filed down slightly (a sharp burr was present from the wear). It is not advised to adjust the clutch. Next steps: open and close the vault with no trays engaged to see if the issue persists (perhaps weight distribution was the issue), and then try different combinations of weight distribution to try to replicate the issue. After this, measure separation distance between guide rails at different points and try to identify the source of the skew issue and rectify it.
 

Edit [2023-11-20]: Maico and Adam performed further investigation by opening and closing the vault door under 3 different configurations: no trays engaged, 2 trays engaged on West side, 2 trays engaged on East side. The previously observed stopping issue was not observed this time under multiple cycles with each configuration. It is noted that the door appears to slow down slightly and experience a bit of a "chugging along" motion towards the end of travel when opening. Based on these observations, it is concluded that the cleaning and filing helped enough to allow the door to fully travel open/close without getting stuck. The root cause of the issue still remains to be fixed, but for now there is no major concern. Before end of 2023, measurements and planning will be performed to develop a proper repair for the root cause. It is expected that either late 2023 or early 2024, the repair will be attempted.


Edit [2023-11-22]
: during a routine spent target exchange, the issue was not observed when opening tray number 2. 


Edit [2023-11-24]: a dial indicator was set up on the vault on the right side (looking down from above), mounted on the traveling part with the tip touching the black structural member where the wear is observed. The purpose is to determine how much out of alignment the door is with respect to the structural assembly. The following was observed: approximately halfway through the travel, the indicator read approximately 185 thou of travel. This corresponds to when the wear marks start to occur and where the small red enclosure around the roller wheel interferes with the structural member (causing the wear strip). At this point, as expected, the indicator no longer changes because the roller wheel has bumped up against the structural member. This implies the gap between the structural member and the roller wheel, when the door is closed, is approx. 185 thou on the right side (and 0 on the left side). These values reverse around the midpoint of travel. It is suspected that because of this, and because there is a small observable gap between the door and the vault when it is fully close, the right and left side of the door are not parallel with respect to each other. In other words, adjusting the angle so that the starting gap is roughly 92.5 thou on each side should resolve the issue. Measurements to confirm parallel-ness between each side will be performed, and then an adjustment will be made to create even gaps between each side at the starting point. After this, a dial indicator will be set up again to confirm that, when opening the door, the gap is maintained throughout the duration of travel. Small deviations are acceptable, but in general what should be observed is a roughly constant gap, and no interference (i.e. if the gap begins at 92.5 thou, it should not drop to 0 or not exceed 185 thou, but should hover somewhere on the order of 20 to 140 thou, for example).

 

Edit [2023-11-24, 2]: a dial indicator was set up on the left side of the vault in a similar manner as described above. In this case, the indicator's reading remained roughly constant during the start of travel (starting with the door closed and opening it up), with only up to around 10-20 thou variation at first slowly, followed by a slow increase to up to approximately 135 thou. This is similar to the 185 thou observed on the other side. One suggested means of resolving the issue is: raise the entire door slightly with overhead crane, translate it sideways approximately half of door's lateral travel distance (i.e. around 90 thou) and then lowering it back down. This should, in theory, be acceptable. It may not resolve the issue of whether the door is rotated, but should give enough clearance on both sides throughout the entire range of motion to be deemed an acceptable fix. Other opinions will be gathered on the subject to determine if this could work. 

Entry  Friday, November 17, 2023, 11:12, Adam Newsome, Spent Target Vault, Standard Operation, , , Four pails moved from main storage to mini storage Target_Index_2023-11-17.pdf

The following four pails were moved from the main storage vault to the mini storage vault, to stage for shipping in Jan. 2024:

1. Pail 260 (SiC#41), Tray 5B
2. Pail 271 (SiC#42), Tray 2B
3. Pail 246 (Nb#10), Tray 6C
4. Pail 265 (UCx#36), Tray 2A

There is current one open slot in the mini storage vault which is planned for the Ta#58 target (formerly in Pail 211, to be repacked in Dec. 2023).

Target Index spreadsheet updated.

See attached printout with mini storage status.

 

Entry  Wednesday, November 08, 2023, 12:14, Frank Song, South Hot-Cell, Standard Operation, TM4, UCx#43, electrical check/leak check TM4_electric_and_leak_checked_after_UCx#43_installed_2023-11-08.pdf

 TM4 with new target UCx#43 was electrical and leak checked on SHC.

Entry  Tuesday, November 07, 2023, 13:55, Frank Song, ITE, Standard Operation, TM4, Ta#65, module disconnection TM4_with_Spent_Target_Ta#65_disconnection_in_ITE_2023-11-07.pdf

TM4 with spent target Ta#65 was disconnected in ITE and moved to SHC.

Entry  Tuesday, November 07, 2023, 13:42, Frank Song, South Hot-Cell, Standard Operation, TM4, Ta#65, electrical check with the spent target TM4_with_Spent_Target_Ta#65_electrical_check_on_SHC_2023-11-07.pdf

TM4 with spent target Ta#65 was electrical checked right after being moved to SHC. 

Entry  Tuesday, October 31, 2023, 12:12, Travis Cave, Spent Target Vault, Standard Operation, , , Spent target measurements Target_Index_2023-10-31.pdf

 All 20 targets in the vault were measured. The target spread sheet updated. See attached PDF for details.

Entry  Friday, October 13, 2023, 11:51, David Wang, ITE/ITW, Maintenance, , , ITH:MP1 is replaced due to its poor performance.  

ITH:MP1 is replaced this morning due to its poor performance started yesterday afternoon. The general field in pit is about 260usv/hr. the contact field on pump is 2.0 msv/hr. New pump works good. Lubricant in pump will be drained next week. then motor will be removed. The pump body will be bagged and stored in silo area.

Entry  Friday, October 13, 2023, 11:46, David Wang, Cooling, Maintenance, , , HALCW system O2 sensor service and calibration. 

HALCW system O2 sensor service and calibration were done in Sep 26th. electrolyte and membrane on rose mount sensor 499ADO were refilled and replaced. Sensor was zero and full scale calibrated. The sensor works fine after the job.

Entry  Friday, October 06, 2023, 10:47, Travis Cave, Spent Target Vault, Standard Operation, , Nb#11, Spent Target Move Target_Index_2023-10-06.pdf

 The spent Nb#11 target was removed from the south hot cell and place in the spent target vault. It was placed in pail #283 and place in spot 7B is was 65.7mSv/hr upon removal. see pdf for further vault details.

Entry  Thursday, October 05, 2023, 13:50, Frank Song, ITW, Standard Operation, TM2, Ta#66, Module Connection TM2_with_Ta#66_connection_in_ITW_2023-10-04.pdf

 TM2 with new target Ta#66 was connected in ITW. 

Entry  Wednesday, October 04, 2023, 10:41, Frank Song, South Hot-Cell, Standard Operation, TM2, Ta#66, electrical check/leak check TM2_with_Ta#66_electical_and_leak_check_in_SHC_2023-10-04.pdf

 TM2 with new target Ta#66 had an electrical check and leak check on SHC. 

Entry  Tuesday, October 03, 2023, 14:28, Frank Song, South Hot-Cell, Standard Operation, TM2, Nb#11, electrical check TM2_with_spent_target_Nb#11_electrical_check_right_after_moving_from_ITW_to_SHC.pdf

 An electric checked right after TM2 was moved from ITW. 

Entry  Tuesday, October 03, 2023, 07:56, Frank Song, ITW, Standard Operation, TM2, Nb#11, module disconnection TM2_with_Nb#11_Disconnection_in_ITW_2023-10-03.pdf

 TM2 with target Nb#11 has been disconneted in ITW. The HS line was purged with Nitrogen in station. 

Entry  Thursday, September 14, 2023, 11:16, Adam Newsome, Spent Target Vault, Development, , Ta #58, Investigation of Pail 211 (Ta #58) Report_on_Inspection_of_Pail_211_on_2023-09-14.pdf

Upon attempting to lower Pail 211 into their tile hole, CNL encountered issues with the pail getting stuck. They shipped the pail back to TRIUMF and requested we perform an investigation. The investigation report is attached.

The pail contents must be re-packaged into a new pail.

Note: the F-308 is currently sitting in the Meson Hall warm cell at approximately 250 uSv/h at 0.5 m.

 

Dose for primary worker (Chad Fisher) who inspected the cable, unbolted the flask lid, and handled the pail briefly: approx. 104 uSv

Dose for secondary worker (Danka Krsmanovic) who swiped the pail and flask to check for contamination: approx. 70 uSv

 

More photos available upon request from Adam Newsome.

Entry  Wednesday, September 06, 2023, 08:07, Frank Song, ITE, Standard Operation, TM4, Ta#65, Module Connection TM4_with_Ta#65_connection_in_ITE_2023-09-05.pdf

 TM4 was connected in ITE with new target Ta#65 installed. see attachment in detail.

Entry  Friday, September 01, 2023, 10:36, Adam Newsome, Spent Target Vault, Standard Operation, , UCx#42, Spent Target Move Target_Index_2023-09-01.xlsm

UCx #42 moved from North Hot Cell to Storage Vault in Pail #282. Placed in slot 6B. Tray 6 is now full. Pail measured at 34.9 mSv/h at ~1 m upon removal from the hot cell. See attached updated spreadsheet. 

Entry  Tuesday, August 29, 2023, 14:32, Frank Song, North Hot-Cell, Standard Operation, TM4, Ta#65, electrical check/leak check TM4_electric_and_leak_check_after_Ta#65_installed_2023-08-29.pdf

 TM4 with new target Ta#65 has been E/L checked at NHCPost.

Entry  Tuesday, August 29, 2023, 14:32, Frank Song, North Hot-Cell, Standard Operation, TM4, Ta#65, electrical check/leak check TM4_electric_and_leak_check_after_Ta#65_installed_2023-08-29.pdf

 TM4 with new target Ta#65 has been E/L checked at NHCPost.

Entry  Tuesday, August 29, 2023, 10:45, Frank Song, North Hot-Cell, Standard Operation, TM4, UCx#42, electrical check  TM4_with_UCx42_electric_check_with_spent_target_at_NHCPost__2023-08-29.pdf

  TM4 with spent target UCx#42 has been electric checked at NHCpost right after transferred from ITE.

Entry  Tuesday, August 29, 2023, 09:33, Frank Song, ITE, Standard Operation, TM4, UCx#42, module disconnection TM4_with_UCx42_Disconnection_in_ITE_2023-08-29.pdf

 TM4 with spent target UCx#42 was disconnected in ITE and has been remote moved to NHC this morning.

Entry  Tuesday, August 29, 2023, 09:28, Frank Song, ITW, Repair, TM2, Nb#11, Module Connection TM2_with_Nb#11_connection_in_ITW_2023-08-28.pdf

 Module was connected yesterday and all turbo pumps are running at their top speed. 

Entry  Tuesday, August 29, 2023, 09:07, Frank Song, ITW, Repair, TM2, Nb#11, electrical check TM2_with_Nb#11_electical_check_in_ITW_2023-08-28.pdf

 TM2 with new target Nb#11 replaced has been electric checked one more time in ITW.

Entry  Monday, August 28, 2023, 12:16, Frank Song, North Hot-Cell, Repair, TM2, Nb#11, electric/leak check TM2_with_Nb#11_electical_and_leak_check_in_NHC_2023-08-28.pdf

 TM2 with new target Nb#11 has been E/L checked sitting on NHC.

Entry  Friday, August 25, 2023, 07:22, Frank Song, ITW, Repair, TM2, Nb#10, module disconnection TM2_with_Nb#10_disconnection_at_ITW_2023-08-24.pdf

 TM2 with target Nb#10 was disconnected in ITW yesterday for beam production issue investigation.

Entry  Wednesday, August 23, 2023, 10:45, Travis Cave, Spent Target Vault, Standard Operation, , TiC#6, Spent Target Move Target_Index_2023-08-23.pdf

 TiC #6 moved from north hot cell to spent target vault placed in pail #232 put in spot 6A and the field was 151mSv/hr when removed from the north hot cell. See attached PDF for details about spent target vault.

Entry  Tuesday, August 15, 2023, 13:58, Frank Song, ITW, Standard Operation, TM2, Nb#10, Module Connection TM2_with_Nb#10_connection_in_ITW_2023-08-15.pdf

 TM2 with new target Nb#10 was moved to ITW from TCS and re-connected in pit. TPs are running at their full speed. 

Entry  Wednesday, August 09, 2023, 13:43, Carla Babcock, North Hot-Cell, Standard Operation, TM2, TiC#6, TiC#6 PIE 

PIE on TiC#6 was done in the NHC. The target assembly looked brand new when we took it out, no heating spots or deposits (pictures on docushare). Online we measured a 400kOhm connection between TGHT-TBHT-COIL to HV common (TGHT and COIL shorted in TM2 service tray) and anode was unstable above ~300V. After the module move and before the target removal David found TGHT-TBHT-COIL was a dead short to HV common and the anode was at 39kOhms to HV common.

1. Wanted to see if the TGHT-TBHT-COIL short was on the COIL. Measured with ohmmeter the COIL lines to HS and got about 700Ohms. But with the target lying down the COIL lines drop and touch the heat shield so to do this measurement Chad had to lift the lines, which could cause them to touch something else. So not sure how reliable this measurement was. It jumped around a lot, saw 0L occasionally.

2. Measured both target legs and tantalum gas line to HS, got about 5kOhms repeatedly using the ohmmeter.

3. Meggered across the gas line insulator to the gas line going into the target and got open circuit at 250V, so the gas line wasn't coated.

4. Target container looked vaguely red in the areas where the target material was, otherwise still no deposits on the inside. The container was not overly crystalized as seen on the legs and end caps.

5. Some sparking marks on the EE and some slightly asymmetric deposits

Continuing Aug. 22 2023:

6. Found what looks like a hole in the insulation on the COIL, maybe the cause of our short? Found a corresponding line mark on the copper plates that hold the coil down but not sure if it is related. Pics on docushare.

7. Grid looks perfectly new. Where was that current going?

8. Copper plates that hold coil were loose and bolts that hold coil in just fell out as well.

9. What can be seen of the anode wire looks good.

Entry  Wednesday, August 09, 2023, 13:13, David Wang, Conditioning Station, Standard Operation, TM2, Nb#10, Tm2 Nb#10 has been connect at TCS. 

TM2 Nb#10 has been connect at TCS. TCS water system and vacuum system have been started. Everything looks ok so far. TCS Faraday cage is secured for TM2 conditioning at TCS.

Entry  Wednesday, August 09, 2023, 09:41, David Wang, North Hot-Cell, Standard Operation, TM2, Nb#10, TM2 Nb# 10 electrical and leak check at NHC Nb_#10_electrical_and_leak_check_at_NHC.pdf

Nb#10 has been installed on TM2 . electrical and leak check on HS line are good. See attachment.

Entry  Tuesday, August 08, 2023, 13:01, David Wang, North Hot-Cell, Standard Operation, TM2, TiC#6, TM2 TiC#6 post run electrical check at NHC. TiC#6_post_run_electrical_check.pdf

TM2 TiC#6 post run electrical check has been done at TCS. See attachment

Entry  Tuesday, August 08, 2023, 12:59, David Wang, ITW, Standard Operation, TM2, SiC #6, TM2 SiC#6 dhas been disconnected in ITW TiC#6_TM2_disconnection_checklist.pdf

TM2 SiC#6 has been disconnected in ITW. See check list

Entry  Thursday, August 03, 2023, 12:24, Jason Zhang, Crane, Development, , , Cleanup of camera installation on target hall crane, installation of replacement laser LaserProgramCalibrationLocation.pngSICK_Laser_Upgrade_Calibration.xlsxInstallation_IMG.png

 The cleanup of the ISAC Target Hall crane and installation of the new SICK laser which replaced the IBEO laser for the EW crane position was completed on Aug 03 2023.

The clean up tasks which were completed: (Removal of tape viewing camera, Removal of tape, Installation of extension cord, Consolidation of power supplies for the lasers and removal of old laser) 

Currently power bar is still present to act as an extension cable. This will be removed when 2m extension cord is made and put in next target exchange cycle.
   

The installation and testing of new SICK Laser:

1. Calibration points were taken at the 4 corner limits of the crane. North South and East West positions were recorded.

2. Crane was parked at the ladder access position and mounting bracket was machined and installed.

3. A new cable was made and installed for the SICK laser. Continuity test was performed from the control room and crane to ensure pinout of the laser worked with existing serial communication setup in the control room PC.

4. The feedback values from the new SICK laser and old IBEO laser were compared to determine that a calibration offset of 0.06m was needed in the Laser Position Feedback program.

5. Laser Position Feedback program was re-compiled to communicate with 2x SICK lasers with the calibration offset value included in the EW feedback position. (Laser Crane PositionDlg.cpp)

6. Calibration points were taken at the 4 corner limits of the crane again with the new Laser. North South and East West positions were recorded.

There was less than 0.1% variance between the new laser and old laser which is well within the tolerance of the lasers themselves. It can be determined that it was properly calibrated.

 

Entry  Tuesday, August 01, 2023, 09:06, Adam Newsome, Crane, Development, , , Measuring Tape and Camera Removed from Target Hall Crane 

In an effort to clean up the camera installation on top of the ISAC target hall crane to resolve a fault, the position measuring tape and its associated camera were removed from the target hall crane on July 31, 2023.

 

Still to do: clean up power bar installation.

Entry  Friday, July 28, 2023, 10:21, Adam Newsome, Spent Target Vault, Maintenance, , , Mini Storage Vault: Bearing Lubrication PXL_20230728_162515733.jpg

The bearings on the mini storage vault were lubricated. It is suspected that this has never been done. It is suggested that this be performed every two years.

A draft procedure will be created for this job, but at a high level, this process involves:

  • Opening the door fully
  • Disconnection of the motor, limit switches, and cable management system
  • Attachment of a lifting magnet to the door itself
  • Raising the door
  • Lubricating bearings
  • Reversing the process to re-assemble

The entire job took less than 1 hour to complete.

 

Entry  Friday, July 28, 2023, 10:09, Adam Newsome, Spent Target Vault, Maintenance, , , Main Storage Vault: Bearing Lubrication 

Bearings for the main storage vault door were lubricated on 2023-07-28. It is unknown when this was last done. It is suggested that this be a recurring maintenance task every two years.

Entry  Tuesday, July 25, 2023, 16:25, Carla Babcock, North Hot-Cell, Standard Operation, , SiC#45, SiC#45 post irradiation inspection 

Looked at SiC#45 in the hot cell. Looked very clean, no deposits on the heat shield or other components. Target also looked very straight. Only issue we saw was sparking marks on the EE side that faces the ground electrode, in several spots. This target had a bout of sparking when ramping up the protons, so I guess that was the location. Will look for matching spark marks on the ground electrode next time TM4 is in the hot cell. Forgot to take picutres...

Entry  Wednesday, July 19, 2023, 08:09, Frank Song, North Hot-Cell, Standard Operation, TM4, UCx#42, electrical check E__check_after_UCx42_installed_on_TM4.pdf

 An electrical check was made after new target installed on TM4.

Entry  Wednesday, July 19, 2023, 08:04, Frank Song, ITE, Standard Operation, TM4, UCx#42, Module Connection TM4_with_UCx42_connection_in_ITE_20230718.pdf

 TM4 with new target UCx#42 was connected in ITE. 

Entry  Tuesday, July 18, 2023, 10:08, Frank Song, North Hot-Cell, Standard Operation, TM4, SiC#45, module disconnection & electrical check right after transferred from ITE to NHC TM4_with_SiC45_disconnection_and_e_check.pdf

 TM4 with spent target SiC#45 was disconnected ITE  and an electrical check made right after moved on NHC. 

Entry  Wednesday, July 12, 2023, 22:21, Carla Babcock, North Hot-Cell, Standard Operation, , TiC#5, TiC#5 post irradiation inspection results 

The TiC#5 post irradiation inspection was done on Wed. June 14 and Mon. June 19. This target didn't have any obvious issues but it didn't produce much beam. The inspection revealed that the container was quite embrittled and showed significant damage, though it was not broken. The FEBIAD grid looked fine, despite the large anode current draw (indicating that current was flowing elsewhere). The gas line looked fine though the gas injection to this target looked as if it wasn't connected. But there was a plug on the unused line, so it must have been correct. No other obvious signs that would explain the poor performance. Pictures are can be found here https://documents.triumf.ca/docushare/dsweb/View/Collection-37913

Entry  Wednesday, June 21, 2023, 14:39, Adam Newsome, Safe Module Parking, Maintenance, , , Annual electrical and mechanical inspection of Safe Module Parking PXL_20230621_210144119.MP.jpgPXL_20230621_210546559.jpgPXL_20230621_210146892.jpg

An annual electrical and mechanical inspection was performed on the SMP today by Adam Newsome, Travis Cave, Eric Lahe, Maico Dalla Valle, Antoniette Yap, and Jason Zhang as per Work Permit I2023-06-21-4. The following items were checked:

  • Check condition of wiring for physical/radiation/UV damage
    • OK, no signs of significant damage
  • Check for cable tray debris or damage
    • There were multiple items in the cable tray which do not belong there - misc. pieces of wood and metal... these items were not disposed of but should be in the near future
  • Check inside control panel: components and wiring, labeling
    • Labeling intact, components in good condition
    • Misc. random wires pulled to check... one ground wire was loose - it was tightened
  • Verify camera views
    • This was not inspected in detail but signal status was checked, and is checked prior to remote operation
  • Check connectors for damage
    • All connectors OK
  • Check pendant for damage and verify labeling intact
    • Pendant OK
  • Lid open/close test
    • Lid was opened and close multiple times - smooth operation, no concern
    • Lid close logic was checked - OK
  • Vessel rotation and limit switch check
    • Both CW and CCW limits were checked, functioning
    • No concern on rotation - chain drive, rotary limit switch, and cable reel all functioning normally
  • Lubricate chains
    • Not done - should be done next year
  • Inspect tensioners
    • Done - OK
  • Tighten fasteners
    • Not all fasteners were checked - washers will be replaced soon so this was not deemed necessary
    • Approximately 50 washers are missing for socket head screws in slotted parts. Not safety critical but they should be replaced soon.
  • Visual inspection
    • All OK

Overall the inspection was successful.

Entry  Wednesday, June 21, 2023, 09:51, Travis Cave, Spent Target Vault, Standard Operation, , TiC#5, Spent Target Move Target_Index_2023-06-21.pdf

 TiC#5 moved to the spent target vault from the north hot cell. Placed in pail#279 in spot 3A, 40mSv/h when removed from NHC. See attached PDF for further details.

Entry  Tuesday, June 20, 2023, 12:37, Adam Newsome, Assembly/Bench Test, Development, , , Modifications to wire ropes for pails within existing F-308s 6x

Based on a request from CNL (attached), modifications were made to the wire ropes protruding through the tops of F-308s to add a crimped loop which acts as a lifting feature. Tests were performed (report attached) on 10 sample units to validate the strength of these loops, since each loop could not be tested in-situ once the pails were already packed in F-308s. CNL has reviewed and approved the test report.

Wire ropes within the following F-308s, which were staged for shipping as of June 20, 2023, were modified to include the lifting loop:

  1. 06
  2. 13
  3. 15
  4. 16
  5. 19
  6. 20
  7. 21
  8. 22

Each lifting loop was:

  • Crimped according to the same procedure, using the same parts and tools, as the 10 sample units
  • Measured using a tape measure to confirm the 3" size specified by CNL
  • Checked using a go/no-go gauge provided from the crimp tool manufacturer
  • "Pull tested" by hand as a quick check to confirm the crimps were successful (not a quantitative and official test, but a secondary qualitative "feel good" check)

As of the time of writing this e-log, TRIUMF believes these F-308s to be ready to ship.

Entry  Wednesday, June 14, 2023, 13:37, David Wang, ITE, Standard Operation, TM4, , ITE water signal interlock check 

ITE water signal interlock check including HS,EE, TA, TU, MSP. Coil1 , C-window ,2a-window, 2A tank, 2A shielding plug , 2A dump, 2A collimator  are done. All things work.

Entry  Wednesday, June 14, 2023, 07:10, Frank Song, ITE, Standard Operation, TM4, SiC#45, TM4 with SiC#45 connection in ITE TM4_with_SiC#45_connected_in_ITE_20230613.pdf

 TM4 with new target SiC#45 was connected in ITE, all TPs are running at their full speed.

Entry  Tuesday, June 13, 2023, 11:49, Frank Song, North Hot-Cell, Standard Operation, TM4, SiC#45, electrical check and leak check TM4_with_SiC#45_leak&electric_check_on_top_of_NHC.png

 TM4 with new target SiC#45 installed has been leak checked and electrical checked on top of NHC.

Entry  Tuesday, June 13, 2023, 11:45, Frank Song, North Hot-Cell, Standard Operation, TM4, TiC#5, electrical check TM4_with_spent_target_electric_check_right_after_moving_to_NHC.png

 TM4 with spent target TiC#5 electric check after moving from ITE to NHC.

Entry  Tuesday, June 13, 2023, 09:55, Frank Song, ITE, Standard Operation, TM4, TiC#5, module disconnection TM4_with_TiC#5_(FEBIAD)disconnected_in_ITE_20230613.pdf

 TM4 with TiC#5 was disconnected in ITE and moved to NHC.

Entry  Monday, June 12, 2023, 07:36, David Wang, Conditioning Station, Standard Operation, , , TCS water filters annual change.  

Plant group changed TCS water filters last Friday. 4 filters on resin can inet /outlet sides and filters(4 in one cartridge house)on pump return line have been changed. Triumf maintenance tags on filters have been updated. No water leak after job. The TCS TK2 water level dropped  from 20" to 16" because of the job. I will refill the level to 28" today. 

TCS:TK2 is refilled to 28".

Entry  Tuesday, June 06, 2023, 17:36, Carla Babcock, ITW, Standard Operation, TM2, TiC#6, Module conditioning 

Conditioned TM2 up to 48kV in ITW. Some sparks and current is not very stable. Drawing about 178uA at 48kV.

Entry  Tuesday, June 06, 2023, 15:10, Antoniette Yap, Spent Target Vault, Maintenance, , , Annual Inspection of Main and Mini Storage Vaults 

The annual inspection of the mini-storage vault and main storage vault was completed June 23, 2023. The following items were checked:

  • Cabling and cable management
  • Connectors
  • Controls box - internal wiring and components, functionality
  • Limit switches - functionality, wiring, mounting
  • Motor
  • Bearings
  • Set screws
  • Miscellaneous fasteners

The inspection was generally successful. A couple of minor findings were:

  • Bearings for both the main and mini storage vaults must be greased. This is planned for a different day as it involves removing the mini vault's door.
  • There was a small piece of metal on the track for the mini storage vault which was causing the door to "bump" over it as it passed over. This piece was removed and the door behaved normally.
  • The wheel track for the main storage vault was dirty - it was cleaned
  • It was suggested that the 120 VAC power cable for the mini storage vault controls box should be connectorized - this will be added to the "to-do list" for the future

 

Entry  Tuesday, May 30, 2023, 14:19, David Wang, ITE/ITW, Standard Operation, , , BL2A MAA primary beam exclusion area ASU test.  

MAA ASU test have been done following document 154779. All three tests in document are passed. DCR Jas has all test documents.

This test includes the functional test on TH emergency roof hatch which is located at the west end of TH roof. The hatch could be opened and closed properly from TH inside.

Entry  Tuesday, May 30, 2023, 14:15, David Wang, ITW, Standard Operation, , , ITW water signal interlock check is done. 

ITW water signal interlock check is done. All ITW water signals including HS, EE, Coil , Ta, Tu, MSP, C-window, HVC1, HVC2, 2A-dump, 2A -shielding plug, 2A-tank, 2A-window, and 2A-collimator are checked. All  water signal interlock work fine.

Entry  Tuesday, May 30, 2023, 12:30, Frank Song, ITW, Standard Operation, TM2, TiC#6, gas lines pump out in ITW Faraday Cage gas_lines_pumped_out_to_ITW.JPG

 Gas lines pumped down at electric room for TM2 at ITW is done, leak rate 0.0e -8 <1.0e -3 T P pressure

Entry  Tuesday, May 30, 2023, 12:23, Frank Song, ITE, Standard Operation, TM4, TiC#5, gas lines pump out in ITE Faraday Cage Argon_supplied_at_6psi_to_TM4_in_ITE.JPG

argon is being supplied at 6 psi to TM4. 

Entry  Monday, May 29, 2023, 12:52, Frank Song, ITW, Standard Operation, TM2, TiC#6, Module Connection TM2_with_TiC#6_connected_in_ITW_(FEBIAD)_20230529.pdf

 TM2 with TiC#6 was connected in ITW (FEBIAD), turbo pumps were started successfully.

Entry  Thursday, May 25, 2023, 13:10, David Wang, Conditioning Station, Maintenance, TM2, , TCS MP1 is replaced due to poor performace.  

TCS MP1 is replaced due to poor performance( system shows unstable and high reading on TCSCG1A and high TP1,TP2 current draw) . The pump is edward 15i scroll pump. Since vacuum group has no same spare pump, i have to use SMP roughing pump SMP:MP1 which is a  same pump to replace it.. After the replacement ,the TCS:CG1A and TP1, TP2 current draw are back to normal. The original TCSMP1 was surveyed. Swipes on intake and exhaust port are 300 counts and 1000counts. RAM contact field measurement are from 0.2 to 0.5 usv/hr. It is stored in TH. We will try to refurbish this pump first and use as for SMP:MP1. If we can not refurbish it, a new 15i pump will be purchased for SMP:MP1.

2023-05-31: Opened pump tip seal chamber and swiped chamber inside. The contamination level :1200 counts on 44-2.  The tip seal and tip seal chamber o ring need to be replaced . Checked gas ballast knob. The O-ring inside knob is in good condition. Checked exhaust port o-ring. it is in good condition. spare part PO will be issued soon.

2023-06-14:Tip seals and o-ring have been replaced on original TCS:MP1. After, it was tested at TCS for 48 hours. The pump is much quiet on operation, and the pump body temperature is mild. The final  inlet pressure this pump could get with TCS PV1 closed is about 23 mtorr.  The result is good. I installed it back to TCS vacuum station and reinstalled SMP:MP1 back to SMP vacuum station.  

 

Entry  Wednesday, May 24, 2023, 17:25, Carla Babcock, ITE, Repair, TM4, TiC#5, Issues with anode short 

When I tried to raise the anode voltage in cathode bias mode on May 23 evening, I found the target or tube shorted to HV common. Investigations in the faraday cage today showed the same. I removed all the new electronics (resistors, gemovs, etc) from the power supply to no effect, so I disconnected the TGHT supply and pushed it away from the busbars. There was still a short. David Frank and I then went down to the pit and disconnected everything to measure the module. The module itself showed no short, and the bus bars in the chase for TGHT showed no short, though the ones for TBHT still showed the short.

David and Frank reconnected the module and I disconnected the TBHT supply in the faraday cage, then I found no shorts to TGHT/TBHT. When I reconnected everything there were still no shorts. There must have been a short in the TBHT line in the faraday cage, and another short in the TGHT line in either the faraday cage or on the module top. Both these shorts got resolved by taking everything apart. Still not sure how it happened.

Next I found I could not raise the anode voltage above 230V, it looked like it was current limiting but since the current limit was high, I figured it had something to do with the new electronics installed. I disconnected them all the in cage and that solved the problem, and then reconnecting the gemovs that go from the PSU terminals to HV common caused the problem again, so I left those disconnected.

Entry  Wednesday, May 24, 2023, 08:34, David Wang, Conditioning Station, Standard Operation, TM2, TiC#6, TM2 HS line helium pressure check and gasline fittins leak check. 

TM2 HS line helium leak check is done. leak detector base LR 1.8xE-8atm.cc/sec.  helium pressure 70 psi. 5 minutes test. no change on LD leak rate.    I spray lots helium to gas line adaptor and fittings. No leak.has been found  at this base leak rate level.  Since the TCS MP1 has some  issue ,this time the base leak rate on LD only can get to 1.8Xe-8 atm.cc/sec at this moment instead of 0.0xE-9.  The low E-8  level is not perfect, but  i  have no concern on it.

Entry  Monday, May 22, 2023, 15:06, Carla Babcock, ITE, Standard Operation, TM4, TiC#5, Module conditioning 

Yesterday and today module conditioning was done on Tm4 in ITE. This is the first ramp up after the shutdown and ITE is planned to run at high voltages for the first weeks. The module is behaving well - went up to 40kV yesterday, stayed there for an hour, and up to 46kV today. Current draw is 113uA at 46kV. No serious sparking.

 

Tuesday, May 23, 2023, 09:32 :  Ramping up again, easy to 45kV. Drawing 132uA at 49kV. Still behaving quite well.

Entry  Friday, May 19, 2023, 09:39, Frank Song, South Hot-Cell, Standard Operation, TM2, TiC#6, leak/electrical check TM2_with_TiC#6_leak_and_eletrical_check.png

 TM2 with TiC#6 was checked on SHC, see pic attached pls.

Entry  Friday, May 12, 2023, 09:56, Adam Newsome, Spent Target Vault, Standard Operation, , , Emergency Close Mechanism Test 

 The emergency close mechanism for the Storage Vault door was tested by Travis Cave, Nadia Jorgenson, Adam Newsome, and Jason Zhang. The door was opened to its fully open limit, then closed with the emergency system. 

The test was successful.

Entry  Wednesday, May 10, 2023, 08:40, Frank Song, ITE, Standard Operation, TM4, TiC#5, Module Connection TM4_with_TiC5_connection_in_ITE_20230509.pngTM4_with_TiC5_all_set_in_ITE_20230510_758AM.JPG

 TM4 was connected in ITE.  pics attached FYI.

Entry  Monday, May 08, 2023, 10:59, Frank Song, North Hot-Cell, Standard Operation, TM4, TiC#5, electrical check/leak check TM4_with_TiC#5_20230508.png

 TM4 with target TiC#5 installed has been leak checked and electric checked on NHC.

Entry  Thursday, May 04, 2023, 07:14, David Wang, Safe Module Parking, Standard Operation, TM4, , SMP vacuum pumpimg down is stopped.  

SMP  vacuum pumping down is stopped. SMP and TM4 venting to atmosphere will be started soon.

Entry  Wednesday, May 03, 2023, 13:22, David Wang, ITE, Standard Operation, , , Argon vented ITE station.  

Argon vented ITE station. ITEVV1S and ITGT SV3 were closed after venting.

Entry  Wednesday, May 03, 2023, 11:04, Adam Newsome, Crane, Maintenance, , , Pail Handling Tool - Annual Inspection PXL_20230503_172503014.jpgPXL_20230503_172457837.jpgPXL_20230503_172454009.jpg

The pail handling tool which is used to move 5 gallon pails around the target hall was inspected by A. Newsome, N. Jorgenson, and E. Lahe. The main tool as well as spare were checked for the following items. The tools are in good, working condition. It is noted that some fasteners on the hook assembly were slightly loose, but have been tightened.

  • Inspect structural integrity of long tube - check for bending, warpage, dents, cracks, rust/corrosion
  • Inspect structural integrity of hook assembly - check for bending, warpage, dents, cracks, rust/corrosion
  • Inspect fasteners - check all fasteners installed as per drawings, fasteners are tight
  • Inspect crane interface assembly - check for damage and wear where the tool connects to the crane
  • Check alignment - verify the tool connects to the crane and hangs vertically with no major misalignment (this step was not done - alignment is regularly checked during operations, and there was no concern as the tube was straight)

 Note: these tools are being inspected monthly by D. Wang and F. Song.

Entry  Tuesday, May 02, 2023, 17:18, David Wang, ITE, Standard Operation, , , ITE 4 turbopumps are started for preoperation check.  

ITE TP3,4, 1S,and 4S were started successfully this afternoon. All pump current draws  were below 1.5A . IG1S was switched on. I have no local controller so TP1 and TP2 on TM4 at  MSP can not be checked.  IG1S was hard to switch on at first. It timed out and showed error 09 code. I removed the connector back cap, and it could be switched on after. I will look on this issue. 

Turbo -pumps were stopped  last night at  6 pm. All four pumps worked good during check. For IG1S switching on issue, the problem either caused by over pressure(No TP1, 2 in ITE)   or because coaxial cable was pinched by connector cap and caused bad contact on pin to cable.   I modified the connector cap inside by opening more space for cable passing through the cap. The cap is installed back.   The gauge will be switched on next week again. We keep watch on it

Entry  Friday, April 28, 2023, 21:39, David Wang, Conditioning Station, Standard Operation, , , TCS cooling water system was started and tested this Wednesday 

TCS cooling water system was started and tested this Wednesday. Chiller compressor 2 and 3 was in operation cycle twice without issue. TCS:TK2 was refilled to 28 inches. Water system works fine. system was switched off after test.

Entry  Monday, April 24, 2023, 10:18, David Wang, Cooling, Maintenance, , , HALCW flowmeter transmotters inspetion and calibration.  

ITW, ITE, ITW +ITE total , and low active cooling water return flow meter transmitters are inspected and calibrated.  Result:

ITW , PX-750-06Di , Calibrated to  4-20 mA for 0 to 6" H2O DP, linear.    Transmitter works fine.

ITE. PX-750-06Di, calibrated to 4- 20mA for 0 to 6" H2O DP, linear.   Transmitter works fine.

ITE+ITW total, PX-750 -30 SQDI.  It looks like electronic board for square root output is broken. It can not be calibrated  to 4mA @ 0 inch H2O DP. The transmitter is calibrated to 10.25mA - 25.25mA for 0 to30" H2O DP, linear. Transmitter works fine.

 Low active cooling water return, Px-750-30di, smart.  The transmitter is broken. The output current stuck at 44.5mA on all DP.  I tried zero and reset it by following instruction manual, but failed to bring it back. The electronic boards are broken mostly. The production is discontinued by Omega Engineering. A new Omega transmitter PX3005-25WDWBI (linear) will be ordered for its replacement.

2023-06-28: A new Omega transmitter PX3005-25WDWBI (linear) has been installed back to LALCW system in target hall. Transmitter is calibration by manufacturer @ 4-20mA output@0 to 25 in H2O DP. Control group will finish the cable connection in TH, electrical room, and reprogram   on epic page on July -11th.

2023-07-12: Cable connection, formula reprogram, and epic page reboot are done yesterday by Ray.M. New transmitter works fine. All flow rates are displayed on epic page properly with new program formulas.

Entry  Tuesday, April 18, 2023, 07:28, chad fisher, North Hot-Cell, Maintenance, , , NHC entry summary 

NHC was entered on April 17, 2023 for inspection and maintenance. Summary :

Compressible and non-compressible waste was loaded into a 55 gal drum and removed from the NHC. This same drum will be inserted into the SHC at a later date to be sorted, compressible waste compressed, and drum filled more.

Manipulator remote end tong cables checked. Tong cables didn't show any wear but both east and west had tong cables had hopped off the third highest pulley (see detailed write up . This was fixed by tying the tongs in the closed position to provide slack in the cables then inserting a t-handle through the wrist and offering the cables back onto the pulleys. Cable hopping is most likely due to aggressive ratcheting and releasing of the tong during operation.

Manipulator booting flanges were removed from both manipulators as it was previously found that  the booting interferes with access to the inside of the containment box so it could not be used. Flanges were remove to provide even more clearance.

Containment box cover removal arm - linkage fasteners were removed one at a time and blue locktite added then reassembled and tightened appropriately to allow arm to swing freely (see detailed write up) . Lack of locktite during initial assembly was allowing fasteners that pass through bushings into the linkage arms to loosen over time/cycling.

Exhaust pre-filter changed.

Target insertion jig - The target insertion jig was rumored to had a missing fastener. A loose nut was found that appeared to belong to it but after much inspection a location for it could not be found...i.e. all parts appeared to be counted for. During this inspection it was noted that some over the fasteners in the main hinge were loose. Again these were removed one at a time, blue locktite added and fasteners tightened to allow proper movement (see detailed write up).

Window inspected for leak. No sign of any leakage from the "hot" side.

 

Entry  Friday, April 14, 2023, 10:01, Adam Newsome, Assembly/Bench Test, Repair, , , Assaying Turntable Repair 

The spent target assaying turntable was repaired. It was tested today with a load exceeding the maximum it would need to handle during rotation (100 kg). It works as expected and is ready for operation.

Entry  Tuesday, April 11, 2023, 11:35, chad fisher, North Hot-Cell, Standard Operation, , , NHC fields post sample removal 

The fields in the NHC after removal of Ferran's graphite sample is 238 uSv/h. This again seems to emanate for the items in the 5 gal pail...the copper tubing from the beam window or, as I mentioned in my previous elog, the peek samples. I did ask about removing these during the graphite sample removal but was told they were not "hot".

Entry  Monday, April 03, 2023, 07:55, chad fisher, North Hot-Cell, Standard Operation, , , NHC, SHC field check 

NHC is 1.26 mSv/h inside approximately .5m from table surface, between manipulators

 

SHC 186 uSv/h inside approximately .5m from table surface and between manipulaotrs

Entry  Thursday, March 30, 2023, 14:29, Frank Song, ITE/ITW, Development, , , Preparation of target stations for FEBIAD runs 1_(5).png1_(2).png

Helium cylinder and  Argon cylinder are installed in both ITE/ITW faraday cages , regulator for outlet pressure are not set yet.

 

TO ITE :  Argon bottle size 14"L x 4"D with SV2 connected at pressure 900 Psi ( 70 bar )

               Helium bottle size 18"L x 7"D with SV1 connected at pressure 2000 Psi ( 130 bar )

TO ITW: Argon bottle size 15"L x 2"D with SV2 connected at pressure 1000 Psi ( 80 bar )

              Helium bottle size 18"L x 7"D with SV1 connected at pressure 2000 Psi ( 130 bar )

An Neon cylinder size 20"L x 6"D  at less than 100 psi ( <10 bar ) pressure stored in the cabinet of ITW cage without connection

two gas line connection pictures are attached here for reference.

Entry  Monday, March 13, 2023, 11:25, Carla Babcock, ITE/ITW, Development, , , 10kOhm resistors installed in ITE/ITW faraday cages ITE_ITW_BIASresistor.docx

On Sept. 14 2022, a 10kOhm 30W resistor was installed in each target station faraday cage, in line with the HV bias supply. This was an effort to reduce the current draw from the BIAS supply and protect the power supply controls cards which have been repeatedly breaking due to HV sparks (we think). In the end we still broke cards after the installation, so it doesn't seem to have helped. See below for details on the electrical side:

At 30kV, HV currents are around 100-150uA, meaning the voltage drop over the resistor is around 1.5V. When operating at higher voltages, with higher current draw, the voltage across the resistor could be over 2V and we could get into a situation where it would have an effect outside the normal adjustments needed on the mass separator. We made this decision based on the fact that the power supply's setting resolution is on the order of 1 x 10-4.

When the resistance of the water changes, this affects the current draw from the power supply and this in turn affects the voltage over this resistor. Based on some sample numbers of running times, there is not much variation in the current except from sparks and if there is some issue, like water leaking between HV and ground. During normal running, the voltage change across the resistor should be less than 0.5V during normal operation. This is on the same order as the 8 hour stability of the power supply.

 

 

Entry  Wednesday, March 08, 2023, 13:57, David Wang, Cooling, Standard Operation, , , HALCW ITC:MP1/MP2 pump and motor temerature measurements 

HALCW ITC:MP1/MP2 pump and motor temperature measurements result:

MP1: pump discharging  port: 78F,  motor rear bearing house:72F  , Motor housing 140F(60C). 6F difference between them is less than 15F manufacturer clarified up limit in instruction manual. 

MP2: pump discharging port:78F,  motor  rear bearing house:72F, Motor housing 122F(50C).

MP1 is better than MP2 on motor status. It could be seen on phase current measurements as well.

Other notes on pump performance:    total flow rate 60GPM , discharging gauge pressure  99 to 100 psi on both pumps with one station all of TM water circuits bypassed + other station  two of TM water circuits bypassed + both stations 2A beam related water circuits  on(2X5).

Entry  Wednesday, March 08, 2023, 09:19, David Wang, Cooling, Standard Operation, , , HALCW ITC:MP1/MP2 motor phase current measurement.  

HALCW ITC:MP1/MP2 motor phase current measurement is done by Joel from electrician group. MP1:17.1A/17.2A/16.7A.  MP2: 17.9A/17.9A/17.3A.   19.5A is manufacturer notified on full load phase current.on operating  instruction manual. 

Entry  Wednesday, March 08, 2023, 06:32, David Wang, Cooling, Maintenance, , , HALCW flow sensors replacement.  

HALCW flow sensors replacement job is done. All ITE/ITW(except ITE HS) return line water flow sensors including paddle wheels and coils are replaced.  After job, water interlock signal have been checked in electrical room .  Everything works fine. Visually inspections for possible water leak on HCLCW system have been done as well. one valve on ITE dump return line has a very small water seeping through valve stem. I will watch on it.  Other than that,  No major concern.

2023-03-08: leak on 1/2" ITE dump return line valve is fixed.

Entry  Monday, March 06, 2023, 11:31, Adam Newsome, North Hot-Cell, Repair, , , Spare Telemanipulator: Y-Motion Linear Actuator Repair 

The linear actuator used for the Y-motion motor assistance on the spare telemanipulator was replaced and tested. It was observed around September 2021 that the former one which was installed was causing fuses to blow for the main 120 VAC power supply in the control box. After some troubleshooting, it was determined that the linear actuator itself did not operate smoothly - it was suspected that this caused motor overload due to additional friction. This suspicion was confirmed by operating the linear actuator independently with a power supply and measuring current draw. The part has been replaced by Thomson PPA90-58B65-08NXXX. Note: this part took over 1 year to arrive since it was first ordered. The spare telemanipulator is confirmed operational.

 

Update 2024-09-11: noting that this was for serial number 9351

    Reply  Tuesday, March 07, 2023, 10:37, chad fisher, North Hot-Cell, Repair, , , Spare Telemanipulator: Y-Motion Linear Actuator Repair 

Adam Newsome wrote:

The linear actuator used for the Y-motion motor assistance on the spare telemanipulator was replaced and tested. It was observed around September 2021 that the former one which was installed was causing fuses to blow for the main 120 VAC power supply in the control box. After some troubleshooting, it was determined that the linear actuator itself did not operate smoothly - it was suspected that this caused motor overload due to additional friction. This suspicion was confirmed by operating the linear actuator independently with a power supply and measuring current draw. The part has been replaced by Thomson PPA90-58B65-08NXXX. Note: this part took over 1 year to arrive since it was first ordered. The spare telemanipulator is confirmed operational.

 During this repair it was noted that the Y-axis electrical translation is locked out when the Z-axis is in the fully retracted position (i.e. the Z-axis limit switch engaged). I have made a note of this in the operator manual (CRLD-1046-B Rev1 ) which can be found in docushare collection 26780

Entry  Wednesday, March 01, 2023, 10:01, David Wang, ITE/ITW, Development, , , vacuum pit ventilation upgrade.  

vacuum pit ventilation upgrade was done last week. The jobs include: installed two industrial cooling  fans.  One is placed in pit on resin tan cover. Other one is placed on and opening to pit by shielding blocks.  They are installed for better air circulation in pit. Also,  2x two small 20W cooling fans are installed on ITH MP1 and MP1S to low the pump  operation temperature.  The result is positive. The ventilation status in pit meets the pump operation requirement (good ventilation and 40 Celsuis below) .  ITH CG2S 0.0 mtorr.  ITH CG2 0.26mtorr.

Entry  Wednesday, March 01, 2023, 09:34, David Wang, Cooling, Maintenance, , , Visual inspection of HALCW for possible small water leak or drip.  

I visually inspected HALCW system including water station section, both target pits, and de-ionizer system.  No small leak and drip was found .  The inspection in both target pits will be repeated after flow sensors are replaced.

Entry  Wednesday, March 01, 2023, 09:27, David Wang, Cooling, Maintenance, , , Two filters on HALCW resin circuit have been replaced.  

Two filters on HALCW resin circuit have been replaced. O-ring 235# were changed on both filter cartridge houses.  25micron  10"x 2.5" 3M cartridge new filters  are used. Old filters are not very dirty. They are bagged and stored in vacuum pit. Residual water from cartridge houses are collected and stored in high active storage jug with sealed cap.  No leak on resin circuit before and after the job.

Entry  Wednesday, February 22, 2023, 09:22, Carla Babcock, ITE/ITW, Standard Operation, , , HV testing of ITE/ITW Screenshot_from_2023-02-16_13-19-44.pngScreenshot_from_2023-02-22_09-20-14.pngScreenshot_from_2023-02-24_17-41-33.png

Feb. 16 2023: HV tests done on ITE station. Ramped up to 59kV but was not stable there, current draw was very unstable and was sparking every ~6mins. Ramped down to 58kV and it was stable there for 3 hours drawing 285uA.

Feb. 24 2023: HV tests done on ITW station. Ramped easily to 60kV with no sparking - suspicious. Has been stable at 60kV for 45mins with no sparks and current draw of 200uA. Cannot find any reason that things aren't connected properly...

Entry  Tuesday, February 14, 2023, 11:36, David Wang, Assembly/Bench Test, Repair, , , Turbo pump BVs o-ring replacement.  

Five of used  internal leaked  TP BVs are serviced and repaired. Internal plunge  o-ring and case o-ring are replaced on all five BVs. Leak checked valves after  . They are ok to be used as spare parts.  The are active parts stored in TH now.

Entry  Monday, February 13, 2023, 09:57, David Wang, ITW, Maintenance, , , ITW/ITE primary vacuum back up lines and BVs leak check in target pit.  

In past two weeks, ITW/ ITE primary vacuum back up lines and BVs in ITW/ITE pit have been leak checked.  ITW BV1 and BV2 on back up line side were leak. They are replaced with old leak free BVs.  ITE TP2 NW25 SST  flexible line right after pump were leak . It is replaced with new NW25 SST flexible line. Two leak were found on ITW side KF 50 O-rings connected to NW 50 SST flexible coupling. They were replaced with new KF50 o-rings. After job, both  stations primary back up lines in pit were leak checked .  They are good.

Entry  Monday, January 30, 2023, 11:30, Travis Cave, Spent Target Vault, Standard Operation, , UC#41, Spent Target Move Target_Index_2023-01-30.pdf

 The spent UC#41 was moved from the south hot cell to the spent target vault, placed in spot 1C, in pail #231. See attached PDF for details. 

Entry  Friday, January 27, 2023, 07:25, David Wang, Crane, Standard Operation, , , Inspection of TH crane below hook attachment pins and plates ITA6550-01 

Tom Kauss inspected target hall crane below hook attachment pins and plates ITA6550-01 yesterday. He certified the use of these pins and plates. The inspection of these pins and plates was in Target hall crane annual check list. It was issued as a calibration index by Isaac Earle in 2022-Feb-08.  After inspection, The inspection tag  was issued and attached to pin. Tom has an inspection record on this job

Entry  Friday, January 27, 2023, 07:18, David Wang, Crane, Standard Operation, , , Inspection of target module lifing frame ITA0494-1997-01 and ITA0494-1997-02 

Tom Gauss inspected  two target module lifting frames ITA0494-1997-01 and ITA0494-1997-02 yesterday. He certified the use of these two frames for 2023. Inspection tags have been issued and attached to frames. He has inspection record on them. 

Entry  Friday, January 27, 2023, 07:15, David Wang, Crane, Standard Operation, , , Target hall Crane annual inspection has beend done. 

Tom Kauss  finished TH crane annual inspection yesterday. The crane woks fine. Tom has this inspection record in his file. The crane inspection tag has been issued for 2023.

Entry  Friday, January 27, 2023, 07:11, David Wang, Crane, Standard Operation, , , Target hall Crane annual inspection has beend done. 

Tom Kauss inspected target hall crane yesterday. The crane works fine. Tom has this inspection record in his file. The inspection tag has been issued.

Entry  Wednesday, January 25, 2023, 06:52, David Wang, ITE, Standard Operation, TM4, UCx#41, ITE primary and secondary vacuum vessel air to vacuum seals leak check.  ITE_vacuum_vessel_leak_check_2023..pdf

ITE primary and secondary vacuum vessel air to vacuum seals leak check was done this week. One leak has been found on IG1S feed through to entrance module surface seal. It explains what we saw on ITE IG1S readings change(from low E-7 torr to 1Xe-6 torr) on December 22, 2022.  This leak seal will be replaced soon.

2023-Jan -27.  O-ring seal 229# was replaced on ITEIG1S feedthrough to entrance module surface sealing. Also o-ring seal 034# was replaced on the blank off cover beside the feed through to entrance module surface sealing. Since these o-rings are too close to each other. It is better to replace both of them to avoid misreading in leak check.

Entry  Tuesday, January 24, 2023, 14:22, David Wang, South Hot-Cell, Standard Operation, TM4, UCx#41, TM4 electrical check with and without target at SHC TM4_electrical_check_with_UCX41_and_without_target_2023_Jan.pdf

TM4 electrical check with UCX41target and without target at SHC.  The results are good. See attachment.

Entry  Tuesday, January 24, 2023, 08:46, David Wang, ITE, Standard Operation, TM4, UCx#41, TM4 has been disconnected in ITE.  UCx#41_TM4_disconnection_checklist_in_ITE.pdf

TM 4 has been disconnected in ITE.  See attachment for disconnection checklist.

Entry  Tuesday, January 24, 2023, 07:26, David Wang, Conditioning Station, Standard Operation, , , TH floor moping and garbage collelctions. 

Plant group and us  finished TH floor mopping and garbage collections last Wednesday. Th moping head had 800 count after using. all garbage were bagged , checked, tagged, and sent to radwaste area.

Entry  Tuesday, January 24, 2023, 07:21, David Wang, ITW, Maintenance, , , ITW pit general clean up.  

 ITW  was cleaned with vacuum canister in Jan 10th. HV  cage inside and blue nylon insulators were wiped.  Garbage inside the pits were cleaned out.

Entry  Tuesday, January 24, 2023, 07:17, David Wang, ITE, Standard Operation, TM4, UCx#41, TM4 water lines helium pressure test 2023.  TM4_water_lines_helium_presuure_test_2023.pdf

TM4 water lines helium pressure test was done yesterday at ITE. All water lines were air purged one day ahead  for the test. No leak  has been found on TM4 waterlines during the test. See attachment for detail

Entry  Wednesday, January 11, 2023, 11:34, Travis Cave, Spent Target Vault, Standard Operation, , UC#40, Spent Target Move Target_Index_2023-01-11.pdf

 UC#40 was moved from the north hot cell to the spent target vault. It was placed in pail #278 put in spot 1B and was 15.6 mSv/hr when removed from the north hot cell.

Also Ta#62 in pail #256 was moved from spot 7B back to 7A where it was originally located. This pail in the future will have to be repacked due to the fact it lacks a reinforcing disc in the bottom of the pail.

attached is vault details.

Entry  Tuesday, January 10, 2023, 10:15, Frank Song, Safe Module Parking, Standard Operation, TM2, UCx40 removed, TM2 electrical check with no target attached on SW silo TM2_electrical_check_without_UCx40_on_SW_silo.png

 TM2 with no target on SW silo be electrical checked right after module moving.

Entry  Monday, January 09, 2023, 14:19, Frank Song, ITW, Standard Operation, TM2, UCx#40, TM2 with UCx40 disconnection in ITW TM2_with_UCx40_disconnection_in_ITW.png

 TM2 with target UCx40 was disconnected in ITW and moved to NHC.

Entry  Friday, January 06, 2023, 10:38, David Wang, ITW, Standard Operation, TM2, , ITW/TM2 vacuum vessels leak check and TM2 internal cooling lines helium pressure test.  ITW_vacuum_leak_check_2023.pdf

ITW and TM2 primary and secondary vacuum vessel leak check is done. Leak detector is connected to ITW TP1. Base leak rate on leak detector is 0.0 x E-9 atm.cc/sec.   See attachment for the result.  No big issue. Two old leaks we found last year at location D and E disappeared in this check. We did Vacseal resin spray on them last year.  It looks like the Vacseal spray works .  From the result , I can see the o-ring between exit 1 module and T - flange is closing to the end of the life.  There are two small leaks on this o-ring now at A and B location. We plan to change this o-ring next winter shut down. We do vacseal spray on them this year. The big O-ring between tank vessel and T -flange looks still ok. Two small leaks are found on location F and G on this O-ring. Not much we can do on them. The leak on location C and B were sprayed with resin yesterday after leak check. They are leak free after spray on check. I will double check them. Leak on location A will be resin sprayed after TM2 is removed and ITW is under vacuum.   All TM2 internal water-cooling lines are helium pressurized (70 psi) for 5 minutes each. HS shows 2.5 X E-9atm.cc/sec leak rate. The rest lines are 0.0 X E-9 atm.cc/sec.

Entry  Friday, January 06, 2023, 09:41, Adam Newsome, Spent Target Vault, Standard Operation, , , Pails moved to mini-storage vault Target_Index_2023-01-06.pdf

The following three pails were moved from the main storage vault to the mini-storage vault:

1. #211, Ta#58 (formerly vault location 3C)
2. #217, ZrC#8 (formerly vault location 3A)
3. #228, UC#37 (formerly vault location 1B)

 

The target index spreadsheet has been updated.

Entry  Friday, December 16, 2022, 16:39, Adam Newsome, Crane, Standard Operation, , , Crane powered off for holidays 

[edit 2023-01-03] The crane was powered back on this morning - there do not appear to be any faults and it seems that the crane was unaffected by the power outage.

The ISAC target hall overhead crane was powered off for the holidays. Note that this may result in the commonly observed PLC battery failure issue when the crane is powered back on in the new year.

Entry  Friday, December 16, 2022, 16:35, Adam Newsome, Spent Target Vault, Standard Operation, , , Pails measured, moved to mini-storage vault Target_Index_2022-12-16.pdf

The following five pails were moved to the mini-storage vault today under work permit I2022-12-16-1:

  • #239 (formerly vault location 7A): 1.38 mSv/h @ 1m
  • #245 (formerly vault location 6B): 1.56 mSv/h @ 1m
  • #264 (formerly vault location 6A): 748 uSv/h @ 1 m
  • #267 (formerly vault location 1C): 708 uSv/h @ 1 m
  • #268 (vault location 7C): 809 uSv/h @ 1 m

The mini-storage vault is now full and ready for transfer to F-308 flasks.

The following measurements were made on other pails:

  • #211 (vault location 3C): 4.21 mSv @ 1 m
  • #217 (vault location 3A): 1.05 mSv/h @ 1 m
  • #246 (vault location 6C): 1.98 mSv/h @ 1m
  • #274 (vault location 1A): 4.78 mSv/h @ 1 m
  • #228 (vault location 1B): 3.86 mSv/h @ 1 m
  • #256 (vault location formerly 7A, now 7B): 3.60 mSv/h @ 1 m
  • #260 (vault location 5B): 1.46 mSv/h @ 1 m

The target index spreadsheet has been updated to reflect these changes. See attached PDF print.

Entry  Thursday, December 01, 2022, 13:45, Carla Babcock, North Hot-Cell, Standard Operation, TM4, C#4, Post irradiation inspection C#4 20221122_152435.jpg20221122_153033.jpg20221122_152407.jpg

Post irradiation inspection of C#4 which was running in TM4/ITE was conducted at the NHC on Nov. 22 2022.

The yields from this target had been dropping and its behaviour was erratic, with the voltages on the tube and target jumping all over the place sometimes. The ion current on the FCs followed the voltages. We took this to mean the target container was breaking down.

Upon inspection we found the container looked pretty damaged - highly crystallized and distorted. The container had gone banana-shaped, but not in the usual direction. It had curved  in the direction of the ion source (see photos). The heat shield and other surrounding components were super clean, no deposits or marks at all.

Entry  Thursday, December 01, 2022, 08:20, Frank Song, ITE, Standard Operation, TM4, UCx#41, Module Connection TM4_with_UCx#41_connection_in_ITE.png

 TM4 with UCx#41 was connected in ITE on Tuesday (2022-11-29) 

Entry  Tuesday, November 29, 2022, 11:03, Adam Newsome, ITE, Standard Operation, TM4, C#4, TM4 Move - TCS to ITE 

TM4 was moved from the Conditioning Station to the East Target Station with C#4.

Entry  Thursday, November 24, 2022, 11:32, Adam Newsome, Spent Target Vault, Standard Operation, TM4, C#4, C#4 Spent Target Moved to Storage Vault Target_Index_2022-11-24.pdf

C#4 spent target was moved to the storage vault, in pail 277. Dose rate at approximately 1 m when leaving the hot cell was 164 mSv/h. The pail has been placed in vault location 4C. See updated vault layout attached.

Entry  Wednesday, November 23, 2022, 12:10, Adam Newsome, Conditioning Station, Standard Operation, TM4, UCx#41, TM4 Move - NHC to TCS 

TM4 was moved from the North Hot Cell to the Target Conditioning Station with UCx#41.

Entry  Wednesday, November 23, 2022, 11:27, Frank Song, North Hot-Cell, Standard Operation, TM4, UCx#41, electric and leak check after new target installed TM4_with_UCx#41_electric_and_leak_check_on_NHC.png

 an electric check and leak check done on NHC, TM4 with new target UCx#41 is ready moving to TCS.

Entry  Tuesday, November 22, 2022, 14:53, Carla Babcock, North Hot-Cell, Maintenance, TM4, , Multipin connector alignment pin on TM4 module loose 

The pin on TM4 has become loose again, making it very difficult to remove the multipin connector with the last target, C#4. For the installation of the next target, UCx#41, we will drill out the hole on the target side bracket so that it doesn't contact the multipin pin. Will try to remove this pin by force in January, or if needed change out the whole multipin bracket.

Entry  Tuesday, November 22, 2022, 12:41, Frank Song, North Hot-Cell, Standard Operation, TM4, C#4, electrical check TM4_with_C#4_electrical_check_right_after_moving_to_NHC.png

 TM4 with C#4 is checked on NHC right after moving from ITE.

Entry  Tuesday, November 22, 2022, 10:37, Adam Newsome, North Hot-Cell, Standard Operation, TM4, , TM4 Move - ITE to NHC 

TM4 was moved from ITE to NHC with C#4.

Entry  Tuesday, November 22, 2022, 09:44, Frank Song, ITE, Standard Operation, TM4, C#4, module disconnection TM4_with_C#4_disconnected_in_ITE.png

TM4 with C#4 was disconnected in ITE

Entry  Tuesday, November 15, 2022, 13:33, Frank Song, ITW, Standard Operation, TM2, UCx#40, Module Connection TM2_with_UCx#40_connection_in_ITW.png

 TM2 with UCx#40 is connected in ITW.

Entry  Thursday, November 03, 2022, 16:41, Carla Babcock, North Hot-Cell, Standard Operation, , UCx#39, Post irradiation inspection UCx#39 

Did the PIE on UCx#39-IGLIS on Thursday Nov. 2 2022, couple pictures uploaded to docushare. Did not remove the target, just the heat shield cover.

Final electrical check on the module showed a dead short from TGHT/TBHT to HV common, which we did not see online. Seems like it must have occurred after ramp down? It persisted on the target after we removed it from the module. We couldn't find any obvious contact points, because it seems it did not happen while current was running in the target. Possible locations are the bottom support leg for the TBHT and the top of the right side target leg, though it was difficult to confirm with the camera.

Otherwise the only thing to note was a blacker-than-usual spot on the inside of the Cu heat shield, downstream in the proton direction.

 

Entry  Thursday, November 03, 2022, 13:15, David Wang, Conditioning Station, Standard Operation, TM2, UCx#40, HS line helium pressure test. TM4 with UCx#40at TCS. 

Helium 70 psi. tested 5minutes at base leak rate 0.9 xE09 atm.cc/sec on HS line.  No leak.

Entry  Thursday, November 03, 2022, 10:08, Travis Cave, Spent Target Vault, Standard Operation, , UC#39, Spent Target Move Target_Index_2022-11-03.pdf

 The spent UC#39 target (pail #276) was removed from the north hot cell and place in the spent target vault (spot 4B) it was 14.4 mSv/hr when removed from the north hot cell. See attached PDF for further details. 

Entry  Wednesday, November 02, 2022, 11:11, Frank Song, North Hot-Cell, Standard Operation, TM2, UCx#40, electrical check TM2_with_UCx40_electrical_check_on_NHC.png

an electrical check was done on NHC, TM2 with new target UCx40 is ready moving to TCS.

Entry  Tuesday, November 01, 2022, 12:40, Frank Song, North Hot-Cell, Standard Operation, TM2, UCx#39, electrical check electical_check_for_TM2_with_spent_target_UCx39_on_NHC.png

 TM2 with spent target UCx#39 had an electric check in NHC.

After UCx 39# target was removed out., I did electrical check on TM2.   @500 V B to C is 5M ohm. all Others between are above 25Mohm. HV to Chasis is 650Mohm.  A to P is still short.

Entry  Tuesday, November 01, 2022, 12:37, Frank Song, ITW, Standard Operation, TM2, UCx#39, disconnection TM2_with_UCx39_disconnection_in_ITW.png

 TM2 with spent target UCx#39 was disconnected in ITW then moved to NHC.

Entry  Wednesday, October 19, 2022, 12:04, Carla Babcock, Conditioning Station, Repair, , , TCS:TBHT taken as replacement for ITE:TBHT 

During the last ITE run with the SiC#44 target, the ITE:TBHT controls card was fried twice. The first time we put in our spare, and the second time we just continued to run without controls readback. For the C#4 run starting Oct. 19, we used the conditioning station supply. As soon as one of the other supplies is fixed, we will install it in the conditioning station. The equipment list (https://triumfoffice365-my.sharepoint.com/:x:/g/personal/cbabcock_triumf_ca/EQPffP4p1P9JqEDWIHGRPfsBVDSQjMCv-M8ZNg4ngkyGHw?e=fnLVYe) tracks these movements.

Entry  Wednesday, October 19, 2022, 12:00, Carla Babcock, North Hot-Cell, Standard Operation, TM4, SiC#44, PIE on SiC#44 SiC44_PIE_20221012_150145.jpgSiC44_PIE_20221012.jpgSiC44_PIE_20221012_161755.jpg

Conducted PIE on SiC#44, which failed online. It had a cathode short, a target short and an anode short by the time we called the experiment off. In the post irradiation examination, two clear marks where the target legs touched the heat shield were found (see attachments 1 and 2). No marks were found to indicate where the cathode short would have been. The fibreglass sheath covering the anode wire where it passes over top of the coil was destroyed, must have been a result of sparking (see attachment 3). No other issues noticed, grid looked fine, though close inspection is difficult.

Entry  Monday, October 17, 2022, 08:07, David Wang, ITE/ITW, Repair, TM4, , A small leak on target station secondaryvacuum back up line by ITH MP1S.  
A small leak in target station secondary vacuum back up line is observed. It affects ITH CG2S,CG1S and CG4SA. Current draw on TP1s and TP4S is getting higher(above 1A) because of it. An internal leak in ITH MP1S is suspected by first round investigation. Close watching on system and further investigation are needed.
Initial Action Taken: none

17-Oct-2022 Comment by David Wang: On OCt 14th, Replaced a flexible hose on MP1S pump exhaust port,but did not solve the issue. High frequency vibration was sensed by hand on MP1S pump inlet and outlet ports. Pump height and position in pit are adjusted slightly in pit to reduce vibration. After, ITHCG2 and ITW CG4SA got a huge improvement in past 3 days. All back up line pressure are stabilized at normal operation status. Still, close watching on this issue is needed to ensure the present status is stabilized in long term.

The issue was returned after shielding block installation Monday morning at 8:30am. Investigated further,  I temporarily installed a turbopump used cooling fan on MP1s to improve pump heat dissipation. And a room fan is put outside on shielding blocks opening hole to increase air circulation into pit. Since then,  everything is perfect. All secondary turbo pumps current draw is around 0.5 to 0.6A which is the best.  I guess that short duo 10 pump life we observed in past could be related to high pump operation temperature in pit as well. We may increase the pump life if air circulation around the pump could be improved. A permanent solution is needed for it.

Entry  Thursday, October 13, 2022, 09:32, Travis Cave, Spent Target Vault, Standard Operation, , SiC#44, Spent Target Move Target_Index_2022-10-13.pdf

 Spent target move done. The SiC#44 was moved from the north hot cell to the spent target vault. It was placed in pail#275 and placed in spot#4A. It was 42.6mSv/hr when removed from the north hot cell. See attached PDF for further details about the vault.

Please note we will only have two free spots in the vault at the start of the running period after the winter shutdown 2023.

Entry  Tuesday, October 11, 2022, 12:39, Frank Song, ITE, Standard Operation, TM4, C#4, Module Connection TM4_with_C#4_connection_in_ITE.png

 TM4 with Target C#4 was connected in ITE.

Entry  Friday, October 07, 2022, 14:46, Adam Newsome, South Hot-Cell, Development, , , Addition of lift table to E-stop circuit ISAC_SHC_Lift_Schematic_updated_20221007.jpgPXL_20221007_185635660.MP.jpgPXL_20221007_185649720.jpg

A modification was made to integrate the hot cell's lift table into the E-stop circuit. See work permit I2022-10-07-1

The E-stop mounted on the right side of the small enclosure adjacent to the operator station will now serve to stop the lift table's up and down motion, as well as the turntables up/down and CW/CCW motions. Functionality was checked by B. Webster (electrical services) and A. Newsome.

 

Note: it is recommended next time there is a hot cell entry to inspect whether or not the limit switch specified in the schematic is actually installed. The schematic should be updated to match the drawing.

 

Redlined electrical drawing photo attached to this e-log, and the paper drawing is left inside the lift table's control box. The schematic will be revised based on the redline updates, likes as part of work request #6342 (to integrate this drawing into the turntable controls drawing package).

Entry  Wednesday, October 05, 2022, 09:31, David Wang, Conditioning Station, Standard Operation, TM4, C#4, HS line helium pressure test. TM4 with C#4 at TCS. 

TM4 HS line helium pressure test is done. 70psi helium pressure@ 3XE-8 atm.cc/sec . No leak.

Entry  Tuesday, October 04, 2022, 07:19, Frank Song, North Hot-Cell, Standard Operation, TM4, C#4, electrical check tm4_with_C#4_installed.png

 an electrical was done for TM4 with target C#4 installed on NHC.

Entry  Monday, October 03, 2022, 14:58, Matthew Gareau, North Hot-Cell, Repair, TM4, SiC#43 and C#4, Loose multipin guide pin MicrosoftTeams-image.pngMicrosoftTeams-image_(1).pngMicrosoftTeams-image_(2).png

 Today while I was removing the SiC#43 it was noticed that the multipin guide pin was loose.

This made it difficult to remove the target, and the multipin shoulder bolts removal was required.

With the loose pin it was not possible to attach the multipin for the target C#4.

Chad was able to tighten the multipin guide pin enough, however it became obvious that the pin could not be removed when it was attempted.

With the pin tightened, the target C#4 was installed and all checks were good.

It was recommend that once the C#4 target is removed the TM4 will need some repair to remove the multipin guide pin. 

 

Chad - Also it was noted that the guide pin (ITA6453) in question showed signs of plating or heat (see pictures I've added)

Entry  Monday, October 03, 2022, 14:28, Keith C Ng, Assembly/Bench Test, Maintenance, , , ITA2826 rev E assembly 

A fully built steerer sub assembly ITA2826 revision E was boxed and sealed and put on rack storage in ISAC B2 South Hot Cell area. It is contained in a blue bin and green tag. 

It is advised if this assembly is used, it should be inspected for damage before using in a source tray.

Entry  Monday, October 03, 2022, 09:42, Frank Song, ITE, Standard Operation, TM4, Sic#44, module disconnection TM4_with_SiC#44_disconnected_in_ITE.png

 TM4 with SiC@44 was disconnected in ITE.

Entry  Wednesday, September 28, 2022, 13:15, Matthew Gareau, North Hot-Cell, Maintenance, , , topped up the NHC window oil through the oil expansion tank IMG_20220928_121000.jpgIMG_20220928_124253.jpgIMG_20220928_124258.jpg

Myself and Maico were able to top up the NHC window oil.

The oil was filled through the expansion tank

- the Nitrogen line closed and the Nitrogen pressure valve was disconnected to ensure that no oil would go in to them.

- the pressure relief valve was disconnected to act as an air bleed line while we filled the oil

- with a funnel we slowly added the oil until the oil level could be read, showing about half full

- about 1.5 liters of oil were added

- once filled the Nitrogen line was reattached and the pressure was returned to recommended level 

- the remaining oil was returned the RH shop

Now the oil level will be monitored, which will help identify if there is any leak in the system.

Entry  Wednesday, September 28, 2022, 12:58, Matthew Gareau, North Hot-Cell, Repair, , , Chad repaired the right operator side manipulator IMG_20220926_091024~2.jpgIMG_20220926_091040.jpgIMG_20220926_091047.jpgIMG_20220926_091153.jpg

On 26/Sept/2022

Chad disassembled the right operator side manipulator, and noticed that gears in the handle were quite tight especially when compared to the left operator side manipulator. 

Once a dry grease was added, and the handle reassembled all seemed to be in working order.

There was noticeable wear on a shaft and Chad has suggested to order some spare parts for the wrist and handle. 

Entry  Thursday, September 15, 2022, 11:25, Travis Cave, Spent Target Vault, Standard Operation, , UC#38, Spent Target Move Target_Index_2022-09-15.pdf

 The spent target UC#38 was packed into pail #274 and placed in spot 1A of the vault. It was 33.3mSv/hr when removed from the north hot cell. See attached PDF for more vault details.

Entry  Wednesday, September 14, 2022, 13:45, Adam Newsome, Spent Target Vault, Development, , , Storage Vault: cable replaced and e-chain upgrade PXL_20220914_183329159.jpg

The motor cable for the storage vault was replaced as the old one was showing signs of wear. The U-track that the old cable ran through was also bent as a result of being hit.

In the process of replacing the cable, an e-chain was installed for cable management purposes. Mounting brackets were modified and a new U-track was installed as well. The new hardware is more robust than what was previously installed.

The vault door was opened and closed multiple times while observing the e-chain - everything behaved as expected. The system is operational.

 

Solidworks model IRH0189 is updated to show the changes

Entry  Tuesday, September 13, 2022, 14:10, Frank Song, ITW, Standard Operation, TM2, UCx#39, Module Connection TM2_with_UCx#39_connection_in_ITW.png

 TM2 with UCx#39 is connected in ITW.

Entry  Thursday, September 08, 2022, 09:06, David Wang, Conditioning Station, Standard Operation, TM2, UCx#39, HS line helium pressure test. 

TM2 with UCX#39 HS line helium pressure test is done at TCS. 70 psi helium 3minutes. No leak @0.0XE-9 atm.cc/sec.

Entry  Thursday, September 08, 2022, 07:20, Frank Song, North Hot-Cell, Standard Operation, TM2, UCx#39, electrical check TM2_with_UCx#39_E_Check.png

 An electrical check was done on NHC yesterday.

Entry  Tuesday, September 06, 2022, 14:05, Frank Song, North Hot-Cell, Standard Operation, TM2, UCx#38, electrical check after disconnection  TM2_electrical_check_on_NHC_with_spent_UCx38_on.png

 An electrical was done on the NHC for TM2 with spent Target UCx#38 on

Entry  Tuesday, September 06, 2022, 13:58, Frank Song, ITW, Standard Operation, TM2, UCx#38, module disconnection TM2_with_UCx38_disconnection_in_ITW.png

 TM2 with Target UCx38 was disconnected in ITW and moved to NHC

Entry  Tuesday, August 23, 2022, 11:33, Carla Babcock, ITE, Repair, , , ITE:ANODE swapped with TCS:ANODE 

ITE:ANODE supply reading strange currents - 17mA with the power supply on and no voltage. Checked anode circuit from electrical room:

Anode wire in electrical room shows 0L at 250V

Circuit with 50kOhm resistor mostly looks good (49-52kOhms) but a couple times read 28kOhms, no idea why. Tried jiggling all cables, unplugging and replugging and everything looks fine.

But power supply still seems to be giving out signal for 17mA readback. Decided fastest to swap with TCS power supply and troubleshoot this one on the bench.

Entry  Tuesday, August 23, 2022, 10:51, Carla Babcock, ITE, Repair, TM4, SiC#44, TBHT to HV common short on SiC#44-TM4 

TM4 with SiC#44 installed developed a short TBHT to HV common during its first heating in ITE. Was fine before installation. Now with everything cold TBHT to HVC is 25kOhms. Removed short in electrical room, will rely on short in the module.

Entry  Thursday, August 18, 2022, 10:41, Frank Song, ITE/ITW, Standard Operation, TM4, SiC#44, TM4 with SiC#44 connection in ITE TM4_with_SiC#44_connection_in_ITE.jpg

 TM4 with target SiC#44 was connected in ITE on Tuesday.

Entry  Thursday, August 18, 2022, 10:13, Travis Cave, Spent Target Vault, Standard Operation, , Ta#64, Spent Target Move Target_Index_2022-08-18.pdf

 The spent Ta#64 target in the north hot cell has been packaged and placed in the spent target vault. Pail#273 spot #5C 86.6mSv/hr upon removal from the north hot cell. For detail on the vault see attached PDF.

Entry  Thursday, August 11, 2022, 09:10, David Wang, Conditioning Station, Standard Operation, TM4, SiC #44, HS line helium pressure test. Gas line fitting on module top and gas line leak check.  

HS line helium pressure test is done at TCS. No leak. I also leak checked gasline adapter and fittings on TM4 top. No leak.  1/4 copper gas line between module and ITE was leak checked yesterday. It is good.

Entry  Wednesday, August 10, 2022, 08:10, Frank Song, North Hot-Cell, Standard Operation, TM4, Sic#44, electrical and leak check  TM4_with_Sic#44_eletrical_and_leak_check.jpg

 TM4 with Sic#44 installed and had an electrical / leak check at NHC. 

Entry  Tuesday, August 09, 2022, 12:23, Frank Song, North Hot-Cell, Standard Operation, TM4, Ta #64, Electrical Check for TM4 with Ta#64 after beam at NHC tm4_with_Ta#64_after_beam_at_NHC.jpg.jpeg

 An electrical check made at NHC right after TM4 moving from ITE.

Entry  Tuesday, August 09, 2022, 12:19, Frank Song, ITE, Standard Operation, TM4, Ta#64, TM4 with Ta#64 disconnection in ITE TM4_with_Ta#64_disconnection_in_ITE.jpeg

 TM4 with Ta#64 has been disconnected in ITE.

Entry  Friday, July 29, 2022, 12:05, Carla Babcock, North Hot-Cell, Repair, TM2, UCx#38, Repair of UCx#38 EE short in ante room 20220726_111649.jpg20220726_111641.jpg

UCx#38 developed a short between the plasma electrode and the extraction electrode about 30mins after reaching full temperature in the conditioning station. The decision was made to bring it into the anteroom and try to clean it there.

To do this, it was uninstalled, the parasitic attachments were removed and it was brought into the ante room.

I removed the EE and the PE, and cleaned quite a lot of material from them both with methanol. I think put the ionizer foil bar down the ionizer to help dislodge any material there, and I also turned the target over and tapped gently to get any material out. The first two times some flakes came out, the third time nothing came out. I then reinstalled the electrodes using the EE alignment tool (not sure how successfully, didn't push it into the ionizer too much because I was worried about catching the Rh foil).

The taret was meggered at 500V then reinstalled and electrical checks were done. Everything looks back to normal. Conditioning in ITW was successful.

Entry  Thursday, July 28, 2022, 10:47, Travis Cave, Spent Target Vault, Standard Operation, , SiC#43, Spent Target Move Target_Index_2022-07-28.pdf

 The spent target SiC#43 was moved from the north hot cell in pail #272 and place in 5A of the spent target vault. See attached PDF for details.

Entry  Wednesday, July 27, 2022, 08:11, Frank Song, ITW, Standard Operation, TM2, UCx#38, Module Connection TM2_with_UCx38_connection_at_ITW.jpg

 TM2 with Target UCx#38 was connected in ITW.

Entry  Tuesday, July 26, 2022, 13:50, Frank Song, North Hot-Cell, Standard Operation, TM2, UCx#38, TM2 electrical check with Target and No external Connections TM2_with_UCx38_echeck_on_NHC.jpg

 A standard electrical check was done for TM2 after the short issue be fixed.

Entry  Thursday, July 21, 2022, 10:24, Frank Song, North Hot-Cell, Standard Operation, TM2, UCx#38, electrical check TM2_with_UCx38_echeck_on_NHC.jpg

 A electrical check was done for TM2 with UCx#38

Entry  Tuesday, July 19, 2022, 11:53, Frank Song, North Hot-Cell, Standard Operation, TM2, SiC#43 Febiad, electrical check e_check_for_TM2_with_SiC43_Febiad.jpg

 A electrical check was done at NHC, see the pic attached with please.

Entry  Tuesday, July 19, 2022, 11:47, Frank Song, ITW, Standard Operation, TM2, SiC#43 Febiad, TM2 with SiC#43 disconnected in ITW  TM2_with_SiC43_disconnection_in_ITW.jpg

 the module was disconnected in pit and moved to NHC.

Entry  Wednesday, July 06, 2022, 10:30, Travis Cave, Spent Target Vault, Standard Operation, , SiC#42, Spent Target Move Target_Index_2022-07-06.pdf

 The spent SiC#42 was moved from the north hot cell to the spent target vault, it was placed in pail #271 and put in spot 2B. see attached PDF for more details.

Entry  Monday, July 04, 2022, 11:54, Nadia Jorgenson, Spent Target Vault, Maintenance, , , Added Lubrication,fittings need to be changed Mini_Vault_Grease_Fitting.jpg

Dan lubricated components on the target storage vault (This was an outstand task from annual inspection). No issues on the main storage vault but we were not able to lubricate the mini storage vault because the position of the grease nipple on the fittings makes them inaccessible, see attached pictures. All four should be replaced with 90 deg fittings. 

Entry  Monday, July 04, 2022, 11:44, Nadia Jorgenson, Safe Module Parking, Standard Operation, , , Annual Inspection of Safe Module Parking - Mechanical  SMP_Missing_Washers_1.jpgSMP_Missing_Washers_2.jpgSMP_Missing_shims.jpg

 

An annual mechanical inspection was performed on the SMP today by Dan McDonald and Nadia Jorgenson. The following items were checked:

 

  • Lubricate chains
    • Not needed
  • Inspect tensioners
    • No issues found
  • Tighten fasteners
    • A few slightly loose, most are in need of washers, see attached pictures
    • Could use some shims in a few places, see attached picture
  • Inspect components during rotation - chain drive, rotary limit switch, and cable reel etc.
    • No issues
Entry  Thursday, June 30, 2022, 14:28, Nadia Jorgenson, Safe Module Parking, Standard Operation, , , Annual Inspection of Safe Module Parking - Electrical  

 

An annual electrical inspection was performed on the SMP today by Travis Cave and Nadia Jorgenson as per Work Permit I2022-06-30-2. The following items were checked:

 

Electrical Inspection of Safe Module Parking:

  • Check condition of wiring for physical/radiation/UV damage
    • OK, no signs of damage
  • Check for cable tray debris or damage
    • Some objects stored in the cable tray but nothing concerning, no damage noted
  • Check inside control panel: components and wiring, labeling
    • Labeling intact, components in good condition
    • Wiring in good condition
  • Verify camera views
    • Checked, no issues
  • Check connectors for damage
    • All connectors OK
  • Check pendant for damage and verify labeling intact
    • Pendant OK
  • Lid open/close test
    • Lid was opened and close multiple times - smooth operation, no concern
    • Lid close logic was checked - OK
  • Vessel rotation and limit switch check
    • Centre, CW and CCW limits were checked, functioning

 

Still to be done – Mechanical Inspection:

  • Lubricate chains
  • Inspect tensioners
  • Tighten fasteners
  • Inspect components during rotation - chain drive, rotary limit switch, and cable reel etc.
Entry  Tuesday, June 28, 2022, 14:13, Frank Song, ITE, Standard Operation, TM4, Ta#64, Module Connection tm4_with_Ta#64_connection_in_ITE.jpg

 TM4 with Ta#64 was connected in ITE. see attachment please.

Entry  Thursday, June 23, 2022, 13:04, David Wang, Conditioning Station, Standard Operation, TM4, Ta#64, helium pressure test on TM4 HS line.  

With Ta#64 installed , TM4 HS line was helium pressure tested at TCS. base leak rate is 0.0XE-9 atm.cc/sec. HS line tested leak rate is 3x E-7 atm.cc/sec on 5 minutes 50 psi helium testing. Leak check result wasgood at NHC by helium spray method. We decided to apply water to HS and all other water lines still. The vacuum status is closely being watched. So far, TCS pumping down trend is still good. HS line supply water valve was switched on and off couple of times at TCS IG1 1.15 XE-6 range, and no vacuum spike was observed. More information will be logged in during the TM4 and target conditioning stage at TCS. 

Entry  Thursday, June 23, 2022, 10:22, Travis Cave, Spent Target Vault, Standard Operation, , UC#37, Spent Target Move Target_Index_2022-06-23.pdf

 UC#37 was placed in pail #228 and place in spot 1B it was removed the north hot cell. See attached PDF for more details of it and the vault.

Entry  Thursday, June 23, 2022, 07:11, Frank Song, North Hot-Cell, Standard Operation, TM4, Ta#64, electrical check Ta#64.jpg

 New Target Ta#64 was installed on TM4. Electrical measurement result is good. c/w attachment.

Entry  Wednesday, June 22, 2022, 09:14, David Wang, South Hot-Cell, Standard Operation, TM2, SiC#42 and SiC#43. , Three of TM2 moves related to SiC#42 to SiC #43 target switching job.  

Monday morning June 20th: TM2 with SiC # 42 was moved from ITW to NHC.

Monday afternoon: TM2 with no target was moved from NHC to SHC due to 10 pin connector guide pin loose issue. The guide pin has to be moved out in SHC due to NHC manipulator configuration limit .

Monday afternoon: TM2 with SiC # 43 was moved from SHC  to ITW.

all module moves are smooth.

Entry  Wednesday, June 22, 2022, 09:03, David Wang, ITE, Standard Operation, TM4, UCX37# P2N, Remotely removed TM2 from ITE to NHC 

TM2 with UCx#37 P2N target  was removed from ITE to NHC yesterday morning. The move is good.

Entry  Tuesday, June 21, 2022, 18:43, Frank Song, North Hot-Cell, Standard Operation, TM4, UCx#37, electrical check p2n_ucx37_electrical_check.jpg

 A p2n target in TM4 was electrical measured on NHC. see attachment pls.

Entry  Tuesday, June 21, 2022, 18:30, Frank Song, ITW, Standard Operation, TM2, SiC#43 Febiad, Module Connection TM2_with_sic_42_connected_in_ITW.jpg

 TM2 with Febiad Target SiC #43 was connected in ITW. NOTE: the number of TARGET in attached picture should be #43. 

Entry  Tuesday, June 21, 2022, 17:49, Frank Song, ITE, Standard Operation, TM4, UCx#37, TM4 disconnection TM4_with_UCx#37_disconnection_in_ITE.jpg

 the module with target UCx37 was disconnected in ITE.

Entry  Tuesday, June 21, 2022, 15:36, Matthew Gareau, North Hot-Cell, Repair, TM2, SiC#42, SiC#43, multipin guide pin issues 

 While removing the SiC#42 it became apparent that the multipin guide pin had become loose again and was not allowing the target to dismount from the module.

The multipin shoulder bolts were removed and then the multipin was able to be pried off.

However the NHC manipulator were not able to reach the guide pin to remove it, which would be required before the SiC#43 could be installed.

The target module was then moved to the SHC where the guide pin could be removed and the installation of SiC#43 took place, along with the transfer of the parasitic attachment onto the SiC#43.

This problem seems to suggest that the multipin could use some redesign to ensure smoother target exchanges.

Entry  Monday, June 20, 2022, 18:03, Frank Song, South Hot-Cell, Standard Operation, TM2, Sic#43, electrical check TM2_with_SiC43.jpg

 TM2 with new target SiC#43 was electrical checked at SHC. please see attachment.

Entry  Monday, June 20, 2022, 11:00, Frank Song, North Hot-Cell, Repair, TM2, SiC#42, Failed Sic#42 electrical measurement at NHC Failed_Sic#42_electrical_measurement_at_NHC.jpg

 An electrical check was done at NHC, see attachment pls.

Entry  Thursday, June 09, 2022, 09:47, Matthew Gareau, South Hot-Cell, Repair, TM2, SiC#42, containment box repair, Einzle lens, multi pin 

On June 2 2022, while attempting to install target SiC#42 a gasket fell off the water line. I attempted to remove the target to have the gasket reattached, however the multi pin connector guide pin was loose and was preventing the target from being removed. During the attempt to remove the target it was noticed that an electrical cable in the back of the module had become loose and was dangling. The target was then secured to the module, and then the module was moved to the SHC to complete the job/repairs.

June 3 2022, containment box was removed, Einzle Lens cable reattached and tested, and the multi pin guide pin was retightened.

On June 6 2022, the containment box was damaged while lifting the containment box back onto the module.

The left rear corner of the box caught on the module and the corner weld snapped and folded the corner down about 90 degrees.

With help from Chad, we were able to restraighten the corner with a C-clamp, enabling the box to be reattached to the module.

However the 2 bolts that were on the corner that attach to the module were not able to be aligned and were not used.

The target was reattached to the module, and to save time was brought directly to ITW, skipping the conditioning station. 

Entry  Tuesday, June 07, 2022, 14:15, Frank Song, ITE/ITW, Standard Operation, TM2, SiC#42, Module Connection TM2_with_sic_42_connected_in_ITW.jpg

 TM2 with Febiad target SiC#42 was connected in ITW.

Entry  Monday, June 06, 2022, 14:15, Frank Song, South Hot-Cell, Standard Operation, TM2, SiC#42, TM2 FEBIAD with Target and No external Connections TM2_with_FEBIAD_SiC_42_electrical_check.jpg

 An electrical check was done at SHC for TM2 with FEBIAD SiC #42 Target. 

Entry  Wednesday, May 25, 2022, 13:43, Frank Song, ITW, Standard Operation, TM2, Febiad-Test, module disconnection tm2_disconnection.jpg

 TM2 with a test target was disconnected in ITW.

Entry  Wednesday, May 25, 2022, 13:23, David Wang, ITE, Standard Operation, TM4, , Annual ITE water signal interlocks. 

Annual ITE water signal interlocks check is done with Rob Shank. All ITE water signal  interlocks work fine.

Entry  Wednesday, May 25, 2022, 10:23, Nadia Jorgenson, Spent Target Vault, Repair, , , F-308 Loading, Mini-Storage Vault Failure 

5 pails were moved from the mini-storage vault into F-308's

At one point during the loading the mini-storage vault door would not close. Cause was a blown fuse, which was replaced and operations were able to continue as usual. Possible reason the fuse blow was a tilted pail that may have become jammed between the tray and the roof of the mini-storage vault. 

 

[Edit 2022-12-01, Adam Newsome]: the pails which were removed were: 220, 227, 233, 235, 238

Entry  Thursday, May 19, 2022, 15:05, Frank Song, ITE, Standard Operation, TM4, UCx#37, UCx#37 P2N connection on TM4 01_UCx37_P2N_connection_on_TM4.jpg02_UCx37_P2N_connection_on_TM4.jpg03_UCx37_P2N_connection_on_TM4.jpg

 TM4 with UCx#37 was connected in ITE. Attachment available.

Entry  Thursday, May 19, 2022, 11:42, Travis Cave, Spent Target Vault, Standard Operation, , Sic#39, Ta#59, C#2, UC# 32 & 30, Targets moved to the mini vault. Target_Index_2022-05-19.pdfMini_Vault_Target_Index_2022-05-19.pdf

 Sic#39, Ta#59, C#2, UC# 32 & 30 have been moved from the spent target vault to the mini vault. See the attached pdf for details of the vaults.

Entry  Wednesday, May 18, 2022, 13:52, Frank Song, South Hot-Cell, Standard Operation, TM4, UCx#37, electrical check  1.jpg2.jpg3.jpg

 The TM4 with installed target #UCx37 had been electric checked at SHC. PICs attached.

Entry  Wednesday, May 11, 2022, 16:29, Nadia Jorgenson, Spent Target Vault, Standard Operation, , , Routine mechanical inspection: storage vault Motor_wiring_ISAC_storage_vault.jpg

 An inspection was performed on drive systems for the main storage vault by Dan McDonald, Travis Cave and Nadia Jorgenson. The functionality was not tested. Some areas for improvement noted, but otherwise nothing concerning was discovered. 

 

Notes:

  • The wire insulation to the motor is showing wear and tear. Should be replaced in the future. For now was patched with electrical tape, see picture. May be beneficial to add an e-chain for the portion of the wiring that moves when door is opening and closing

  • Emergency close mechanism cable should be changed to have a 5/32” Nico Sleeve

  • Moving parts still need to be lubricated


  • Chain inspected (OK)

  • Gearbox inspected - OK

  • All drive system set screws checked and tightened

  • Sprocket alignment checked - OK

  • Limit switches checked - OK

  • Emergency close mechanism cable checked - OK

 

 

 

Entry  Wednesday, May 11, 2022, 16:15, Nadia Jorgenson, Spent Target Vault, Standard Operation, , , Emergency Close Mechanism Test 

 The emergency close mechanism for the Storage Vault door was tested by Travis Cave, Nadia Jorgenson, and Dan McDonald. The door was opened to its fully open limit, then closed with the emergency system. 

The test was successful.

Entry  Friday, May 06, 2022, 10:12, Adam Newsome, Spent Target Vault, Maintenance, , , Annual Inspection of Mini-Storage Vault 

The annual inspection of the mini-storage vault was performed today. The following items were checked:

  • Cabling and cable management
  • Connectors
  • Controls box - internal wiring and components, functionality
  • Limit switches - functionality, wiring, mounting
  • Motor
  • Bearings
  • Set screws
  • Miscellaneous fasteners (some loose, but were tightened)

Everything appears to be in good working order.

Note: in the near future, the bearings should be greased. This is planned to take place during the next inspection of the main storage vault.

Entry  Thursday, April 28, 2022, 08:16, David Wang, ITW, Standard Operation, TM2, , Annual ITW water signal interlocks check . 

Annual ITW water signal interlocks check was done with TM2 in ITW.   Water signal interlocks on all water circuits related to TM and 2A beam lines in ITW work fine. 

Entry  Thursday, April 28, 2022, 07:24, Frank Song, ITW, Standard Operation, TM2, Febiad Test Target, Module Connection module_connection_checklist20220426.jpg

 TM2 was connected in ITW with a Febiad Test Target. 

Entry  Thursday, April 21, 2022, 13:29, Frank Song, South Hot-Cell, Standard Operation, TM2, Febiad TEST, TM2 FEBIAD WITH A TEST TARGET TEST_FEBIAD_TARGET_E_CHECK.jpg

 A Test Febiad Target was installed and checked at SHC. 

Entry  Wednesday, April 13, 2022, 11:54, Carla Babcock, South Hot-Cell, Maintenance, TM2, , EZL cable change MicrosoftTeams-image_(25).png

Chad changed the EZL cable and plugs on TM2. New cable runs along the cable trays.

Entry  Monday, April 04, 2022, 21:04, Carla Babcock, Conditioning Station, Development, TM2, , HV testing of IGLIS wires in TM2 

TM2 is in the TCS without containment box for HV testing following the installation of the IGLIS wiring.

Not great results so far - sat at 42.5kV for nearly 2 hours, current around 200uA and occasional sparks. I did not have time to go higher, will do this tomorrow. The sparks could be conditioning but it looks a bit suspicious to me. We will see if the ramp up tomorrow is very easy and how high we can go. I have data from HV testing of TM2 in December for comparison.

The EZL was reacting to all sparks, so I went into the target hall to see if it was sparking on the module top, but there was no sparking there.

 

Possible mitigations:

  1. Re-do the connections on top of the service cap to remove the extra length on the wires inside the service cap and inspect the routing carefully to make sure nothing is in the wron place.
  2. Inspect the wiring in the source tray to see if there is evidence of sparking in a certain area.

 

Second round of testing Tuesday April 5 2022:

Much better results, seems most of the sparking was conditioning. Went right up to 42.5kV with no issues. Spent quite a while getting up to 50kV, and didn't leave it there for more than a couple mins. May be running into the limitations of the HV cage at this point. Bias current was much lower, something like 140uA at 45kV.

 

Third round of testing Wednesday April 6 2022:

Ramped easily back to 45kV, a little more sparking above that. Sat at 47kV for ~30mins with no sparks. Won't try to go higher in case of issues with the cage. Will try to condition up to 50kV in the station. Other than the possible low megger value between B and C, all looks good.

Entry  Monday, April 04, 2022, 10:44, Nadia Jorgenson, South Hot-Cell, Repair, , , Turntable Chain Repair Hot_Cell_Chain_1.jpgHot_Cell_Chain_2.jpg

 Last week we repaired the South Hot Cell turntable chain/sprocket. Chain was loose and there was a few section where the chain was not lining up properly with the sprockets.

3 issues were discovered:

 

-        One of the pins was bent. It’s been replaced but is a temporary fix. Need to replace them with stronger pins.

 

-        The smaller sprockets near the motor were too far from the main turntable sprocket which was causing the links to not immediately line up with the teeth on the turntable sprocket. With too much slack in the chain, it’s likely that this is were the misalignment was starting. This was fixed by adjusting the motor position and the position of the yellow plate bolted to the floor.

 

-        The yellow plate that is bolted into the floor has oversized holes relative to the bolts/washers used. This allows us to adjust the position, but the washers are to thin and are being bent/pulled into the holes. Should be replaced with thicker washers that can withstand the tension and this will help prevent the plate from sliding out of position.

Entry  Wednesday, March 02, 2022, 10:51, David Wang, ITE/ITW, Standard Operation, , , Replaced old turbopump and 2A3M20 wire scanner are transferred to cyclotron tunnel.  

Replaced 9 old turbo pumps from ITE/ ITW and  one 2A3M20 wire scanner from ITE are transferred to cyclotron tunnel for storage. It is TH RAD waste cleanup task in winter shut down.

Entry  Tuesday, March 01, 2022, 11:51, David Wang, Spent Target Vault, Maintenance, , , UCx #32 has been repacked in NHC.  

UCx 32# P2N target in vault slot 1B is repacked is morning for Ferran to take out his samples( in two small plastic containers) stored in pail last July when Chad did the spent target job. The job went well.  Old pail # is 254# and new pail # is 233. It is put back to 1B in vault.

Entry  Friday, February 25, 2022, 10:22, Adam Newsome, South Hot-Cell, Development, , , Addition of E-Stops and Turntable Vertical Motion Limit Switch 

Two changes have been made to the control system to the South Hot Cell:

  1. Addition of two emergency stop buttons: one located in the Target Hall on the wall adjacent to the hot cell, and one located on the control panel adjacent the operator station.
  2. Addition of limit switches to the turntable's vertical drive system to prevent over-travel at both the upper and lower limits.

 

The emergency stops will both stop all turntable motion: vertical and rotational.

An update to operating procedures: in order for the vertical motion system to function, the limit switch cable must be plugged in. When plugging in the vertical drive motor to the wall outlet as per normal operating procedure, it is now required to also connect the limit switch (which is mounted near the motor on the driveshaft) to the cable coming from the appropriately labelled junction box on the South wall (M12 connector).

 

These changes are based on electrical drawings IRH2083 - IRH2085 and mechanical assembly drawing ITA6739. The changes have been commissioned according to commissioning plan Document-218490. The commissioning report will be uploaded to DocuShare. The work permit for this upgrade was I2022-02-15--3.

 

Entry  Thursday, February 24, 2022, 13:23, David Wang, ITE/ITW, Maintenance, , , Polyurethane water cooling lines replacement in ITE and ITW.  

Polyurethane  water cooling lines in ITE and ITW  HV shroud are replaced.  Both stations Ta, Tu, MSP, HS, Coil , EE in HV shroud are new lines.

Entry  Thursday, February 17, 2022, 13:24, David Wang, Spent Target Vault, Maintenance, , UCx #34, Repackage of UCx #34in NHC. 

UCX34# in pail 258(Vault lot 7C) has been repacked today. It is an investigation to find a possible leak source of radioactive Iodine in vault. The new pail number is 268. It is back to vault 7c . I wrote down the information in log book. The job is smooth today. I retrieved UCx 34 old pail and liner to TH. The liner from UCx#34 only has 3000 counts.  I bagged it. It could be used later. However, the pail has 500K counts contamination on bottom outside rim. It may accidently be slided out of plastic bag and touched the NHC table during the repackage. I bagged it and store it in silo area. When we do drum clean up, I will throw it in the drum.

Entry  Wednesday, February 16, 2022, 15:19, Frank Song, Cooling, Repair, , , high active cooling water valves repaired/replaced RETURN_drain_valve_in_ITE.jpgFEBIAD_COIL_in_ITW.jpgENTRANCE_COLLIMATOR_RETURN_in_ITW.jpgMAIN_S_and_R_VALVES_in_ITW.jpg

 A 3/8 inch drain valve on return cooling line was replaced in ITE. In the meantime two 1/2 inch valves labeled FEBIAD COIL and ENTRANCE COLLIMATOR RETURN at ITW were replaced . The 2 inches leaky supply/return water valves in ITW were repaired as well. Pls check pics

attached here for detail.

Entry  Tuesday, February 15, 2022, 11:18, Frank Song, Cooling, Repair, , , Replace 2 leak valves on high active water system v10_v11.jpgv10.jpgv11.jpg

 The valves #V10 & V11 beside high active water pumps were replaced in Target Hall, pics attached.

 

Entry  Thursday, February 10, 2022, 12:42, David Wang, ITE, Standard Operation, , , ITE HV test woithout mdoule was done. 

Carla did the test. That is what she wrote in Feb 04th:  "I am done with the HV testing at ITE - the results were the same as at ITW. It stayed at 59kV for 30 mins with no issues. Trying to go above 59.5kV is probably possible but a bit more risky. ITE also has a band, from 54-56kV, where the current jumps around like crazy".

Entry  Thursday, February 10, 2022, 12:24, David Wang, ITW, Standard Operation, , , ITW HV test without mdoule.  

  Carla did the test. and reported the result as following: HV testing of ITW is complete. It was pretty well behaved up to 59.5kV, and sat at 59kV for 30mins with no sparks (that EPICS caught). There was some strange behaviour of the current between 51kV and 53kV - it was jumping by 20uA or more - but there didn't seem to be any voltage response, and it went away after 53kV (though it returned on the way back down). The test was done in Feb 02.

Entry  Thursday, February 10, 2022, 11:45, David Wang, Spent Target Vault, Standard Operation, , UCx#33., Spent target UCx #33 has been repacked with a new pail and lid in NHC.  

Spent target UCx #33 has been repacked with a new pail and lid in NHC. Old pail #255. New pail # 267. Location: Vault slot 1C.  it is an investigation job for  a possible leak pail in vault.  

Entry  Wednesday, February 02, 2022, 11:05, David Wang, Crane, Standard Operation, , , Target hall overhand crane annual insepection.  

Tom Kauss finished target hall overhead crane annual inspection today. The crane works fine. He issued new inspection tag and e-logged the job. 

Entry  Tuesday, January 25, 2022, 12:49, David Wang, ITE/ITW, Standard Operation, , , Target station vacuum system visual inspection.  

Two shielding blocks  above vacuum station at TH west end were opened for inspection. Checked ITH:MP1, MP2 lubricant color and level through sight gauge on pumps. They are still ok.  Restored the shielding blocks.  Checked ITM:MP1 by decay tank (Mirror checked  sight gauge by north wall). Added lubricant to ITM:MP1 to middle level on sight gauge.  

Entry  Tuesday, January 25, 2022, 08:57, David Wang, ITE/ITW, Standard Operation, , , ITE/ITW have been cleaned with vacuum canister.  

ITE/ITW  are cleaned with vacuum canister. HV  cage inside and blue nylon insulators are wiped.  Garbage inside the pits are cleaned out.

Entry  Monday, January 24, 2022, 11:18, David Wang, ITE/ITW, Standard Operation, , , TH emergency exit hatch functional check 

TH emergency exit hatch which is located on TH west end roof is opened and closed for functional check. The hatch works fine. The limit switch on hatch is in position. No obstacle on hatch way to the roof. 

Entry  Thursday, January 20, 2022, 11:09, Travis Cave, Spent Target Vault, Standard Operation, , Ta#63, Spent Target Move Target_Index_2022-01-20.pdf
The spent Ta#63 has been moved from the north hot cell to the spent target vault. It was place in pail#266 and 
placed in spot #3B of the vault. see attached PDF for more details.
Entry  Thursday, January 20, 2022, 08:18, David Wang, North Hot-Cell, Standard Operation, TM4, No target, TM4 was removed from NHC to S_W silo yesterday.  

TM4 was removed from NHC to S_W silo yesterday.  The remove is smooth and successful.

Entry  Wednesday, January 19, 2022, 13:36, David Wang, Crane, Standard Operation, , , Targe hall crane below hook attachment pins and plates annual inspection.  2022-01-19_174.jpg2022-01-19_172.jpg

Tom Kauss inspected target hall crane below hook attachment pins and plates ITA6550-01. He certified the use of these pins and plates. The inspection of these pins and plates was in Target hall crane annual check list. It was issued as a calibration index by Isaac Earle in 2022-Feb-08.  After inspection, The inspection tag  was issued and attached to pin. Tom has an inspection record on this job. See attachments.

Entry  Wednesday, January 19, 2022, 13:26, David Wang, Crane, Standard Operation, , , Inpection of Target module lifting frames ITA0494-1997-01 and ITA0494-1997-02.  2022-01-19_170.jpg2022-01-19_173.jpg2022-01-19_175.jpg2022-01-19_176.jpg

Tom Gauss inspected  two target module lifting frames ITA0494-1997-01 and ITA0494-1997-02.. He certified the use of these two frames. Inspection tags have been issued and attached to frames. He has inspection record on them. See attachments.

Entry  Wednesday, January 19, 2022, 09:00, Frank Song, North Hot-Cell, Standard Operation, TM4, Ta #63, Electrical check on TM4 at NHC without target 20220119_080049.jpg

 David did electrical check after target removed from TM4 at NHC. see attachment pls.

Entry  Tuesday, January 18, 2022, 11:02, Frank Song, North Hot-Cell, Standard Operation, TM4, Ta #63, TM4 SIS with Target and No external Connections tm4_with_Ta#63_on_NHC.jpg

 David made an electric check after TM4 been moved to NHC from ITE. The target is still on the module. Please find out attached pic for detail.

Entry  Monday, January 17, 2022, 10:44, Frank Song, South Hot-Cell, Standard Operation, TM2, UC#36 (the target removed), TM2 electrical check without Target. TM2_without_UCx36_at_SHC_(2).jpg

 An electric check was done right after module moving from SMP to SHC. 

Entry  Wednesday, January 12, 2022, 14:09, Travis Cave, Spent Target Vault, Standard Operation, , UC#36, Spent Target Move Target_Index_2022-01-12.pdf

 The spent UC#36 target in the north hot cell has been removed and placed in the spent target vault. See attached PDF for detail note that the PDF does not show that spot 2B is occupied by the 2A3M20 pail.

Entry  Tuesday, January 11, 2022, 11:51, David Wang, North Hot-Cell, Standard Operation, TM2, , TM2 has been moved from NHC to SMP. 

TM2( no target ) has been moved  from NHC to SMP.  The moving is smooth and successful.

Entry  Tuesday, January 11, 2022, 11:50, David Wang, ITW, Maintenance, , , ITW Exit module 1 side sqaure panel O-ing seal replacement. 

Frank and I replaced ITW Exit module 1 side square service panel o-ring seal. Also, The target module pit top flange o-ring seal in ITW pit is replaced.  

Entry  Monday, January 10, 2022, 12:38, David Wang, North Hot-Cell, Standard Operation, TM2, , TM2 has been moved from ITW to NHC. 

Travis and Nadia moved TM2 from ITW to NHC this morning. The move is smooth and successful.

Entry  Monday, January 10, 2022, 09:31, David Wang, ITE, Standard Operation, TM4, , ITE primary and secondary vacuum vessel leak check.  

ITE primary and secondary  vacuum vessel leak check has been down.  Base leak rate 0.0x E-9 atm.cc/sec on LD. Only 2.8 XE-9 atm.cc/sec leak has been found on big T tank seal which is very tiny. all other seals are perfect leak free.   No concern

Entry  Thursday, January 06, 2022, 13:54, David Wang, ITE, Standard Operation, TM4, , helium pressure test on TM4 internal cooloing lsine at ITE. 

Helium pressure 70 psi. 3 minutes on each circle untill LR on LD is balanced. Base leak rate on LD:0.0xE-9 atm.cc/sec.   The result:

A:   slowly to1.8Xe-8atm.cc/sec after 2 minutes and balanced there. 

B:   slowly to 2.0XE-8 atm.cc/sec after 2 minutes and balanced there.

C:  quickly response  to 3.1XE-8 atm.cc/sec and balance there.

D : slowly to 3.0X E-9 atm.cc/sec and balanced there.

All others including coil1, coil 2 ,MSP, EE, HS, window are perfectly leak tight. No response on LD.

 The leak rate on A,B,C,D are in low E-8 or E-9 atm.cc/sec range.  They should seal cooling water without leak.    No concern. 

 

Entry  Thursday, January 06, 2022, 10:37, David Wang, ITW, Standard Operation, TM2, , ITW vacuum vessel and TM2 internal cooling lines leak check in pit.  

Frank and I finished ITW and TM2 leak check. TM2 internal water-cooling lines are leak free. They passed 70 psi helium pressure test. We found some small leaks on ITW primary and secondary vacuum vessel. I list them here:

  1. Exit module 2 service cap top plate to cap body O-ring at SW corner. Leak rate 2XE-8 atm.cc/sec. It is an old leak we found before. Solution: I sprayed high vacuum resin to leak area. It is improved to 3Xe-9atm/sec now. We can leave it there.
  1. Exit module 1 module to tank flange o-ring at target module side and north side. Leak rate 3XE-8atm.cc/sec. Solution: replace the o-ring. It involves in disconnect exit module 1 and remove it out. We may or may not change it. Let's check the schedule and discuss it later. We need Travis help on module moving out.
  2. Exit module 1 north side sqaure service panel o-ring. Leak rate 2XE-7 atm.cc/sec.  Solution: replace the o-ring. It is a straight forward job.  It will be done this shut down.
  3. Exit module 1 north side round roughing valve panel o-ring. Leak rate 8XE-9 atm.cc/sec. Solution: Replace the o-ring. It involves in disconnecting and removing ITW RV4.  It could be done this shut down.
  4. Big T tank o-ring seal underneath the flange at exit 1 module north side . Leak rate 3XE-8 atm.cc/sec. Solution: None. All modules and module base flange have to been moved out to replace this big o-ring.  It is a huge project to change this o-ring .  I checked this big o-ring seal every year. It is first time a small leak is found.  Maybe, we could try high vacuum resin spray first.
  5. Dump module flange o-ring at the side by Target module. Leak rate 8XE-9 atm.cc/sec. It cannot be confirmed since the TM o-ring is just beside it. Mostly, the leak is on dump module side. We changed TM flange o-ring every year. But we never changed dump module flange o-ring in history. Many copper cooling lines above the dump module has to be removed to remove the dump module out. I do not think we have time to do it this year. Also,  the leak rate is pretty small. Maybe, we can schedule it next year.

  Most these small leaks are close to turbopumps. This could be the reason the ITW vacuum on gauges are still pretty good.

Entry  Wednesday, January 05, 2022, 12:45, Frank Song, ITW, Maintenance, TM2, UC#36, TM2 SIS with Target and No external Connections TM2_with_UCx36.jpg

 electrical checked in ITW

Entry  Wednesday, January 05, 2022, 09:38, Frank Song, ITE, Maintenance, TM4, Ta #63, TM4 SIS with Target and No external Connections tm4_with_Ta#63.jpg

 electric check done in ITE. 

Entry  Tuesday, November 30, 2021, 12:51, David Wang, ITE, Standard Operation, TM4, Ta#63., Tm4 has been connected in ITE.  from_my_cellphone_2598_647.jpgfrom_my_cellphone_2598_648.jpgfrom_my_cellphone_2598_649.jpgfrom_my_cellphone_2598_650.jpg

TM4 has been connected in ITE. See attachment for checklist.

Entry  Tuesday, November 30, 2021, 11:03, David Wang, ITE, Standard Operation, TM4, Ta#63., Remotely remove TM4(Ta#63) from TCS to ITE. 

Remotely remove TM4(Ta#63) from TCS to ITE. The move is smooth and successful.

Entry  Monday, November 29, 2021, 12:16, David Wang, Spent Target Vault, Standard Operation, , , Five spent targets have been loaded into F308s 

We loaded UCx #29 , SiC #38  , Ta#53, Ta#56 ,and Ta#57 from mini storage  into F308 flasks.  Later, the flasks are transferred from TH to B2 HC service area. In TH, Working area and Mini storage are cleaned and surveyed.  Tools are cleaned and surveyed as well. No contamination.   Mini- storage is empty now.

Entry  Friday, November 26, 2021, 10:52, Adam Newsome, Spent Target Vault, Standard Operation, , UC#35, Spent Target Move Target_Index_2021-11-26.pdf

The spent UC#35 target has been moved from the south hot cell to the spent target vault. It was placed in pail #264 and put in spot 6A of the vault. See attached PDF for more details.

Entry  Thursday, November 25, 2021, 10:33, David Wang, Conditioning Station, Standard Operation, TM4, Ta#63. , helium pressure test on TM4 HS line at TCS.  

Helium pressure test on TM4 HS line at TCS is done.  LD base leak rate 0.0 xE-9 atm.cc/sec. Helium pressure 70psi. HS line had been helium pressurized for 5 minutes during the test. No response on LD. HS line with Ta#63 is leak free.

Entry  Wednesday, November 24, 2021, 09:08, Adam Newsome, Conditioning Station, Standard Operation, TM4, , Remotely moved TM4 from SHC to TCS 

TM4 was moved from the South Hot Cell to the Conditioning Station.

Entry  Wednesday, November 24, 2021, 07:17, Frank Song, South Hot-Cell, Standard Operation, TM4, Ta #63, TM4 SIS with Target and No external Connections IMG_4469.JPG

the TM4 with new target Ta #63 installed in SHC and an electric check was made by David. 

Entry  Tuesday, November 23, 2021, 10:58, Adam Newsome, South Hot-Cell, Standard Operation, TM4, , TM4 Move 

TM4 was moved from ITE to SHC. Shield plug installed in ITE.

Entry  Tuesday, November 23, 2021, 10:46, Frank Song, ITE, Standard Operation, TM4, UCx#35, module disconnection IMG_4456_(2).JPG

 the TM4 with UCx#35 was disconnected in ITE.

Entry  Monday, November 22, 2021, 12:44, Adam Newsome, Crane, Repair, , , Crane PLC Fault: 0004h Fault_code_when_connecting_Nov_22_2021.png

An issue was observed in which the target hall crane was not functioning: the N-E-S-W and up/down motions did not work, however the rotation motion did work. These symptoms were similar to what was observed in the past under https://elog.triumf.ca/TIS/RH-ISAC/2039 and https://elog.triumf.ca/TIS/RH-ISAC/1845

The crane control console was not powered (i.e. pressing the ON/OFF buttons when the selector switch was set to remote mode, even when safety conditions were met, did not enable/disable remote functionality). The power supplies were checked and everything appeared to be powered as would be expected, except for items which depended on the main contactor (O-K1) being energized. This contactor needs the PLC to be in an operational state, fault-free. The PLC was checked and the red fault light was flashing. The battery light was not on (i.e. battery was OK).

The program was re-downloaded to the PLC. During an attempt to go online with the PLC, error code 0004h appeared (see attached image for description). This is an unfamiliar error code - typically the aforementioned symptoms arise due to a battery failure and the program being lost. In this case it is uncertain at this time what the cause of this fault is. It will be monitored in the future to determine if it occurs again, and further investigation will be performed.

After re-downloading the program and placing the PLC in RUN mode, the crane was fully restored to its operating state - the main contactor was able to be energized once again. The crane was put into remote mode and a brief functionality test on the motion axes was performed: OK.

 

 

Entry  Friday, November 19, 2021, 12:48, Adam Newsome, South Hot-Cell, Development, , , Vertical motion limit switch installation PXL_20211119_172142852.jpg

A rotary limit switch was installed, attached to the shaft adjacent to the drive motor for the vertical drive system. This limit switch is not yet wired to the control system and operational - this will be done at a future date and the e-log will be updated.

Relevant electrical drawings: IRH2083 to IRH2085

 

Edit (2022-03-02): see e-log https://elog.triumf.ca/TIS/RH-ISAC/2309

Entry  Thursday, November 18, 2021, 09:47, Travis Cave, Spent Target Vault, Standard Operation, , SiC#38 and UC#29, Spent Target Move Target_Index_2021-11-18.pdfTarget_Index_2021-11-18_mini_vault.pdf

 The spent targets SiC#38 and UC#29 have been removed from the spent target vault and placed into the mini storage. See attached PDF for details.

Entry  Wednesday, November 17, 2021, 11:42, Travis Cave, Spent Target Vault, Standard Operation, , Ta#57, Repacking of the targets. Target_Index_2021-11-17.pdfTarget_Index_2021-11-17_mini_vault.pdf

 Ta#57 was repacked and placed in the mini vault. The pail was changed from #174 to #263. See attached PDF for more details.

Entry  Monday, November 15, 2021, 12:15, Adam Newsome, South Hot-Cell, Repair, , , Squeaking noise during turntable rotation - chain misalignment and improper tension PXL_20211119_190640081.jpg

It was noted on Nov. 9 that a squeaking noise was present when the turntable was rotated CCW with a module present.

 

Upon inspection, it appears the issue could be due to drive chain misalignment and improper tension. Furthermore, it was noted that a shaft collar on one of the existing chain tensioners was broken (a replacement was ordered).

 

Repairs will be performed on Nov. 19 to resolve these issues by re-aligning the chain, and resetting the tensioners. The turntable will be tested. This e-log will be updated once the work is complete and the system is returned to a functioning state. See Work Permit I2021-11-09--3

 

Edit, Nov. 19: the aforementioned repairs were completed and the turntable has been tested and is operating correctly. No squeaking noise is present. It is suggested to increase the diameter of the two chain tensioner shafts (and thus modify related bearing and shaft collar components) in order to prevent bending of the shaft which was observed. This will be done in the near future.

Entry  Monday, November 15, 2021, 12:00, Travis Cave, Spent Target Vault, Standard Operation, , Ta#53, Repacking of the target. Target_Index_2021-11-15.pdfTarget_Index_2021-11-15_mini_vault.pdf

 Ta#53 was repacked and placed in the mini vault it was changed from pail#164 to pail#262. See attached PDF for further details.

Entry  Wednesday, November 10, 2021, 11:06, Travis Cave, Spent Target Vault, Standard Operation, , C#3, Spent Target Move Target_Index_2021-11-10.pdf

 The spent C#3 target has been moved from the south hot cell to the spent target vault it was placed in pail #270 and put in spot 2C of the vault. See attached PDF for more details.

Entry  Wednesday, November 10, 2021, 08:32, Frank Song, ITW, Standard Operation, TM2, UC#36, Module Connection IMG_4323.JPG

 TM2 with target UC#36 was connected at ITW.

Entry  Wednesday, November 10, 2021, 08:29, Frank Song, South Hot-Cell, Standard Operation, TM2, UC#36, electrical check IMG_4322.JPG

 An electrical check of TM2 with target UC#36 and no external connections was finished at SHC. 

Entry  Tuesday, November 09, 2021, 14:35, Adam Newsome, South Hot-Cell, Standard Operation, TM2, UCX#36, Module Move 

TM#2 was moved from ITW to SHC, then moved back to ITW.

Entry  Tuesday, November 09, 2021, 09:58, Frank Song, ITW, Standard Operation, TM2, C#3, module disconnection IMG_4315.jpg

 the module TM2 with target C#3 was disconnected at ITW and is being remoted moving to SHC.

Entry  Friday, October 29, 2021, 12:27, Travis Cave, Spent Target Vault, Standard Operation, , Ta#56, Repacking of the target. Target_Index_2021-10-29.pdfTarget_Index_2021-10-29_mini_vault.pdf

 Ta#56 in pail #169 was repacked and placed into #269 and was placed in the mini vault at the back. It was 3.86mSv/hr upon removal from the NHC. See attached files for details.

Entry  Tuesday, October 26, 2021, 11:01, Frank Song, ITE, Standard Operation, TM4, UCx#35, shielding blocks transfer 

 the five shielding blocks have been moved from ITW to ITE. 

Entry  Wednesday, October 13, 2021, 11:54, Travis Cave, North Hot-Cell, Standard Operation, , SiC#41, Spent Target Move Target_Index_2021-10-13.pdf

 The spent SiC#41 target has been placed in pail #260 and placed in spot 5B of that spent target vault. See attached PDF for details. 

Entry  Friday, October 08, 2021, 12:39, Frank Song, ITE, Standard Operation, TM4, UCx#35, Module Connection IMG_3742.jpgIMG_3741.jpgIMG_3743.jpgIMG_3744.jpg

 the module with target UC#35 was connected in ITE and being pumped down.

Entry  Friday, October 08, 2021, 11:19, Frank Song, North Hot-Cell, Standard Operation, TM4, UCx#35, TM4 IGLIS target electrical tests IMG_3739.jpgIMG_3740.jpg

 the tests were done when TM4 was on NHC. see attached photos please.

Entry  Wednesday, October 06, 2021, 10:42, David Wang, ITE, Repair, , , ITE IG1S cable end connector replacement 

ITE IG1S cable end connector replacement has been finished by Roy Huang.

Entry  Monday, October 04, 2021, 10:52, Travis Cave, North Hot-Cell, Standard Operation, TM4, SiC#41, Module move 

 TM#2 moved from ITE to NHC SiC#41 removed and then moved back to ITE.

Entry  Monday, October 04, 2021, 09:37, Frank Song, ITE, Standard Operation, TM4, Sic#41, module disconnection IMG_3715.jpgIMG_3716.jpgIMG_3717.jpg

 TM4 was disconnected and moved to NHC. 

Entry  Monday, October 04, 2021, 09:33, Frank Song, North Hot-Cell, Standard Operation, TM2, C#3, TM2 with target connection test IMG_3710.jpg

 the test was done when TM2 sit on NHC.

Entry  Monday, October 04, 2021, 09:27, Frank Song, ITW, Standard Operation, TM2, C#3, Module Connection IMG_3711.jpgIMG_3712.jpgIMG_3713.jpgIMG_3714.jpg

 TM2 been connected with new target C#3 in ITW. 

Entry  Monday, September 27, 2021, 14:29, Travis Cave, ITW, Standard Operation, TM2, Graphite #3, Module move 

 TM#2 with C#3 has been moved from the north hot cell to ITW. Also for the up coming site wide power outage, the ISAC Target Hall crane has been turned off and powered down, also the remote crane console has also been power down as well so that mean no ISAC TV for a few days.

Entry  Thursday, September 23, 2021, 19:04, Adam Newsome, Spent Target Vault, Development, , , Mini-Storage: Remote Capability 

Remote capability was added for the mini-storage door control. The control signals originate from the Opto 22 Module box that is used for the SMP remote control (this is located just above the storage vault).
The controls signal assignment document has been updated and can be found in C:\PDM Vault\PDM_Vault\_models\isac\isac1\wpn-3919 - safe module parking\Electrical

In order to operate remotely:
- Plug the mini-storage control box power cable into a wall outlet (adjacent main storage vault, under stairs)
- Plug the motor output cable into the mini-storage door motor
- Unplug the local pendant from the box
- Plug the cable that comes from the remote module box into the connector that the pendant was plugged into (M12, 5 pole Murr connector)
- Using the remote control program from the ISAC RH control room, click on the Mini-Storage option and then click buttons for open and close to operate the door (note: it is important to verify both opening and closing functions work before attempting any remote operation).

Remote and local functionality have been tested and verified working.

It is recommended to mount the mini-storage control box in a convenient area near the mini-storage (possibly on the wall adjacent the main storage vault).

Please contact me if you have any further questions.

Entry  Wednesday, September 22, 2021, 11:13, Travis Cave, Spent Target Vault, Standard Operation, , UC#34, Spent Target Move Target_Index_2021-09-22.pdf

 The spent UC#34 target was moved from the north hot cell to the spent target vault. See attached PDF for details.

Entry  Tuesday, September 21, 2021, 13:47, Travis Cave, North Hot-Cell, Standard Operation, TM2, UC#34, Module move 

 TM#2 with UC#34 has been moved from ITW to the north hot cell had the target removed and then moved to the south west silo.

Entry  Friday, September 17, 2021, 14:28, Travis Cave, Spent Target Vault, Standard Operation, , Ta#62, Spent Target Move Target_Index_2021-09-17.pdf

 The spent Ta#62 target along with 2A2M19 were placed in pail #256 and placed in spot 7A of the spent target vault. See attached PDF for vault details.

Entry  Friday, September 17, 2021, 12:34, Frank Song, ITE, Standard Operation, TM4, Sic#41, Module Connection IMG_3602.jpgIMG_3601.jpgIMG_3600.jpgIMG_3599.jpg

 TM4 with a new target was moved back from NHC to ITE and reconnected at pit. The 5 shielding blocks were installed as well. Copies of connection checklist are attached here.

Entry  Friday, September 17, 2021, 12:20, Frank Song, North Hot-Cell, Standard Operation, TM4, Sic#41, TM4 SIS with Target and No external Connections IMG_3603.jpg

 TM4 electric check with new target was done by David. A pic attached here for ref.

Entry  Wednesday, September 15, 2021, 08:39, Travis Cave, ITE, Standard Operation, TM4, SiC#41, Module move 

TM#4 with SiC#41 has been moved from the NHC to ITE.

Entry  Tuesday, September 14, 2021, 09:18, Travis Cave, South Hot-Cell, Repair, TM4, SiC#40, Module move 
TM#4 with SiC#40 has been moved from the east target station to the south hot cell.
Entry  Thursday, August 12, 2021, 14:13, Adam Newsome, ITW, Repair, , , West Entrance Module Move to ITW 

The West Entrance Module has been moved from the South Hot Cell to the West Target Station.

Entry  Wednesday, August 11, 2021, 11:15, Adam Newsome, Spent Target Vault, Development, , , Mini-Storage: Cable track for e-chain installed PXL_20210811_165201449.jpg

A cable track was installed between the mini-storage vault and the silos, for the purpose of implementing a retractable cable chain (e-chain). This will allow for cables to be managed during door opening/closing, so that remote control operation of the door will be possible in the future. See Work Permit I2021-08-11-2 (Aug 11)

Holes were drilled into the motor mounting plate (IRH2089) to allow for mounting a limit switch on the plate. See Work Permit I2021-08-17-7 (Aug 17)

Preliminary testing was completed in which the e-chain was fixed to the door with a C-clamp. Local and remote functionality were checked, and limit switch functionality was verified. Everything is working as expected. A final test will be conducted once the e-chain is fixed to the door and cabling routed through it. See Work Permit I2021-08-19-1 (Aug 19)

 

The e-chain has not yet been fixed to the vault door - holes will be drilled in-situ after preliminary testing is complete to confirm positioning.

 Edit [2021-09-23]: the installation is complete and has been tested.

Entry  Tuesday, August 10, 2021, 10:16, Adam Newsome, South Hot-Cell, Repair, , , West Entrance Module Move to South Hot Cell 

The West Entrance Module has been moved to the South Hot Cell for repair.

Entry  Friday, August 06, 2021, 11:52, Travis Cave, North Hot-Cell, Standard Operation, , UC#33, Spent Target Move Target_Index_2021-08-06.pdf
UC#33 has been packed and moved from the north hot cell to the spent target vault. See attached PDF for 
deatails
Entry  Wednesday, August 04, 2021, 17:24, David Wang, North Hot-Cell, Standard Operation, TM2, UCx34#, UCX 34# on TM2 electical check and HS leak check at NHC. UCX34_TM2_electrical_check.pdf

The job is done with Matt at NHC. All TGHT and TBHT bolts are torque wrench tight in NHC. HS leak check result is good.

helium pressurized HS line at TCS. No leak.

Entry  Friday, July 30, 2021, 16:31, Carla Babcock, ITE, Repair, , , ITE re-wire ISK4425D-rev9._APshortmitigationsvg_july27update.png

See the attached for the way ITE has been re-wired for the Ta62 run. Note also that the copper block in the schematic on TBHT negative may not actually be connected. Wiring verification on Aug. 4.

Entry  Friday, July 30, 2021, 16:19, Carla Babcock, ITE, Repair, TM4, Ta#62, Electrical issues on Ta62 
TLDR: TBHT voltage too high and rising too quickly with TGHT current - voltage limited. TGHT power supply tripped breakers somehow. ITE:EL not outputting voltage.

 

A short between feedthroughs A and P developed at the end of the p2n run in this module, and was fixed by Chad prying apart the lines in the source tray with a long teflon bar. We did not take the containment box off to fix it properly for reasons of time and also potential damage to the containment box. This seemed to fix it and David measured around 13MOhms between A-P when the module was installed in ITE. To make sure we could recover if the short reappeared during the run, David did not connect the P/Q feedthrough to HV common on the module top as usual, but it was connected in the electrical room. I also unhooked the busbar from the coil power supply.

When trying to start the TGHT ramp up, it was discovered that ITE:TGHT had a fault in its readback circuit, which was showing negative voltages. Not sure how this happened, since the power supply was not used for the previous p2n run, maybe an HV spark? This supply was replaced with the spare (SN 1161-9894).

When TGHT and TBHT were able to be ramped up, we found that the tube heater voltage was increasing too much with the target current. Normally the rate of increase is about 0.0004 V per amp on TGHT. This time it was 0.004 V/A. This was causing the TBHT to be voltage limited, which I thought could be related to the AP short. So I re-wired it such that the P feedthrough (#7 in the electrical room) was disconnected from everything except it was tied to feedthrough A (#1) using a 100 Ohm resistor. This should prevent it from floating and also prevent current from going through. See documentation in the Target Records folder (https://documents.triumf.ca/docushare/dsweb/Get/Document-204373/July272021_ITETM4_electricalissues.pdf).

During the subsequent ramp up, the TGHT power supply tripped the breakers when it was at 500A, 8V. The cause of this is still uncertain, and the TBHT voltage issue persisted after the wiring change. In the interest of time we decided to stay conservative on the currents used and continue to run like this. It may also be possible that the copper block which is supposed to reference TBHT negative to HV common is not attached.

Finally ITE:EL is still not working. It shows a value on the front of the PSU but doesn't draw enough current and doesn't affect the beam. We are running without it and it will hopefully be fixed on the Aug. 4 maintenance day.

These electrical issues bear some resemblance to those with Ta61, but I don't think we ever determined the cause there.

Entry  Tuesday, July 20, 2021, 09:46, Adam Newsome, ITE, Standard Operation, TM4, , Remotely moved TM4 from TCS to ITE 

TM4 was moved from the conditioning station to the East target station.

Entry  Thursday, July 15, 2021, 09:02, Adam Newsome, Spent Target Vault, Standard Operation, , , Emergency Close Mechanism Test 

The emergency close mechanism for the Storage Vault door was tested by Adam Newsome and Travis Cave. The door was opened to its fully open limit, then closed with the emergency system.

The test was successful.

Entry  Thursday, July 08, 2021, 11:45, David Wang, South Hot-Cell, Standard Operation, TM4, Ta#62, TM4 Ta#62 leak check and lectrical check result at SHC and TCS.  Ta#62_Tm4_elecrical_check_and_leak_check_result_at_SHC.pdf

At SHC: HS line no leak . electrical check result is fine. At TCS: helium pressurized HS line to 70psi, 3 minutes. LD  leak rate 0.0xE-9atm.cc/sec , no response.

Entry  Thursday, July 08, 2021, 11:36, David Wang, Conditioning Station, Standard Operation, TM4, Ta#62, Remotely remove TM4(Ta#62) from SHC to TCS. 

Remotely remove TM4 (ta# 62) from SHC to TCS.  The moving is smooth.

Entry  Wednesday, July 07, 2021, 11:59, Adam Newsome, Safe Module Parking, Maintenance, , , Annual Electrical and Mechanical Inspection Capture.PNGPXL_20210707_162143876.jpgPXL_20210707_162918257.jpg

An annual electrical and mechanical inspection was performed on the SMP today by Adam Newsome, Dan McDonald, and Jason Zhang as per Work Permit I2021-07-07-3. The following items were checked:

  • Check condition of wiring for physical/radiation/UV damage
    • OK, no signs of significant damage
  • Check for cable tray debris or damage
    • There were multiple shards of plastic in the cable tray - they were removed and disposed of
  • Check inside control panel: components and wiring, labeling
    • Labeling intact, components in good condition
    • One COM wire for the relay array was loose - it was tightened
  • Verify camera views
    • This was not inspected but has recently been checked, and is checked prior to remote operation
  • Check connectors for damage
    • All connectors OK
  • Check pendant for damage and verify labeling intact
    • Pendant OK
  • Lid open/close test
    • Lid was opened and close multiple times - smooth operation, no concern
    • Lid close logic was checked - OK
  • Vessel rotation and limit switch check
    • Both CW and CCW limits were checked, functioning
    • No concern on rotation - chain drive, rotary limit switch, and cable reel all functioning normally
  • Lubricate chains
    • Done
  • Inspect tensioners
    • Done - OK
  • Tighten fasteners
    • Done - OK
    • Note: some concern over socket head screws in slotted parts - they should have washers. Not a critical issue but worth checking into.
  • Visual inspection
    • All OK

Overall the inspection was successful.

Entry  Wednesday, June 30, 2021, 14:11, Matthew Gareau, North Hot-Cell, Standard Operation, , , North Hot Cell Commemorative Opening 

 Yesterday a bottle of Cava (sparkling wine) was place, opened, and poured in the NHC, to commemorate its new operational status.

The NHC is now a functional hot cell and is ready for many years of target exchanges to come.

Entry  Tuesday, June 22, 2021, 15:35, David Wang, ITW, Standard Operation, TM2, UCX33#, TM2 has been connected it ITW.  

TM2 has been connected it ITW.  All turbo pumps are started.

Entry  Friday, June 11, 2021, 10:36, David Wang, Conditioning Station, Standard Operation, TM2, UCX33#, TM2 leak check at TCS 

Leak checked TM2 service cap at TCS. helium pressure checked containment box window and HS cooling lines.  No leak on service cap and waterlines.

Entry  Thursday, June 10, 2021, 14:54, David Wang, North Hot-Cell, Standard Operation, TM2, UCX33, UCX 33 on TM2 electical check at NHC. UCX33_TM2_electrical_check.pdf

TM2 UCX33# electrical check and leak check results. See attachment.

Entry  Wednesday, June 09, 2021, 10:48, David Wang, South Hot-Cell, Standard Operation, TM2, , TM2 containment box leak check.  

Chad installed containment box back to TM2 yesterday. We leak checked VCR joints on window line.    No leak.

Entry  Wednesday, June 09, 2021, 10:15, David Wang, ITE/ITW, Standard Operation, TM4, UCX33. , ITE water signal interlock check.  

Annual ITE water signal interlock check is done.  HS, TAR, TUBE, MSP, EE, COIL 1, containment box window, HVC1, HVC2, 2A window, 2A  shielding plug, 2A dump, 2A collimator, and 2A tank water signal interlock are checked.   Everything is working properly.  

2021-06-22. Annual ITW water signal interlock check is done,  HS, TAR, MSP,  EE, COIL1 , containment box window, HVC1 , HVC2, 2A window, 2A shielding plug, 2A dump, 2A collimator, and 2A tank water signal interlock are checked. Everything works fine.

Entry  Wednesday, June 09, 2021, 09:16, Travis Cave, North Hot-Cell, Standard Operation, TM2, no target, Module move 

 TM#2 has been moved from the SHC to the NHC.

Entry  Thursday, June 03, 2021, 08:33, David Wang, South Hot-Cell, Standard Operation, TM4, UCX32# P2N, P2N UCX 32 on TM4 electical check and leak check at SHC. P2N_UCX33#_target_electrical_chek_at_SHC_2021_0601.pdf

Both electrical check and leak check (HS and Window lines)results are good.   See attachments

Correction: It should be UCx#32 P2N instead of UCx33# in check list attached . UCx#33 is on TM2 in ITW

Entry  Thursday, June 03, 2021, 08:20, David Wang, South Hot-Cell, Standard Operation, TM2, , Remotely remove TM2 from silo to shc 

Remotely removed Tm2 from silo to SHC. The moving is smooth.

Entry  Thursday, June 03, 2021, 08:19, David Wang, ITE, Repair, TM4, UCX33, Replaced ITE TP4  

Replaced  ITE TP4 due to failure start. The new pump works fine.

Entry  Monday, May 31, 2021, 11:28, David Wang, ITE, Standard Operation, TM4, , Remotely remove TM4 from silo to shc 

Remotely remove tm4 from silo to shc. The moving is smooth.

Entry  Tuesday, May 25, 2021, 16:20, Anders Mjos, Conditioning Station, Maintenance, , , TK2 refilled 

Tank refilled from 12 in to 25 in using the new valve.

Entry  Tuesday, May 25, 2021, 16:20, Anders Mjos, Conditioning Station, Maintenance, , , Chiller maintenance 

A contractor on site today for chiller maintenance. CP2 and CP3 circuit is leaking and shall not be used. CP1 can still be used. The contractor will contact Plant Group with a quote for repair and upgrades.

Entry  Tuesday, May 25, 2021, 15:59, Matthew Gareau, North Hot-Cell, Development, , , Removed boot from left hot manipulator 7x

 Myself and Isaac removed the boot from the left hot manipulator.

- opened the hatch in the TH to get access to the top of the boot

- released the latch on the boot and loosened the boot from above

- closed TH hatch

- with the right manipulator we were able to detach the rest of boot

This test proved that we can remove a boot from the manipulator without having to enter into the hotcell.

Due to the physical restraints that the boot causes for the operator, we have decided to not reattach the boot with its current design.

A new design will be investigated to allow the boot to be fixed without twisting, which is the source of the problems.

 

Entry  Friday, May 14, 2021, 11:29, David Wang, Spent Target Vault, Standard Operation, , , Repack of 4 spent targets. 

Repack of 4 spent targets in TH and SHC.  SiC#37 to new pail249#. SiC#36 to new pail 250#. Nb#8 to new pail 247#, SiC#33 to new pail 248#.  They are all in mini storage. Also, UCx 31 are transferred to mini storage.  There are 5 spent targets in mini storage now.  

2021-05-20: 5 spent targets have been loaded into F308's. We transferred two more spent targets into mini storage this morning for next week loading.

Entry  Monday, May 03, 2021, 15:14, Frank Song, ITE, Maintenance, , , High voltage test in ITE 

 Anders and I prepared ITE high voltage test in April 30 ( Friday morning), The MAA is locked for this.

Entry  Friday, April 30, 2021, 14:09, Luca Egoriti, ITE/ITW, Development, TM4, , TM4 resistance measurements for P2N 

 Friday, April 30, 2021, 14:06

Anders and Luca

Resistance measurements on each electrical feedthroughs (A,B,C,D,E,I,P,Q,R,U,60kV,ground) taken with no target or no short attached to the module. Results as expected:

P-Q = 6.439 mOhm

R-U = 6.019 mOhm

All other combinations = Open Loop

Entry  Monday, April 26, 2021, 13:02, David Wang, South Hot-Cell, Repair, TM4, , TM4 new steerer cable installation. 

New steerer cables are installed in TM4. Cables are properly routed in containment box and service cap top. After job, TP2 is installed back onto module top.

Entry  Thursday, April 22, 2021, 08:41, David Wang, South Hot-Cell, Repair, TM4, , TM4 steerer electical check at SHC and TH. 

Using SHC electrical test cables routed to to TH,  We tested TM4 steerer  4 polarities. At 100v megga test, left, right , up and down to ground are all OL. TM4 steerer has no short.

Entry  Wednesday, April 21, 2021, 11:18, David Wang, Cooling, Maintenance, , , Refilling high active wtaer system and starting HA water pumps.  

High active water system is refilled. Air are drained out of  system before pump to be started. Following sequence are used to bring the whole system back to operation:

1. close ITE , open ITW. Switch on the pump. Only 2A beam line related 5 water circuits are in loop in ITW.  Switch off pump when system pressure is stable above 100 psi.

2. Close ITW, open ITE. Switch on the pump. Only 2A beam line related 5 water circuits are in loop in ITE. Switch off pump when system pressure is stable above 100psi.

3. Open ITW, Open ITE. Switch on pump. both ITW and ITE beam line related water circuits are in loop.  Switch  off pump when system pressure is stable above 100psi.

4. Close ITE open ITW.  Bring ITW  target module water circuits back to loop by connecting bypass fittings on to circuits. Only bring one circuit back to system at first. Switch on pump. Wait for system pressure stabilized. Then Close ITW. bring next circuit back  to system.  Open ITW .  wait for pressure stabilized.  repeat the process until all water circuit and connected with bypass fittings in ITW.

5. Check possible leak on valves, fittings, and flow sensors in ITW pit.

6. Go to electrical room, check all ITW water signal status.

7. Close ITW, Open ITE. Repeat same procedure as step 4 on ITE target module water circuits.

8. Check possible leak on valves, fittings and flow sensors in ITE pit.

9. Go to electrical room, check all ITE water signal status.

10. Open ITW.  At this stage, full ITE station and half of ITW station water circuits are in operation.  Check possible leak on pumps, valves, fittings, gauges on water station at TH west end.

11. Keep system in operation. Watch on - tank level , system pressure, and conductivity on resin circuit and whole system.

Entry  Wednesday, April 21, 2021, 10:34, David Wang, South Hot-Cell, Standard Operation, TM4, , Remtely remove TM4 from Silo to SHC.  

On 2021- 04-20,  Tm4 is removed from Silo to SHC. The moving is smooth.

Entry  Wednesday, April 21, 2021, 10:32, David Wang, South Hot-Cell, Standard Operation, TM3, , Remotely remove TM3 from SHC to silo 

On 2021-04-19, Frank and I remotely removed Tm3 from SHC to silo . The moving is successful.

Entry  Monday, April 12, 2021, 13:47, Anders Mjos, Assembly/Bench Test, Repair, TM4, , Steerer wiring TM4_Steerers_electric_check.pdf

Travis assembled and tested the steerer wires March 31st (see attached)

Entry  Monday, April 12, 2021, 13:45, Anders Mjos, Cooling, Maintenance, , , New T installed for instrumentation loop on HALCW system MicrosoftTeams-image_(9).png

Adrian and co installed a new T to be able to add an instrument loop for O2 and pH monitoring on the low conductivity water systtem (photo). See WP I2021-04-09-4

Entry  Friday, March 26, 2021, 12:22, Adam Newsome, Crane, Development, , , Aux Hoist Pendant Upgrade 

The crane pendant for the auxiliary hoist was upgraded to a FLEX EX2 style pendant by Canco Cranes. The installation work was performed by Canco, supervised by Tom Kauss and David Wang. Installation work was performed in one day (I2021-03-26-1).

Items installed include: new pendant (2 motion, 2 speed)

The existing antenna and receiver box located in the Target Hall were used.

The new system was tested by David Wang. Everything is reported to be in working condition.

Entry  Thursday, March 25, 2021, 10:38, David Wang, Spent Target Vault, Standard Operation, , C#1, Remove pail 237 spent target C#1 from storage vault to mini storage.  

Pail 237 only has 200u sv/hr field at 0.5 meter. On contact measurement: 0.9 to 1.6 m sv/hr.and less than 80 count contamination outside the pail.   It is moved to mini storage. We will transfer this pail to cyclotron vault and store it there later.

Entry  Thursday, March 25, 2021, 08:55, Anders Mjos, Conditioning Station, Maintenance, , , Filters inspected and cleaned on water circuit 

By Curtis. See Work Permit I2021-03-24-1 for details.

Entry  Tuesday, March 23, 2021, 09:47, David Wang, South Hot-Cell, Standard Operation, TM3, , TM3 has been moved from TCS to SHC. 

Frank and I removed Tm3 from TCS to SHC. The move is successful.

Entry  Wednesday, March 17, 2021, 11:43, Frank Song, ITE, Repair, , , Re-connect Entrance Module in ITE  job_done_by_following_#190510.pdf

 David and I re-connect Entrance module at ITE after the monitor been replaced at SHC. 

Entry  Wednesday, March 17, 2021, 09:10, Travis Cave, ITE, Standard Operation, , , Entrance module move 

 The east entrance module is now back at the east target station.

Entry  Monday, March 15, 2021, 13:01, Isaac Earle, Crane, Development, , , Plate & pin lift assembly load testing (ITA6550) 11x

In mid-2020 design analysis was completed on the steel plate & pin assemblies (ITA6550) used to connect the ISAC target hall crane hook block to the module lifting yoke assembly ITA0494.  The released design note is Document-184431.  

In November 2020 fabrication was completed on two full plate & pin assemblies (photos attached below).  As per the relevant ASME standards (identified in the design note), each assembly has been identified with serial numbers (#1 and #2).  Material test reports for the steel plate and round bar material used for fabrication are attached in PDF format.  For both materials the tested tensile yield strength (from the MTR) exceeds the value used in design calculations (from Document-184431):  117ksi vs 100ksi for the plate material;  138si vs 103ksi for the round bar material.

On February 8, 2021 both plate and pin assemblies were load tested by David Wang and Frank Song.  The total load applied to each was 31,400 lbs (as per the ISAC target hall crane load cell) which exceeds the 125% of rated capacity (31,250 lbs) required for the test.  The lifts were conducted successfully and no deformations or other damage to the assemblies were observed.  Photos of the load test are also attached.

Both plate & pin assemblies are now certified for use up to their rated capacity.  As specified on drawing ITA6550 and in Document-184431, a monthly visual inspection must be performed to check for structural deformation, cracks, excessive wear, and loose or missing fasteners.  In addition, an annual inspection must be performed to check for structural deformation, cracks, excessive wear, loose or missing fasteners, and missing or illegible markings or safety labels.  A written record of the annual inspection must be documented and kept readily available.

 

Entry  Friday, March 12, 2021, 11:36, Travis Cave, South Hot-Cell, Maintenance, , East Entrance Module, Entrance module move 

 The East Entrance Module has been moved from the East Target Station to the South Hot Cell.

Entry  Thursday, March 11, 2021, 11:42, Frank Song, ITE, Maintenance, , , ITE water flow wheels and coils replacement. 

 ITE water flow wheels and coils are replaced. Wheels and coils on Oven, Tube, HS, EE, MSP, Febiad coil, containment box window, dump, dump plug, 2A window, and tank return circuits are replaced with new parts.

Entry  Friday, March 05, 2021, 09:12, Matthew Gareau, North Hot-Cell, Development, TM3, , Containment box door removal and swivel arm test Containment_door_arm_testing_on_TM3.jpg

First thing I entered into the NHC to install to the target kart mounting clip, and remove excess tools and materials from the hotcell

After the TM3 without a target was lowered into the NHC.

Once inside, with the use of the manipulators, I was able to remove the containment box door, place it on the swivel arm, move the arm out of the way, after the door was return to the containment box and reattached.

Containment_door_arm_testing_on_TM3.jpg

Entry  Thursday, March 04, 2021, 16:30, Isaac Earle, North Hot-Cell, Development, , , NHC gas delivery lines leak checked 

 The North Hot Cell gas delivery lines (labeled 1, 2, and 3 on the hot and cold side panels) were leak checked today.  5psi helium gas was applied to each line in turn with the appropriate solenoid valve opened and a Staubli connector with plastic tubing and the leak check wand attached to the matching connector inside the cell.  The end of the wand was sealed using tape.  The Agilent G8601 leak detector was used on "sniffing" mode to check for escape of helium gas from all joints and connectors.  With the sniffing line attached the leak detector test port pressure was 3.9E-1 Torr and the baseline leak rate was 1.7E-6 Torr*L/s.  There was no response while testing all of the three lines.  For all three there was a leak detector response after disconnecting the Staubli fitting, which confirmed that the lines were properly charged with helium.

Entry  Thursday, March 04, 2021, 13:54, David Wang, Conditioning Station, Standard Operation, TM3, , TM3 has been moved to NHC from silo 

TM3 has been moved from silo to NHC. The move is successful. NHC ram stand and NHC protection railings are checked and installed. Everything works fine.

2021-03-05. TM3 has been moved from NHC to silo. The move is successful.

Entry  Thursday, March 04, 2021, 11:20, David Wang, ITW, Maintenance, , , ITW water flow wheels and coils replacement. 

ITW water flow wheels and coils are replaced. Wheels and coils on Oven, Tube, HS, EE, MSP, Febiad coil, containment box window, dump,dump plug, 2A window, and tank return circuits are replaced with new parts.

Entry  Tuesday, March 02, 2021, 08:12, David Wang, Conditioning Station, Standard Operation, , , TCS leak check.  

TCS leak check: TCS IG1S1.6 XE- 6 torr. LD  0.0XE-9atm.cc/sec.We used a long pole to spray helium to TCS vacuum seals on diagnostic box and vessel body. Lots helium have been sprayed around the check area.  no leak has been found.

Entry  Thursday, February 25, 2021, 10:09, Frank Song, ITE, Repair, , , Disconnect Entrance Module in ITE 

 David and I disconnected entrance module in ITE by following the procedure # 190510. And, the yoke was installed and left on for remote handling later. 

Entry  Tuesday, February 23, 2021, 09:00, David Wang, Assembly/Bench Test, Maintenance, , , target staion vacuum pumps inspection. 

Edi and I inspected roughing pump ITM MP1, primary backup pump ITHMP1, and secondary backup pump ITHMP2. We checked oil level and color on all pumps.  Refilled lubricant to ITMMP1. ITHMP1 and MP2 oil level is fine. ITH MP1 oil color is darker than MP2. But, both them are ok still. Shielding block has been restored after the job.

Entry  Thursday, February 18, 2021, 12:59, David Wang, Assembly/Bench Test, Maintenance, , , TM3 source tray and old resin can storage in lower cyclotron basement 

TM3 old source tray, old target hall high active water resin tank, and  old 2A window RH clamp are transferred from TH to cyclotron lower vault basement 10 and 10A location for storage. They are placed beside and in front of old TM1 and TM2 source tray boxes which stored there in 2018. 

Entry  Thursday, February 18, 2021, 12:33, David Wang, ITE, Repair, , , ITE:TP1S 

ITE TP1S new pump is installed today. Reset pump life time on controller to 0 hr.

Entry  Tuesday, February 16, 2021, 14:00, Adam Newsome, Crane, Development, , , Crane pendant upgrade PXL_20210216_183711834.jpg

The crane pendant for the main hoist was upgraded to a FLEX EX2 style pendant by Canco Cranes. The installation work was performed by Matt at Canco, supervised by Tom Kauss, David Wang, and Adam Newsome. Installation work was performed in two phases since the initial installation did not provide adequate range and an antenna issue needed to be resolved (I2021-01-14-1, and I2021-02-16-1).

Items installed include:

  • New pendant
  • New antennae
  • New receiver box, mounted on main crane control panel in the crane control room

The old receiver control box will be kept for some time in case there is a need to revert to the previous system for some reason.

The new system was tested by David Wang - including using the pendant at the far end of the target hall where range was previously an issue. Everything is reported to be in working condition. Remote mode is functioning as expected.

 

 

Entry  Friday, February 12, 2021, 07:07, David Wang, ITE, Maintenance, , , ITW and ITE clean up. 

Vacuum cleaned ITW and ITE station. 

Entry  Wednesday, February 10, 2021, 13:30, David Wang, Safe Module Parking, Standard Operation, , , TM2 and TM4 electrical check without targets. TM2_and_TM4_electrical_check_without_target.pdf

 TM2 at SMP under vacuum. TM4 at silo.  Frank and I did the tests. Everything is fine on TM4 check.  On TM2,  all mega test at 500V are around 200K ohms which is so abnormal. We will move TM2 to TCS and  start investigation there.

Entry  Wednesday, February 10, 2021, 11:34, David Wang, Assembly/Bench Test, Standard Operation, , , Old resin can and 2A window RH clamp field measurement at silo.  

Old resin can:  0.5 meter 360 degree rotation above silo area, 350u sv/hr.   On contact  3.0 to 3.5 msv/hr.  It was replaced during 2017 winter shut down, and stored in silo since then.

2a window RH clamp: 0.5 meter, 160 usv/hr.  On contact, hottest spot 3.5msv/hr, general,1.8 msv/hr. 

 Both of them were raise out of storage silo with TH crane. Pole monitor was used for field check.

Entry  Wednesday, February 03, 2021, 09:14, David Wang, Conditioning Station, Standard Operation, TM4, , TM4 from TCS to SW silo. 

TM4 is moved from TCS to SW silo. The moving is smooth.

 

 

 

 

 

 

 

 

 

 

 

Entry  Wednesday, January 27, 2021, 14:30, David Wang, Cooling, Development, , , High active water system purging 

High active water are purged to holding tank at B2  level. There should be around 48 gallons are purged out of system. No purging on dump circuits on both ITW/ ITE.

Entry  Monday, January 25, 2021, 12:33, David Wang, ITW, Standard Operation, , , ITW bias HV test 

Ramp up ITW bias to 57KV. no spark. 200uA leaking current at 57KV. The test is done without target module in station.   ITW water circuits are looped in pit.  EE , EL are switched off during the test. 

Entry  Monday, January 25, 2021, 10:57, David Wang, South Hot-Cell, Repair, TM4, , TM4 steers short investigation. 

Cables were disconnected for steers in containment box. The Megga measurement (500V) result from the top of the module:

Left to right: OL, left to top OL,  left to bottom OL, right to top OL, right to bottom OL,  Top to bottom OL. And all of them to ground are OL.  No short on cables from module top to steers itself. The short should be inside the steers. It will be confirmed with directly test on steers.  

Entry  Friday, January 22, 2021, 12:34, David Wang, ITE, Standard Operation, , , ITE HV test. 

ITE annual HV test is done. No module in station. The bias power supply has been ramped up to 49KV on control page. We still have voltage limit issue on this PS at 48KV so it only can go to 47.7 KV on PS panel. No major spark during test.. The test result is same as last year test which was did in March 2020. 

Entry  Tuesday, January 19, 2021, 11:32, Travis Cave, Safe Module Parking, Standard Operation, TM2, Nb#9, Module move 

 TM#2 with Nb#9 was moved from ITW to SHC and then with no target it was moved from the SHC to the SMP.

Entry  Monday, January 18, 2021, 12:29, David Wang, ITW, Standard Operation, TM2, Nb#9, ITW vacuum and TM2 water lines leak check . 

ITW primary and secondary vacuum vessel leak check are done. There is a 5XE-8 atm.cc/sec leak on Exit service cap NW side square panel.  The leak is small. And, it is close to ITW TP3 so it is not affect ion beam line vacuum during operation. We will replace the seal on the panel later.   The rest leak check on air to vacuum seals are good. TM2 water lines are pressurized with 70 psi helium. We did it  3 hours after water lines are purged. No leak was showed during the check.

2021-02-24th: The o-ring on exit 1 NW side square panel is replaced by David Wang and Frank Song. 

Entry  Friday, January 08, 2021, 09:40, Travis Cave, South Hot-Cell, Standard Operation, TM4, Ta#61, Module move 

 TM#4 with Ta#61 has been moved from the east target station to the south hot cell.

Entry  Wednesday, January 06, 2021, 10:39, David Wang, ITE, Standard Operation, TM4, , ITE and TM4 annual leak check. 

Frank and I finished ITE and TM4 primary and secondary  vacuum vessel  leak check. LD bease leak rate 0.0x-9atm.cc/sec. No leak has been found.Also, All TM4 water lines  have been pressurized with 70psi helium fro 3 minutes on each circuit. All water lines in TM4 are good. No resopne on LD during test. 

Entry  Monday, January 04, 2021, 12:13, Adam Newsome, Conditioning Station, Development, TM3, , TM3 Move 

TM3 was remotely moved from the South Hot Cell to the conditioning station. No containment box.

Entry  Thursday, December 24, 2020, 09:00, Matthew Gareau, North Hot-Cell, Development, , , NHC USB connection 

24/Noc/2020

USB was discovered to be in the reverse direction and will need to be change around to become operational

 

01/Dec/2020

USB was pulled from conduit

While attempting to re-pull the USB in the correction direction, the ethernet cable was damaged and need to be replaced,

(thanks to the Hubert's team for the wire help) 

It was decided that it was too problematic to re-pull the wires with all other wires in the way. Therefore all the wires were removed from the operator control panel, and pulled so that the USB, USB power cord, and ethernet could be re-pulled all together.

However, even once all the wires were re-pulled and reconnected it was discovered that the USB had become damaged, and was removed again.

 

23/Dec/2020

- A new conduit was added through to the NHC, for only the USB

- USB was fed through, reconnected, and tested

- Putty will need to be added around the conduit to ensure a good seal into NHC

Entry  Monday, December 21, 2020, 11:22, Adam Newsome, Crane, Standard Operation, , , Crane Shutdown for Power Outage 

The Target Hall Crane has been shut down in preparation for the power outage tomorrow (Dec 22). Power will be restored on Dec 23.

 

Dec 23 update: power has been restored. The crane appears to be in working condition as there is no fault indicator on the PLC.

Entry  Thursday, December 10, 2020, 15:07, Adam Newsome, South Hot-Cell, Development, TM3, , TM3 Move 

TM3 was remotely moved from the conditioning station to the South Hot Cell. No containment box.

Entry  Monday, December 07, 2020, 12:20, Adam Newsome, Conditioning Station, Development, TM3, , TM3 Move 

TM3 has been moved from the South Hot Cell to the Conditioning Station. No containment box.

Entry  Wednesday, November 25, 2020, 09:05, Adam Newsome, South Hot-Cell, Standard Operation, TM3, , Module Move 

TM3 has been moved from the Silo to the South Hot Cell.

Entry  Tuesday, November 24, 2020, 12:56, David Wang, ITW, Standard Operation, TM2, Nb#9, TM2 has been connected in ITW TM2_Nb#9_module_connection_checklist.pdf

TM2 has been connected to ITW. Turbo pumps are stared. ITW pumping down is fine so far.

Entry  Tuesday, November 24, 2020, 09:37, Adam Newsome, ITW, Standard Operation, TM2, , Module Move 

TM2 has been moved from the Conditioning Station to ITW. 

Entry  Thursday, November 19, 2020, 12:00, Adam Newsome, Spent Target Vault, Standard Operation, , C#2, Spent Target Move 

C#2 has been moved from the south hot cell to the spent target vault. It is in spot 8A of the vault in pail # 235 and was 185 mSv/hr upon removal from the south hot cell.

The Target Index spreadsheet has been updated on DocuShare.

Entry  Thursday, November 19, 2020, 09:00, David Wang, Conditioning Station, Standard Operation, TM2, Nb#6, Helium pressure check on TM2 HS line at TCS. 

LD 0.0 Xe-9 atm.cc/sec , 70 psi helium 3 minutes.  No leak.

Entry  Wednesday, November 18, 2020, 15:28, David Wang, South Hot-Cell, Standard Operation, TM2, Nb#6, electrical check and HS leak check. Screenshot_2020-11-18_Mail_-_David_Wang_-_Outlook.png

Everything looks good. A still short to P before target installation. We will float P,Q as before on module top.

Entry  Tuesday, November 17, 2020, 10:17, Adam Newsome, South Hot-Cell, Standard Operation, TM2, , Module Move 

TM2 has been moved from ITW to the South Hot Cell.


Reading at ITW: 114 mSv/hr

Reading at SHC: 85 mSv/hr

Entry  Thursday, November 12, 2020, 10:02, Travis Cave, Spent Target Vault, Standard Operation, , UC#31, Spent Target Move 

 UC#31 has been moved from the south hot cell to the spent target vault. It is in spot 8B of the vault in pail # 224 and was 3.71mSv/hr upon removal from the south hot cell.

Entry  Thursday, November 05, 2020, 10:48, Travis Cave, ITE, Standard Operation, TM4, Ta#61, Module move 

 TM#4 with Ta#61 has been moved from the south hot cell to the east target station.

Entry  Thursday, November 05, 2020, 10:23, David Wang, Spent Target Vault, Standard Operation, , , TM2 old source tray and TM4 optic tray in vault tray#9. 

TM2 old source tray and TM4 optic tray are stored together in vault tray#9. The fielding measurement at SHC post 0.5 meter distance:
 

March 1st 2019, maximum 14.6msv/hr, minimum 4.78 msv/hr

Nov 2nd 2020, max 7.11m sv/hr, min 2.5msv/hr.

Entry  Tuesday, November 03, 2020, 10:52, Travis Cave, South Hot-Cell, Standard Operation, TM4, UC#31, Module move 

 TM#4 with UC#31 has been moved from the east target station to the south hot cell.

Entry  Friday, October 30, 2020, 09:02, Travis Cave, Spent Target Vault, Standard Operation, , Ta#48,51,54 SiC#35, and UC#25, Repacking of the targets. Target_Index_2020-10-30.pdf

 Targets Ta#48,51,54 SiC#35, and UC#25 were repacked and placed in the mini vault. In the following order back to front. SiC#35 (240), Ta#54(241), UC#25(244), Ta#48(243), Ta#51(242).

Also during this repacking Ta#60 was also placed in the Spent Target Vault in spot 7B in pail# 239.

Entry  Tuesday, October 27, 2020, 11:46, Matthew Gareau, North Hot-Cell, Repair, , , Ratcheting repair issues with both left and right master  

 

The were issues with both left and right master ratcheting;

- the left handle was getting stuck in a close position when there was a higher ratcheting tension added

- the right ratcheting was not tightening preventing proper use of the manipulator


Chad and myself were able to identify a missing set screw for the tong cable.

Once this was added the issue with the left master ratcheting seems to be solved.


Lubricant was added to the left master ratchet and this seems to solve this problem as well.


There was also an observation of missing set screws on the spare manipulator for attaching the wrist to the ratcheting handle, which will need to be ordered and attached.

 

 

  


 

 

Entry  Tuesday, October 20, 2020, 10:14, Travis Cave, ITW, Standard Operation, TM2, C#2, Module move 

 TM#2 with C#2 has been moved from the south hot cell to the West Target Station.

Entry  Monday, October 19, 2020, 12:52, David Wang, South Hot-Cell, Standard Operation, TM2, C#2, TM2 electrical and leak check at SHC Tm3_bunker_set_up_018.JPG

TM2 electrical check and leak check are done at SHC with C#2 target installed. The results are good.  

Entry  Friday, October 16, 2020, 10:36, Travis Cave, ITW, Standard Operation, TM2, Ta#60, Module move 

 TM#2 with Ta#60 is now in the south hot cell.

Entry  Thursday, October 15, 2020, 12:48, Travis Cave, ITE, Standard Operation, TM4, UC#31, Module move 

 TM#4 is now back in the east target station.

Entry  Tuesday, October 13, 2020, 10:16, Travis Cave, ITE, Repair, TM4, UC#31, Module move 

 TM#4 is now in the south hot cell from the east target station.

Entry  Wednesday, September 30, 2020, 09:54, Travis Cave, South Hot-Cell, Standard Operation, TM3, no target, Module move 

 TM#3 is now in the south hot cell.

Entry  Tuesday, September 29, 2020, 14:28, David Wang, South Hot-Cell, Standard Operation, TM4, UC#31, TM4 UC#31 Electrical check and HS leak check TM4_UCx31_elctrical_and_leak_check_at_SHC..pdfScanned_from_a_Xerox_Multifunction_Printer.pdf

Tm4 UCx 31# electrical check result. See attachment.

Entry  Tuesday, September 29, 2020, 12:29, Travis Cave, ITE, Standard Operation, TM4, UC#31, Module move 

 Module move of TM#4 with UC#31 was finished to today at around 10:30AM.

Entry  Tuesday, September 29, 2020, 12:12, David Wang, ITE, Repair, TM4, , TM4 steerers staus after" left " grounding issue, and first stage investigation 

Left (short) is switched with bottom. So on module:

"Top" is still top.

"Left" is bottom in module actually

"Bottom and Right" is Left and right in module actually.

 For the connection in ITE:

Left  cable is connected to "left" ( bottom  in module actually)

Top cable is connected to " Bottom and Right"( left and right in module actually)

Bottom and Right cable is connected to "Top" which is top in module.

Frank and I removed the panel, disconnected the "Left"cable  inside panel,  and checked  cable to ground resistance. "Left "is dead short to ground on ohmmeter check still. So the short could be on cable or inside source tray.  Further investigation is planned to confirm the short  location.

Entry  Thursday, September 24, 2020, 11:25, David Wang, Conditioning Station, Standard Operation, TM4, UC#31, TM4 HS line leak check at SHC and TCS. 

Both helium spray and helium pressurize on TM4 HS line withUCx31 target are done at SHC and TCS. No leak.

Entry  Thursday, September 24, 2020, 10:34, Travis Cave, Spent Target Vault, Standard Operation, , UC#30, Spent Target Move Target_Index_2020-09-24.pdf

 UC#30 has been placed into the spent target vault, it was placed in pail 238 and in spot 1A of the vault. It was 81.5 mSv/hr when removed from the south hot cell. 

Entry  Wednesday, September 23, 2020, 10:56, chad fisher, South Hot-Cell, Standard Operation, TM4, UC#31 P2N, Uc#30 removed UC#31 P2N installed 

UCx#30 has been removed from TM#4 and put in a can with argon. 5(10) pin connector had to have guide screws removed to be uninstalled.

UCx#31 P2N installed.

Entry  Tuesday, September 22, 2020, 10:56, Travis Cave, South Hot-Cell, Standard Operation, TM4, UC#30, Module move 

 TM#4 with UC#30 has been moved from ITE to the south hot cell.

Entry  Friday, September 11, 2020, 11:25, Travis Cave, ITW, Standard Operation, TM2, Ta#60, Module move 

 Both the west entrance module and TM#2 with Ta#60 have been moved back into ITW.

Entry  Tuesday, September 08, 2020, 10:37, Travis Cave, ITW, Standard Operation, , no target, Entrance module move 

 The West Entrance module has been moved to the south hot cell for repairs.

Entry  Thursday, August 27, 2020, 13:18, Anders Mjos, Conditioning Station, Maintenance, TM2, , New Power Supply installed for TGHT 

Arthur installed a new Magna Power PS for the TGHT yesterday. The old power supply has been moved to Evaporator 2. The power supply was configured for remote operation and tested successfully with low current (30 A).

Entry  Thursday, August 27, 2020, 11:14, Travis Cave, Spent Target Vault, Standard Operation, , Graphite #1, Spent Target Move Target_Index_2020-08-27.pdf

 Graphite #1 along with the broke 2A2M19 wire scanner have been placed in the spent target vault see attached PDF for deatails.

Entry  Thursday, August 27, 2020, 09:42, Anders Mjos, Conditioning Station, Maintenance, TM2, Ta#60, Refilled TK2 

Refilled TCS:TK2 from 10 in to 22 in using the newly installed valve.

Entry  Thursday, August 27, 2020, 08:21, David Wang, Conditioning Station, Standard Operation, TM2, Ta#60, Helium pressure check on TM2 HS line at TCS. 

Helium pressurize on TM2 HS line at TCS is done.    Base LR is 0.0X E-9 atm.cc/sec.  70 psi helium 3 minutes.   No response.   Also, The TCS vacuum pumping down over night is good. 

Entry  Wednesday, August 26, 2020, 09:52, David Wang, South Hot-Cell, Standard Operation, TM2, Ta#60, Ta#60 target electrical check and leak check at SHC. Ta_60_electrical_checklist.pdf

Electrical check and leak check at SHC. NO leak. electrical check ok.   Before target on, A is short to PQ, RU is short to HS ( 60KV bias) as we measured before.

Entry  Tuesday, August 25, 2020, 09:38, Travis Cave, South Hot-Cell, Standard Operation, TM2, Graphite #1, Module move 

 TM#2 with Graphite #1 has been moved from the conditioning station to the south hot cell.

Entry  Monday, August 24, 2020, 10:11, Adam Newsome, ITW, Standard Operation, , , Entrance Module to ITW 

Entrance Module was moved from South Hot Cell to ITW Station.

Note: weight of entrance module, as shown via overhead crane's load cell, is 14,900 lbs.

Entry  Wednesday, August 19, 2020, 10:17, Adam Newsome, South Hot-Cell, Standard Operation, , , ITW Entrance Module moved to SHC 

ITW Entrance Module was moved from west station to South Hot Cell.

Entry  Tuesday, August 18, 2020, 09:57, Adam Newsome, Conditioning Station, Standard Operation, TM2, , TM2 Moved to Conditioning Station 

TM2 was moved from ITW to the Conditioning Station.

Entry  Tuesday, August 18, 2020, 09:06, David Wang, ITW, Standard Operation, TM2, , TM2 and ITW entrance module have been disconnected in ITW 

Tm2 and itw entrance module have been disconnected in ITW. I will attach disconnection checklist later.

Entry  Thursday, August 06, 2020, 14:33, Adam Newsome, Spent Target Vault, Development, , , Safety Group Relay Interface Installation IMG_20200806_091438.jpg

A relay contact-based interface module was installed in between Safety Group's storage vault door enable junction box and Remote Handling's control module for the vault door.

The purpose of this module, which contains a diode bridge and relay, is to isolate the safety system from the control module to prevent back-voltage on the safety system which can damage the PLC's power supply.

In the new configuration, rather than receiving a 24 VDC signal from the safety PLC, this signal activates the relay, whose normally closed contacts supply 24 VDC (from internal) to the safety relay inside the control module. Wiring was modified inside the control module to account for this change.

In investing how to achieve the same functionality as before this change, it was determined that the control module's electrical schematic was not correct and did not reflect the actual wiring. A new schematic was created for this based on the actual wiring, including new changes.

The system was tested by locking out the target hall, and verifying that:
- No failure occurred on the power supply for the safety PLC
- This new relay actuated when the target hall was locked out (i.e. received signal from PLC)
- This new relay correctly supplied 24 VDC to the safety relay within the control module, allowing for the Opto-22 control unit to output control signals to the motors

 

Note: currently the soft limit switches for the vault door close/open have been bypassed. This is not a safety issue; the door can still be fully opened and closed remotely (but the open override and close override buttons are rendered useless). The bypass will be rectified in the coming weeks and this e-log will be updated accordingly.

Edit (Aug. 13, 2020): the issue regarding the limit switches has been resolved. The entire system is functioning as it was prior to the safety interface installation.

Entry  Thursday, July 30, 2020, 09:57, Travis Cave, ITW, Standard Operation, TM2, Graphite #1, Module move 

 TM#2 with Graphite #1 has been moved back to the west target station from the conditioning station.

Entry  Wednesday, July 29, 2020, 09:20, Travis Cave, ITW, Maintenance, , , Entrance module move 

 The West Entrance module has been moved from the south hot cell back to the West Target Station.

Entry  Tuesday, July 28, 2020, 09:26, chad fisher, South Hot-Cell, Repair, , , Entrance Module Wire Scanner 

Entrance module wire scanner has been replaced. Pictures to follow.

Entry  Monday, July 27, 2020, 10:00, Travis Cave, South Hot-Cell, Maintenance, , , Entrance module move 

 The West Entrance module has been moved from the west target station to the south hot cell for repairs.

Entry  Friday, July 24, 2020, 09:43, Travis Cave, Conditioning Station, Maintenance, TM2, Graphite #1, Module move 

 TM#2 has been moved from the west station to the conditioning station. ITW entrance module moved will take place on Monday morning. 

Entry  Tuesday, July 21, 2020, 14:22, Adam Newsome, Spent Target Vault, Standard Operation, , , Emergency Close Mechanism Test 

The emergency close mechanism for the Storage Vault door was tested by Adam Newsome and Travis Cave. The door was opened to its fully open limit, then closed with the emergency system.

The test was successful.

Entry  Thursday, July 16, 2020, 10:20, Adam Newsome, Safe Module Parking, Maintenance, , , SMP: Annual Electrical Inspection 

An electrical systems check was performed on the SMP by Adam Newsome and Travis Cave. Overall, there were no issues to note. The following is a summary of the inspection (Work Permit I2020-07-16-1):

- Checked condition of wiring for physical/radiation/UV damage
- Checked for cable tray debris or damage
- Checked inside control panel: components and wiring, labeling
- Verified camera views
- Checked connectors for damage
- Checked pendant for damage and verified labeling intact
- Checked limit switch wiring and condition

Entry  Monday, July 13, 2020, 10:01, Travis Cave, Conditioning Station, Standard Operation, TM3, no target, Module move 

 TM#3 has been moved from the conditioning station to the silo.

 

Entry  Tuesday, July 07, 2020, 17:43, Carla Babcock, ITE, Development, TM4, , RF tests on new IG-LIS wiring 

Tested RF from RF driver into new IGLIS wires at ITE. Used 5V, 1MHz (2MHz setting because of internal halving issue).

As expected there was a very slight mismatch visible (original cable ~ 68 Ohms, new cable ~ 53 Ohms).

The matching resistor will be changed and it will be retested.

Entry  Tuesday, July 07, 2020, 09:16, Travis Cave, Conditioning Station, Standard Operation, TM3, no target, Module move 

 TM#3 has been moved from the silo to the conditioning station, where David and Frank will start on the gutting of the module.

Entry  Monday, July 06, 2020, 12:20, David Wang, ITW, Standard Operation, TM2, C#1, Five shielding blocks to ITW 

Five shielding blocks are transferred to ITW

Entry  Monday, July 06, 2020, 07:54, David Wang, ITE, Standard Operation, TM4, UCx 30, TM4 has been connected in ITE connection  Tm4_UCx_30_connection_checklist.pdf

TM4 has been connected in ITE. Vacuum pumping down is good so far.

Entry  Friday, July 03, 2020, 14:08, Travis Cave, ITE, Standard Operation, TM4, UC#30, Module move 

 TM#4 with UC#30 has been moved from the south hot cell to the east target station.

Entry  Friday, July 03, 2020, 13:23, David Wang, South Hot-Cell, Standard Operation, TM4, UCx#30, TM4 UCx#30 Electrical check and HS leak check TM4_UCx30_elctrical_and_leak_check_at_SHC..pdf

Electrical and leak check are good. See attachment.

Entry  Friday, July 03, 2020, 08:46, chad fisher, South Hot-Cell, Standard Operation, TM4, UcX#30, UCx#30 installed onto tm4 

UCx#30 has been installed onto TM4 with new high current fasteners torqued to 130 in lbs.

Entry  Friday, July 03, 2020, 07:03, David Wang, South Hot-Cell, Standard Operation, TM4, BEFORE TARGET INSTALLATION, ELECTRICAL CHECK BEFORE TARGET INSTALLATION. TM4_ELECTRICAL_CHECK_20220_07_02.pdf

PQ SHORT TO RU. A TO PQ 1.8 M OHM AT 500 V. THE REST ARE OL

Entry  Friday, July 03, 2020, 06:57, David Wang, ITW, Standard Operation, TM2, C#1, TM2 CONNECTION CHECKLIST  TM2_C#1_CONNECTION_CHECKLIST.pdf

SEE ATTACHMENTS. EVERYTHING IS GOOD.

Entry  Tuesday, June 30, 2020, 10:18, Travis Cave, South Hot-Cell, Standard Operation, TM4, Test Proton to Neutron Target, Module move 

 TM#4 has been moved from the east target station to the south hot cell.

Entry  Monday, June 29, 2020, 10:09, David Wang, ITE, Standard Operation, TM4, P2N test., ITE turbo pumps are stopped 

ITE venting is in processing.

Entry  Friday, June 26, 2020, 15:00, David Wang, ITW, Maintenance, , , ITW TP1 and TP1S. 

ITW TP1 can not be started yesterday. Also, TP1S was difficult to start , and had a high current draw after.  We changed both of them in pit today. TP1 and TP1S are started successfully after replacement.

Entry  Friday, June 26, 2020, 10:43, Adam Newsome, Spent Target Vault, Standard Operation, , , Routine mechanical inspection: storage vault and mini-storage drive systems IMG_20200626_092538.jpgIMG_20200626_093208.jpgIMG_20200626_093924.jpgIMG_20200626_093951.jpg

An inspection was performed on drive systems for both storage vaults (main and mini) by Adam Newsome and Dan McDonald. The functionality was not tested. Overall, nothing concerning was discovered.

Main Storage Vault:

  • Chain inspected (OK) and lubricated
  • Gearbox inspected - OK
  • All drive system set screws checked and tightened (note: chain drive screw slightly loose)
  • Sprocket alignment checked - OK
  • Limit switches checked - OK
  • Emergency close mechanism cable checked - OK

Mini-Storage:

  • Chain inspected - OK
  • Set screw checked - OK
  • Gearbox inspected - OK (need inventory/spare in stock)
  • Roller wheels checked - OK

 

Entry  Thursday, June 25, 2020, 09:45, Travis Cave, ITW, Standard Operation, TM2, Graphite #1, Module move 

 TM#2 with the graphite #1 target has been moved from the south hot cell to the west target station.

Entry  Tuesday, June 23, 2020, 10:56, David Wang, Safe Module Parking, Standard Operation, , , SMP annual service.  

Dan and I did the SMP annual  maintenance service today. Lid open/close , vessel rotation and limit switch check, lubricate chains, tighten fasteners, and visual inspection.  Everything works fine.

Entry  Friday, June 19, 2020, 11:21, David Wang, ITE, Repair, TM4, P2N test., ITE TP3 is replaced. 

ITE TP3 is replaced. ITE is under vacuum again. All turbo pumps are started successfully. Current draw on pumps are normal so far.

Entry  Thursday, June 18, 2020, 13:25, David Wang, ITE, Standard Operation, TM4, P2N test., Disconnect TM4 in ITE. 

TM4 has been disconnected in ITE. Vacuum pumps and gauge are not disconnected yet.

Entry  Thursday, June 18, 2020, 13:22, David Wang, ITW, Standard Operation, TM2, C#1, Remove of TM2 from ITE to SHC. 

Remotely remove TM2 from ITW to SHC. The move is good.  Shielding plug is put back to ITW.

Entry  Thursday, June 18, 2020, 09:11, Travis Cave, ITW, Standard Operation, TM2, Graphite #1, Module move 

 TM#2 with the graphite #1 target has been moved from the south hot cell to the west target station.

Entry  Wednesday, June 17, 2020, 09:53, David Wang, South Hot-Cell, Standard Operation, TM2, C#1, C#1 target electrical check and leak check at SHC. C#1_target_electrical_and_leak_check.pdf

Target to HS is 400 ohm. The rest check is good. See attachment.

Entry  Wednesday, June 17, 2020, 09:49, chad fisher, South Hot-Cell, Standard Operation, TM4, C#1, C#1 installed C#1_Target.jpg

Target C#1 has been installed on TM4 with new high current fasteners torqued to 130in lbs.

 

 

Entry  Tuesday, June 16, 2020, 09:37, Travis Cave, South Hot-Cell, Standard Operation, TM2, no target, Module move 

 TM#2 with no target has been moved from the south west silo to the south hot cell.

Entry  Thursday, June 11, 2020, 12:36, David Wang, Safe Module Parking, Repair, TM3, , TM3 containment box and service tray field measurement.  
At 15cm distance: Containment box window 21msv maximum. Service tray 8.0msv maximum.
At 0.5 meter distance 360degree rotation: containment box high 10msv, low 4.3msv.
Maximum 170 to 180 counts(44-2) on swipes taking from service cap inside.
0 to 20 counts(44-2) on air sample at 0.5 meter to containment box window panel.
80 counts(44-2) on air sample taking from service cap inside.  The contamination level in service cap is low.

 

Entry  Thursday, June 11, 2020, 11:49, David Wang, ITE, Maintenance, , , ITW and ITE thermocouple status. 

  ITW - 2A2

o    2A2DSP-TC3 - not connected in El room

o    2A2COL-TC2 - does not work inside module

o    2A2COL-TC3 - does not work inside module

·         ITE - 2A3

o    2A3COL-TC3 - works, but plug needs repair in ITE pit

 Anders and I checked ITW and ITE thermocouple status. See result above.  Frank and I will fix the 2A3COL-TC3 loose cable to plug issue.

Entry  Thursday, June 04, 2020, 10:51, David Wang, Conditioning Station, Standard Operation, , , TH floor mop up. 

Jason Sargeant mopped up TH floor this morning. The mop head was checked after the job. There are 1500 counts on it. He think this level is reasonable low. 3000 counts would be normal in past.

Entry  Thursday, June 04, 2020, 10:40, David Wang, Conditioning Station, Maintenance, , , Three manual valves are closed on TCS water system  TCS_return_line_closed_valves_001.JPGTCS_return_line_closed_valves_002.JPG

Three manual valves are closed on TCS water system return line in experimental hall. See attachments. It is for TCS TK2 water level slow drop trouble shooting.  These valves will be opened again right after troubleshooting.  

TCS TK2 water level no change(11.1 inches) in this week after valves are closed. I will keep these three valves closed for one more week.

I opened these valves. In two week times, The TK2 level dropped 0.1 inches. The water level change could be a result of evaporation of water in system. We will keep watching on it.

Entry  Monday, June 01, 2020, 12:46, David Wang, ITE, Maintenance, , , ITH:CM6 ,CM6S and ITM:CM3 calibration. 

Edi calibrated ITH:CM6, CM6S and ITM:CM3. By the same time,  ITH:MP1 and MP2  lubricate oil level are checked. Everything looks fine. No oil  leak on both pumps. 

Entry  Monday, June 01, 2020, 12:40, David Wang, Crane, Maintenance, , , TH crane festoon cable maintenance 

Tom Kauss corrected the TH crane  festoon cable loops. He lubricated festoon cable wheels as well.    The maintenance is done.

Entry  Friday, May 22, 2020, 13:26, David Wang, ITW, Repair, , , ITW water leak. itw_water_leak_001.JPGitw_water_leak_005.JPGitw_water_leak_009.JPGitw_water_leak_013.JPG

A water leak was found on a fitting connecting ITW dump return line pressure gauge on top of exit module. TM tank flange, o-ring slot and o-ring were contaminated by water and water rust. Frank and I cleaned the flange and o-ring slot . We changed a new TM tank o-ring, vacuumed around other 3 module flanges. The leak fittings with pressure gauges were removed . I put a blind cap on removed fitting spot.. Water are switched back to ITW. No leak on blind cap.

Entry  Wednesday, May 20, 2020, 13:30, David Wang, Safe Module Parking, Maintenance, , , Silo area radio active waste clean up.  

Sorted and packed one 55 gallon drum with low contamination and active stuffs which are placed around silo area in the past. They include old poly water cooling lines replaced from ITE, ITW and TCS, contaminated paper  rags , gloves, and plastic bags,air cooling fans for turbo pumps, EE resistor packaged used on module top before, flow meters and cables used in ITW, etc. After packing, The field outside the drum on contact is less than 10 usv/hr.

Entry  Wednesday, May 20, 2020, 13:19, David Wang, ITE, Maintenance, , , Restart of ITE turbo pumps.  

PLC6 drop out in weekend caused the ITH MP1 and MP1s stopped. ITE turbo pumps were running still after that. Without back up pump, TPs started to trip off  later .  I found TP1,TP3, and TP4 were  tripped off this morning. And , The rest pumps ran with high current draw.  Jon Aoki restarted back up pumps and ITE turbo pumps. The ITE vacuum system works fine now.

Entry  Wednesday, May 20, 2020, 13:08, David Wang, Cooling, Standard Operation, , , Start of HALCW sysytem 

High  active water pump is started. The system resistance is recovering now. Everything works fine so far. Check ITW and ITE water leak after pump is started. Tiny very slow seep on two small ball valves pack seal. No big concern.                                 

Entry  Friday, March 27, 2020, 08:45, Matthew Gareau, North Hot-Cell, Maintenance, , , Issues with the manipulators 

 This is a link to all of the issues with the NHC manipulators that I know of

https://documents.triumf.ca/docushare/dsweb/View/Collection-27663/Document-180176

Entry  Thursday, March 19, 2020, 15:48, Anders Mjos, Conditioning Station, Maintenance, , , Filter replacement in water system March 5th 

Filters were replaced by Curtis von Cube on March 5th. See work permit for details I2020-03-05-5

Entry  Wednesday, March 18, 2020, 10:40, David Wang, ITE, Development, TM4, , TM4 P2N target connection checklist. P2N_TM4_connection_checklist.pdf

TM4 has been connected in ITE. See checklist.

Entry  Tuesday, March 17, 2020, 14:59, David Wang, ITE, Development, TM4, P2N, ITE turbopumps are started. 

They work fine. Current draw on all pumps are normal. I asked operator to switch on IG1 , IG1S and PNG4.

Entry  Tuesday, March 17, 2020, 12:58, David Wang, South Hot-Cell, Development, TM4, , P2N target electrical check and leak check at SHC. P2N_target_electrical_chek_at_SHC.pdf

See attachment. Everything looks good.

Entry  Tuesday, March 17, 2020, 11:42, Travis Cave, ITE, Standard Operation, TM4, P to N target, Module move 

 TM#4 with the P to N target has been moved from the south hot cell to the east target station.

Entry  Monday, March 16, 2020, 09:25, Travis Cave, South Hot-Cell, Standard Operation, TM4, no target, Module move 

 TM#4 has been moved from the silo to the south hot cell.

Entry  Friday, March 13, 2020, 09:24, Travis Cave, ITE, Standard Operation, , , Entrance module move 

 The east entrance module has been moved from the south hot cell back to the east target station.

Entry  Thursday, March 12, 2020, 13:48, David Wang, ITE, Repair, , , Entrance module TP1S broken piesces clean up. 

The broken pieces in ITE entrance vacuum pit are vacuumed out.  At SHC, There are 4 pieces on module collimator block top,  wiring scanner top. Chad removed them out at SHC. Electrical check at module top is done by diagnostics group. Everything works fine.

Entry  Thursday, March 12, 2020, 13:42, David Wang, ITE/ITW, Development, , , New ITE IGLIS cables installation  

New IGLIS cables installation is done. Two bundle of new cables are pulled from ITE to electrical room. They are in one PVC conduit. The old cables are not removed yet. I will pull old cables out when new cables are installed onto device in ITE Faraday cage.

Entry  Wednesday, March 11, 2020, 10:39, Travis Cave, ITE, Maintenance, , , Entrance module move 

 The entrance module has been moved to the east station to the south hot cell for inspection from the turbo pump explosion.

Entry  Monday, March 09, 2020, 14:31, David Wang, ITE/ITW, Standard Operation, , , TH emergency exit test.  

Frank and I did the test.  The emergency exit hatch on roof was opened and closed twice. Everything works fine.

Entry  Friday, March 06, 2020, 09:51, David Wang, South Hot-Cell, Standard Operation, TM2, , TM2 was moved from SHC to SMP yesterday. 

TM2 was moved from SHC to SMP yesterday.  The move is successful. TM2 is located at SMP. There is no hot target on module so SMP vacuum is not started.

Entry  Friday, March 06, 2020, 09:35, David Wang, Spent Target Vault, Standard Operation, , SiC #39, Spent target SiC#39 removal from SHC to storage vault. 

Spent target SiC#39 is removed from SHC to storage vault at 4C in pail #227.The move is successful.  Note:The small aluminum block holding wire on pail lid could be contaminated by SHC manipulator during the lid installation in SHC.

Entry  Thursday, March 05, 2020, 07:16, David Wang, South Hot-Cell, Standard Operation, TM2, SiC #39, TM2 SiC #39 post run electrical checklist  SiC_#39_post_run_cheklist..pdf

 Electrical check result is fine.  See attachment.

Entry  Wednesday, March 04, 2020, 14:30, David Wang, Safe Module Parking, Standard Operation, TM2, , Remove of TM2 from SMP to SHC. 

Frank and I removed TM2 from SMP to SHC. The move is successful.

Entry  Wednesday, March 04, 2020, 11:52, David Wang, ITE, Standard Operation, , , ITE HV test without module 

ITE bias test is done to 48KV. No spark. We can not raise bias above 48KV. It looks like we have a current limit issue on control system when testing above 48KV.  John Cow checked current limit on PS locally. It is set to 8mA which is much higher than the test current. Isac operator issued an e-fault to control group.  

 John Chow did a local test on PS. Everything works fine.The problem is on control system. We have a 48KV voltage limit problem on control system. We decide to end the test now. 48KV is good enough before this year mini-shut down. 

Entry  Friday, February 28, 2020, 09:36, David Wang, ITE, Repair, , , Entrance module TP1S broken piesces clean up.  

Using the camera,  Frank and I inspected the broken blades in vacuum duct bending section. We are pretty sure some of  the broken parts are fallen into  bottom of entrance module and vacuum vessel since the broken pars are over on the edge of bending section. The blades rotated at high speed. Basically, They were shoot to the duct opening when they were broken from the pump. Frank and I carefully swiped all broken parts  from the edges  back to center of duct first. Then, We use vacuum cleaner sucked all broken parts out of the entrance module. We can see lots aluminum dust  during the clean up. This kind of aluminum dust also could  fallen down to bottom of module and vessel.  After clean up, We inspected duct with camera. We can see all broken pieces and dust are cleaned out.  The removed broken pieces will be stored with broken pump when the vessel bottom clean up is done.

Entry  Thursday, February 27, 2020, 16:08, Anders Mjos, North Hot-Cell, Maintenance, , , Hot Cell Entry NHC_2020-02-27.pdf

Chad entered the NHC today to tighten set-screws on both slave side manipulators and re-align the West side slave. Work took place using the HC Confined Space Entry procedure. See attached checklist. WP I2020-02-27-4

Entry  Thursday, February 27, 2020, 10:37, David Wang, Safe Module Parking, Standard Operation, TM2, , Start of SMP vacuum pump. 

TM2 in SMP with old SiC #39 target on it. SMP vacuum pump is started.

Entry  Thursday, February 27, 2020, 09:50, Travis Cave, Safe Module Parking, Standard Operation, TM2, SiC#39, Module move 

 TM#2 with SiC#39 has been moved from the east station to the smp.

Entry  Wednesday, February 26, 2020, 08:45, David Wang, Conditioning Station, Standard Operation, TM4, , Remove of TM4 from TCS to SW silo 

TM4 has been moved from TCS to SW silo. The move is fine.

Entry  Thursday, February 20, 2020, 09:27, David Wang, Spent Target Vault, Standard Operation, , , Inventory of mini storage and vault. Mini_Vault_2020-02-20.pdfVault__2020-02-20.pdf

Repacked nSiC#1 in SHC and moved it to mini storage vault. Transferred UCx26 and UCx28# from vault to mini-storage. See attachment for vault and mini-storage inventory.

Entry  Friday, February 14, 2020, 14:13, David Wang, South Hot-Cell, Standard Operation, TM4, , SIS dummy target for IGLIS TM4 electrical check Dumm_SIS_target_for_IGLIS_test_on_TM4.pdf

Electrical check and HS, window leak check result at SHC. See attachment.

Entry  Friday, February 14, 2020, 14:06, David Wang, Conditioning Station, Standard Operation, TM4, , TCS vacuum system and water sytem are switched on. 

All turbo pumps are started. 

Entry  Friday, February 14, 2020, 11:25, Travis Cave, Conditioning Station, Standard Operation, TM4, Dummy Target, Module move 

 TM#4 with dummy target has been moved from the south hot cell to the conditioning station.

Entry  Friday, February 07, 2020, 08:05, chad fisher, South Hot-Cell, Development, TM4, , Containment box off for IGLIS 

The containment box has been removed from TM4 in prep for the IGLIS wiring job.

Entry  Thursday, February 06, 2020, 13:32, Adam Newsome, South Hot-Cell, Maintenance, TM4, , TM4 moved from Conditioning Station to South Hot Cell 

 TM4 was moved from conditioning station to south hot cell in preparation for wiring replacement. No target.

Entry  Thursday, February 06, 2020, 13:31, Adam Newsome, Spent Target Vault, Standard Operation, , UC#29, UC#29 moved to vault location 6A, in pail 225 

 UC#29 in pail 225 was moved to the storage vault, location 6A. Field measured at 22.4 mSv/hr at ~1m. 

Entry  Wednesday, February 05, 2020, 11:03, David Wang, South Hot-Cell, Standard Operation, TM4, UCx 29, UCx 29 post run electrical check UCx29_post_run_electrical_check..pdf

UCx 29 TM4 post run electrical check is done before target is removed. Everything is normal on measurements.

Entry  Wednesday, February 05, 2020, 10:54, David Wang, Conditioning Station, Standard Operation, TM4, , Roughing out TM4 at TCS. 

TCS MP1 is started to rough out TM4 and TCS. TCS and TM4 will be under roughing only today and tomorrow. No plan to start TCS and TM4 turbo pumps this time.

Entry  Wednesday, February 05, 2020, 10:49, David Wang, Conditioning Station, Standard Operation, TM4, , Remove of TM4 from SHC to TCS. 

TM4 has been moved from SHC to TCS. No target on module. The move is successful.

Entry  Wednesday, February 05, 2020, 08:22, chad fisher, South Hot-Cell, Standard Operation, TM4, UCx#29, UCx#29 removed 

UCx#29 has been removed from TM$ and placed in a pail backfilled with argon until it can be moved to the storage vault.

Entry  Tuesday, February 04, 2020, 14:22, Travis Cave, South Hot-Cell, Standard Operation, TM4, UC#29, Module move 

 TM#4 with UC#29 has been moved from the west target station to the south hot cell.

Entry  Monday, February 03, 2020, 09:14, David Wang, ITW, Standard Operation, TM4, UCx 29, TM4 UCx 29 disconnection checklist  UCx29__disconnection_checklist.pdf

TM4 has been disconnected in ITW. See attachment checklist.

Entry  Monday, February 03, 2020, 09:10, David Wang, ITW, Standard Operation, TM4, , ITW TPs are switched off. started of ITW argon venting. 

ITW is argon venting now.

Argon venting of ITW is done. It took about 4.0 to 4.5 hours to vent the ITW with 2-3 psi argon. The CG4 and CG4S showed 35 to 36 torr on epic page when mechanical gauge is 760torr in electrical. Argon gas bottle is closed in electrical room.

Entry  Thursday, January 30, 2020, 12:06, David Wang, ITW, Standard Operation, TM4, , ITW primary and secondary vacuum seals leak check.  

Connected LD to ITW(TM4) TP1. Base LR 0.0Xe-9 atm.cc/sec. Base pressure 0.0Xe-4 torr. All ITW primary and secondary air to vacuum seals are helium spray checked. There is a 5XE-9 atm.cc/sec leak on  exit2 module top cover plate o-ring seal. The location is on west  side, south corner of the plate. Hi- vacuum resin are sprayed to leak area, and leak checked  again. The leak is gone.   The other seals on ITW vacuum vessel are good.

 

Entry  Thursday, January 30, 2020, 10:22, David Wang, ITW, Standard Operation, TM4, , TM4 water lines helium pressure leak check.  

  TM4 internal water lines helium pressure leak check at ITW : 70psi helium 5 minutes on  each circuits. Base leak rate 0.0X E-9 atm.cc/sec. Base pressure 0.0X E-4torr. Only B line(Oven -) has a tiny 1.5Xe-9 atm.cc/sec response on LD during the check . All others all perfect good. 

Entry  Wednesday, January 29, 2020, 12:37, David Wang, ITE, Standard Operation, TM2, , ITE primary/secondary vacuum vessel leak check. 

Leak check on ITE vacuum vessel is done. LD base leak rate 0.0XE-9atm.cc/sec. base pressure 0.0Xe-4torr. Sprayed helium on all ITE primary and secondary vacuum vessel seals(including TM2). No leak . Also,70psi helium  pressurized TM2 waterlines inside the module for each circuit 3 minutes. No leak on all operating TM2 waterlines.  

Entry  Monday, January 27, 2020, 10:40, David Wang, Cooling, Maintenance, , , ITE/ITW supply water presuure on dump circuits.  

With both stations in operation,ITE dump supply gauge reading is 27 psi. ITW is 20 Psi.  I adjusted ITW dump pressure to 25 psi by changing the return line side pressure relieve valve.

ITE full operation+ ITW no TM: ITE dump pressure 27psi, ITW dump pressure 27psi.

2019-01-30: Water only supply to 2A beam lines only on both side, No TM2 and TM4 in water loop.  ITE dump pressure 27psi, ITW dump pressure 27psi.

Entry  Friday, January 24, 2020, 08:19, David Wang, ITW, Standard Operation, TM4, , ITW water signal interlock check. 

ITW water signal interlock check is done. Everything works fine. ITW 2A2 tank water signal is broken and is not ok on XT2A2  page. I will fix it next week.

Entry  Thursday, January 16, 2020, 09:37, Travis Cave, Conditioning Station, Standard Operation, TM3, no target, Module move 

 TM#3 has been moved from the conditioning station to the centre east silo.

Entry  Tuesday, January 14, 2020, 10:19, David Wang, Conditioning Station, Standard Operation, TM3, , TCS vacuum system is switched off.  

TM3 TP1 and TP2 work  fine in past 4 days. During operation, The current draw on pumps were 0.7A to 0.8 A. TM3 will be moved back to silo tomorrow.

Entry  Tuesday, January 14, 2020, 10:12, David Wang, Conditioning Station, Standard Operation, TM3, , Helium spray leak check on TCS. 

Using a long pole with a probe to spray helium on TCS vacuum seals and joints which are installed in  TCS service pit. No response has been found on leak detector during leak check. TCS is leak free.

Entry  Monday, January 13, 2020, 14:19, Travis Cave, Spent Target Vault, Standard Operation, , Ta#49 and Ta#52, spent target repackaging and moved to mini vault. 

 Targeta Ta#49 and Ta#52 have been repackaged anf moved to the mini vault. Ta#49 was taken out of pail number 146 and placed into pail 229. Ta#52 was taken out of pail number 152 and placed into pail 230.

Entry  Friday, January 10, 2020, 10:26, David Wang, ITE, Standard Operation, , , ITE water signal inerlock check. 

ITE water  signal interlock   check is done.  Everything is good. It is a annual check we do in winter shut down time.

Entry  Thursday, January 09, 2020, 14:14, David Wang, Conditioning Station, Standard Operation, TM3, , Start of TCS roughing pump for TM3. 

I started TCS roughing pump. TM3 TP1 and TP2 will be started tomorrow morning.

Entry  Thursday, January 09, 2020, 13:49, Travis Cave, Conditioning Station, Standard Operation, TM3, no target, Module move 

 TM#3 has been moved from the south west silo to the conditioning station.

Entry  Wednesday, January 08, 2020, 10:34, David Wang, Assembly/Bench Test, Development, , , Module lifting assembly ITA0490 

The second module lifting assembly ITA0490 is moved into TH and installed onto TM3 . It will stay with TM3. I adjusted the  CofG on the assembly. It is same to the first lifting assembly we are using now. After adjustment, The installation of assembly on TM3 are smooth. 

Entry  Tuesday, January 07, 2020, 09:37, David Wang, ITW, Standard Operation, , , 5 shielding blocks are moved out of ITW top. 

5 shielding blocks are moved out of itw top.

Entry  Tuesday, January 07, 2020, 08:02, David Wang, Cooling, Standard Operation, , , Switch on HALCW MP2 

HALCW MP2 is switched on this morning after yesterday cooling tower maintenance. LALCW P5 and P6 pumps are started by isac operator  as well. The system is good so far.

Entry  Friday, January 03, 2020, 13:15, Adam Newsome, Crane, Repair, , , Target Hall Crane PLC Module/Battery Replacement 
The Target Hall Crane bridge and trolley motion was lost after a period of the crane having power disconnected over winter holidays. This is reported in the following e-log: https://elog.triumf.ca/TIS/RH-ISAC/2039. This issue is a duplicate of what happened in 2019 at this time: https://elog.triumf.ca/TIS/RH-ISAC/1845

It was determined from troubleshooting via PLC indicator lights that the memory battery had died during the power-off time, and because of this, the program stored was lost. Note that this is an anomaly - the battery should have lasted much longer than the shutoff duration of ~2 weeks.

The SLC500 module was replaced with a spare, which contained a new battery. The old SLC500 module is still functioning but the battery has been removed (spares will be ordered) - this module is stored in a cabinet drawer in the control room. It will need to be re-programmed if re-installed as the program was lost. The original program titled TargetHallCrane.RSS was downloaded to the module. The crane was tested in local mode and determined to be functioning.

The following links are resources for resolving this issue:
https://isaccontrols.wiki.triumf.ca/index.php/ISAC_Target_Hall_Crane
https://isaccontrols.wiki.triumf.ca/index.php/SHUTDOWN_2015_Tasks#ISAC_Target_Hall_Crane_Controls_DM_-_Completed
Entry  Thursday, January 02, 2020, 10:10, David Wang, Crane, Standard Operation, , , TH crane issue. 

Target hall crane does not work properly after TH crane main power is switched off during Christmas time in control room. I switched the main power back this morning. The only movement could be operated is crane rotation. Power is supplied crane. The control  on N-S, E-W and up-down movements do not work. We had the same problem last year. After trouble shooting, It was pointed to a PLC battery issue. Control group changed the battery and reloaded the program. I guess  the battery is drained out very fast for some reason. So, We face the same problem again this year.

Adam checked control room main power supply. I checked in TH crane again. The problem is still there. We can confirm this is the same issue like last year. 

Entry  Thursday, January 02, 2020, 09:55, David Wang, Cooling, Standard Operation, , , I turned on HALC water pump MP2. 

HALCW MP2 is switched onnow. There is a small amount of air trapped in system. The pump works fine.  Water level and system resistivity will be monitored for a while.

LALCW P5 and P6 are switched on  for cooling HALCW.  HALCW MP2 is in operation now.

Entry  Thursday, December 12, 2019, 14:39, Isaac Earle, Safe Module Parking, Development, , , SMP assembly shifted 1.0" north 

The SMP assembly was shifted approximately 1.0" north today by pushing it, braced against the south wall, using a 100 Ton capacity air lifting bag supplied by Beamlines Group.  The move was one of the action items identified at the Gate 4A/4B close-out review.  During commissioning of the SMP, TM3 was installed into the vacuum vessel, which required the crane to be all the way at its south limit, so the move is to provide some margin for future use, particularly if TM1 is put in the SMP as the extent of its shielding is slightly larger than the other modules.

 

One of the air fittings for the lid actuation cylinder on the north side was damaged during the move.  It was replaced and correct functionality of lid actuation was then confirmed.

Entry  Tuesday, December 03, 2019, 12:45, Adam Newsome, Spent Target Vault, Standard Operation, , SiC#38, SiC#38 in Pail 205 moved to Storage Vault: 4B Target_Index_2019-12-03.pdf
SiC#38 in Pail 205 was moved to section 4B of the storage vault. Dose rate when retrieving from Hot Cell was 22.2 mSv/h.
Entry  Friday, November 29, 2019, 13:10, David Wang, ITE, Standard Operation, TM2, SiC 39# febiad, TM2 SiC#39 connection check list. SiC_#_39_febiad_connection_checklist.pdf

TM2 has been connected  in ITE.  All turbo-pumps are started.

Entry  Friday, November 29, 2019, 11:03, Travis Cave, South Hot-Cell, Standard Operation, TM2, SiC#39, Module move 

 TM#2 with the SiC#39 target has been moved from the south hot cell to the east target station.

Entry  Friday, November 29, 2019, 11:02, Travis Cave, South Hot-Cell, Standard Operation, TM2, SiC#38 SiC#39, Electrical Check Elec_chk_SiC#38_SHC_post_beam_TM2_11-26-2019.pdfElec_chk_SiC#39_SHC_TM2_11-29-2019.pdf

 Results from the electrical check with the old SiC#38 target and the new SiC#39.

Entry  Wednesday, November 27, 2019, 13:46, David Wang, Conditioning Station, Standard Operation, TM2, SiC 38# febiad, TM2 SiC #38 disconnection checklist. SiC_#_38_febiad_disconnection_checklist.pdf

TM2 was disconnected in ITE yesterday.

Entry  Tuesday, November 26, 2019, 10:24, Travis Cave, South Hot-Cell, Standard Operation, TM2, SiC#38, Module move 

 TM#2 with SiC#38 has been moved from ITE to the south hot cell.

Entry  Tuesday, November 19, 2019, 13:41, David Wang, ITE, Standard Operation, TM2, SiC 38# febiad, TM2 SiC#38 connection check list. SiC_#_38_febiad_connection_checklist.pdf

TM2 was connected in ITE 12th Nov. attach checklist

Entry  Thursday, November 14, 2019, 13:52, Travis Cave, Spent Target Vault, Standard Operation, , UC#22,23,24, Targets repackaged Target_Index_2019-11-14_Mini_Vault.pdf

 The targets UC#22,23,24 have been repackaged into the newer stronger pails, and have been placed back in the mini vault with new numbers. See attached PDF for details.

Entry  Tuesday, November 12, 2019, 10:07, Travis Cave, Spent Target Vault, Standard Operation, , Ta#59, Spent Target Move Target_Index_2019-11-08.pdf

 The spent Ta#59 was moved from the south hot cell to the spent target vault. See the attached for details.

Entry  Tuesday, November 12, 2019, 10:02, Adam Newsome, ITE, Standard Operation, TM2, SiC#38, TM2 Move 

TM2 was moved from the Conditioning Station to ITE, with SiC#38 target.

Entry  Thursday, November 07, 2019, 08:56, David Wang, Conditioning Station, Standard Operation, TM2, SiC#38, TM2 in TCS. 

Helium pressure leak check on TM2 HS line at TCS is done. No leak. Also, Helium are sprayed to gas line adapter and fittings. No leak. TM2 is connected at TCS. Anode plug on TCS is connected to module 52pin connector. Water system is started. Vacuum pumping down is good. HV cover will be installed today.

    Reply  Thursday, November 07, 2019, 10:39, Anders Mjos, Conditioning Station, Standard Operation, TM2, SiC#38, Conditioing SiC#38 SiC#38_ANODE_bias_2019-11-07.PNG

Thursday, November 07, 2019, 10:35: Tested source to 30 A on TGHT, TBHT and COIL. ANODE at 100 V.


Tuesday, November 12, 2019

The FEBIAD source worked well over the weekend. The anode current limit was adjusted twice to stop voltage limiting. About 5E-8 A on the FC with TGHT=580A, TBHT=300A, ANODE=200V,150 mA, COIL=50A. Bias was conditioned to 30 kV

Entry  Tuesday, November 05, 2019, 14:27, Travis Cave, South Hot-Cell, Standard Operation, TM2, Ta#59, Electrical Check Elec_Chk_TM2_with_Ta59_post_beam_SHC_Nov_05_2019.pdfElec_Chk_TM2_SHC_no_target_Nov_5_2019.pdf

 Results of the electrical check of TM#2 with the old Ta#59 target and target free.

Entry  Tuesday, November 05, 2019, 12:46, chad fisher, South Hot-Cell, Standard Operation, TM2, ta#59, Ta#59 removed 

Ta#59 has been removed from TM2 and it is now ready for electrical check.

Entry  Tuesday, November 05, 2019, 11:57, David Wang, ITE, Standard Operation, TM2, Ta 59, Ta#59 disconnection checklist Ta#59_disconnection_checklist.pdf

See attachment

Entry  Tuesday, November 05, 2019, 10:19, Travis Cave, South Hot-Cell, Standard Operation, TM2, Ta#59, Module move 

 TM#2 with Ta#59 has been moved from the ITE to the south hot cell.

Entry  Thursday, October 31, 2019, 10:17, David Wang, Assembly/Bench Test, Maintenance, TM2, , Febiad target gas line leak check. 

Feibiad gas line for ITE and its adapter fittings for TM2 are tested today by installing them on a dummy water stem. No leak on VCO fitting, adapter o-rings, and all Swagelock fittings of this assembly. Manual valve on gas line works fine.  The positional check on gas line between TM2 and ITW will be fulfilled next Tuesday during module disconnection. 

Entry  Thursday, October 31, 2019, 08:49, Anders Mjos, Conditioning Station, Repair, , , Water leak on non-active cooling water circuit 

Yesterday a leak was discovered in the ISAC-I experimental hall. The leak appears to be at the connection between the evaporator and the return water line. 1 in of water was lost from TCS:TK1. The water is currently valved off to prevent further leakage.

A fault reportt has been submitted to mechanical services - awaiting response.


Friday, November 01, 2019

Leak repaired by Mechanical Services. A brass fitting had cracked and was replaced with a galvanized fitting.

Entry  Wednesday, October 30, 2019, 11:18, David Wang, ITW, Standard Operation, TM4, UCx 29, UCx 29 connection checklist UCx_29_connection_checklist.pdf

See attachment

Entry  Tuesday, October 29, 2019, 10:00, Adam Newsome, Safe Module Parking, Development, , , SMP Updates to E-stop circuit and feedback signals 

The SMP main control panel and remote control module were updated in order to implement the following items which were deemed desirable during commissioning:
 

  •     24 VDC line added to E-stop circuit:

    Previously the E-stop relay cut power to only 120 VAC. This means that the lid rotation motor would stop instantly, but since the lid open/close valve is powered by 24 VDC which comes from a power supply unit, there would be a short delay while the unit powers off in which the valve was still active. This could result in a situation in which, for example, someone is operating the pendant to close the lid and another person recognizes a hazard and presses the E-stop on the main panel, but the lid does not stop closing for approximately 3 seconds while the operator is still holding the "close" button down.

    To rectify this issue, the 24 VDC line was routed through a NO contact of the same E-stop relay that controls the entire 120 VAC supply to the system. This was tested on Oct. 25, 2019 - working.

     
  • Status feedback signals to remote control room:

    Previously status signals for "Lid raised", "Lid Centred", "CW Limit", and "CCW Limit" were only displayed as light indicators on the main control panel. It was determined during remote operation that it would be helpful to have these signals sent back to the software interface so that an operator does not need to use a camera to look at the light indicators.


    Electrical drawings and cable schedule have been updated to reflect these changes. The SMP will be tested again using the commissioning plan checklist to confirm no there were no inadvertent effects on the rest of the same from these changes.

 

Entry  Monday, October 28, 2019, 12:00, Isaac Earle, Safe Module Parking, Development, , , SMP shielding attenuation measured & compared to theoretical values 

The attenuation of the SMP shielding was measured as part of SMP commissioning (Document-170404, R1, Section 4, Test #8)

The field on the shutter side of TM3 was measured without any shielding as it was removed from a storage silo.  At 0.5m from the edge of the module the maximum field was 5.00mSv.  After installation into the SMP the maximum field outside the SMP shielding at 0.5m from the edge of the module was found to be 27uSv/hr. The resulting attenuation is 185x

Expected attenuation was calculated by Joe Mildenberger assuming that the majority of the activated components in that module are either copper or aluminum.  With 6" of steel shielding (SMP shield vessel plus vacuum vessel), the attenuation factors were found for the following isotopes: 

 

Na-22 (created in Al): 115

Co-60 (created in steel (Fe) or Cu): 70

Mn-54: (created in steel (Fe) or Cu): 200

 

Based on these figures, the measured result of 185 seems to be reasonable.

Entry  Monday, October 28, 2019, 11:50, Travis Cave, Spent Target Vault, Standard Operation, , UC#28, Spent Target Move Target_Index_2019-10-28.pdf

 UC#28 has been moved from the south hot cell to spent target storage. The target was placed in pail number 219 and placed in spot 1C of the vault, it was 12.6mSv/hr upon removal from the south hot cell. Also the spent target vault is now full and can not currently accept anymore targets.

Entry  Friday, October 25, 2019, 06:43, David Wang, Safe Module Parking, Development, TM3, , SMP vacuum 

TM3 was moved into SMP Oct 25 morning.  After two nights pumping down, SMP CG1 read 30mtorr this morning.  The pump is stopped. SMP will be vented soon for TM3 moving back to silo. 

Entry  Thursday, October 24, 2019, 14:11, Travis Cave, ITW, Standard Operation, TM4, UC#29, Module move 

 TM#4 with UC29 has been moved from the south hot cell to the west target station.

Entry  Wednesday, October 23, 2019, 07:58, chad fisher, South Hot-Cell, Standard Operation, TM4, UCx#28, UCx#28 Removed 

UCx#28 has been removed from TM4. Guard screws on 5(10) pin connector had to be removed to get the connector to un-seat properly for removal.

Entry  Wednesday, October 23, 2019, 06:56, David Wang, ITW, Standard Operation, TM4, UCX 28, TM4 UCx 28 disconnection checklist UCx_28_disonnection_CL.pdf

TM4 was disconnected in ITW.  See checklist.

Entry  Tuesday, October 22, 2019, 16:26, Isaac Earle, Safe Module Parking, Development, , , SMP shield box grounding 

A braided grounding strap was attached to the aluminum gear box support on the SMP shield box structure, and grounded by attaching it to the exterior of an electrical conduit located in the south-west corner of the B2 area at the top of the silo in that corner.  The braiding was also connected to the stainless steel support structure for the SMP vacuum pump.

Entry  Tuesday, October 22, 2019, 11:19, Adam Newsome, South Hot-Cell, Standard Operation, TM4, UC# 28, TM4 Move 

TM4 with UC# 28 target has been moved from ITW to the South Hot Cell. Shield plug installed in ITW.

Entry  Thursday, October 17, 2019, 11:49, Travis Cave, Spent Target Vault, Standard Operation, , SiC#31,32 and UC#19,20,21, Loading F-308 

 The targets in the mini storage have been loaded into the F-308.

Entry  Tuesday, October 15, 2019, 16:42, Isaac Earle, Safe Module Parking, Development, , , SMP flange alignment tested using shield plug smp1.jpgsmp2.jpgsmp3.jpgsmp4.jpg

 As a preliminary test in preparation for SMP commissioning, one of the steel module shield plugs was installed into the SMP to check the positional and rotational alignment procedures.  The following is a summary of the steps performed:

  1. Shield plug lifted with crane and rotated to an arbitrary (non-orthogonal) position
  2. Using the crane pendant the shield plug was roughly aligned over the SMP and lowered until the base was within 15cm of the top of the flange
  3. The SMP flange was rotated to roughly match the orientation of the shield plug 
  4. Precise positioning of module achieved visually from within the Target Hall using crane for NESW position and SMP for rotation
  5. Module lowered into SMP vessel (not resting on base of vessel)
  6. Target Hall crane was then set to "Test Mode" and operated from the crane control room
  7. Crane position with the module centered in the SMP vessel was recorded as E-W: 18.5495m,  N-S: 4.9065m
  8. The shield plug was lifted from the SMP, moved to an arbitrary location in the Target Hall, and set to a different arbitrary rotational position
  9. The SMP flange was returned to the "centered" position
  10. The shield plug was moved to the previously recorded location over the SMP and lowered to within 15cm of the top of the flange (using cameras)
  11. Steps 3-5 were repeated using only camera views to achieve alignment (SMP rotation was controlled using the pendant with instructions by phone from the crane room operator because the module for remote control currently requires a part to be changed)

Official commissioning of the SMP will now be planned as per the commissioning plan Document-170404

 

 smp1.jpg

 

smp2.jpg

 

smp3.jpg

 

smp4.jpg

Entry  Thursday, October 10, 2019, 16:17, Adam Newsome, Safe Module Parking, Development, , , SMP Main Panel: Relay Addition for E-Stop Circut Changes_to_IRH1869.JPGIMG_20191009_153336_-_new_relay_for_E-stop.jpg

An update was made for the E-stop and power supply system in the SMP main panel. Upon testing remote control, it was determined that the Opto 22 AC module was not sufficiently rated to handle the current draw of the motor (5A fuse versus motor 5.7A current draw). The design was modified so that the E-stop chain, which supplies 120 VAC line voltage through the main panel E-stop then the remote module (or local pendant when plugged in), will now activate a relay rather than run directly to the motor and 24 VDC PSU. This means that this E-stop chain will not carry the current draw of the entire system. Rather, the relay that is toggled when the E-stop circuit is closed will supply the system with power - this relay is rated for 15 A so the main 10 A fuse will blow before the relay fails in the event of a current spike. The new relay was installed on Oct 9, 2019. The local pendant was tested at this time and worked as expected (motion control, E-stops). On Oct 10, 2019, remote control was tested again and is working as expected (motion control, E-stops). In the attached schematic screenshot, the modification is CR7. In the image of the panel, this relay is located in the top left.

 

Edit: TRIUMF electrician Joel Semilla has seen the design change and verified it is acceptable.

Entry  Wednesday, October 09, 2019, 13:28, Travis Cave, Spent Target Vault, Standard Operation, , UC#27, Spent Target Move Target_Index_2019-10-09.pdf

 The spent target in the south hot cell has been moved to the spent target vault. It was placed in spot 1B of the vault in pail number 218. See attached for vault details.

Entry  Tuesday, October 08, 2019, 09:02, Travis Cave, South Hot-Cell, Standard Operation, TM4, UC#27 and UC#28, Electrical Check TM_elec_chk_with_UC27_shc_post_beem_Oct-04-2019.pdfTM4_elec_chk__with_UC28_shc_Oct-04-2019.pdfTM4_elec_chk_no_tgt_shc_Oct-04-2019.pdf

 Results of the electrical check of TM4 without target and with UC27 and 28

Entry  Monday, October 07, 2019, 14:03, David Wang, ITE, Standard Operation, TM2, Ta 59, TM2 has been connected in ITE. Ta_59_TM2_ITE__connection_checklist..pdf

Tm2 with Ta 59 has eben connected in ITE. Turbo pumps are started. See checklist

Entry  Monday, October 07, 2019, 09:56, Adam Newsome, ITE, Standard Operation, TM2, Ta 59, TM2 Move 

TM2 has been moved from the Conditioning Station to ITE with Ta#59 target.

Entry  Friday, October 04, 2019, 16:50, David Wang, South Hot-Cell, Standard Operation, TM4, , UCx 28 target with TM4 SHC leak check and electrical check.  

TM4 HS Leak check result is good . No leak. electrical check after target installation: Bias to chassis 550 Mohm. Coils are shorted each other and shorted to 60 KV bias. ABCD to 60KV bias 500V Megga measurement are 100M at least which is good. EE to bias are OL at 500V. The electrical check result is good.

Entry  Friday, October 04, 2019, 16:43, David Wang, Conditioning Station, Standard Operation, TM2, , TM2 has been connected at TCS. 

TM2 has been connected at TCS this morning. helium pressure test on Tm2 HS line is done. No leak.

Entry  Friday, October 04, 2019, 14:53, Travis Cave, South Hot-Cell, Standard Operation, TM4, UC#28, Module move 

 TM#4 with UC#28 has been moved from the south hot cell to the west target station.

Entry  Thursday, October 03, 2019, 10:25, Travis Cave, Spent Target Vault, Standard Operation, , ZrC#8, Spent Target Move Target_Index_2019-10-02.pdf

 The spent ZrC#8 was moved from the south hot cell to the spent target vault. It was placed in pail 217 and the pail was placed in slot 3A of the vault, it was 205mSv/hr when removed from the hot cell. Also the pail was filled with junk stuff that included 

wire, a wire scanner, IMG guage, target bolts and a water block bolts. Also there are only two spots left in the vault.

Entry  Wednesday, October 02, 2019, 08:25, chad fisher, South Hot-Cell, Standard Operation, , ZrC#8, ZrC#8 PIE 20191002_081653[1].jpg

Heat shield has been removed from ZrC#8.

Entry  Tuesday, October 01, 2019, 16:30, Anders Mjos, Conditioning Station, Standard Operation, TM2, Ta#58, Conditioning of Ta#58 

Tuesday, October 01, 2019, 15:15: Started roughing.

Tuesday, October 01, 2019, 16:30: Started TPs

Tuesday, October 01, 2019, 16:34: All TPs at speed


Conditioning completed over the weekend by RIB operations. The shutter was left closed on the module, so no beam could be seen on the FC. Conditioning otherwise OK.

Entry  Tuesday, October 01, 2019, 14:38, Travis Cave, South Hot-Cell, Standard Operation, TM2, Ta#59, Electrical Check TM2_no_target_SHC_elec_chk_Oct-1-2019.pdfTM2_Ta59_SHC_elec_chk_Oct-1-2019.pdf

 The results of the electrical check on TM#2 with the Ta#59 target and without before the target was mounted on the module.

Entry  Tuesday, October 01, 2019, 10:22, chad fisher, South Hot-Cell, Standard Operation, TM2, ZrC#8, ZrC#8 Removed Ta#59 installed 20190930_140918[1].jpg

ZrC#8 has been removed from TM2. Upon removal of the high current tube heater bolts it was noticed that the tube was broken. Also the 9 pin connector has an arc mark (see pictures attached).

Ta#59 has been installed with new fasteners. High current fasteners torqued to 130 in lbs.

Entry  Tuesday, October 01, 2019, 09:23, Don Jackson, ITE, Maintenance, TM2, ZrC #8, 60KV Common Connections TM2_Wiring.jpg

1 Jumpers between 60KV common and FEBIAD lines were connected in an unusual way.  This should of had no impact on the ZrC run but would have to be corrected for any future FEBIAD runs.

2 Feedthrough U was mislabeled (label has been removed)

 

Entry  Monday, September 30, 2019, 14:05, Travis Cave, South Hot-Cell, Standard Operation, TM2, ZrC#8, Electrical Check TM2_elec_chk_ZrC8_post_beam_SHC_09-30-2019.pdf

 Results of the electrical check on TM#2 with ZrC#8 post beam.

Entry  Monday, September 30, 2019, 11:36, Travis Cave, South Hot-Cell, Standard Operation, TM2, ZrC#8, Module move 

 TM#2 with ZrC#8 has been moved from the east station to the south hot cell.

Entry  Monday, September 30, 2019, 11:27, Isaac Earle, Safe Module Parking, Development, , , SMP vacuum vessel modifications completed 

The SMP vacuum vessel welds were reinforced to match the specifications on IRH1710 Rev D.  In addition a tube stub was added on the side of the vessel for installation of a PRV.  The relief valve installed was Accu-Glass 113150, with 2psi setpoint (not the MDC 420036 model specified on IRH1710 Rev D).  The drawing will be updated to reflect this.

Welding was performed in the TRIUMF machine shop.  A larger capacity forklift was rented to move the vessel back and forth between the shop and the Meson Hall loading bay where the main crane was used to flip the vessel between welds.

After welding the vessel was leak checked using a blank-off plate (helium leak tight).  The vessel was then returned to the Target Hall, the top flange IRH1755 was re-installed, and the TCS shield plug was installed on the flange.  The vessel was pumped down over the weekend using the SMP vacuum pump, and reached 8mTorr by Monday morning.  A helium leak check was performed in the Target Hall:  baseline leak rate 0.0E-9 atm-cc/sec, 0.0E-4Torr port pressure, no response to generous helium spray on PRV and around both seal locations for the top flange.

Remaining re-assembly of the SMP will now proceed.

Entry  Monday, September 23, 2019, 13:21, Travis Cave, Spent Target Vault, Standard Operation, , , Repacking of the targets. Target_Index_2019-09-23_Mini_Vault.pdf

 All targets in the mini vault have been repackaged and are now ready to be loaded into F-308s. All the target pails have new numbers see attached sheet for details.

Entry  Thursday, September 19, 2019, 10:11, Travis Cave, Spent Target Vault, Standard Operation, , , Repacking of the targets. 

 Another target in the mini storage has been repackaged into the new pails. With one remaining to do which will be done on Monday.

Entry  Wednesday, September 18, 2019, 14:28, Travis Cave, Spent Target Vault, Standard Operation, , , Repacking of the targets. 

 Three of the five targets in the mini storage have been repackaged into the stronger pail.

Entry  Tuesday, September 17, 2019, 07:37, Carla Babcock, ITE, Development, TM2, ZrC#8, end of run HV investigations HVtests_TM2_Sept172019.xlsx

Ramping up HV to ~30kV, encountered problems and had to drop back to 28kV. No response on IG1 or anything else during sparks. Lots of charging-type behaviour on the bias current. Protons at 55uA

Tuesday, September 17, 2019, 02:02 : 15 mins with only 1 spark at 30kV so increased the bias

Tuesday, September 17, 2019, 02:31 : 32kV. Current unstable

Tuesday, September 17, 2019, 02:41 : Current continues extremely unstable but not much sparking....

Tuesday, September 17, 2019, 02:53 : Proton beam trip initially settled the bias current down, but then current began climbing pretty steeply with protons still off

Tuesday, September 17, 2019, 03:28 : Protons dropped to 40uA from 55uA, Bias current is much more stable and no sparks for 25mins

Tuesday, September 17, 2019, 03:36 : Raising voltage easy to about 33.5kV then instability and sparking similar to around 31kV at 55uA p+

Tuesday, September 17, 2019, 04:45 : Lowered protons to 25uA and no sparks though the current is not stable

More things but forgot to write them down. Spreadsheet attached.

Entry  Friday, September 13, 2019, 13:36, David Wang, ITW, Standard Operation, TM4, UCX27, TM4 conenction in ITW checklist TM4_UCx27_connection_checklist.pdf

TM4 was connected in ITW this Tuesday. See attachment for checklist.

Entry  Thursday, September 12, 2019, 09:26, David Wang, ITW, Repair, TM4, , ITW bad vacuum issue and trouble shoot. 

ITW secondary vacuum was bad in last two days after TM4 was connected in ITW. Today when check the exit 2 module, I found a small needle valve on exit 2 module top was slightly opened for some reason in past months. The valve is closed . ITW vacuum is returned to normal status.

Entry  Tuesday, September 10, 2019, 14:04, David Wang, ITW, Standard Operation, , , ITW water interlock check. 

ITW water interlock check is finished. Everything is good.

Entry  Tuesday, September 10, 2019, 10:10, Adam Newsome, ITW, Standard Operation, TM4, UC#27, TM4 Move 

TM4 has been moved from the Conditioning Station to ITW with UC#27 target.

Entry  Tuesday, September 10, 2019, 08:25, David Wang, Conditioning Station, Standard Operation, TM4, UCx27, Argan vent TCS. 

TCS is argon vented. TM4 is disconnected at TCS.

Entry  Monday, September 09, 2019, 06:38, David Wang, Conditioning Station, Standard Operation, TM4, UCx27, HS and window line leak check. 

TM4 HS and window line are helium pressure checked at TCS. 70 psi helium 5 minutes. No response @1.2XE-8 atm.cc/sec. They are leak free.

Entry  Thursday, September 05, 2019, 14:26, Travis Cave, South Hot-Cell, Standard Operation, TM4, UC#27, Electrical Check TM4_elec_chk_with_UC27_at_SHC_Sept_5_2019.pdf

 The results of the electrical check of TM#4 with UC#27 attached to it.

Entry  Thursday, September 05, 2019, 14:26, Travis Cave, South Hot-Cell, Standard Operation, TM4, UC#27, Electrical Check TM4_elec_chk_with_UC27_at_SHC_Sept_5_2019.pdf

 The results of the electrical check of TM#4 with UC#27 attached to it.

Entry  Thursday, September 05, 2019, 14:18, Adam Newsome, South Hot-Cell, Standard Operation, TM4, UCx#27, TM4 Move 

TM4 with UCx#27 target has been moved from the South Hot-Cell to the Conditioning Station.

Entry  Thursday, September 05, 2019, 11:37, chad fisher, South Hot-Cell, Standard Operation, TM4, UCx#27, UCx#27 install 

Dummy Ta target has been removed from TM4 and UCx#27 installed

Entry  Wednesday, September 04, 2019, 13:53, chad fisher, South Hot-Cell, Repair, TM4, , TM3 CB to TM4 

The TM3 containment box has been installed onto TM4. No issues, leak checked ok.

 

Entry  Tuesday, September 03, 2019, 10:49, Adam Newsome, South Hot-Cell, Standard Operation, TM4, , TM4 Move 

TM4 has been moved from the Conditioning Station to the South Hot-Cell.

Entry  Tuesday, September 03, 2019, 10:48, Adam Newsome, South Hot-Cell, Standard Operation, TM3, , TM3 Move 

TM3 has been moved from the South Hot-Cell to the Middle-East silo.

Entry  Thursday, August 29, 2019, 12:54, Adam Newsome, South Hot-Cell, Standard Operation, TM3, , TM3 Move 

TM3 has been moved from the Middle-East silo to the South Hot Cell.

Entry  Tuesday, August 27, 2019, 13:12, Adam Newsome, Safe Module Parking, Development, , , SMP Remote Control Wiring Inspection 

The wiring for the SMP remote control module was inspected by Joel Semilla (TRIUMF electrician). The module was plugged in to verify there were no issues. No changes were suggested, and then wiring was approved.

Entry  Friday, August 23, 2019, 14:27, Isaac Earle, Safe Module Parking, Development, , , SMP camera video cabling installed and tested 

 Installation of the video lines for the SMP cameras was completed yesterday according to IRH1670 Rev B.  All four cameras were confirmed to be displaying properly in the crane control room.  The cameras are powered from an outlet wired to circuit 35/37 on Panel #443 (located in the NHCSA).  This is independent from the power supply for other existing camera systems in the Target Hall.  The SMP turntable was rotated through the full range of motion (reached CW and CCW limits) and the cable routing and reel take-up system performed as expected.

Entry  Thursday, August 22, 2019, 09:20, Travis Cave, South Hot-Cell, Standard Operation, TM4, no target, Module move 

 TM#4 has been moved from the south west silo to the south hot cell.

Entry  Friday, August 16, 2019, 14:23, Carla Babcock, ITE, Repair, TM2, ZrC#8, TM2 electrical checks in ITE 

Ramped voltage on TM2 up to 30kV with no problems. Bias current is at 29uA, same as original TM2 bias current (see archiver for ITE June 15th, before protons) and similar to 31uA right after protons went off on Aug. 6.

TGHT=0A

TBHT=0A

BIAS V=30kV

BIAS current = 29uA

EZL V= 15kV

EZL current= 51uA

EE V= 1kV

EE current= 0.952mA

IG1= 8.6e-7

protons=0

This seems ok despite poor electrical checks showing 300 MOhm resistance between HV and ground. These values indicate a resistance of 1 GOhm. Let's see what happens when protons are on.

For future (optimistic) reference when testing protons:

BIAS=35kV, 35uA

EZL-17.5kV, 60uA

BIAS=38kV, 37uA

EZL=18.5kV, 63uA

Entry  Friday, August 16, 2019, 08:52, David Wang, Conditioning Station, Standard Operation, TM4, , TM4 is moved from TCS to SW silo. 

TM4 is moved from TCS to SW silo this morning. The move is good.

Entry  Friday, August 16, 2019, 08:51, David Wang, Conditioning Station, Repair, TM4, , TM4 waterlines helium pressure test at TCS. 

LD base leak rate, 0.0Xe-9atm.cc/sec. Helium pressure, 70psi. 5 minutes each circuit. No response on all water line except containment box window which has a VCR leak issue now. Window line leak rate, 2.3Xe-4 atm.cc/sec.

Entry  Friday, August 16, 2019, 08:46, David Wang, ITE, Standard Operation, TM4, ZrC #8., TM2 has been connected in ITE. 

TM2 has been connected in ITE. turbo pumps have been started. ITE  and TM2 vacuum are good.

Entry  Thursday, August 15, 2019, 09:45, Travis Cave, South Hot-Cell, Standard Operation, TM2, ZrC#8, Electrical Check TM2_elec_chk_with_ZrC8_at_SHC_Aug_17_2019.pdf

 Electrical of TM#2 with ZrC#8 at the south hot cell. See attached for details.

Entry  Thursday, August 15, 2019, 09:36, Adam Newsome, ITE, Standard Operation, TM2, ZrC #8, TM2 Move 

TM2 was moved from South Hot Cell to ITE. ZrC #8 target.

Entry  Wednesday, August 14, 2019, 11:43, Travis Cave, South Hot-Cell, Standard Operation, TM2, Ta#58 and no target., Results of electrical checks post beam at the south hot cell. TM2_elec_chk_Ta58_post_beam_shc.pdfTM2_Elec_chk_no_tgt_shc_Aug-14-2019.pdf

 Here are the results of the electrical done at the south hot cell post beam of with the Ta#58 target attached and with just the module no target attached.

Entry  Wednesday, August 14, 2019, 08:55, David Wang, ITE, Standard Operation, TM2, , TM2 has been disconnected in ITE. 

TM2 has been disconnected in ITE. The bias jumper between U and T was burned out during the last beam time.

Entry  Tuesday, August 13, 2019, 09:49, Adam Newsome, South Hot-Cell, Standard Operation, TM2, Ta 58, TM2 Move 

TM2 was moved from ITE to South Hot Cell. Tantalum 58 target.

Entry  Thursday, August 08, 2019, 09:33, Carla Babcock, ITE, Development, TM2, Ta#58, TM2 HV conditioning with protons, round 1 

Starting HV tests on TM2 with 50uA of protons.

Tuesday, August 06, 2019, 03:37 : Ramping up 500V every 2mins or so, couple of sparks, then consistent sparks at 34kV. No vacuum response on IG1 for any sparks, even though the current spikes from around 40uA to 1300uA. Brought it down to 28kV to stop sparking. See a response on the EZL frequently.

Tuesday, August 06, 2019, 05:24 : Going above 30kV proves very difficult, lots of up and down, frequent sparks, still no vacuum response. Still seeing an EZL response.

Tuesday, August 06, 2019, 05:58 : Up to 31.5kV on bias, 1046V on EE and 15kV on EZL.

Tuesday, August 06, 2019, 06:50 : Controls are being sticky - not responding well.

Tuesday, August 06, 2019, 07:25 : Sat at 32 kV > 20mins with 2 sparks

Tuesday, August 06, 2019, 08:03 : lots of sparking at 36kV, went back down to 35kV. Current draw is 50uA.

Tuesday, August 06, 2019, 08:10 : lots of sparking after 9 mins at 35kV, had to turn it down to 34kV

Tuesday, August 06, 2019, 08:11 : Still sparking at 34, down to 33

Tuesday, August 06, 2019, 08:31 : At 33kV, sparked twice in 20mins and was going for another when the protons went off.

With protons off, the bias current dropped quickly from 66uA to 40uA and raising the bias to 40kV was not difficult.  Later bias up to 50kV. Still no conclusion on if the sparking was inside or outside of the vacuum. No vacuum response seems to indicate outside, however the influence of protons would indicate inside. To be investigated visually when TM2 comes to the HC.

Entry  Tuesday, August 06, 2019, 01:13, Carla Babcock, Conditioning Station, Repair, TM4, Dummy HP SIS target, Checks on EE line leak fix and window line leak (not fixed) 

TM4 has developed 4 leaks so far:

  1. Line B - seems to be solved with an indium gasket (some testing already done)
  2. Line D - seems to be solved with an indium gasket (some testing already done)
  3. EE - indium gasket installed, preliminary tests are good
  4. Window cooling line - David found with 70 psi helium, leak detector response went from 3E-7 atm.cc/sec to 4E-4torr atm.cc/sec in 1 min and stayed there. When water was put through the circuit, there was an initial vacuum increase to about 1E-6, then a couple hours later it began to fall and has been falling for ~14hrs, now in the 7E-7 range for IG1.

Testing indium seals on lines B, D, EE. No repair has been done for window line. Ramping heaters to TGHT=450A, TBHT=200A. Everything behaving normally.

Wednesday, ramped up BIAS, EZL and EE to 36kV, 17kV, 1.5kV. Sparking at about 1 spark per 20 - 30 mins. Bias current somewhere between 66uA and 78uA, varying with the chiller ON/OFF.

Thursday morning around 2am everything tripped off. No spark visible on strip tool, seems this is from an increase in the window water leak. Vacuum recovered on its own and heaters were ramped back up.

Entry  Wednesday, July 31, 2019, 08:57, Adam Newsome, South Hot-Cell, Standard Operation, TM4, No Target, TM4 Move 

TM4 has been moved from the Conditioning Station to the South Hot Cell. No target.

Entry  Monday, July 29, 2019, 16:17, Carla Babcock, Conditioning Station, Repair, TM4, Dummy LP SIS, New leak on EE water line while testing new In seals 13_PM.png15_PM.png

Original Problem:

Leaks on the B and D copper blocks, probably due to corrosion between the blocks and the inserts. Final solution, after many tries, was to make an indium sheet the size of the copper blocks and use that to seal the entire surface.

So far offline tests seem to show these seals working, though long term tests are needed to say for sure.

 

New Problem:

TM4 was in the conditioning station, running water and under vacuum. 50A on the target and tube heaters from Friday evening to Saturday afternoon.

Sunday morning 9:30am target heating increased to 200A, 100A on the tube heater, ramp finishing around 1:30pm.

At around 3pm, the vacuum stops dropping and begins to climb very slowly, continuing until Monday morning (see first attachment).

Tests on the individual water lines show an immediate vacuum response only to the EE lines, the other lines show no response (note the window line is blanked off since the containment box is not on).

With water in the EE lines, the vacuum sits around 1e-6 near the target.

 

Testing:

Ramped target to 400A and tube to 200A. Sitting there for several hours shows no change in the vacuum response, though there is a variation that corresponds to the chiller turning on and off (see second attachment).

Ramped target to 450A and tube stayed at 200A. Vacuum staying in the low 10^-6 range, seems to be entirely due to EE leak, other seals are holding well.

 

Entry  Friday, July 26, 2019, 15:43, Isaac Earle, Safe Module Parking, Development, , , SMP vacuum control system completed SMP_vacuum_system_EPICS_screen.png

 The SMP vacuum control system has been wired and setup to be controlled from EPICS.  Backing valve control (SMP:BV1) was tested by connecting to the turbo pump solenoid on TM3 located in the silo directly north of the SMP.  The SMP pump (SMP:MP1) was turned on and off through the EPICS interface and responded as expected.  Both convectron gauges (SMP:CG1 and SMP:CG2) responded as expected when the pump was turned on.  The readings from the two gauges were consistent throughout the mili-Torr range.


The work was done by Ray Mendoza under WP I2019-07-24-4 (work request #5239).

 

SMP_vacuum_system_EPICS_screen.png

Entry  Friday, July 26, 2019, 11:41, David Wang, South Hot-Cell, Standard Operation, TM4, , TM4 with spare target electrical check and leak check. 

Electrical check on TM4 with spare test target. PQ is still shorted to RU. But, The short between 60KV bias and PQRU which we found last time is gone.  Target to PQRU at 250V mega measurement: 22.08 M. All conductivity between ABCD are about 5.0 m ohm which are good. All other ohm meter and Mega measurements are OL. Helium spray leak check on HS target VCR fittings is passed. Two blank offs are installed on source tray window cool lines. They passed  leak checked at SHC as well. 

Entry  Friday, July 26, 2019, 11:28, David Wang, South Hot-Cell, Standard Operation, TM4, , TM4 move from SHC to TCS. 

Tm4 has been moved from SHc to TCS without containment box. It is a new source tray on TM4.  A layer of plastic sheet was put on TH floor on module pass route during the move.

Entry  Monday, July 22, 2019, 14:51, Adam Newsome, South Hot-Cell, Standard Operation, TM4, No Target, TM4 Move 

TM4 has been moved from the South West silo to the South Hot Cell. New source tray, no target.

Entry  Tuesday, July 16, 2019, 08:44, Travis Cave, Conditioning Station, Standard Operation, TM4, no target, Module move 

 TM4 has been moved from the conditioning station to the south west silo. Module was placed with the turbo pump facing south which puts the windows facing north and south and the shutter facing west. 

Entry  Monday, July 15, 2019, 13:29, David Wang, Conditioning Station, Development, TM4, , Vacuum surge when TM4 B line iwas supplied with water. vacuum_surge_on_B_line_with_water.png

Yesterday, TM4 B line was supplied with water at TCS for testing.  TCS: IG1 and IG2 had big response on it. See attachment. The water was disconnected right away, and line was purged. Vacuum recovered after overnight pump.

Entry  Wednesday, July 10, 2019, 11:59, Carla Babcock, Conditioning Station, Repair, TM4, Dummy HP SIS target, Conditioning TM4 w/ new ST up to 50kV 

David raised the bias to 49.5kV. Module is still sparking mainly on top. Humidity is super high.

Wednesday, July 10, 2019, 09:50 : sitting at 49.7kV for a coupe mins, big spark in vacuum took everything down.

Wednesday, July 10, 2019, 10:16 : Bias at 50kV drawing 0.1mA but looking pretty jumpy. Left it here for ~5 mins then had to turn down bias for TH work.

Wednesday, July 10, 2019, 13:33 : Back at 50kV on bias with no problems.

Wednesday, July 10, 2019, 13:46 : 10 mins at 50kV, will try to go a bit higher

Wednesday, July 10, 2019, 14:06 : Everything sparked off while sitting at 50.6kV. This seems a bit futile....

Wednesday, July 10, 2019, 14:15 : Back at 50.1kV with no problems

 Wednesday, July 10, 2019, 14:33 : Up to 51kV

Wednesday, July 10, 2019, 15:20 : Difficult to go above 51.4. Turning up EZL since there were a couple sparks to it. -> Putting this up causes significant sparks between HV bias and EZL in vacuum at 5kV on the EZL, 51.1kV on bias. Leaving EZL @ 5kV

Wednesday, July 10, 2019, 16:04 : Around 52.2 sparking on the top of the module

Wednesday, July 10, 2019, 16:36 : 53kV

Wednesday, July 10, 2019, 17:16 : up to 54kV without much trouble

Wednesday, July 10, 2019, 17:53 : Sitting at 55kV for about 4mins when a spark tripped off everything. Will try to bring it back to sit stable at 55kV tomorrow


 

Thursday, July 11, 2019, 10:28 : TM4 up to 54.9kV without too many problems, EZL at 25kV. Will sit here for a little while

Thursday, July 11, 2019, 10:48 : 20mins at 54.9kV, going to 55kV

Thursday, July 11, 2019, 11:14 : 25 mins at 55kV and everything sparked off

Thursday, July 11, 2019, 11:26 : Back up to BIAS / EZL = 54.8kV / 26kV. Checked that the TGHT and TBHT power supplies have not been killed by sparks, everything looks fine.

Thursday, July 11, 2019, 12:56 : Sat at 49.6kV for 1.5hrs with one spark.

Thursday, July 11, 2019, 14:02 : Been sitting at 55kV for 2 hrs now with one spark.


Friday, July 12, 2019, 08:09 : Back up to 52kV easily, then had to reduce step size to 100V to keep going

Friday, July 12, 2019, 08:47 : 56kV

everything sparked off at 56.5 or so

 

Entry  Tuesday, July 09, 2019, 09:15, Carla Babcock, Conditioning Station, Repair, TM4, Dummy HP SIS target, Conditioning TM4 w/ new ST up to 45kV 

Left TM4 at 40kV overnight with no previous heating. There was only one real spark which turned off TP2 but ops turned it back on. Ramping up again.

Tuesday, July 09, 2019, 09:13 : At 45kV the module is sparking on the top pretty regularly. Turned down and David will remove cover and lock out target hall.

Tuesday, July 09, 2019, 16:30 : Went up to 45kV pretty easily now.

Tuesday, July 09, 2019, 16:32 : Everything tripped at 46.5kV. Looks to be a spark outside the vacuum. TM4 sparking much more outside the vacuum than last checks done without the source tray...

Tuesday, July 09, 2019, 16:43 : Everything easy up to 46.8kV, then sparking a bit. Most of the sparks are outside the vacuum. Sitting at BIAS / EZL = 47.1kV / 28kV for a couple mins before ramping down.

Tuesday, July 09, 2019, 16:57 : 10 mins at 47.1kV with not problems. Continuing up still looks like it is really sparking a lot outside the vacuum.

Entry  Monday, July 08, 2019, 14:56, Carla Babcock, Conditioning Station, Repair, TM4, Dummy HP SIS target, First TM4 conditioning with new source tray 

Ramping up TM4 with new source tray in. Current condition: new source tray but no water running in lines B, D or window. Multipin on the source tray grounded but no lines running into the service tray. Vacuum at 1e-6T.

Small sparks at each BIAS voltage increase starting at 30kV. First real spark around 38kV.

Going up in more than 100V steps causes spikes that take out TP2.

Monday, July 08, 2019, 14:54 : TP2 sparked off at BIAS/EZL = 44kV/25.1kV after 10mins at this point... will leave it here for a couple hours

Monday, July 08, 2019, 16:44 : 6 sparks in last 2hrs, some very strange vacuum response in which the pressure rose steadily and stayed high for 30mins before coming back to normal.

Monday, July 08, 2019, 17:25 : After 30mins at 45kV, started sparking, so will ramp down to 40kV and leave it overnight

Entry  Thursday, July 04, 2019, 08:57, Isaac Earle, Safe Module Parking, Development, , , SMP vacuum system installed 20190703_122635.jpg20190703_122646.jpg20190703_122702.jpg

 July 3:

- Assembled exhaust line flexible hose and fittings as per ISK0529 Rev D then leak checked: 1.4E-1 Torr test port pressure, 1.1E-7 atm-cc/s leak rate, no response to helium spray at both ends of flexible line (all vacuum fittings purchased from Kurt Lesker under Requisition #1046936)
- Connected exhaust of SMP vacuum pump to nuclear ventilation duct using flexible hose assembly as per ISK0529 Rev D
- Installed convectron gauges at pump inlet as per ISK0529 Rev D 
- Installed TCS plug block (IRH1646) in SMP
- Connected plug block vacuum port to SMP pump using flexible corrugated hose
- Connected SMP:CG1 to portable pressure display: ~700Torr 
- Turned on SMP:MP1 at 4:17pm, after approximately 25 minutes was down to 75 Torr, at 1hr 40 minutes was 90mTorr, left pumping over night
 
 
July 4:
- Pressure at 4mTorr at 8am, will leave pumping longer to see if it gets any lower
- Submitted Work Request #5239 to PLC Controls for wiring of the pump and convectron gauges and integrations with EPICS
 
20190703_122635.jpg
 
 
20190703_122646.jpg
 
 
20190703_122702.jpg
Entry  Friday, June 21, 2019, 07:16, David Wang, South Hot-Cell, Development, TM4, , TM4 new source tray leak check at SHC. 

New source tray was installed on TM4 yesterday. LD was used to pump down all water lines. Tube heater +D circuit has a big leak  around water block area. At base LR5.5 XE-5 atm.cc/sec, base pressure 170 mtorr, When Chad  moved this helium probe close to  water block area, The leak rate on LD went to maximum level right away. When the probe was moved out of water block area, the LR went back to base level. The test repeated again with same result. Also, Before helium spray test, I applied 80 psi air into the circuit. The air pressure can not be held in the circuit. The pressure drop on the line is quick. This shows a big leak on  D line as well. The rest water lines are fine. I pumped all of them down to LD bottom scale without problem. Chad and I helium sprayed window and MSP water blocks. No leak has been found.  The only line we have problem is the D line.

D line is still leak after repair and installation. We suspected the c-seals issue on this module. So, all water lines have been sprayed with helium for leak check.  Found "B" line target oven negative  is also leak. The rest line are good on helium spray leak check.  The further investigate on thi issue is taken place now.

Entry  Thursday, June 20, 2019, 15:09, Isaac Earle, Safe Module Parking, Development, , , SMP motor wiring inspected by electrician 

The AC wiring for the SMP motor was inspected by Randy Boehm (TRIUMF electrician) as recommended by Franco Mammarella (TRIUMF electrical engineer).  After inspecting the system Randy required the following changes:

  1. AC wiring inside the control panel be increased to 16awg minimum (14awg preferred)
  2. Wiring between the control panel and motor control box be increased to 14awg
  3. Power cable to the motor be increased to 14awg
  4. Current rating for MS connectors be checked and replaced if below 10A
  5. Prefer that motor control box components be relocated to the control panel to reduce number of AC wires and connections (preferred but not mandatory)
  6. A dedicated ground wire is required in the cable going to the motor (if not already in place)

After these changes have been made the inspection will be repeated.

 

July 31, 2019 update:

Items 1, 2, 3, and 6 from above were completed.  14awg wiring was used for wiring inside the control panel (Item 1).  Current rating for the MS connectors was checked and is over 10A (Item 4).  Motor control box components were not relocated to the control panel at this time (Item 5).

Randy repeated his inspection today, and approved of the updated 120V wiring.

Adam updated the SMP electrical and control schematics (IRH1868-1874)

Entry  Friday, June 14, 2019, 08:15, David Wang, ITE, Standard Operation, TM2, , 5 shielding blocks are moved to ITE.  

ITE is configured to take proton beam.

Entry  Thursday, June 13, 2019, 10:55, David Wang, Conditioning Station, Repair, TM4, , TM4 HV test at TCS without source tray. 

I brought up TCS bias to 57.5 KV on TM4 without source tray at TCS. It was kept at this level about 1.0 hours. Some intermediate sparks. No spark trip on devices. 57.5KV is very close to the HV up limit of this module.

Entry  Thursday, June 13, 2019, 09:09, Travis Cave, South Hot-Cell, Standard Operation, TM4, no target and no source tray, Module move 

 TM#4 has been moved from the conditioning station to the south hot cell. The module has no source tray.

Entry  Wednesday, June 12, 2019, 08:56, Carla Babcock, Conditioning Station, Maintenance, TM4, No target, More TM4 conditioning without source tray 

The conditioning station was ramped down overnight and David ramped it back up this morning. Currently trying to get it to sit stable at something higher than 55kV.

 

Wednesday, June 12, 2019, 08:11 : Sitting at BIAS / EL = 53.9 / 28, 2 sparks to ground, one turned off TP2

Wednesday, June 12, 2019, 08:53 : Been at BIAS / EL = 56 / 28 for >10mins with no real sparks. Will continue up.

Wednesday, June 12, 2019, 08:54 : Spark to EL at 56.1

Wednesday, June 12, 2019, 09:34: Sitting at 55kV for 40 mins. 2 sparks to ground, 1 spark to the EL.

Wednesday, June 12, 2019, 09:49 : Leaving it at 56.6 for a while

Wednesday, June 12, 2019, 09:56 : Either there was a spark to IG1S or there is a vacuum limit that does not accept a 1.2e-6T spike. Everything turned off, but everything seems to still be working.

Entry  Monday, June 10, 2019, 18:12, Carla Babcock, Conditioning Station, Maintenance, TM4, No target, Attempt to push bias > 56kV Screenshot_-_06102019_-_06_43_17_PM.png

Monday, June 10, 2019, 16:59 : TM4 back up to BIAS / EL = 56.1kV / 29.5kV

Monday, June 10, 2019, 17:14 : After 57kV on the bias, things seem to be getting sketchy. The EL voltage and current are a bit jumpy and stepping that voltage up seems to produce a slight spike in the bias current.

Monday, June 10, 2019, 17:31 : At BIAS / EL = 58 / 30.3, looks ok.

Monday, June 10, 2019, 18:11 : Sitting at 59.5kV, could probably push further but will sit here for ~30mins and make sure it is relatively stable. Note 59.5kV set point is really 56.9kV on readout.

Monday, June 10, 2019, 18:18 : some current inconsistencies (not really sparks probably corona discharges...) so went down to 59kV

Monday, June 10, 2019, 18:23 : still getting some sparks at 58kV, going down to 57.5.

Monday, June 10, 2019, 18:37 : went back up to 58, spent 10 mins there but was getting these corona-discharge-type-sparks where the vacuum responds and current is drawn but voltage is maintained. Went down to 57kV, still getting them....

Monday, June 10, 2019, 18:40 : Going down to 56 to see if they stop....

Monday, June 10, 2019, 18:42 : Trying 55 kV now... see attached screenshot for example of sparks

Monday, June 10, 2019, 18:48 : No luck at 55 or 54kV. Going down to BIAS / EL = 50 / 27 for a while to see if this resolves

Monday, June 10, 2019, 19:20 : 30 mins at 50kV, a couple little sparks, but no big deal. Ramping up to 55 and let's see if it is ok.

Monday, June 10, 2019, 19:30 : 55 still not working, going down to 54

Monday, June 10, 2019, 20:16 : Held bias at 54kV for about an hour - dropped it down once to alleviate some sparking. Leaving it at 50kV overnight, ops have instructions to keep an eye on it and shut it off if anything seems strange.

Entry  Monday, June 10, 2019, 16:22, Carla Babcock, Conditioning Station, Maintenance, TM4, No target, Ramping V on TM4, no HV cover in TH 

Ramped down the bias so David could remove the HV cover and lock out the target hall.

Ramped back up to BIAS / EL = 50kV / 26kV quickly with no sparks.

Monday, June 10, 2019, 15:35 : BIAS / EL = 52kV / 26kV

Monday, June 10, 2019, 15:45 : BIAS / EL = 54kV / 28.5kV. It seems that keeping the EL at 1/2 the bias voltage is right on the edge of what is acceptable - the HV seems to be sparking to the EL instead of to ground (either that or the EM interference from the sparks it producing a reaction in the EL...) I will run the EL higher and see if that helps.

Monday, June 10, 2019, 15:57 : Sat at 54kV for > 10mins, will continue up

Monday, June 10, 2019, 16:11 : At BIAS / EL = 55.8kV / 29kV got some sparks, some to EL and some to ground. Back at 55kV.

Monday, June 10, 2019, 16:24 : Sitting at 56kV for a couple mins

Monday, June 10, 2019, 16:37 : Sitting at 56.3kV bias, a spark tripped off the IG1S, which tripped the turbo and shut down all the HV. Back to zero!

Entry  Monday, June 10, 2019, 14:13, Travis Cave, Spent Target Vault, Standard Operation, , , Old TM#4 source tray moved 

 The old TM#4 source tray in the south hot cell was moved to the spent target vault. The tray had a low of 7.5mSv/hr to a high of 22.1mSv/hr though a 390 degree rotation.

Entry  Monday, June 10, 2019, 08:26, Carla Babcock, Conditioning Station, Maintenance, TM4, No target, Ramping voltage on TM4 w/o source tray 

TM4 in conditioning station with no source tray, extraction electrode set to HV bias. Brought up to 30kV over the weekend by ISAC ops with no issues.

BIAS=30kV

EL=15kV

IG1=9.4e-7T

 

Monday, June 10, 2019, 08:21 : At 32.4kV on bias, EL at 15kV, bias sparked to EL. Every bump of 100V on bias is accompanied by a small vacuum jump and often by a small current increase from ~60uA to 120uA.

* Conditioning station read back and set values are off by 2kV but archive values show this has always been the case. Which to trust? *

Monday, June 10, 2019, 08:54 : Spark while sitting at 38kV on bias, 19kV on EL. Seems to be a spark to EL.  Sitting at 38kV for ~10mins

Monday, June 10, 2019, 09:32 : Sat at 40kV for ~10mins or so, bumping up again.

Monday, June 10, 2019, 09:38 : Spark to EL while sitting at BIAS / EL = 42kV / 20.5kV

 

Monday, June 10, 2019, 13:57 : Ramped to BIAS / EL = 43 / 21.2. No problems other than what seems to be the usual conditioning station stuff.

 Monday, June 10, 2019, 14:17  : Couple sparks on the way to 48kV, seems to be to the EL.

Monday, June 10, 2019, 14:36 : Up to BIAS/EL = 51/25.5 with no big problems. Will stay here for a couple mins

 

Entry  Friday, June 07, 2019, 13:11, David Wang, Conditioning Station, Development, TM4, , TCS and TM4.  

TM4 has been connected at TCS for HV test. TCS water system and vacuum pumps are switched on.

Entry  Friday, June 07, 2019, 08:56, Travis Cave, Conditioning Station, Standard Operation, TM4, no target, Module move 

 TM#4 has been moved from the south hot cell to the conditioning station.

Entry  Thursday, June 06, 2019, 10:01, Travis Cave, South Hot-Cell, Standard Operation, TM4, no target, no source Tray, Electrical Check TM4_Electrical_Check_No_source_Tray_SHC_June_6_2019.pdf

 Results from the electrical check of TM#4 at the south hot cell with no source tray. R&U are shorted and when meggered A&P have a value of 193k ohms. See attached for details.

Entry  Tuesday, June 04, 2019, 08:46, David Wang, ITE, Standard Operation, TM2, , ITE water signal interlock check. 

ITE water signal interlock check is done. Everything is good. Coil 2   circuit no longer used in ITE . PQRU are looped as one circuit fro coil 1 circuit on Module since now.

Entry  Friday, May 24, 2019, 09:11, Travis Cave, South Hot-Cell, Standard Operation, TM4, no target, Module move 

 TM#4 has been moved from the south west silo to the south hot cell.

Entry  Thursday, May 23, 2019, 11:22, Travis Cave, South Hot-Cell, Maintenance, , , Removing garbage from the south hot cell. 

 A 55 Gal. drum was remotely lowered into the south hot cell. It was then filled with compressable waste. Then the drum was remotely removed from the south hot cell. The drum measured about 20microSv/hr upon removal from the south hot cell.

Entry  Thursday, May 23, 2019, 08:39, Travis Cave, South Hot-Cell, Standard Operation, TM1, no target, Module move 

 TM#1 has been moved from the south hot cell to the northwest silo.

Entry  Wednesday, May 22, 2019, 11:52, David Wang, Conditioning Station, Maintenance, TM1, , TM1 inpsection. 

TM1 shielding plates and their holding bolts are inspected. No corrosion.  TM1 is located at TCS now. Both TP1 and TP2 are started.

Entry  Wednesday, May 22, 2019, 11:50, David Wang, ITE, Standard Operation, TM4, , TM2 has been connected in ITE. Ta58#TM2ITE_2019_June_._Conenction_checklist.pdf

TM2 has been connected in ITE. high active water system and vacuum pumps are started. The pumping down on TM2 and ITE is good  so far.

See attachment for connection checklist.

Entry  Wednesday, May 22, 2019, 08:33, Travis Cave, Conditioning Station, Standard Operation, TM1, no target, Module move 

 TM#1 has been moved from the north west silo to the conditioning station for the day it will be moved back to the silo tomorrow morning.

Entry  Friday, May 17, 2019, 16:46, Adam Newsome, Safe Module Parking, Development, , , SMP Controls Installation Update IMG_20190417_100838.jpgIMG_20190417_100843.jpgIMG_20190517_162230.jpgIMG_20190517_162305.jpg

 

The following controls-related items were installed for the SMP project:

- Cable tray

- Main control panel

- Motor starter box

- Wiring from limit switches and rotation motor to main control panel

- Air fittings at supply (quick disconnect)

- Main air supply hose from supply to control panel (quick disconnect)

- Air tubing from lid control valve at control panel to lid cylinders

 

Air fittings stem off existing air supply lines on the South wall, below a manual shutoff valve. A quick disconnect was installed. When SMP is not in use, manual shutoff valve should be left off.

 

Main control panel and motor starter box were mounted on the North wall. Wire duct runs from the main control panel to the grated floor. Cabling/air runs underneath the mezzanine platform, along existing and new cable tray, to the SMP.

 

Cable tray was installed on the South wall, from the corner to the SMP module. A cutout was made to accommodate for existing tubing. An additional ~1 ft. of tray will be added to the end, near the corner, at a future time.

 

Remainder of installation work to be done before commissioning:

- Mount and install new Opto-22 module
- Chain new Opto-22 module to existing one (power, comms) below mezzanine on North wall

Entry  Friday, May 17, 2019, 10:47, Travis Cave, ITE, Standard Operation, TM2, Ta#58, Module move 

 TM#2 with Ta#58 has been moved from the south hot cell to the east target station.

Entry  Thursday, May 16, 2019, 14:35, Travis Cave, South Hot-Cell, Standard Operation, TM2, Ta#58, Electrical Check Ta#58_TM2_SHC_electrical_chk_May_16_2019.pdfElectrical_Chk_TM2_no_target_May_15_2019_SHC.pdf

 Results of the electrical check of TM#2 without target and with the new Ta#58 target.

Entry  Thursday, May 16, 2019, 12:31, chad fisher, South Hot-Cell, Standard Operation, TM2, Ta#58, Ta #58 installed 

Ta #58 has been installed onto TM2. All new silver plated high current fasteners. All torqued to 130 in lbs.

Entry  Wednesday, May 15, 2019, 16:06, Isaac Earle, Safe Module Parking, Development, , , SMP module support flange installed and leak checked 20190515_094730.jpg20190515_094740.jpg20190515_103253.jpg20190515_103824.jpg

The SMP module support flange sub-assembly (IRH1755) was installed today according to drawing IRH1683.  Dow Corning 111 sealing compound was used to keep the o-ring adhered to the lower groove during transportation and installation.  The TCS shield plug (IRH1646) was then installed on the SMP module flange which has vacuum connections for leak checking.  Vacuum was pulled on the SMP vessel using the Varian 979 leak detector.  After approximately 3.5 hours of pumping the test port pressure was at 2.4E-2 Torr and leak rate was 7.9E-8atm*cc/s.  Helium was configured with the regulator set at 10psi and flow rate of >10 bubbles per second in Windex and then applied slowly around the perimeter of the vacuum flange (IRH1686) and it's mating components on both  the top and the bottom.  There was no response on the leak detector indicating the seals on both sides of the module flange are leak tight.

 

20190515_094730.jpg

 

20190515_094740.jpg

 

20190515_103253.jpg

 

20190515_103824.jpg

 

 

 

 

 

Entry  Monday, May 13, 2019, 11:22, David Wang, ITW, Repair, , , ITW entrance module has been connnected. 

Entrance module has been connected back to ITW. Everything is normal.

Entry  Monday, May 13, 2019, 09:55, Travis Cave, ITW, Standard Operation, , , Entrance module move 

 The West Entrance module has been moved from the south hot cell to the west target station.

Entry  Friday, May 10, 2019, 10:23, chad fisher, South Hot-Cell, Repair, , , West Entrance module wire scanner replacement 20190509_085908.jpg20190510_101235.jpg

West entrance module - visible broken or disconnected wire visible on old/existing wire scanner. Wire scanner removed, new one installed.

Entry  Wednesday, May 08, 2019, 10:29, Travis Cave, South Hot-Cell, Standard Operation, , , Entrance module move 

 The entrance module has been moved from the west station to the south hot cell.

Entry  Thursday, May 02, 2019, 09:37, Travis Cave, Spent Target Vault, Standard Operation, , UC#26, Spent Target Move Target_Index_2019-05-02.pdf

 The spent UC#26 target was moved from the south hot cell to the spent target vault. It was place in pail #209 and put in spot 1A in the vault and was 2.42mSv/hr upon removal from the south hot cell.

Entry  Wednesday, May 01, 2019, 10:45, Travis Cave, South Hot-Cell, Standard Operation, TM4, no target, Electrical Check TM4_elec_chk_no_tgt_shc_may_1_2019.pdf

 Electrical check of the TM#4 with no target attached at the south hot cell before being moved to the south west silo.

Entry  Wednesday, May 01, 2019, 09:34, Travis Cave, South Hot-Cell, Standard Operation, TM4, no target, Module move 

 TM#4 has now been moved to the south west silo.

Entry  Wednesday, May 01, 2019, 07:49, chad fisher, South Hot-Cell, Standard Operation, TM4, UC#26, UC#26 removal 20190501_072940[1].jpg

UC#26 has been removed from TM4.

Entry  Tuesday, April 30, 2019, 11:19, Travis Cave, South Hot-Cell, Standard Operation, TM4, UC#26, Electrical Check Elec_CHk_UC26_SHC_post_beam.pdf

 Electrical check of TM#4 with UC#26 post beam at the south hot cell. See attached.

Entry  Tuesday, April 30, 2019, 08:59, Travis Cave, South Hot-Cell, Standard Operation, TM4, UC#26, Module move 

 TM#4 with UC#26 has been moved from ITE to the south hot cell.

Entry  Monday, April 29, 2019, 09:32, Travis Cave, Spent Target Vault, Standard Operation, , SiC#31,32 and UC#19,20,21, Spent targets moved to mini vault. 

 The following targets have been moved from the spent target vault to the mini vault:

#127 - SiC#31 (front)

#132 - SiC#32 

#145 - UC#19

#150 - UC#20

#159 - UC#21 (back) 

Entry  Monday, April 29, 2019, 07:56, chad fisher, South Hot-Cell, Development, , , Pail transfers 20190425_133750.jpg20190425_134106.jpg

Two pail transfers took place April 25th.

Ta#47 transfered from pail 137 to pail 201. existing plastic bag from 137 showed many areas of typical age/rad damage related failure.

 

Ta#45 in pail 124 was transfered to pail 202. Pail 124 also contained the shutter and "roof mounted" img gauge from TM2 that were removed in 2015 in addition to a bunch of fasteners, heat shrink tubing (from lock lever rings from an previous methods of spent target packaging) etc. The original plastic bag in pail 124 had completely failed and shredded and flaky. The shutter and extraction electrode from Ta#47 were put in pail 202 with Ta#45...cabling of the shutter being completely intertwined with the target.

Entry  Thursday, April 18, 2019, 10:04, Travis Cave, South Hot-Cell, Maintenance, , Ta#50, SiC#34, Ta#46, Ta#47, and Ta#45, Target transfer from old pail to new pail. 

 Targets Ta#50 and SiC#34 have been transferred from their old pails to new ones. Ta#50 was done on April 12th 2019 it was moved from pail #148 to pail #200 and a new field measurement was done and found to be 3.57mSv/hr. SiC#34 was done on April 18th 2019 it was moved from pail #143 to pail # 206 and a new field measurement was done and found to be 2.20mSv/hr. Both measurements were done by the RAM that is mounted at the south hot cell.

 

April 24 2019

Target Ta#46 has now been transferred to a new pail with a number 207 from pail 143 it was 3.62 mSv/hr when removed from the south hot cell.

 

April 25 2019

Target Ta#47 has now been transferred to a new pail with a number 201 from pail 137 it was 2.25mSv/hr when removed from the south hot cell. The bag that the target was in has shown signs of degradation.

Target Ta#45 has now been transferred to a new pail with a number 202 from pail 124 it was 1.45mSv/hr when removed from the south hot cell. The bag that the target was in was destroyed. Also in the pail was a shutter, IMG Gauge, some altem parts, wire and bolts.

The extraction electrode from Ta#47 was added to this pail as it was left behind from last transfer.

Entry  Wednesday, April 17, 2019, 12:03, chad fisher, South Hot-Cell, Repair, , , Manipulator repair 

Broken handle cable of east manipulator has been replaced and manipulator is operational again.

Entry  Friday, April 12, 2019, 11:44, chad fisher, South Hot-Cell, Standard Operation, , , Pail transfer 

Pail transfer was undertaken in the south hot cell. went very well except near the end the master tong cable of the right hand manipulator broke. Not entirely a surprise due to the amount of use it has seen lately.

Entry  Friday, April 05, 2019, 13:44, chad fisher, Spent Target Vault, Development, , , 2019 Pail drop tests 
  • Drop test performed January 8, 2019 with 25 lb target, UN pail and lug cover. Drop failed. Lug cover half removed. Pictures and video in docushare collection 24626.
  • Second test January8, 2019 UN pail, "new" dish cover, old lock lever ring, 25 lb target. Single drop from 1.2m onto latch, no sealant. No leaks 24 hours later. Pictures in docushare collection 24626

 

  • Drop test performed April 2, 2019 repeat of previous test using until that was loaded in north hot cell test. Target punctured can. Pictures in docushare collection 24626.

 

  • Drop test performed April 5, 2019 repeat of previous test with the addition of a aluminum sleeve (0.05" thick) inside the pail between pail and target.

New UN rated pail with 9.55 kg target, 1.2 kg 16 gauge Al sleeve (10.75 OD x 14.75" tall), 3 liters of water with red food coloring no sealant on gasket.

First drop standard drop test from 1.2m onto latch

Second drop test 1.2m onto bottom of pail

Third drop 1.2m onto side of pail

Drops 4-6 1.2m onto lid

Pail was left inverted for an hour after the first three drops with no leaks after 1 hour.

No leaks after the remaining 3 drops .Bottom very damaged suggesting need for protective disc in bottom of pail.

Pictures can be found in docushare Collection-24627

 

  • Drop tests performed May 2, 2019 with 9.7 kg target, 1.346 kg of mixed module and target components, sleeve and disc. First drop on latch from 1.2m, no leak, second drop straight on bottom from 1.2m, no leak, third drop on side from 1.2m leak. Drop test described in more detail in document drop test witness document on docushare. Pictures and video in docushare collection 24626.

 

 

 

Entry  Thursday, April 04, 2019, 14:49, Isaac Earle, Safe Module Parking, Development, , , SMP vacuum vessel support roller friction check CRR_check_for_as-built_SMP_-_April_4_2019.pdf

With the SMP vacuum vessel now installed inside the shield box, a test was performed to measure the torque required to rotate the vessel.  At a moment arm distance of 2.0m a force of 89N was required to rotate the vessel (with no module installed) resulting in a torque of 178Nm.  Based on this, the coefficient of rolling resistance (CRR) was calculated to be 0.007;  This is fairly close to available data for similar applications such as cast iron wheels on steel rail (https://en.wikipedia.org/wiki/Rolling_resistance).  The CRR used for design of the SMP drivetrain was 0.054 which was based on empirical data for a similar product.  Because this is significantly higher than the friction of the as-built system the drive-train components are stronger than required and should have no problem rotating the vessel when loaded with a module.

Further details and calculations included in the attached PDF.

Entry  Monday, April 01, 2019, 14:56, Isaac Earle, Safe Module Parking, Development, , , SMP shield box and vacuum vessel installed in final location 20190401_101459.jpg20190401_110433.jpg20190401_144133.jpg20190401_110353.jpg

 Last week drilling of the additional required holes in the SMP shield box was completed in the Target Hall.  This morning the shield box (IRH1675) was moved to its final installation position in the silo area on the B2 level.  The vacuum vessel (IRH1806) was then installed inside the shield box.  The center of the vacuum vessel is 2-3" north of the south travel limit of the crane.  Photos as well as measurements of the final position are attached below.

 

20190401_101459.jpg

 

20190401_110353.jpg

 

20190401_110433.jpg

 

20190401_144133.jpg

 

 

Entry  Thursday, March 28, 2019, 10:27, David Wang, Conditioning Station, Repair, TM2, dummy febiad test target, TM2 new source tray helium pressure test at TCS. 

Helium pressure test on TM2 all water circuits is done. 70 psi helium , 10 minutes test time. Leak detector :base leak rate 0.0XE-9 atm.cc/sec, base pressure 0.0Xe-4torr. No any response on LD during the test. All TM2 water circuit are leak free.

    Reply  Thursday, March 28, 2019, 12:48, Anders Mjos, Conditioning Station, Repair, TM2, dummy febiad test target, TM2 new source tray helium pressure test at TCS. 

David Wang wrote:

Helium pressure test on TM2 all water circuits is done. 70 psi helium , 10 minutes test time. Leak detector :base leak rate 0.0XE-9 atm.cc/sec, base pressure 0.0Xe-4torr. No any response on LD during the test. All TM2 water circuit are leak free.

 Thursday, March 28, 2019, 12:40: Found valve to expansion tank TCS:TK2 to be closed. Opened valve. This allow air to escape out of the system and the water system is running as expected again


Friday, March 29, 2019, 11:15: Changed EE to conditioning mode

Friday, March 29, 2019, 11:35: BIAS / EZL 20 / 10 kV

Friday, March 29, 2019, 13:47: BIAS / EZL: 25 / 12.5 kV

Friday, March 29, 2019, 16:09: BIAS / EZL: 30  / 15 kV

Friday, March 29, 2019, 17:23: No sparks for >60 min

Friday, March 29, 2019, 17:26: BIAS / EZL off


Monday, April 01, 2019, 08:13: BIAS / EZL: 30  / 15 kV

Monday, April 01, 2019, 08:33 BIAS / EZL: 35  / 17.5 kV

Monday, April 01, 2019, 09:00: Sparking at about 37.5 kV BIAS. Lowered below 20 kV to stop. Now sparking at around 20 kV

Monday, April 01, 2019, 10:00: BIAS/EZL 22 / 20 kV. Occasional sparking on BIAS as voltage is increased.

Monday, April 01, 2019, 10:05: Change of strategy. Will heat target to bake out the vacuum before continuing with HV conditioning.

Monday, April 01, 2019, 10:43:

BIAS / EZL / EE: 15 / 7.5 / 1.5 kV
COIL / ANODE: 10 A / 200 V
Ramping TGHT / TBHT at 1 A/min. Good/bad vacuum (IG2): 1E-6 / 2E-6 Torr

Monday, April 01, 2019, 19:16: TGHT / TBHT: 500 / 270 A. Vacuum increasing. IG1/2 1.2E-7 / 1.4E-6 Torr


Monday, April 08, 2019, 09:28: BIAS / EZL: 20 / 10 kV (some periods of multiple sparks)

Monday, April 08, 2019, 10:28: BIAS / EZL: 30 / 15 kV (some periods of multiple sparks)

Monday, April 08, 2019, 11:24: 3 sparks for the last 60 min

Monday, April 08, 2019, 14:43: BIAS / EZ: 40 / 20 kV (after two periods of sparking around 39 kV requiring voltage to be reduced below 30 kV to recover)

Monday, April 08, 2019, 15:57: Two sparks in 70 min


Tuesday, April 09, 2019, 12:40: BIAS / EZL 40 / 20 kV with >90 min without sparking

Tuesday, April 09, 2019, 16:00: BIAS / EZL 48 / 24 kV

Tuesday, April 09, 2019, 16:07: Sparking tripped TPs and IG1S, then power supplies.


Tuesday, April 16, 2019, 16:41: BIAS / EZL 50 / 25 kV for 1 hour without sparking.


Wednesday, April 17, 2019, 15:23 : Continued without problems to 50 kV earlier, but sparks tripped off vacuum just above 50kV. Continue later.

Entry  Tuesday, March 26, 2019, 11:17, Travis Cave, South Hot-Cell, Standard Operation, TM2, no target, Electrical Checks of TM#2 during the source tray change. Elecrictal_Check_TM#2_Old_source_Tray_Jan_11_2019.pdfElectrical_Check_TM#2_No_Source_Tray_Feb_25_2019.pdfElectrical_Check_TM#_New_source_Tray_Mar_22_2019.pdfElectrical_Check_TM#2_new_source_tray_Mar_25_2019.pdf

 The four electrical check done on TM#2 during the source tray change.

Entry  Tuesday, March 26, 2019, 11:10, Travis Cave, Conditioning Station, Standard Operation, TM2, Dummy Target, Electrical Check Electrical_Check_TM2_Dummy__Target_CS_Mar-26-2019.pdf

 Electrical Check of TM#2 with the dummy target attached.

Entry  Tuesday, March 26, 2019, 09:32, Travis Cave, Conditioning Station, Standard Operation, TM2, Dummy Target, Module move 

 TM#2 with a new source tray and the dummy target has been moved from the south hot cell to the conditioning station.

Entry  Monday, March 25, 2019, 10:11, Aaron Schmidt, South Hot-Cell, Repair, TM2, , LP-FEBIAD Test Target (empty)  TM2_-_FEBIAD_target_-_Electrical_Test.pdf

Link to previous target information: https://elog.triumf.ca/TIS/RH-ISAC/1039

Monday, March 25, 2019, 10:00: Target electrical checks (See Attachment 1)

Tested for TM2 

Entry  Thursday, March 21, 2019, 09:56, chad fisher, South Hot-Cell, Repair, TM2, , Tray insertion 20190321_091833.jpg20190321_094625.jpg

This morning new water block fasteners and gas line capture nut fasteners were inserted into the hot cell. Window waterline blank off was removed from TM2, surfaces inspected and given a polish with Veltex (30 seconds, 70 psi) as there was a small bit of c seal residue. Transfer try with new source tray has been latched to the module.

Entry  Wednesday, March 20, 2019, 11:19, Travis Cave, South Hot-Cell, Standard Operation, TM2, no target, Module move 

 TM#2 has been moved from the conditioning station to the south hot cell.

Entry  Monday, March 18, 2019, 07:25, David Wang, Conditioning Station, Maintenance, TM3, , TCS vacuum pumps have been stopped. 

 The TCS will be vented soon for TM2 move.

Entry  Monday, March 18, 2019, 07:23, David Wang, Conditioning Station, Repair, TM2, , TM2 window line helium test 

New seals with a blank off cap are installed on TM2 window line water block.   The seals are checked at TCS with 70 psi helium for 5 minutes with LD at 0.0xE-9atm/cc.sec. No response on LD during test. Seals are good.

Entry  Friday, March 15, 2019, 08:51, Travis Cave, Conditioning Station, Standard Operation, TM2, no target, Module move 

 TM#2 has been moved from the south hot cell to the conditioning station.

Entry  Thursday, March 14, 2019, 10:25, chad fisher, South Hot-Cell, Repair, TM2, , Water Block Polishing status Blocks_final_polished.jpg

Phase 2 (intermediate) and Phase 3 (Final) polishing is complete on all water blocks on TM2 (minus ground electrode circuit which has only had a cursory cleaning). Phase 2 with 2000 grit wet sand paper and isopropynol for 1 minute with tool at 75 psi, Phase 3 with Veltex polishing cloth for 1 minute with tool at 75 psi.

Entry  Tuesday, March 12, 2019, 09:13, chad fisher, South Hot-Cell, Repair, TM2, , Water Block Polishing status Blocks_Stage_1_Polish.jpg

Stage 1 polish has been achieved on all single seal water blocks using the single pad tool run at 75 psi, 2 3 minute cycles per block using red scotch brite.

Entry  Monday, March 11, 2019, 14:34, chad fisher, South Hot-Cell, Repair, TM2, , Water Block Polishing status 

Stage 1 polishing (water scale and at least 99% of visual indium removed) has been achieved on all 2 seal water blocks that will be used (Ground electrode has not been polished). Process required 3-4 3minute cycles of the tool using scotch brite pads with the tool running at approximately 75 psi.

Entry  Friday, March 08, 2019, 14:10, chad fisher, South Hot-Cell, Repair, TM2, , Water block polishing B_after_SB_(2).jpg

After trials with 2000 grid wet paper I have moved up to "red" scotch brite. This seems to have worked the best so far although it took two minutes to remove the ring that the other materials could not remove (see picture).

I have moved to next circuit. Currently at 3 minutes and 30 seconds with scotch brite but significant ring remains.

Entry  Thursday, March 07, 2019, 13:59, chad fisher, South Hot-Cell, Repair, TM2, , Polishing 

Polishing of the water block sealing surfaces has commenced. First attempt was on block B with low nap brown polishing pad (the least aggressive pad prepared) and isopropyl for 30 seconds. This cleaned a little but did not remove the "ring" which I believe is water scale. I will step up to 2000 grit wet sand paper and iso next.

Entry  Thursday, March 07, 2019, 12:20, chad fisher, South Hot-Cell, Repair, TM2, , Pre-polishing pictures 

Pictures of the water blocks before polishing can be found on docushare, collection 24400

Entry  Thursday, March 07, 2019, 12:02, chad fisher, South Hot-Cell, Repair, TM2, , Box Off water block jig on 20190307_113548.jpg

The containment box has been removed from TM2 and the water block jig installed in preparation for water block polishing.

Entry  Thursday, March 07, 2019, 09:12, David Wang, Conditioning Station, Standard Operation, TM2, , TM2 move from TCS to SHC. 

TM2 has been moved from TCS to SHC. The move is smooth.

Entry  Tuesday, March 05, 2019, 14:29, chad fisher, South Hot-Cell, Repair, , , Tray Transfer Fixture Repair Complete 20190305_130312.jpg20190305_132303.jpg20190305_133800.jpg20190305_141346.jpg

Repair of the tray transfer fixture is complete (minus testing).

A distorted ball nut lock plate was replaced and thread loc added. to the ball nut/plate assembly. Testing will take place tomorrow once the thread lock has a chance to cure.

Entry  Tuesday, March 05, 2019, 09:38, chad fisher, South Hot-Cell, Repair, , , Transfer Fixture Repair 20190305_092228.jpg20190305_092231.jpg20190305_092326.jpg20190305_092558.jpg

Transfer fixture has been remotely disassembled to the point where the ball nut lock plate assembly can be inserted into the tool port and the plate replaced by hand in the tool port without having to enter the hot cell. Straight head screws will be replaced with SHCS to facilitate easier re-assembly and future disassembly.

Entry  Tuesday, March 05, 2019, 07:20, David Wang, Conditioning Station, Repair, TM2, , TM2 HV test at TCS 

Spark between HV cover vertical mesh plate and HS 60KV  bias connecting clamp 90degree angle at 55 KV on TM2 top. HV cover is removed to test above  55KV. The spark triggered TH and SHC ventilation secondary alarm.

Entry  Friday, March 01, 2019, 10:23, Travis Cave, Spent Target Vault, Standard Operation, , , Source tray moved 

 The old TM#2 source tray and TM#4 optics tray have been removed from the vault and placed into the spent target storage on tray 9 which is meant for source trays.

Entry  Friday, March 01, 2019, 09:57, chad fisher, South Hot-Cell, Repair, TM2, , TM2 Source tray removal 20190228_095131.jpg20190228_143718.jpg20190301_074849.jpg20190301_092907.jpg

TM4 optics tray was installed onto the old TM2 source tray yesterday and tray filled with non-active metal scrap. Tray inserted into transfer frame 95% yesterday. During insertion the ball nut of the transfer jig became unfastened from its drive plate. This will have to be fixed before the jig can be used reliably again however we were able to finish the job...the transfer jig is 20 years old now so it is not entirely suprising that it needs some attention.

Today the Tm2 tray final install into the transport tray occurred by driving the tray drive screw and bringing the tray into the transfer frame the last inch 1/2 or so. "Feet" (ITA2380) had to be removed from sliding tray assembly to fit in the box however upon attempting this is was immediately clear that one of the screws was stuck and must have been cross threaded during assembly. As as result the entire drive bracket (ITA2375) had to be removed form the source tray to allow final insertion into the box.

11 handles from spent target transfers, 1 plastic bin box, Ta LP test target TRI coil, 1 aluminum box, sockets and extensions from spent target transfers and 5 obsolete legs from previous source tray replacements were amoung the items disposed of with the spent source tray.

Entry  Friday, March 01, 2019, 08:42, Anders Mjos, Conditioning Station, Standard Operation, TM2, , Conditioning TM2 without source tray TM2_BIAS_current_vs_voltage_2019-03.xlsxTM2_HV_Conditioning_2019-03-01.docx

BIAS and EZL connected. No water flowing into the module (water looped on top of module)

Friday, March 01, 2019, 08:20: 10kV

Friday, March 01, 2019, 08:40: 20kV

Friday, March 01, 2019, 08:57: 30kV

Friday, March 01, 2019, 11:00: 40kV

Friday, March 01, 2019, 15:23: 50kV


Monday, March 04, 2019, 08:50: 50kV

Monday, March 04, 2019, 09:22: 52.5kV

Monday, March 04, 2019, 10:01: Spark tripped TPs at 54kV

Monday, March 04, 2019, 10:04: 50kV

Monday, March 04, 2019, 10:14: Multiple sparks at 54kV. Lowered to 30kV to stop.

Monday, March 04, 2019, 10:15: 40kV

Monday, March 04, 2019, 10:16: Sparking at 42kV. Lowered to 40kV

Monday, March 04, 2019, 10:19: 42kV

Monday, March 04, 2019, 10:48: 50kV

Monday, March 04, 2019, 11:11: 52.5kV

Monday, March 04, 2019, 11:25: 54kV

Monday, March 04, 2019, 11:50: 55kV

Monday, March 04, 2019, 13:33: 3 sparks observed for the last 1.5h

Removed HV cover to avoid sparking between F/T and cover.

Monday, March 04, 2019, 14:02:20kV

Monday, March 04, 2019, 14:06: 50kV

 Monday, March 04, 2019, 14:12: 55kV

Monday, March 04, 2019, 14:20: Multiple sparks at 56kV. Lowered to 30kV to stop.

Monday, March 04, 2019, 14:27: 40kV

Monday, March 04, 2019, 14:29: 50kV

Monday, March 04, 2019, 14:32: 55kV

Monday, March 04, 2019, 14:40: 56kV

Monday, March 04, 2019, 14:55: Multiple sparks at 57kV. Lowered to 30kV to stop

Monday, March 04, 2019, 15:01: 55kV

Monday, March 04, 2019, 15:36: 57kV

Monday, March 04, 2019, 15:51: 57.5kV

Monday, March 04, 2019, 16:30: ~1 spark in 0.5h, somewhat unstable current (see attached Word file)

Monday, March 04, 2019, 16:30: HV off

Entry  Tuesday, February 26, 2019, 10:33, Travis Cave, Conditioning Station, Standard Operation, TM2, no target, Module move 

 TM#2 with no source tray has been moved from the south hot cell to the conditioning station.

Entry  Tuesday, February 26, 2019, 08:51, chad fisher, South Hot-Cell, Repair, TM2, , TM2 containment box 

The containment box has been reinstalled onto TM2 in prepatation for testing in the conditioning station.

Entry  Monday, February 25, 2019, 09:44, chad fisher, South Hot-Cell, Repair, TM2, , Water block jig 

module side water block jig has been removed in preparation for electrical checks.

Entry  Friday, February 22, 2019, 10:31, chad fisher, South Hot-Cell, Repair, TM2, , TM2 Source tray removal 6x

The source tray has been removed from TM2.

Entry  Thursday, February 21, 2019, 15:10, Isaac Earle, Safe Module Parking, Development, , , Seismic requirements for SMP 

Dragan Mitrovic, TRIUMF structural engineer, was consulted earlier this week regarding seismic requirements for the SMP assembly.  Installation location, overall dimensions, total weight, and the center of mass for assembly IRH1670 were provided to him by e-mail.  On Feb 20th he communicated verbally that he had analyzed the assembly for seismic loads, and concluded that this equipment does not require anchoring or any other form of seismic restraint.

Update (May 30, 2019): Confirmed with Dragan that the approach he used for analysis was that specified in the BC Building Code (both 2012 edition and updated 2018 edition).

Entry  Wednesday, February 20, 2019, 09:07, chad fisher, South Hot-Cell, Repair, TM2, , Module side waterblock jig 

I have installed the module side water block jig.

Entry  Tuesday, February 19, 2019, 11:56, chad fisher, South Hot-Cell, Repair, TM2, , Optics tray removal 

Aaron has removed the optics tray in TM2 in preparation for source tray removal.

Entry  Tuesday, February 19, 2019, 10:20, chad fisher, South Hot-Cell, Repair, TM2, , Containment box removed 

Containment box has been removed from TM2 in preparation for source tray removal. I will walk Aaron through removal of the optics tray today also.

Entry  Friday, February 15, 2019, 12:09, David Wang, ITE, Maintenance, TM4, , ITE water system maintenance. 

The ITE water system maintenance job is done. Changed all paddle wheels and coils on ITE flow sensors. All using water poly-tubes in ITE are replaced .  Started high active water pump, and checked ITE water signals. They are good. No leak has been found on  replaced tubes and related fittings.

Entry  Friday, February 15, 2019, 12:05, David Wang, ITE, Maintenance, TM4, , ITE annual vacuum leak check.  

Helium pressure test on all water lines: 70psi , 3 minutes. HS has a quick response to 9Xe-9atm.cc/sec for 20 seconds. No response on other lines. All water lines are good. Air to vacuum  leack check on ITE and TM4: TM4 IG1 / Steers side panel has a low E-6 atm.cc/sec leak. The o-ring need to be changed when TM4 is located at TCS. All other air to vacuum seals are good on both primary and secondary vacuum vessel.

Entry  Thursday, February 14, 2019, 14:02, Travis Cave, South Hot-Cell, Standard Operation, TM2, no target, Module move 

 TM#2 has been moved from the conditioning station to the south hot cell.

Entry  Thursday, February 14, 2019, 07:13, David Wang, Conditioning Station, Standard Operation, TM2, , TCS vacuum pumps have been stopped. 

Preparation on TM2 move from TCS to SHC.

Entry  Monday, February 11, 2019, 10:26, Isaac Earle, Safe Module Parking, Development, , , SMP shield box and vacuum vessel moved to Target Hall 6x

  On February 8th the SMP shield box (IRH1675) and the vacuum vessel (IRH1806) were both raised from a horizontal to vertical orientation in the ISAC-1 Experimental Hall.  Hamilton "Mini-Mite" S-MM2-43FS caster wheels were then installed on the base of the shield box and it was lowered down the hatch to the B2 level.  The vacuum vessel was then lowered into the shield box, supported by the rollers, as designed.  The shield box and vessel combination were then moved south along the steel plated floor until positioned under the hatch leading to the Target Hall.  Movement along the floor was achieved by pushing the back of the vessel with an electric fork truck and pulling from the front with a cable winch attached to a plate mounted in the floor in the SHC service area, centered east/west between the Ante Room doors.  The fork truck alone was sufficient to move the assembly on the smooth section of the plates, but the winch was needed on the section paitned with textured grit.  The vacuum vessel was then lifted into the Target Hall and placed in a temporary storage location in the silo area.  The shield box was then lifted, casters removed, and then lifted up into the Target Hall.  It was a very tight fit with the tubing which has been installed on the SHC and NHC ducting for the new flow meters, but the move was completed without causing damage.  The shield box was placed on the B2 level in the Target Hall where some final tapped holes will be added on the exterior before moving to the final installation location.

 

 

Entry  Thursday, January 31, 2019, 14:16, Isaac Earle, North Hot-Cell, Development, , , NHC grounding approval NHC_grounding.pdf

 Franco Mammarella was consulted regarding electrical grounding of the NHC design (RS103 of Document-131915).  After discussing the design, and having grounding inspected by Randy Boehm, Franco approved the design and advised that the grounding system should be inspected periodically.  This task has been added to the Remote Handling inspection index on an annual schedule.  A PDF copy of the e-mail correspondence with Franco is attached.

Entry  Monday, January 28, 2019, 10:41, David Wang, Conditioning Station, Repair, TM2, , TM2 water lines helium pressure test at TCS 

leak detector base LR: 0.0Xe-9atm.cc/sec. helium 70 psi. test time : 3 minutes for each circuit.The results in atm.cc/sec are Ta+(A):1.8  XE-8. TA-(B):0.0xE-9. Tu-(C):1.2XE-7. TU+(D):1.6XE-7. Coil 2 (PQ):0.0XE-9. Coil 1 (RU):0.0XE-9. MSP:2.2XE-7. EE:1.0XE-7. HS:N/A. Window:5.8XE-9

Entry  Thursday, January 24, 2019, 10:34, David Wang, ITW, Maintenance, , , Changed 24VDC plugs of TP solenoid valves in ITW 

3 damaged 24VDC plugs of TP solenoid valves are replaced. Inspected other plugs. All of them are in good condition now.

Entry  Tuesday, January 22, 2019, 09:56, David Wang, ITW, Maintenance, TM2, , ITW water system maintenance. 

ITW water system maintenance is done. All working paddle wheels and coils are replaced. ITW water system polyurethane tubes are replaced as well. Two 3/8" leak small valves on return lines are replaced. 85 liters of tritium water are transferred from storage tank to B2 level holding tank. LALC water are refilled into S-tank. Restarted pump and checked system. Everything works fine now. No water leak has been found so far.  

Entry  Monday, January 21, 2019, 16:27, Isaac Earle, North Hot-Cell, Development, , , NHC in-cell camera wired to right side monitor 20190121_154407.jpg

 The NHC right side monitor has been wired to display the signal from the in-cell camera.  This was tested using a snake camera on both of the CPC-4 connectors.

20190121_154407.jpg

Entry  Friday, January 18, 2019, 10:26, Isaac Earle, North Hot-Cell, Development, , , NHC sealing improvements and repeat of RH test for LED lights 

The following NHC development work was completed under WP I2019-01-09-4:

  • Location of RH feature on operator level LED lighting updated to match IRH1800 Rev B design
  • Remote Handling test of the LED fixtures was repeated using a 9' pole with hook attachment through the manipulator slave hatch from the Target Hall: both LED fixtures were removed and reinstalled successfully with relative ease
  • Tool port seal replaced to address an audible air leak: the 1/4" foam seal was removed and replaced with adhesive backed 5/8" wide hollow foam rubber seal (McMaster Carr PN: 93085K81). Prior to the change DPG4 was at 0.63"wc, after the change wit was 0.73"wc with all system variables constant.
  • NHC manipulator access block seal was replaced, likewise to address an audible air leak: the 1/4" foam seal was removed and replaced with adhesive backed 1/2" thick BunA-N rubber strip (McMaster Carr PN: 9023K85).  DPG4 was at 0.94"wc prior to the change, and 1.07"wc after with all system variables constant
Entry  Monday, January 14, 2019, 07:07, David Wang, Conditioning Station, Maintenance, TM2, , Restarted TCS vacuum system . 

No issue.

Entry  Friday, January 11, 2019, 13:59, Isaac Earle, Safe Module Parking, Development, , , SMP motor selection decision 

SMP drivetrain design work is currently underway.  Alejandro has selected a suitable 1200:1 reducer which will give a vessel rotation speed of 0.21rpm with a 1725rpm motor (deemed sufficiently close to the SHC rotation speed of 0.17rpm).  The reducer however is only rated for 0.33hp, and Allon's analysis recommended we use a motor of at least 0.4hp

 
From his calculations the expected power required to turn the loaded vessel is 0.2hp (see Document-161943, p3).  The higher figure of 0.4hp in his final recommendations comes from the power rating of a 40 tooth sprocket (the driver sprocket) with a No. 50 roller chain operating at 10rpm (the lowest speed shown on the table) - meaning this driver sprocket arrangement can handle up to 0.4hp.  We discussed this on the phone on January 4th and agreed that a 1/3hp motor could be used which will match the reducer Alejandro selected, and will supply sufficient power given that calculations indicate only 0.2hp is required.
 
Once the vessel is installed in the shield box a test will be performed to determine the actual torque (and power) required to turn the vessel.  If the value differs significantly from the calculated value the design will be revisited.
Entry  Friday, January 11, 2019, 13:17, David Wang, Conditioning Station, Standard Operation, TM2, , TCS and TM2 vacuum system are switched off for this Sunday power outage.  

I will restart all pumps Monday morning.  

Entry  Friday, January 11, 2019, 11:26, Travis Cave, Spent Target Vault, Standard Operation, , UC#25, Spent Target Move Target_Index_2019-01-11.pdf

 The spent target in the south hot cell has been moved to the spent target vault. It was placed in pail 204 and placed in spot 6B. The pail is made of thicker steel and thus will not need to be repackaged later.  The ISAC spent target vault is full there is no more room for any more targets.

Entry  Thursday, January 10, 2019, 10:45, David Wang, Conditioning Station, Standard Operation, TM2, , TM2 is under vacum at TCS. 

TCS: TP1, TP2 and TP1S are started.

Entry  Thursday, January 10, 2019, 09:26, Travis Cave, Conditioning Station, Standard Operation, TM2, no target, Module move 

 TM#2 has been moved from the south hot cell to the conditioning station.

Entry  Wednesday, January 09, 2019, 13:29, David Wang, ITW, Repair, , , ITH:MP1 

ITH: MP1 has been replaced due to its poor performance.  Its motor and power cable are taken out and reused on new pump. Vacuum group assembled them together, and installed the new pump. The new pump works fine.

Entry  Wednesday, January 09, 2019, 13:08, Travis Cave, South Hot-Cell, Standard Operation, TM2, UC#25, Electrical Check Electrical_Chk_TM#2_UC#25_post_beam_Jan-09-2019.pdf

 Electrical check of the target module with the UC#25 attached after the beam run.

Entry  Wednesday, January 09, 2019, 10:47, Travis Cave, South Hot-Cell, Standard Operation, TM2, UC#25, Module move 

 TM#4 with UC#25 has been moved from ITW to the south hot cell.

Entry  Wednesday, January 09, 2019, 06:26, David Wang, Conditioning Station, Standard Operation, , , TCS vacuum pumps have been stopped. 

The tCS will be vented soon for TM2 move later this week.

Entry  Tuesday, January 08, 2019, 08:49, David Wang, ITW, Standard Operation, TM2, , TP1 TP1 have been disconnected in ITW 

Started argon venting of ITW now.

Entry  Friday, January 04, 2019, 14:38, Isaac Earle, North Hot-Cell, Development, , , NHC cameras tested NHC_flange_East_and_West_views.JPGNHC_flange_North_and_South_views.JPGCamera_view_through_operator_viewing_window.JPG

The NHC module support flange cameras (4 total) as well as the NHCSA camera were tested today and confirmed to be working properly.  All cameras were angled and focused properly, and displaying clearly on the monitors in the ISAC RH Control Room.  Photos of the control room monitors are attached below.

 

NHC_flange_East_and_West_views.JPG

 

NHC_flange_North_and_South_views.JPG

 

 Camera_view_through_operator_viewing_window.JPG

Entry  Friday, January 04, 2019, 08:48, David Wang, ITW, Standard Operation, TM2, , TM2 has been disconnected in ITW. UCx25_TM2_disconnection_checklist.pdf

TP1, TP2 are still connected for next week leak check. All water lines in TM2 are purged with 80 psi air, each for 5 minutes.

TP1 and TP2 had been disconnected. TM2 with UCx 25  disconnection checklist, See attachment.

Entry  Thursday, January 03, 2019, 13:41, David Wang, Crane, Repair, , , Target hall crane PLC issue. 

Target hall crane did not work properly after power outage during Christmas time. The only movement could be operated is crane rotation. Power is supplied crane. The control board on N-S, E-W and up-down movement showed  F51 error code which is tripped limit.. All these clues pointed to a PLC control problem.  Don dale was asked for help. He used the crane control PLC program on an old computer  in RH control room reset the PLC system. Everything works fine after his reset.

Entry  Thursday, January 03, 2019, 13:30, David Wang, ITW, Repair, , , ITH:MP1 

ITH:MP1 inlet pressure showed 10torr after power outage during holiday. All ITE/W turbo-pumps were tripped because of it. Removed one shielding block above the vacuum station. Visually checked oil level  and condition in pump. oil level is high. oil color is dark. no oil  leak .  Installed a local convectron gauge on pump inlet. After pumping down, It shows pump is good.  Tightened  all KF 25 and 50 clamps on pump inlet side. Reconnected pump to system. Everything works fine so far. All ITW / E turbo pumps are started now.

Entry  Wednesday, January 02, 2019, 10:26, Anders Mjos, Conditioning Station, Standard Operation, , , Restarrted TP1S 

Found pumps off after the holidays. Restarted roughing pump and TP1S

Entry  Wednesday, December 19, 2018, 14:41, Anders Mjos, Conditioning Station, Standard Operation, , No target, Installed Shield Block on TCS 

Frank and Anders installed lid on TCS and started vacuum system yesterday. To run over the Holidays. Retrieved dose badge from operational storage area. Measured field to be ~ 10 mSv/h at ~9am. Beam went off about 8:30am.

Entry  Tuesday, December 18, 2018, 11:13, Isaac Earle, North Hot-Cell, Development, , , NHC manipulator slave-end swap, RH test, and various other work 

The following North Hot Cell work was completed over the last week under work permit I2018-12-12-1:


 

Thurs Dec 13th:

  • Prepared master side according to removal manual (noticed screwing in the right side locking screw was not as smooth to go in as normal; left side was smooth like normal)
  • Removed manipulator roof block and set down in yellow frame (required some stacked wood to prevent light from bottoming out)
  • Removed steel side plates in NHC manipulator hatch
  • Removed the slave end (SN: 9764) – noticed “Right Elevation/Twist Coupler” off of vertical by around 30 degrees
  • Wrist elevation of removed slave end was not locked, lifted it slightly and this brought the coupler to the vertical position and it locked with a click
  • Suspected the thru-tube also would be misaligned, confirmed by inspecting visually in hot cell (Unsure why this misalignment occurred considering we followed the removal procedure properly.  One theory is that when we accidentally left the timing screw in the master side handle cable drum last time it may have caused things to get a little out of alignment)

 

Friday Dec 14th:

  • Un-did the right side locking screw on the master
  • Then could turn coupler on the thru-tube to the vertical position from within the hot cell
  • Re-locked the right side locking screw (this time it went in smoothly)
  • With all couplers on thru-tube vertical we then installed the replacement slave (SN: 9352) as per instructions
  • For future slave end changes should use some sort of long chain or sling instead of having the auxiliary crane hook block within the hatch (some sort of T-hook type lift feature replacing the bail may work better as well)
  • Evaluated the manipulator: seemed to be working normally, Chad tested plugged in LED lamp plug and also opened and closed the work table hatch
  • Noticed Z motion tape on slave end loose when fully extended in Z (nice and tight when retracted) – this seems to be normal
  • Confirmed manipulators can reach all surfaces of the table
  • Then tested remote handling of LED light fixtures from the Target Hall using pole tools through the manipulator roof hatch
    • Started with both LED light plugs un-plugged
    • Used 9’ standard beam lines RH pole tool (this worked fine, but 10-12’ would be better)
    • Curved hook end attachment
    • First lifted cables out of all cable tray sections (the wall mounted Panduit)
    • Then removed the East light fixture assembly (IRH1800) - lifted from designated lift loop (IRH1796) – This went smoothly
    • Hoisted up into the Target Hall, then lowered back down to re-install
    • To reinstall had to hook the assembly at a lower point due to flex of the pole from the weight of the assembly (hooked just below the ballast for installation).  Using this method reinstalling the fixture went smoothly.  I will update the design to move the designated lift point (or add an additional one) at this location.
    • Once the light fixture was on the bracket, replaced the cables in the cable tray using the pole tool.  The final section on the east wall before the outlets was a little tricky, but by viewing and reaching from the north-west corner of the hatch it was do-able
    • Confirmed visually that remote removal and installation of the west fixture can be done using the same procedure as the east
  • Replaced lamp block (stored lifting hardware for hatch side plates above block, below hatch cover)

  

Monday Dec 17th:

  • Left side slave-end boot was installed as per manual instructions.  It was done with two people inside the cell this time which went much smoother than just one last time (the boot was not installed on the slave prior to moving it into the hot cell because we wanted to inspect the tape and cables after installation and the boot would prevent that)
  • The condition of both boots was checked. Both appear to be in new condition with no signs of degradation.  The material seems pliable and strong.
  • Chad Fisher, ISAC Hot Cell Operator, checked the light level from the cold side of the hot cell and confirmed that it is acceptable.  However, without the operator level LED lighting it was too dim.

 

 Tuesday Dec 18th:

  • Lift bails for both manipulator slave ends set to farthest north position which results in face that mates with thru-tube to be close to vertical when hanging from lift bail
  • Work table, stairs, entrance floor area, pre-filter assembly, tool port, window cover, and hot side service connection panel vacuumed and wet wiped to remove dirt and dust.
  • NHC inlet damper (located in Target Hall) adjusted to set NHC depression to around 1.05”wc (the NHC damper is currently not responding to the NVCS and needs to be investigated and repaired by Controls Group and/or Mechanical Services)

 

Entry  Tuesday, December 11, 2018, 14:35, Anders Mjos, ITE, Standard Operation, TM4, UC#26, Block move 

Blocks were moved from ITW to ITE by Frank and David. ITE water flow to dump was re-opened (ITW remains open). A dose badge was installed in the operation storage area. Dose rates were measured to ~10 mSv/h at 1pm. Beam went off approximately 8:30am (with a short period of 2uA ending at 11am).

Entry  Monday, December 10, 2018, 15:31, Isaac Earle, North Hot-Cell, Development, , , NHC remote connection testing with manipulators 

 The following tests have been successfully completed using the NHC manipulators:

  • Ventilation pre-filter (mounted on the NHC/TCS partition wall) removed and re-installed using the manipulators
  • Electrical plugs (two total) for operator-level LED lighting located on east wall of cell interior plugged in, and un-plugged using the manipulators
  • Electrical plug inserted into and removed from each of the 120V outlets (four total) located in front of the viewing window using the manipulators
  • All diagnostic service connections removed and reinstalled using the manipulators (six total, see IRH1765)
  • All Staubli air and gas connections removed and reinstalled using the manipulators (five total, see IRH1749)

 

These tests were performed at various different times over the last several months by Isaac Earle and/or Chad Fisher.

Entry  Friday, December 07, 2018, 10:37, chad fisher, North Hot-Cell, Repair, , , Ariel connector test 

Completed testing of connectors for Ariel using the north hot cell.

Video can be found on docushare; document 161909

Entry  Friday, December 07, 2018, 08:47, chad fisher, North Hot-Cell, Repair, , , North hot cell spare slave repair 20181207_083906.jpg

The tong cable on the spare north hot cell slave has been repaired. Slave came from the factory with the tong cables straddling one of the pulleys they are suppose to run through.

 

 

Entry  Tuesday, December 04, 2018, 12:36, David Wang, ITE, Standard Operation, TM4, UCx 26., TM4 has been connected in ITE/ Checklist. UCx26_TM4_connection_checklist.pdf

TM4 has been connected in ITE. See attachment for connection checklist

Entry  Tuesday, December 04, 2018, 10:26, Travis Cave, ITE, Standard Operation, TM4, UC#26, Module move 

 TM#4 with UC#26 has been moved from the conditioning station to the east target station.

Entry  Friday, November 30, 2018, 10:28, Travis Cave, Spent Target Vault, Standard Operation, , Ta#57, Spent Target Move Target_Index_2018-11-30.pdf

 The spent Ta#57 target has been moved from the south hot cell to the spent target storage it was placed in pail 174 and placed in spot 8C in the vault. See attached PDF for details.

Entry  Thursday, November 29, 2018, 06:38, David Wang, South Hot-Cell, Standard Operation, TM4, , Leak check TM4 UCx 26 at SHC. 

Chad and I did a leak check on TM4 HS line with UCx 26# installed . Base LR 0.0X E-9 atm.cc/sec. Base pressure 0.0XE-4 torr.  No response on leak detector during leak check.

Entry  Wednesday, November 28, 2018, 13:38, Travis Cave, Conditioning Station, Standard Operation, TM4, UC#26, Module move 

 TM#4 with UC#26 has been moved from the south hot cell to the conditioning station.

Entry  Wednesday, November 28, 2018, 11:31, Travis Cave, South Hot-Cell, Standard Operation, TM4, Ta#57 and UC#26, Electrical Check Elec_Chk_Ta57_Post_Beam_SHC_11-28-28.pdfElec_Chk_TM4_no_tgt_SHC_11-28-18.pdfElec_Chk_UC26_SHC_11-28-18.pdfElec_Chk_UC26_IGLIS_part_SHC_11-28-18.pdf

 Electrical check of TM#4 with the old Ta#57, no target and with new IG-LIS UC#26 target. See attached PDF for details.

Entry  Wednesday, November 28, 2018, 07:04, David Wang, ITE, Development, TM4, LpTa 56, New high current flexible cables inspection after LpTa#56 beam run. new_flexibble_cable_in_ITE_after_Ta#56_run_001.JPGnew_flexibble_cable_in_ITE_after_Ta#56_run_004.JPG

Inspected new high current flexible cables during TM4 disconnection. The new cables and adapters work fine.

Entry  Wednesday, November 28, 2018, 06:39, David Wang, Conditioning Station, Standard Operation, , , Disconnection checklist LpTa #56 LpTa#56_disconnection_checklist.pdf

TM4 was disconnected in ITE. Checklist list in attachment.

Entry  Tuesday, November 27, 2018, 13:31, chad fisher, South Hot-Cell, Standard Operation, TM4, Ta#57, Ta#57 removal 

Ta#57 has been removed from TM4.

Entry  Tuesday, November 27, 2018, 11:05, Travis Cave, South Hot-Cell, Standard Operation, TM4, Ta#57, Module move 

 TM#4 with Ta#57 has been moved from the east target station to the south hot cell.

Entry  Monday, November 26, 2018, 12:19, chad fisher, North Hot-Cell, Repair, , , East Manipulator 20181126_113326.jpg20181126_113338.jpg

In preparation for removing the slave for replacement I discovered that the timing screw in the handle cable drum (master side) had been left threaded into the pulley...it should have been completely removed. It was bent from hitting on a casting inside the mater arm which most likely contributed to the hopped pulleys on the slave side. After removing this timing screw I entered the north hot cell and replaced the hopped cable back onto its pulley and Isaac tested the motions that previous caused the hopped cables. These tasks were repeated 4 times without any issues. Also of note is a missing setscrew in the tong cable pulley pin and a somewhat loose tape on the slave, also the tape shows signs of a crimp/bend. Upon further inspection and comparison with the other slaves I also found that one of the "lock-down" fittings tying the Z motion tape drum to the corresponding gear is completely missing. See pictures attached.

Entry  Thursday, November 22, 2018, 14:38, Isaac Earle, North Hot-Cell, Development, , , NHC design approved by High Voltage Engineer NHCHV.pdf

To satisfy RS 101 from the NHC requirements specification (Document-131915) Tomislav Hurskovec was consulted regarding high voltage safety.  After a verbal discussion on various aspects of the NHC design he confirmed that the design satisfies high voltage safety concerns.

A copy of his confirmation e-mail is attached in PDF format.

 

Entry  Thursday, November 22, 2018, 08:55, Anders Mjos, ITW, Repair, TM2, UC#25, ITW:FC5 safety signal limit switch installed FC5_limit_switch.jpg

Yesterday Diagnostics group installed a temporary external limit switch to provide the in signal to the safety system.

Entry  Thursday, November 22, 2018, 08:53, Anders Mjos, ITW, Standard Operation, TM2, UC#25, Block move 

Frank and Anders moved blocks from ITE to ITW yesterday

Entry  Thursday, November 22, 2018, 08:52, Anders Mjos, ITE, Standard Operation, TM4, Ta#57, Closed ITE dump water 

Paddle wheel signal was tripping proton beam in ITW. Valved off ITE dump to divert flow to ITW. Field around valve was about 600 uSv/h

Entry  Wednesday, November 14, 2018, 16:10, Anders Mjos, ITW, Repair, TM2, UC#25, ITW:FC5 safety signal troubleshooting 2018-11-13_FC5.pdf

Measured resistance on safety limit switches for FC5 on Exit Module 2. Determined that the in connected signal did not work (shows not connected irregardless of FC position). Confirmed proper operation of the OUT limit. See attachment for details. The Harp 5 x and y signal connectors were checked and reconnected.

Entry  Thursday, November 08, 2018, 09:27, chad fisher, South Hot-Cell, Maintenance, , , South East Manipulator cable replacement 

The handle cable on the east manipulator of the south hot cell has been replaced. Old cable showed signs of wear but had no broken strands. Manipulator is back together but still needs to be re-tensioned.

Entry  Wednesday, November 07, 2018, 09:50, Anders Mjos, ITW, Standard Operation, TM2, UC#25, TM2 connected in ITW 

TM2 was connected yesterday by Frank and Anders. The West side panel with IG1S on Exit Module 2 was replaced with a new SST panel with 1 CF flange only (dwg). Link to check list on DocuShare.

Entry  Tuesday, November 06, 2018, 10:59, Travis Cave, ITW, Standard Operation, TM2, UC#25, Module move 

 TM#2 with UC#25 has been moved from the conditioning station to the west target station.

Entry  Monday, November 05, 2018, 14:27, Anders Mjos, Conditioning Station, Standard Operation, TM2, UC#25, Target module disconnected 

Frank and Anders disconnected the water and electrical connections this afternoon after the target was conditioned over the weekend. The heater ramping program ran with the wrong gauge selected, causing the vacuum to go higher than planned. The module will be moved to ITW tomorrow.

Entry  Monday, November 05, 2018, 08:24, Travis Cave, Spent Target Vault, Standard Operation, , nSiC#1, Spent Target Move Target_Index_2018-11-02.pdf

 The spent nSiC#1 target has been moved from the south hot cell to the spent target vault. It was placed in pail #172 and placed in spot 7B. See attached PDF for vault details.

Entry  Thursday, November 01, 2018, 11:42, David Wang, Conditioning Station, Standard Operation, TM2, UCx 25., TM2 HS line helium pressure test at TCS and helium spray at SHC.. 

Chad and I did  leak check on TM2 HS line at SHC yesterday. Base LR 0.0XE-9 atm.cc/sec.   No response on LD. during helium spray.   Today , I did helium pressure test at TCS. base LR 0.0xe-9atm.cc/sec. applied 70psi helium for 3 minute. leak rate slowly climbed to2.2 Xe-7 atm.cc/sec ate stopped there.  The result is close to before.

Entry  Wednesday, October 31, 2018, 14:23, Travis Cave, South Hot-Cell, Standard Operation, TM2, nSiC#1 and UC#25, Electrical Check Electrical_Chk__TM#2_nSiC#1_SHC_Post_Beam_Oct-31-2018.pdfElectrical_Chk_TM#2_UC#25_SHC_Oct-31-2018.pdf

 TM#2 with targets nSiC#1 (old target) and UC#25 (new target) electrical check results. See attached for details.

Entry  Wednesday, October 31, 2018, 14:20, Travis Cave, Conditioning Station, Standard Operation, TM2, UC#25, Module move 
TM#2 with UC#25 has been moved from the south hot cell to the conditioning station.
Entry  Tuesday, October 30, 2018, 10:50, Travis Cave, ITW, Standard Operation, TM2, nSiC#1, Modules moved 

 Modules were moved, ITW EX2 was moved from the conditioning station to the west target station and TM#2 ,with nSiC#1,  was moved from the west target station to the south hot cell.

Entry  Monday, October 29, 2018, 10:43, David Wang, Conditioning Station, Repair, , , ITW exit 2 leak check at TCS. 

I did a leak check this morning on exit 2 module at TCS. LD base  leak rate is 4.00XE-9atm.cc/sec, Base pressure is 0.00 X E-4 torr. All seals, bellows, and flanges are checked. The new FC5 bellow is good. There is a big leak up to 2X E-6 atm.c/sec has been found on IG1S side panel . The panel itself  will be replaced this time. Machine shop is working on it.. Two small leaks in E-9  atm.cc/sec range have been found on the  o-ring between service cap steel welding frame and the whole cap top cover plate in different location . All bolts on the top plate pressing down the o-ring are very tight. I can do nothing on them. However, I sprayed some vacuum seal around the leak area. The leaks are small  and close to ITE TP1S. I don not think we have to replace it at this moment.  Basically, The module is good to move to ITW tomorrow morning. 

Entry  Friday, October 26, 2018, 09:44, Travis Cave, Conditioning Station, Standard Operation, , , Exit Module moved 
The west exit #2 module has been moved from the south hot cell to the conditioning station.
Entry  Thursday, October 25, 2018, 11:03, chad fisher, South Hot-Cell, Repair, , , Exit 2 West 8x

Actuator arms, lemos, lemos and banana plug block have been disconnected in preparation for raising of the service tray. Aaron has pictures

Entry  Tuesday, October 23, 2018, 11:32, David Wang, South Hot-Cell, Maintenance, , , ITW RV4S leak check. 

ITW RV4S (A and B) are leak checked. They are good. 

Entry  Tuesday, October 23, 2018, 10:53, chad fisher, South Hot-Cell, Repair, , , Exit 2 East 20181023_104541.jpg

Cover 1 was removed from the exit module. Confirmed with David that the actuator rod that needed to be disconnected was the far left )as viewed by the hot cell operator). The fastener for this rod was un-accessible from this side. Cover 1 was re-installed (two bolts left loose) and cover 2 was removed. fastener holding the actuator together was removed and luckily it does have a remote start.

Entry  Tuesday, October 23, 2018, 10:45, David Wang, ITW, Standard Operation, TM2, SiC nano, TM2 was disconnected in ITW. TM2_SiC_nano_disconnection_in_ITW.pdf

TM2(SiC nano) has been disconnected in ITW. See attachment

Entry  Monday, October 22, 2018, 14:05, Travis Cave, ITW, Repair, , , Module move 

 ITW Exit #2 has been moved from the west station to the south hot cell for a bellows repair.

Entry  Wednesday, October 10, 2018, 10:50, Travis Cave, Conditioning Station, Standard Operation, TM4, Ta#57, Electrical Check TM#4_UC#24_Electrical_Check_SHC.pdfTM#4_Elec_Chk_No_Target_Oct-3-2018.pdfTM#4_Elec_Chk_SHC_Ta#57.pdf

 The various electrical check done on TM#4 after the UC run and before the start of the Ta run.

Entry  Wednesday, October 10, 2018, 07:52, David Wang, ITE, Standard Operation, TM4, Ta#57, TM4 has been connected in ITE. TM4_with_TA#56_connection_in_ITE.pdf

TM4 has been connected in ITE. see attachment.

Entry  Tuesday, October 09, 2018, 13:46, Travis Cave, ITE, Standard Operation, TM4, Ta#57, Module move 

 TM#4 with Ta#57 has been moved from the conditioning station to the east target station.

Entry  Tuesday, October 09, 2018, 12:32, David Wang, Conditioning Station, Repair, TM4, , TM4 steers 4 pin feedthrough CF flange 

TM4 Steers 4 pin feedthrough CF flange is replaced due an inside feed through insulator broken. CF 25 cooper seal is replaced with a new one as well. Travis did anelectrical check. after replacement. Everything looks fine.

 

Note only a megger check was performed on the affected steering lines. Open load was measured on all lines. (Travis Cave)

Entry  Friday, October 05, 2018, 14:41, Travis Cave, Spent Target Vault, Standard Operation, , UC#24, Spent Target Move Target_Index_2018-10-05.pdf

 UC#24 has been moved from the south hot cell to the spent target vault. The target is in pail #171 and placed in spot 4C. See attached PDF for details.

Entry  Wednesday, October 03, 2018, 14:16, David Wang, South Hot-Cell, Standard Operation, TM4, Ta #57, Leak check TM4 Lp Ta# 57 at SHC. 

Tried to leak check TM4 Ta57# at TCS. LD failed to pump down properly at fine range. It always tripped at 4 torr. I cheeked all vacuum lines seals and adapters on top of module to LD. Everything is good. Chad said the VCRs at SHC can not be tightened any more. Discussed with Anders, we decide to move module TCS and helium pressure test there.  The same difficult happened last time on TM4 UCx24# at SHC when leak check. But,it is solved by pressurize the line at SHC last time.  

The HS line was pressurized with 70 psi helium on Oct 04th at TCS.. LD 0,00X E-9atm.cc/sec no change in 2 minutes. No leak.

Entry  Tuesday, October 02, 2018, 09:59, Travis Cave, South Hot-Cell, Standard Operation, TM4, UC#24, Module move 

 TM#4 with UC#24 has been moved from the east target station to the south hot cell.

Entry  Tuesday, October 02, 2018, 09:49, David Wang, ITE, Standard Operation, TM4, UCx 24#, TM4 was disconnected in ITE. TM2_UCx_24#_disconnection_in_ITE..pdf

TM4 was disconnected in ITE yesterday. See attachment for checklist.

Entry  Thursday, September 27, 2018, 13:58, Travis Cave, Conditioning Station, Standard Operation, TM3, no target, Module move 

 TM#3 has been moved from the conditioning station to the centre east silo. This will be its new home after the silo switcher-roo.

Entry  Wednesday, September 26, 2018, 07:14, David Wang, Conditioning Station, Repair, TM3, , TM3 HV test at TCS. 

I did a HV test on TM3 at TCS yesterday. HV Ramp up speed: 1KV per 5 minutes when below 30KV,1KV per 10 minutes from 30-36KV. There is no major spark below36 KV .  I could see  lots small and big vacuum response on IG1 and PNG2 when conditioning from 30-36 KV, especially when closing to 36 KV.  However, At 36.4 KV, There is a big continuous spark occurred. It could not be stopped until I lowed the HV to 14KV. I have to ramp up from 14 KV again.  This behavior on TM3 HV test is same as before we saw. The module can not pass 36KV at present condition.  During the test., EL is tied to 60KV bias. The HV cover on TM3 top is installed. And, Service tray  cover plate is installed on TM3.

Entry  Tuesday, September 25, 2018, 08:48, chad fisher, South Hot-Cell, Maintenance, , , Window leak and torque hot_cell_window_gasket_change_procedure.pdf

The south hot cell window has been found to be leaking oil. Upon inspection yesterday I found that the bolts compressing the gasket on the cold side were "loose". I have re-torqued them to the specification provided by the manufacturer in the attached procedure.

Entry  Tuesday, September 25, 2018, 08:01, chad fisher, South Hot-Cell, Standard Operation, TM2, nSiC#1, nSiC#1 install 20180919_132304.jpg20180919_143535.jpg

On September 18th installation of nSiC#1 was attempted on TM2. As usual, new fasteners were tested previous to insertion into hot cell and employed during installation. the last fastener to be installed was for the circuit D block. The fastener/air ratchet stalled immediately indicating a problem. The fastener was removed and a an attempt was made trying a new spare fastener. That fastener also jammed right away but could not be removed or installed any further.

 

A breaker bar was employed to achieve more torque and the fastener was able to be loosened, although it would not come completely out, dangling and wobbling like it was free. A claw type bar was used to add slight pressure to the fastener while it was loosened allowing the fastener to undo the rest of the way.

Target was removed and discovered that that insulator supporting circuit c and d blocks was quite broken and that a few chunks had fallen off. It was also notice that boefore the breaker bar had been employed that a piece of ceramic was on the table suggesting that the ceramic had been at least partially broken at the time of removal of the previous target. Also, the threads of the insert for circuit d showed damage an swarf.

Swarf was vacuum claned out of the circuit d thread insert and a machine tap ran through the insert twice.

nSiC#1 was reinstalled with new waterline gaskets and new c and d circuit fasteners with a little bit of the first 2-3 threads lightly coated with vacuum grease.

High current fasteners torqued to 130 in lbs.

Entry  Tuesday, September 25, 2018, 07:54, David Wang, Conditioning Station, Repair, TM3, , TM3 is connected for HV test at TCS. 

water loops are by passed on top. All bias, EE, and  EL are tied together. Started water system.

Entry  Monday, September 24, 2018, 14:50, Travis Cave, Spent Target Vault, Standard Operation, , UC#23, Spent Target Move 

 The spent UC#23 target has been moved from the south hot cell to the spent target storage. It was placed in pail #170 and place in spot #4B in the vault.

Entry  Monday, September 24, 2018, 10:21, Anders Mjos, South Hot-Cell, Standard Operation, TM2, UC#23, Post Irradiation Examination (PIE) 20180924_161322929_iOS.jpg

UC#23 experienced short between target and heat shield as it was heated during operation. The inspection of the target after irradiation revealed that the left target leg was close to the heat shield opening and likely the cause of the short. Marks could be seen on the leg indicating contact. See attached photo. More photos are available on DocuShare

Entry  Friday, September 21, 2018, 10:07, David Wang, ITW, Standard Operation, TM2, SiC nano, TM2 with SiC nano target was has been connected in ITW. TM2_with_SiC_nano_connection_in_ITW..pdf

Tm2 with SiC nano has been connected in ITW. See attachment for checklist

Entry  Friday, September 21, 2018, 10:06, David Wang, ITW, Standard Operation, TM2, UCx23, TM2 was disconnected in ITW. TM2_UCx_23#_disconnection_in_ITW..pdf

TM2 was disconnected in ITW this Tuesday. See attachment for checklist.

Entry  Thursday, September 20, 2018, 14:36, Travis Cave, ITW, Standard Operation, TM2, nSiC#1, Module move 

 TM#2 with nSiC#1 has been moved from the south hot cell to the west target station.

Entry  Thursday, September 20, 2018, 14:35, Travis Cave, South Hot-Cell, Standard Operation, TM2, nSiC#1, Electrical Check Electrical_Chk_TM2_SHC_nSiC#1_Sept-20-2018.pdf

 TM#2 with the nSiC#1 target had its check done on it at the south hot cell see attached for results.

Entry  Thursday, September 20, 2018, 08:36, Travis Cave, South Hot-Cell, Standard Operation, TM2, no target, Electrical Check Electrical_Chk_TM2_no_tgt_Sept-20-2018.pdf

 Results of the electrical check on TM#2 with no target after Chad cleaned out the bolt hole on the module where the target mounts.

Entry  Tuesday, September 18, 2018, 12:59, Travis Cave, South Hot-Cell, Standard Operation, TM2, UC#23, Module move 

 TM#2 with UC#23 has been moved from ITW to the south hot cell. The shield plug was also installed remotely as well.

Entry  Friday, September 14, 2018, 09:39, Travis Cave, Conditioning Station, Standard Operation, TM3, no target, Module move 

 TM#3 with no target has been moved from the north east silo to the conditioning station.

Entry  Thursday, September 13, 2018, 16:57, Isaac Earle, North Hot-Cell, Development, , , NHC grounding and mili-ohm testing 

 The following equipment has been connected to the building ground located in the Target Hall by the TCS using 1/2" flat bonding strap:

  • NHC roof structure
  • NHC/TCS partition wall
  • NHC work table

The following equipment has been connected to the building ground by connecting to the work table inside the NHC using 1/2" flat bonding strap:

  • Air and gas supply line mounting bracket inside NHC
  • Receptacle box mounting bracket inside NHC
  • Diagnostic signal box mounting bracket inside NHC

 

The resistance between the following locations and the copper grounding plate located at the base of the NHCSA north wall were measured.  The resistance of the wire used was 258.10mΩ, and has been subtracted from the following results.

Measurements taken in NHCSA:

  • Control panel below viewing window (base plate of box): 4.67mΩ
  • Oil window frame (bare metal drain valve): 55.34mΩ
  • Left manipulator (ground plate near e-stop button): 73.46mΩ
  • Right manipulator (ground plate near e-stop button): 202.58mΩ
  • Air and gas supply line mounting bracket: 40.68mΩ
  • Diagnostic connector box: 12.15mΩ
  • Steel conduit for 110V supply to hot cell interior: 4.81mΩ

Measurements taken inside NHC:

  • Work table: 4.51mΩ
  • Pre-filter bolted to partition wall: 4.84mΩ
  • Table hatch lid: open load
  • Left manipulator thru tube: 515.8mΩ
  • Right manipulator thru tube: 342.0mΩ
  • Left manipulator (slave boot plate bolt): 885.9mΩ
  • Right manipulator (slave boot plate bolt): 1444.0mΩ
  • Grounding strap for air/gas plate: 4.84mΩ
  • Outside of SHV connector on diagnostic signal box: 4.56mΩ
  • Exterior of 110V electrical conduit: 3.88mΩ
  • Male Staubli connector for 1st gas line: 53.7mΩ
  • Welded stud for window cover panel: 6.06mΩ
  • Grounding strap for partition wall: 4.39mΩ
  • Roof structure (measured inside un-painted bolt hole): ~0mΩ
  • Stainless steel module flange: ~0mΩ

Dedicated grounding will be added in the near future for the oil window frame and the manipulator thru-tubes.  Testing will then be repeated for those items.

 

Dec 18, 2018 update:

The oil window frame and both manipulators (where they bolt to the thru-tubes) were connected to the building ground using 1/2" flat bonding strap connected at the cold side of each piece of equipment, and running to the grounded copper sheet located in the NHC service area at floor level.  The connection is made inside the electrical racks located directly west of the NHC operator area on the cold side.  This work was done by Travis Cave in October 2018.

Mili-ohm testing for these items has not yet been repeated.

 

Jan 14, 2019 update:

Grounding was added from the metal plate near the e-stop button on the master arm of both manipulators.  The same 1/2" flat bonding strap was used which was tied into other bonding strap which runns to the grounded copper sheet in the NHCSA.

Mili-ohm testing was repeated for the following items:

  • Oil window frame (bare metal drain valve):  13.6mΩ
  • Left manipulator (ground plate near e-stop button):  16.1mΩ
  • Right manipulator (ground plate near e-stop button):  16.5mΩ

 

Entry  Wednesday, September 12, 2018, 15:30, Isaac Earle, North Hot-Cell, Development, , , Installation of NHC operator-level lighting completed LEDs_and_manipulators.jpgLEDs.jpgcords.jpg

 Installation of of operator-level lighting in the NHC was completed today according to drawing IRH1801.  2" x 2" Panduit was mounted to the wall on aluminum brackets to support the power cables.  These lights can be replaced remotely by unplugging the power cords using the manipulators, lifting the cable out of the Panduit with a hooked pole tool through the manipulator slave end removal roof hatch, lifting the light fixture off the support bracket with the pole tool, then installing a new fixture in the opposite order.  This RH procedure will be tested at a later date as part of NHC commissioning.

 

 LEDs_and_manipulators.jpg

 

LEDs.jpg

 

cords.jpg

Entry  Wednesday, September 12, 2018, 15:22, Isaac Earle, North Hot-Cell, Development, , , NHC air and gas supply lines - test and leak check 

Testing was completed today on the NHC air and gas supply lines.  For each line a Staubli plug was installed on the fitting inside the hot cell, the line was charged with compressed air (50psi for gas lines #1, #2, and #3;  100psi for the air lines #4 and #5).  All connections inside and outside the cell were checked for leaks using Snoop including connections for the solenoid valves.  No leaks were found.  Correct operation of the solenoids was confirmed as well as correct plumbing (no lines crossed).

Entry  Friday, September 07, 2018, 10:55, David Wang, ITE, Standard Operation, TM4, UCx 24#, TM4 has been connected to ITE/ Checklist TM4_UCx_24#__connection_check_list.pdf

TM4 has been connected to ITE on Sep 04th. See attachment  for checklist.

Entry  Friday, September 07, 2018, 10:47, David Wang, ITE, Repair, TM4, UCx24, TM4 TP2 replacement 

TM4 TP2 could not be started  after module was connected back to ITE on Sep 04th. It was replaced with a new pump on Sep 05th. The new pump works fine.

Entry  Thursday, September 06, 2018, 10:25, Travis Cave, Spent Target Vault, Standard Operation, , SiC#34, Ta#45,46,47, 50, Spent Target Move 

 Targets SiC#34 , Ta#45,46,47,50 have been moved from the spent target vault to the mini vault.

Entry  Tuesday, September 04, 2018, 09:57, Travis Cave, Conditioning Station, Standard Operation, TM4, UC#24, Module move 

 TM#4 with UC#24 has been moved from the conditioning station to the east target station.

Entry  Tuesday, September 04, 2018, 08:18, David Wang, Conditioning Station, Standard Operation, TM4, UCx 24#, Stppped TM4 and TCS vacuum and water system at TCS. 

I stopped TM4 and TCS vacuum system at TCS. TCS and TM4 is venting with argon now.

Entry  Thursday, August 30, 2018, 14:16, Travis Cave, South Hot-Cell, Standard Operation, TM4, Ta#56, UC#24, and no target, Electrical Check TM#4_Ta#56_Electrical_Check_Post_Beam_at_SHC.pdfTM#4_No_Target_Electrical_Check_Aug-29-2018.pdfTM#4_UC#24_Electrical_Check_SHC.pdf

 Results of the electrical check with the spent Ta#56 attached, no target attached and the UC#24 attached. These test were performed on TM#4.

Entry  Thursday, August 30, 2018, 11:13, Travis Cave, Spent Target Vault, Standard Operation, , Ta#56, Spent Target Move Target_Index_2018-08-30.pdf

 Ta#56 has been moved from the south hot cell to the storage vault. It was placed in pail#169 and place in slot 2C of the vault. Also the vault is now full with 24 spent targets and can no longer accept any new targets. See the attached PDF for further details.

Entry  Thursday, August 30, 2018, 07:46, David Wang, Conditioning Station, Standard Operation, TM4, , TM4 HS line leak check at TCS and SHC. 

Chad and I leak checked TM4 HS line after UCx 24 is installed. No leak at 5xE-9atm.cc/sec.  Today, I did helium pressure test on HS line at TCS. No leak at 70 psi helium 0.0xE-9 atm.cc/sec.

Entry  Thursday, August 30, 2018, 07:42, David Wang, Conditioning Station, Standard Operation, TM4, , TM4 has been connected to TCS. 

TM4 has been connected to TCS. vacuum system and water system are started. Everything looks fine.

Entry  Tuesday, August 28, 2018, 14:19, David Wang, ITE, Standard Operation, TM4, Ta#56, TM4 Ta#56 disconenction. TM4_Ta#56_disconnection..pdf

TM4 has been disconnected in ITE this morning. See attachment.

Entry  Tuesday, August 28, 2018, 10:53, Travis Cave, South Hot-Cell, Standard Operation, TM4, Ta#56, Module move 

 TM#4 with Ta#56 has been moved from the east station to the south hot cell.

Entry  Monday, August 20, 2018, 09:55, Travis Cave, South Hot-Cell, Standard Operation, TM2, Ta#56 and UC#23, Electrical Check Electrical_Check_TM4_Ta56_SHC.pdfElectrical_Check_TM2_UC23_CS.pdfElectrical_Check_TM2_UC23_SHC.pdf

 Electrical Checks of the last two targets Ta#56 and UC#23

Entry  Tuesday, August 14, 2018, 10:27, Travis Cave, ITW, Standard Operation, TM2, UC#23, Module move 

 Both the West Entrance and TM#2 with UC#23 have been moved back into their places in the west target station. The Entrance module move wasn't completely smooth as it did suffer a little bumpiness when the shield plug part was installed, I was lifted back out again and no visible damage was observed on the delicate items.

Entry  Tuesday, August 07, 2018, 10:44, Travis Cave, South Hot-Cell, Maintenance, , , Entrance module move 

 The west entrance module has been moved from the west target station to the south hot cell, for a bellows replacement.

Entry  Thursday, August 02, 2018, 14:12, Travis Cave, Spent Target Vault, Standard Operation, , Nb#8, Spent Target Move Target_Index_2018-08-02.pdf

 The spent Nb#8 target was moved from the south hot cell to the spent target vault. It was placed in pail #168 and place in spot 2A in the vault. See the attached pdf for vault details.

Entry  Thursday, August 02, 2018, 07:57, David Wang, Conditioning Station, Standard Operation, , , Leak check on TM2 UCx #23 @ TCS and SHC. 

I did a helium pressure test on TM2 HS line at TCS. At 70psi helium, the leak rate is 2.5 xE-7 atm.cc/sec. I think this is the number that close to result before which is 1.7xE-9 atm.cc/sec. WE know there is a small leak on this water block seal. Chad  and I did helium  spray check yesterday at SHC. It was good at bottom scale.  No much worry on this low E-7 range leak.

Entry  Wednesday, August 01, 2018, 15:12, Anders Mjos, South Hot-Cell, Standard Operation, TM2, UC#23, Target mounted - water leak on HS line 20180801_180130904_iOS.jpg

The heat shield water lines were not purged ahead of target exchange in the hot cell. This resulted in water leaking onto the new target assembly (heat shield) when the cooling lines were opened at top and bottom (for connecting leak detector). Excess water was wiped up with paper towels.

Entry  Wednesday, August 01, 2018, 14:48, Travis Cave, Conditioning Station, Standard Operation, TM2, UC#23, Spent Target Move 

 TM#2 with UC#23 has been moved from the south hot cell to the conditioning station.

Entry  Wednesday, August 01, 2018, 09:47, Isaac Earle, North Hot-Cell, Development, , , NHC diagnostic signals and control panel tested 

 On July 30th the NHC diagnostic signals were tested:

- 9 pin CPC: a shorting plug was installed on the hot side - continuity check results were as expected

- 4 pin CPCs:  snake camera installed in both hot side connectors with portable monitor on cold side - both connectors worked as expected

- USB: laptop connected on hot side, USB mouse connected on cold side - worked as expected

- Ethernet: laptop connected on hot side, cold side connected to building ethernet port - connection to network worked as expected

- SHV: a shunt was installed on the hot side - a short circuit was measured from the cold side as expected
            with no shunt installed the line was Megger tested: 1.63 G-ohms recorded @ 1000V

 

The control panel switches for the in-cell receptacles were also tested.  Each switch (a - d) worked as expected.

 

On July 31st the gas supply solenoid valves were tested.  60psi air was hooked to each solenoid inlet.  With the valve closed there was no air flow.  When each push-button or switch was activated air flow was observed through the correct solenoid.

Entry  Tuesday, July 31, 2018, 11:16, Travis Cave, Spent Target Vault, Standard Operation, , UC#22, Spent Target Move Target_Index_2018-07-30.pdf

 Yesterday the spent UC#22 target was moved from the south hot cell to the spent target vault. It was placed in pail #167 and placed in spot 4A see attached PDF for details.

Entry  Tuesday, July 31, 2018, 10:20, Travis Cave, South Hot-Cell, Standard Operation, TM2, Nb#8, Module move 

 TM#2 with Nb#8 has been moved from ITW to the south hot cell.

Entry  Wednesday, July 25, 2018, 13:21, Anders Mjos, ITW, Repair, TM2, Nb#8, Leak check of ITW Entrance_Module_Leak_2018-07-25.docx

ITW Entrance Module was leak checked yesterday with the support of Vacuum Group (Dimo & Edi). The leak detector was connected to primary backing vacuum line. A leak response was found near the bellow for the beam profile monitor on top of the Entrance Module. It could be confirmed today by actuating the monitor, that the leak was indeed at that location. The plan is to move the TM and Entrance Module out for target exchange and repair, respectively. Drawings of the device available on ITA0200and ITA5128

Entry  Monday, July 23, 2018, 10:31, Travis Cave, ITE, Standard Operation, TM4, Ta#56, Module move 

 TM#4 with Ta#56 has been moved from the conditioning station to the east target station.

Entry  Thursday, July 19, 2018, 14:22, Isaac Earle, North Hot-Cell, Development, , , NHC diagnostic signals - connector and wiring details 

Installation of the diagnostic connections between the NHC hot and cold sides has been completed.  The cable bundle was prepared by Travis Cave in the electronics workshop with connectors attached at one end only.  Metal fish tape was first ran through the conduit from the cold side to hot side, the non-terminated end of the cable bundle was attached to the fish tape inside the cell, cable pulling lubricant was applied, then the cable bundle was pulled through the conduit to the cold side, and the cold side terminations were then made.  For future replacement of the cables and connectors the same method should be used, and a minimum of 6m of cable length.  Connector details can be found on drawings IRH1765 (hot side) and IRH1767 (cold side).  Conduit is 1" trade size PVC type (PO#3041531). Wiring details for each connector are attached below:

 

9 pin CPC connector:

Pin 1: Brown
Pin 2: Red
Pin 3: Orange
Pin 4: Yellow
Pin 5: Green
Pin 6: Blue
Pin 7: Violet
Pin 8: Black
Pin 9: No connection

All wires 14 gauge. 
Connector PN: Amp 211768-1
Cap PN: 208652-1

 

4 pin CPC connectors:

Pin 1: Coax RG-179
Pin 2: Red (18 gauge)
Pin 3: Black (18 gauge)
Pin 4: No connection

Connector PN: Amp 206430-1
Cap PN: 208800-1

 

SHV:

Connector: IRH1769 (customized "Kings 1709-1" connector)

 

USB:

5m long powered USB 3.0 cable
Connector: IRH1770 (customized "TE Connectivity PC4B0100-15NY-1-C" connector)
Cap PN: USBFTV 2 N

 

Ethernet:

Wires installed in the following order when viewing the back side of connector with PN lettering right-side-up:

Blue Blue/White   Orange/White   Orange  
Green/White   Green Brown/White Brown

Connector PN: Tyco 1546877
Cap PN: 208652-1

 


 

Entry  Thursday, July 19, 2018, 09:17, chad fisher, South Hot-Cell, Repair, TM4, , New Optics Tray Modification 20180719_TM4_2.jpg20180709_TM4.jpg

The waterline loop bracket has been installed onto the new loop holding bracket and both installed onto the new source tray.

Entry  Wednesday, July 18, 2018, 14:20, chad fisher, South Hot-Cell, Standard Operation, TM4, Ta#56, Ta#56 Installed 

Ta#56 has been installed onto TM4 with new fasteners. High current fasteners torqued to 130 in lbs.

RIB "shield" has been removed in  preparation for insertion of new optics tray.

Entry  Monday, July 16, 2018, 17:41, Anders Mjos, ITE, Standard Operation, TM4, UC#22, Target module disconnected TM4_UCx_22#__disconnection_check_list_1.pdfTM4_UCx_22#__disconnection_check_list_2.pdf

The water and electrical connections were disconnected today as protons remained off after power interruption during the weekend. Vacuum is still connected and operating.

 The vacuum system are disconnected 2018-07-17.  See attachment .

Entry  Wednesday, July 11, 2018, 15:09, Anders Mjos, ITW, Maintenance, TM2, Nb#8, Uncovered ITW to toubleshoot 2A2M19 

The 2A2M19 beam profile monitor did not work and was e-faulted. After initial troubleshooting 2 blocks were removed form ITW to inspect the entrance module where the beam monitor is installed. The cable was found not to be connected and was quickly fixed. Blocks reinstalled. The work was done by Maico, Travis and Anders

Entry  Wednesday, July 11, 2018, 15:06, Anders Mjos, ITW, Standard Operation, TM2, Nb#8, Block move 

Maico and Travis moved blocks from ITE to ITW yesterday

Entry  Tuesday, July 03, 2018, 14:42, David Wang, ITW, Standard Operation, TM2, Nb#8, TM2 has been connected to ITW. Nb#4_Module_connection_checklist.pdf

TM2 has been connected to ITW. All turbo pumps are started. See attachment for connection checklist.

Entry  Tuesday, July 03, 2018, 14:38, David Wang, ITW, Standard Operation, , , ITW water signals interlock check. 

Annual ITW water signals interlock check are done. Everything works good.

Entry  Tuesday, July 03, 2018, 09:57, Travis Cave, ITW, Standard Operation, TM2, Nb#8, Module move 

 TM#2 with Nb#8 has been moved from the south hot cell to the west target station.

Entry  Friday, June 29, 2018, 13:36, Travis Cave, South Hot-Cell, Standard Operation, TM2, Nb#8, Electrical Check TM2_elec_chk_steerers_and_lens_062818.pdfTM2_Nb8_elec_chk_shc.pdfTM2_notgt_elec_chk_shc_062918.pdf

 The results of the various electrical checks performed on the TM#2 with and without the Nb#8 target attached.

Entry  Friday, June 29, 2018, 10:27, chad fisher, South Hot-Cell, Maintenance, , , South Hot Cell Filter Change 

At the end of manipulator repair Thursday the ventilation pre-filter in the hot cell was changed. Old filter remains in the hot cell until such time as it can be removed.

Entry  Friday, June 29, 2018, 10:15, chad fisher, South Hot-Cell, Standard Operation, TM2, , TM2 work and target install 

On Thursday, June 29th the containment box of TM2 was removed and the optics tray re-installed and reconnected. The box was then re-installed.

Friday the window waterlines were leak checked, Nb target installed (with new fasteners, high current torqued to 130 in*lbs) target leak and electrical checked and containment box cover installed with new fasteners.

Entry  Friday, June 29, 2018, 10:12, chad fisher, South Hot-Cell, Maintenance, , , Manipulator Tong Cable Replacement 

Tuesday, June 26 the broken tong cable was replaced on the west manipulator in the south hot cell. Wednesday the tong cable was preemptively replaced on the east manipulator of the south hot cell.

Entry  Wednesday, June 27, 2018, 14:56, Travis Cave, South Hot-Cell, Standard Operation, TM2, no target, Module move 

 TM2 has been moved from the silo to the south hot cell.

Entry  Tuesday, June 26, 2018, 08:56, chad fisher, South Hot-Cell, Standard Operation, , , South Hot Cell Fields 

hot items have been moved and shielded as much as possible. Field at left manipulator has been reduced from 560 uSv/h to 85 uSv/h.

Entry  Monday, June 25, 2018, 16:42, Anders Mjos, Conditioning Station, Development, , , Testing new high current connectors 

Shorted TGHT with new high current connector assembly and heated to 600 A. Temperature measured on half way point on cable ~ 70 deg C and on connector ~60 deg C at 600 A, 45 / 40 deg C at 400 A. Target Hall locked out during test

Entry  Monday, June 25, 2018, 11:31, chad fisher, South Hot-Cell, Standard Operation, , , Fields at Al cover 

The shield door has been opened and fields measured at 77 uSv/h on contact at the AL. panel.

Entry  Friday, June 22, 2018, 13:59, chad fisher, South Hot-Cell, Repair, , , Soth Hot Cell Fields 

Field measurements have been taken to determine the level before entry for repair of manipulators.

Field on contact at manipulator is 560 uSv/h, and at approximately 1/2 meter at table surface 920 uSv\h.

Entry  Thursday, June 21, 2018, 17:15, Isaac Earle, North Hot-Cell, Development, , , Motorla CP200 radio with throat mic tested in NHC 

 A Motorla CP200 portable two-way radio was tested today for use inside the ISAC hot cells.  A High Technology Communications Throat microphone PRO model from Planet Headset was used with the radio.  Chad entered the NHC wearing the throat mic and radio under a air supplied hood to mimic real world conditions.  Communication was clear with the other person in the NHC service area, in the SHC service area, at various locations on the B1 level, and even with an operator in the TRIUMF Main Control Room.

This testing satisfies RS 104 of the NHC requirements specification (Document-131915, Release 1)

Entry  Thursday, June 14, 2018, 11:37, David Wang, ITE, Standard Operation, TM4, UC#22, TM4 UC 22# checklist. TM4_UCx_22#_check_list.pdf

See attachments

Entry  Tuesday, June 12, 2018, 11:26, chad fisher, South Hot-Cell, Repair, TM2, , TM4 Optics Tray fh.jpg

I have "slung" the TM4 optics tray in preparation for its removal.

Entry  Monday, June 11, 2018, 11:30, chad fisher, South Hot-Cell, Repair, TM2, , TM2 containment box on 

Tm2 containment box has been re-installed onto TM2.

Entry  Friday, June 08, 2018, 14:24, Travis Cave, South Hot-Cell, Standard Operation, TM2, no target, Module move 

 TM#2 has been moved from the conditioning station to the south hot cell.

Entry  Friday, June 08, 2018, 11:36, chad fisher, South Hot-Cell, Repair, TM2, , TM2 Source Tray Removal Progress TM2_06082018.jpg

The containment box has been removed from TM2, the Enzel lens and steerers disconnected and optics tray removal has commenced.

Entry  Thursday, June 07, 2018, 11:37, Travis Cave, ITE, Standard Operation, TM4, UC#22, Module move 

 TM#4 ,with UC#22, was moved from the south hot cell to the east target station. Upon lowering the module down it made contact with the IMC, At that point the module was removed and placed back in the south hot cell. The IMC was inspected and problem corrected and the module was moved back to the east target station without a problem.

    Reply  Friday, June 08, 2018, 10:22, Anders Mjos, ITE, Standard Operation, TM4, UC#22, Module move IMC.png

Travis Cave wrote:

 TM#4 ,with UC#22, was moved from the south hot cell to the east target station. Upon lowering the module down it made contact with the IMC, At that point the module was removed and placed back in the south hot cell. The IMC was inspected and problem corrected and the module was moved back to the east target station without a problem.

 The IMC (ITA0160) appears to have a dent in it from the contact with the Target Module. The pressure on the IMC was found to be about negative ~3 mmHg and was increased to ~20 mmHg to attempt to retract the IMC further away from the TM. This pressure is similar to the pressure used at the Conditioning Station. The bellows appears not to be symmetrically compressed. It should be inspected again and pressure checked and monitored for upcoming module moves.

Entry  Thursday, June 07, 2018, 11:33, Travis Cave, South Hot-Cell, Standard Operation, TM4, UC#22, Electrical Check TM4_UC22_Electrical_Check_South_Hot_Cell.pdf

 The results of TM#4 with UC#22 electrical check. See attached PDF.

Entry  Monday, June 04, 2018, 13:27, chad fisher, South Hot-Cell, Repair, TM4, , Window Loop and Shield jhgf.jpg

The tray with window waterline loop and EF Shield has been installed into TM4.

Entry  Thursday, May 31, 2018, 14:22, chad fisher, South Hot-Cell, Repair, TM4, , Loop and beam shield 

Tray with loop and beam shield has been inserted into the hot cell to be installed on TM4 .

Entry  Wednesday, May 30, 2018, 09:55, David Wang, Conditioning Station, Repair, TM2, , TM2 and TCS vacuum pumps are switched off. 

I switched off TM2 and TCS vacuum pumps. The TCS and TM2 will be under vacuum without pumping.

Entry  Wednesday, May 30, 2018, 09:51, David Wang, Conditioning Station, Repair, TM2, , TM2 water lines helium pressure test at TCS. 

I did a helium pressure test on TM2 water lines at TCS. We will remove the TM2 source tray soon so this test is a reference check for future new source. The result:

Helium 70 psi, 2 minutes to each circiut. Leak detector  base LR.0.0x e-9atm.cc/sec, base pressure  0.0x e-4torr

Ta+(A)  0.0x e-9atm.cc/sec

Ta-(B)  0.0x e-9atm.cc/sec

Tu-(C) 7.8x e-7 atm.cc/sec

Tu+(D) 3.5x e-7 atm.cc/sec

Coil 2(PU) 0.0x e-9atm.cc/sec

Coil 1(RU) 0.0x e-9atm.cc/sec

EE 8.2 x e-9atm.cc/sec

MSP 0.0x e-9atm.cc/sec

Containment box window  0.0 xe-9atm.cc/sec

HS  no target and opened. No test.

All water lines on module side in TM2  should be in good condition according to this test . The leak response we found on B and C lines are from water block seals mostly.           

Entry  Monday, May 28, 2018, 14:06, Travis Cave, Spent Target Vault, Standard Operation, , SiC#37, Spent Target Move Target_Index_2018-05-28.pdf

 SiC#37 has been moved from the South Hot Cell to the Spent Target Vault. It was placed in Pail #165 and put in spot 3B of the vault and it measured 25.8mSv/hr upon removal from the hot cell. See the attached PDF for details

Entry  Friday, May 25, 2018, 11:41, Travis Cave, South Hot-Cell, Standard Operation, TM2, no target, Module move 

TM#2 has been moved from the south hot cell to the conditioning station.

Entry  Thursday, May 24, 2018, 15:19, Keith C Ng, Assembly/Bench Test, Repair, TM2, , tm 2 source tray build 20180524_alignmentcheckresults.pdf

Attached alignment check notes after brazing and fabrication.

First page lower half shows establishment of baseline using master jig

Second page top half shows the alignment of the target mounting plate jig and the steerer cone aperture.

Second page bottom half shows alignment of the master target jig. Master target jig needed the 9 pin and heat shield locating features removed to seat the target correctly.

Overall, source tray assembly sits .006" high on average (min .003", max .010"), .003" to the left with respect to ion beam axis.

Entry  Thursday, May 24, 2018, 14:04, Travis Cave, South Hot-Cell, Standard Operation, TM4, no target, Modules moved 

 TM#4 has been moved from the south hot cell to the east target station, and TM#2 has been moved from the south silo to the south hot cell.

Entry  Thursday, May 24, 2018, 10:02, Anders Mjos, ITE, Development, TM4, Empty, Module move ventilation test 

The new module move ventilation procedure was successfully tested (ITM:MP2). ITM:CM4 did not drop below 6 in during the test.

Entry  Wednesday, May 23, 2018, 10:40, chad fisher, South Hot-Cell, Repair, TM4, , Optics Tray Removal 20180523_103405.jpg20180523_103435.jpg20180523_103440.jpg

The optics tray has been removed from TM4.

 

 

Entry  Wednesday, May 23, 2018, 09:48, Travis Cave, South Hot-Cell, Standard Operation, TM4, no target, Module move 

 TM#4 with no target and no containment box has been moved from the conditioning station to the south hot cell.

Entry  Tuesday, May 22, 2018, 10:02, Anders Mjos, Conditioning Station, Repair, , , Water leak from TK1 over the weekend 2018-05-22_TCS_TK1_water_leak.pngBroken_Valve.jpg2018-05-22_TCS_TK1_water_leak_archiver.png

Link to e-log,

Link to efault

Tank level down from 76 to 55 in on TK1

Valve replaced by Curtis today

Entry  Friday, May 18, 2018, 09:34, David Wang, Conditioning Station, Repair, TM4, , water leak on TM4 Tube heater - B line confirmed. TM4_2018-05-18_Water_Leak.docx

At 8:50 AM today, I applied water to TM4 tube heater - (B) line at TCS. All high vacuum gauges got response on this action. Water is leaking through B line on TM4.

It should be D line . David 2018-06-05

Entry  Thursday, May 17, 2018, 13:17, Travis Cave, ITW, Standard Operation, , , Entrance module move 

 The west entrance module has been moved from the silo to the west target station.

Entry  Thursday, May 17, 2018, 11:30, Anders Mjos, Conditioning Station, Maintenance, TM4, , HV test/conditioning of damaged source tray TM4_2018-05-18_Water_Leak.docx

BIAS only. Water lines looped on top. Containment box off.

Thursday, May 17, 2018, 11:20: Vacuum 7.2E-7 Torr

Thursday, May 17, 2018, 11:30: 10 kV

Thursday, May 17, 2018, 11:42: 20 kV

Thursday, May 17, 2018, 12:14: 25 kV

Thursday, May 17, 2018, 12:35: 30 kV

Thursday, May 17, 2018, 16:13: 35 kV

Thursday, May 17, 2018, 17:339: 37.5 kV

Thursday, May 17, 2018, 17:40: vacuum 6.8E-7 Torr

Thursday, May 17, 2018, 18:13: BIAS off.

Entry  Tuesday, May 15, 2018, 10:21, David Wang, Conditioning Station, Standard Operation, TM4, , Tm4 water circles helium pressur test result  

  Helium pressure test on TM4  water lines is done this morning. 70 psi helim , 1 minutes time to each circle. The result:

A(oven+): 0.00xE-9 atm.cc/sec

B(Oven -): 8.1Xe-7 atm.cc/sec

C(tube -): 0.00xE-9 atm.cc/sec

D(tube+): 1.0xE-5 atm.cc/sec

PQ(coil 2): capped on top. water lines were removed because of leak

RU(Coil1): 0.00xE-9 atm.cc/sec

EE: 0.00xE-9 atm.cc/sec

MSP: 0.00xE-9 atm.cc/sec

HS: No target, capped on top. It was fine on last target check in 2017 Oct.

window: Capped on top. Containment box is not installed.

The leak check on D line caused the IG1 small response during test.

B and D circle are double checked. The reasults are same.

D line leak is in E-5 atm.cc/sec range. It is possible to locate it by using helium spray method in SHC. The containment box is not on so it should be easy to do it.

Switch on IGA gauge at TCS and apply helium and water at certain psi to check the IGA response may give us more information on these leaks.

 All lines were test in last year shut down. They were good.

 

Entry  Tuesday, May 15, 2018, 07:44, Travis Cave, Conditioning Station, Standard Operation, TM4, no target, Module move 

 TM#4 was moved to the conditioning station from the south hot cell. The module was moved with out the containment box.

Entry  Wednesday, May 09, 2018, 08:48, David Wang, ITW, Repair, , , 2A2 winodw leak check on ITW vacuum vessel. 

Leak detector is connected to ITW TP4. LD Base leak rate 0.0XE-09 atm.cc/sec. Helium line is connected to existing window leak check 1/8 " copper tube. Applied 18psi helium for 1 minute. No response on LD. The window seal is good on ITW vacuum vessel. 

Entry  Thursday, May 03, 2018, 13:26, Anders Mjos, South Hot-Cell, Repair, TM4, , EZL short troubleshooting 

Yesterday Aaron, Isaac and Anders inspected the EZL connection from the service chase to the optics tray using the goose neck camera in SHC. No issues or shorts could be identified. Containment box was not removed.

Today David and Anders opened up two panels on the service cap and inspected the EZL connection. No issues or shorts could be identified. Photos available on DocuShare.

Next step will likely be to remove the containment box and inspect the optics tray.

    Reply  Friday, May 04, 2018, 15:46, Anders Mjos, South Hot-Cell, Repair, TM4, , EZL short troubleshooting 

Anders Mjos wrote:

Yesterday Aaron, Isaac and Anders inspected the EZL connection from the service chase to the optics tray using the goose neck camera in SHC. No issues or shorts could be identified. Containment box was not removed.

Today David and Anders opened up two panels on the service cap and inspected the EZL connection. No issues or shorts could be identified. Photos available on DocuShare.

Next step will likely be to remove the containment box and inspect the optics tray.

The containment box was removed yesterday. One of the main insulators on the source tray had cracked at the rear close to the bolt to the source tray mounting plate (see photos using link above)

Troubleshooting continued this morning with disconnection of the optics tray from the module. The banana plug copper tube connection was removed form the optics tray side. With the connection removed, the measurement showed open line on top of the module indicating that the problem is on the optics tray

Entry  Friday, May 04, 2018, 11:21, David Wang, ITW, Repair, , , 2A2 winodw leak check in TH 

Anders and I leak checked new 2A2 window seal on ITW side. Leak detector was connected  to ITW TP4.  Base  leak rate 0.0Xe-9 atm.cc/sec. base pressure 0.0xe-4 torr.  Sprayed 15-20 psi directly underneath 2A2 window by using exist 2a2 window leak check copper tube. The leak detector got response in 5 seconds when helium was applied. the leak rate was 5xe-6 atm.cc/sec. Once the helium source was closed, the leak rate dropped quickly back to base level. To confirm the leak is at window , I sprayed 15 psi helium around all top flange seals of TM and entrance module.  There was no direct response during the spray( about 1.5- 2 minutes). There was a weak slow up response (up to 1.0 xe-7 atm.cc/sec) which was started after 1.5 minutes of spray. The weak response is cause by helium drift in my view.   Our conclusion is the 2A2 window seal on ITW side is not perfectly sealed.  The elak we saw on LD is ture , and it is located on window.  The station will be vented soon for shielding plug moving back. .

Entry  Thursday, May 03, 2018, 08:24, Travis Cave, South Hot-Cell, Standard Operation, TM4, no target, Electrical Check TM4_Electrical_Check_notarget_May_2_2018.pdf

 The results of yesterdays electrical check of TM#4 with no target attached. See the attached PDF for details.

Entry  Tuesday, May 01, 2018, 13:40, Travis Cave, South Hot-Cell, Standard Operation, TM4, SiC#37, Electrical Check TM4_electrical_check_SiC37_post_beam.pdf

 Electrical check of TM#4 with SiC#37 attached post beam. A short was found between the Einzel Lens and Chassis. See attached PDF for details.

Entry  Tuesday, May 01, 2018, 11:12, Travis Cave, ITE, Standard Operation, TM4, SiC#37, Module move 

 TM#4 with SiC#37 has been moved from the East Target Station to the South Hot cell.

Entry  Tuesday, May 01, 2018, 10:54, Keith C Ng, ITW, Repair, , , 2a2 window installation and beamtube repair 20180420_2a2beamtuberepair_P1040025.JPG2018_2a2window00017.jpg

Yesterday we installed the 2a2 window, the drive screw was torqued until 70 ft-lbs and we stopped, the yoke is not fully closed to its hard stop with roughly 7/8" to 3/4" still to go. Similar to identical conditions to 2a3 beamline window install, see https://elog.triumf.ca/TIS/RH-ISAC/647 for that install. Otherwise clamp looks centered and installed correctly.

 

2018_2a2window00017.jpg

 

 

Concerns with the cooling lines for the window WRT to the base of the shielding plug: There is no jog bend indicated on drawings for the transition of the window cooling lines from beamline center to the corner of the shield plug penetration. See photo for cooling line position on initial removal of shielding plug. It was decided to not add a jog for the shield plug and to carefully reinsert it being mindful of the cooling lines.  The shielding plug has a chamfer on the corner to allow the cooling lines to be routed to the top.

 

20180420_2a2beamtuberepair_P1040025.JPG

 

 

A new beam tube cradle is being manufactured where the old one will removed and the new one swapped with the beam tube in situ. Both sides of the window still need to be leak checked.

Entry  Friday, April 27, 2018, 15:06, Keith C Ng, ITW, Repair, , , ITW beam tube repair 6x

Vacuumed out remainder of debris from the wall penetration, removed cradle and checked condition. Down stream support bracket sees advanced stages of material loss (OBO 20-30% loss). See attached photos.

RPG reports that the removed beam tube has 15k CPM on the interior of the beam tube.

Tank flange was cleaned as per 2009 repair report, looks OK. Video capture of flange inspection attached as .zip file.

.03" shim was inserted into the clamp indexing block.

 

Entry  Friday, April 20, 2018, 15:33, Keith C Ng, ITW, Repair, , , ITW beam tube repair job 20180420_2a2beamtuberepair_P1040034.JPG20180420_2a2beamtuberepair_P1040030.JPG20180420_2a2beamtuberepair_P1040029.JPG20180420_2a2beamtuberepair_P1040036.JPG

2A2 window has been removed from ITW and beamlines has removed the beamtube from the penetration. The penetration has been sealed with plastic sheeting and duct tape to maintain the ventilation depression between the 2A tunnel and the Target Pit.

Window is currently stored in a lead flask in the target hall. Window fields are 26 mSv/h OC, 1.2 mSv/h at .5m. There is a 10 uSv/h field outside the flask with the window inside it.

Clamp is currently sitting bagged in ITW Station Pit, it is quite corroded.

Tank flange was video inspected but still needs to be cleaned, currently there is a slip on dust cover over the flange to protect it.

Work will resume after the nuclear ventilation comissioning is completed.

 

 

 

Entry  Thursday, April 19, 2018, 10:27, Travis Cave, ITW, Maintenance, , , Entrance module move 

 The west entrance module has been moved from the west target station to the silo.

Entry  Tuesday, April 17, 2018, 11:05, David Wang, ITW, Repair, , , Disconnect ITW entrance module 

ITW entrance module has been disconnected.  All connections are labelled before or during disconnection. The 24VDC electrical plug on ITW TP1S is broken . It will be replaced with a new plug. The lift yoke is installed onto module without difficulty.   

Entry  Monday, April 16, 2018, 14:51, Travis Cave, Spent Target Vault, Standard Operation, , Ta#55, Spent Target Move 

 Ta#55 has been moved from the south hot cell to the spent target vault. It was 30.4mSv/hr upon removal from the hotcell, placed in pail #161 and put in spot 7A of the vault.

Entry  Tuesday, April 10, 2018, 10:43, Travis Cave, South Hot-Cell, Standard Operation, TM4, no target, Module move 

 TM#2 has been moved from the south hot cell to the south west silo.

Entry  Monday, April 09, 2018, 09:57, Travis Cave, South Hot-Cell, Standard Operation, TM2, Ta#55, Module move 

 TM#2 with Ta#55 has been moved from the west target station to the south hot cell.

Entry  Monday, April 09, 2018, 06:36, David Wang, ITW, Standard Operation, , , ITW Turbo -pumps switch off 

I asked MCR to switch off ITW TP3,4 TP1s,2s this morning.

Entry  Thursday, April 05, 2018, 11:29, David Wang, ITW, Maintenance, , , ITH MP1 replacement 

ITH MP1 is replaced today with a new style pump.The new pump is 0.75 inch higher than  old pump on inlet and exhaust so a new solid inlet adapter  (KF50-25) has to been used. For future secondary pump ITH MP1S replacement, we need a new adapter 0.75 inches shorter as well.   The new pumps is started . Everything works fine. Old pumps is drained , bagged, and stored in TH B2 level. All radioactive garbage produced during the job are bagged , tagged, and stored in TH as well.

Entry  Friday, March 23, 2018, 09:34, Travis Cave, Spent Target Vault, Standard Operation, , Many, Spent Target Assay Target_Index_2018-03-23.pdf

 All targets in the ISAC Spent Target Vault have been either assayed and had field measurement done on them or just measurement if to hot to assay.

Entry  Thursday, March 08, 2018, 14:10, David Wang, ITW, Maintenance, , , Two small water leak has been found in ITW.  

Two small water leaks have been found on ITW High active water system. One is from an unused 1/4" copper valve stem. another is on supply 1.5" supply line valve body top sealing. Both of them are seeping water from seal. 1/4" copper valve will be replaced with a new one. 1.5" supply line valve will be replaced by an old valve with all new seals. I have all spare parts in hand.  At present, water supply to ITW are stooped to reduce leak rate. Two aluminum flat tray are put underneath leak valves to hold small amount leak water. Both leak will be fixed in April  mostly.

Entry  Wednesday, March 07, 2018, 10:36, David Wang, ITE/ITW Cooling, Development, , , HALCW resin can flow meter replacment 

HALCW resin can flow meter replacement is done. Less that 100 mL water was drained to a small tray during the job. RPG checked the water. Less than 20 counts. Water are dumped the high active sump.   The HALCW MP1 is started. No leak on new gauges and fittings. Old gauge is labeled , bagged, and stored in TH.

Entry  Wednesday, March 07, 2018, 10:18, David Wang, ITW, Standard Operation, , , Oil leak on target station vacuum primary back pump. 

I can not see oil in sight window of the primary pump during visual inspection. The aluminum tray underneath the pump is filled with oil. The performance on this pump start to drop by watching ITH CG4 reading. A fault report with suggestion is issued to vacuum group.  Everything on secondary pump looks fine.

Entry  Tuesday, March 06, 2018, 09:53, David Wang, ITW, Standard Operation, TM2, , Tm2 and Tm4 vacuum disconnection TM2_TM4_disconnection_Vacuum.pdf

The job is done. See attachment.

Entry  Monday, March 05, 2018, 13:47, Travis Cave, Spent Target Vault, Repair, , Many, Spent Target Assay 

 The spent target assay was aborted today after the first target was finished due to the very old computer that controls the camera and the vault door effectively died. The vault door had to be closed using the emergency door closing winch which worked so it passed that test.

Entry  Wednesday, February 28, 2018, 14:47, David Wang, ITE, Standard Operation, , , leak check ITE primary and secondary vacuum vessel. 

2018-02-27: Anders and I finished leak check on ITE primary and second vacuum vessel seals. LD connected to ITE BV2 valves between. LD, Base Leak rate 1.2 xE-9atm.cc/sec, base pressure 0.0XE-4torr. There is a leak has been found on TM4 service cap KF25 blank off. The o-ring on the blank off will be changed later. It is an easy fix . Other seals are good. The big T tank seal on secondary vessel is leak checked as well. It is still fine.  Helium pressure on TM4 water lines will be fulfilled at TCS to save dose.

2018-02-28 Leak checked ITW today, LD connected to ITW BV2 valves between LD base LR0.0XE-9 atm.cc/sec. base pressure 0.0Xe-4torr. There is leak has been found on exit module 1 service cap  on  topcover plate   o-ring. The leak is located on the south side of east edge on exit 1. This is the side module 2 is close beside. The leak rate is up to middle of E-8atm.cc/sec  range with 1-2 second helium spray. The leak and leak position are double checked and confirmed.  To completely fix this leak, the o-ring for top cover plate need to be replaced on service cap.It will be a major shut down job.  The  leak is close to ITW TP3 so it is less affect on beam line elevation vacuum.  Vacuum group experts will be consulted to see if we could leave it to next year shutdown.  Other seals are good including big T-tank seal on secondary vessel. TM2 source tray will be replaced this yea rso no helium pressure test on water lines is needed at this moment.

Entry  Friday, February 16, 2018, 13:46, Anders Mjos, ITW, Maintenance, TM2, , Parker coupling inspection Used_Parker_FS251_Inspection.pdf

Findings and photos from the inspections attached. The inspection was conducted by Anders, David and Maico.

Entry  Wednesday, February 14, 2018, 10:06, Anders Mjos, ITW, Maintenance, TM2, , Replaced parker couplings on Window cooling line 

By Anders & David. Couplings will be taken apart for inspection.

Entry  Tuesday, February 13, 2018, 13:56, Anders Mjos, ITW, Standard Operation, TM2, Ta#55, Target module disconnected 

TM disconnected by David and Yasmine Feb 8th. One of the water couplings were leaking for a short while when disconnected. NCR 10836 submitted by Max

Entry  Tuesday, February 13, 2018, 13:54, Anders Mjos, ITE, Standard Operation, TM4, SiC#37, Target module disconnected 

TM disconnected by David and Yasmine Feb 8th

Entry  Wednesday, January 31, 2018, 10:32, David Wang, Crane, Standard Operation, , , Target Hall crane annual inspection. 

Gordon crane technician Tom finished annual TH crane inspection today. Everything is normal. The main hoist brake gaps are checked on both side. They are good still.

Entry  Monday, January 29, 2018, 06:51, David Wang, Conditioning Station, Maintenance, TM1, , TCS and TM1 vacuum pumps switched off 

TCS and Tm1 vacuum pumps are switched off this morning. TM1 TP1and TP2 work fine during this test period. Tm1 will be moved back to silo this morning.

TM1 IG1 stopped work during the test period. It could be broken. We will only replace this gauge if TM1 is used in ITW again.

Entry  Wednesday, January 24, 2018, 13:30, David Wang, Conditioning Station, Standard Operation, TM1, , TM1 has been moved to TCS this morning 

Tm1 has been moved to TCS this morning. All turbo-pumps are started successfully at TCS and TM1.

Entry  Monday, January 22, 2018, 07:47, David Wang, Conditioning Station, Standard Operation, TM3, , Restarted TM3 vacuum sysytem after site power bump 

All TCS and TM3  vacuum pumps are started successfully.

Entry  Wednesday, January 17, 2018, 13:54, David Wang, Conditioning Station, Standard Operation, TM3, , Start TM3 turbo pumps at TCS.  

TM3 turbo-pumps are started at TCS. We will keep pumps running until next Wednesday.

Entry  Wednesday, January 17, 2018, 10:38, Anders Mjos, Spent Target Vault, Standard Operation, TM1, , Old TM1 Source Tray moved to Cyclotron basement 

The old TM1 Source Tray from 2011 has been moved to Cyclotron basement this morning. Source tray was stored in location 10. The box was moved from the vault to the ante-room yesterday. No contamination was found on the box. Photos

Entry  Wednesday, January 17, 2018, 06:51, David Wang, Conditioning Station, Standard Operation, , , Stop TCS vacuum pumps  

I stopped TCS vacuum pumps for coming TM3 move.

Entry  Tuesday, January 16, 2018, 10:36, Anders Mjos, Spent Target Vault, Standard Operation, TM2, , Old TM2 Source Tray moved to Cyclotron basement 

The old TM2 Source Tray from 2009 has been moved to Cyclotron basement this morning. Source tray was stored in location 9. The box was moved from the vault to the ante-room yesterday. No contamination was found on the box.

Entry  Tuesday, January 16, 2018, 06:50, David Wang, ITE/ITW Cooling, Standard Operation, , , Field measurement on old resin tank in silo 

The old resin tank has been stored in silo since last year March.  Without crane the tank up, We use the pole monitor measured the field around the bottom of the tank in silo. The average contact field on the bottom is about 4.0msv/hr. @0.5meter , the field is about  900usv/hr. It is still too hot to remove it.

Entry  Thursday, January 04, 2018, 13:28, Anders Mjos, Conditioning Station, Maintenance, , , Troubleshooting IG1S 

TCS:IG1S is reporting vacuum levels that seem to be too low (1E-10 to 1E-8 Torr). The gauge was connected to the controller for IG1, which showed the same value. A degas was performed for ~5 min.

Entry  Tuesday, January 02, 2018, 15:17, Anders Mjos, Conditioning Station, Maintenance, , , Tested chiller 

Tested all 3 compressors and MP2

Entry  Tuesday, January 02, 2018, 14:47, Anders Mjos, Conditioning Station, Standard Operation, , , Pumping on secondary vacuum 

Tuesday, January 02, 2018, 14:45: TP1S started

Entry  Tuesday, January 02, 2018, 11:28, David Wang, ITE, Standard Operation, TM4, , ITE annual water interlock check. 

Eric and I finished ITE annual water interlock check. Everything works properly.

Entry  Tuesday, January 02, 2018, 10:46, David Wang, ITE/ITW Cooling, Standard Operation, , , Start High active water system. 

High active water system  was  checked before restart. A small water leak on resin can supply valve was found. It is fixed. MP1 and MP2 were started and checked separately. System pressure and flow rate are normal.MP1 is in operation now. 

Entry  Friday, December 22, 2017, 11:09, Anders Mjos, ITW, Standard Operation, TM2, , Shut down High Active Cooling water 

Stopped MP1 today in preparation for the power outage over the holidays. both P-25 and P-26 breakers have been switched off to prevent inadvertent start of system

Entry  Thursday, December 21, 2017, 15:11, Anders Mjos, Conditioning Station, Maintenance, , , Powered down devices 

Powered down mechanical pumps in ISAC-I Experimental hall, vacuum gauge and turbo pump controllers in ISAC-I B2 North Hot Cell service area

Entry  Tuesday, December 19, 2017, 10:41, Anders Mjos, Crane, Maintenance, , , Crane powered down 

The target hall crane has been powered down by Don today in preparation for the power shutdown over the Holidays.

Entry  Tuesday, December 19, 2017, 10:40, Don Jackson, Crane, Maintenance, , , Crane Power during winter break 

 The power to the crane and controls were turned off using the power switch in the Crane Control room.  The main disconnect switch in the target hall was not touched.

All site power will be off for a period of time during the Christmas break and this removes the crane from any issues when power is restored.

Entry  Wednesday, December 13, 2017, 15:32, Anders Mjos, Assembly/Bench Test, Maintenance, TM2, , Source Tray inspection 

The Source tray was inspected in the RH shop today by Anders, Friedhelm and Jens. The routing of the lines are satisfactory, however a design proposal to remove the ground electrode line will be made. This design will have to ensure a proper connection from the electrode to ground (using the window cooling lines). All other lines are OK at this point. Some fine adjustments are expected after brazing and soldering to maintain high voltage separation. Photos are available on DocuShare Collection-21401

Entry  Wednesday, December 06, 2017, 09:33, Anders Mjos, Conditioning Station, Maintenance, , , Running chiller for maintenance tech 

 Dakine is on site to do maintenance on the chiller. The tech requested the chiller to operate.

Entry  Friday, December 01, 2017, 16:42, Isaac Earle, North Hot-Cell, Repair, , , NHC manipulator service visit 1512175169704.jpg1512175181553.jpg

Pete Dudley, manipulator service technician from CRL, was on site from Nov 27-30 to service the NHC Model N manipulators (See E-log entry #1578 for background).

He began by evaluating the motion selection and electric drive of the manipulator installed on the blue service cart.  This manipulator had chip A0166R01, same as the right side manipulator which had the failure described in E-Log 1578.  Pete noted that the arm was very slow to switch between the different drive directions, and had a significant lag between when the switch for motion was released, and when the motor actually stopped driving.  This was the case with all directions.  Because of this, he suspected that the right arm Z tape broke because when the manipulator reached the switch at the end of travel, the motor did not stop quickly enough causing over tension and snapping the tape.  A newer chip, A0166R04, was removed from the spare master arm (received Spring 2017), and installed into the master arm on the blue cart.  The test was repeated, and this time the motion selection and drive worked as expected.  The situation which previously caused failure was evaluated:  slave end fully extended in Z, master end fully collapsed in Z.  In this configuration the arm was moved back and forth in the Y direction.  No tape failure occurred, and the Z motion tape tension seemed normal.  Y motion drive was attempted, and was not possible, as expected.  This test was repeated in the opposite configuration (slave end fully collapsed, master end fully extended) with the same results.  Full drive speed was used for all tests.

The right side slave arm (with broken Z tape) was then removed and transported to the HCSA.  Using the bench mounted locking plate, the broken Z tape was replaced, and a full inspection and cable/tape tensioning was performed.  Pete accidentally broke the Z tape on the right side master arm while investigating the failure, which was also replaced.

The other two slave arms were also both inspected, tensioned, and tested in the same way.  Then all three were each in turn installed to the master arm #9348 on the blue manipulator transport cart where all mechanical motions and drives were tested (except X, because mounted on cart), the failure situation described above was also tested for all three slave arms.

The left side manipulator was then installed into the wall.  It was necessary to remove the lead sheilding on the thru-tube and machine it down approximtaely 0.070" in order for the arm to fit into the wall tube.  After installation, the manipulator motions and drives were tested again including the X motion, and the failure scenario situation was also re-tested.  Chad used the left side manipulator to remove and re-install the pre-filter mounted on the west side partition wall.  He also confirmed that he could reach the east wall electrical outlets and the outlets, gas fittings in front of the window.

The right side slave arm was adjusted so that the Y position was moved 1/2 turn of the shaft drive towards the window (this is the maximum adjustment possible before it hits a hard stop).  This was done so that the operator can more easily reach the outlets and air/gas connections inside the cell in front of the window.  Because both the master and slave ends protrude further out from the wall compared to the E-HD manipulators for the SHC, this modification makes the NHC manipulators feel a bit more like the SHC manipualtors for the operator.  After the adjustment, the right side slave arm was installed.  The left side slave arm was removed, adjusted the same as the right side, then reinstalled.  The spare slave arm was also adjusted in the same way.

The right side manipulator was evaluated through all mechanical motions.  We attempted to remove the A0166R04 chip from the left side, and install in the right in order to try the motion drives, however the pins had been damaged from the previous removal/install, and eventually one pin broke so this was abandoned.  CRL will ship us at least three new A0166R04 chips which should arrive in 2-3 weeks.

Upon completion of the work the location of the different arms is as follows:  Right side master #9351, Left side master #9348, Spare master #9763, Right side slave #9349, Left side slave #9764, Spare slave #9352

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Entry  Wednesday, November 15, 2017, 08:55, David Wang, Conditioning Station, Standard Operation, , , Install shield plug onto TCS and pumping down TCS. 

Shielding plug is installed onto TCS. TCS is being pumped down to keep it under vacuum for the rest of the year.

Entry  Tuesday, November 14, 2017, 14:34, David Wang, ITW, Standard Operation, TM2, Ta#55, TM2 has been connected in ITW. 

TM2 has been connected in ITW. All turbo-pumps are started. Everything works fine.

Entry  Tuesday, November 14, 2017, 10:01, Travis Cave, ITW, Standard Operation, TM2, Ta#55, Module move 

 TM#2 with Ta#55 has been moved from the conditioning station to the west target station. The field was measured on the access panel to the service chase and the field was found to be 430uSv/hr at one meter from the module.

Entry  Monday, November 13, 2017, 13:50, Travis Cave, Spent Target Vault, Standard Operation, , Ta#54, Spent Target Move Target_Index_2017-11-13.pdf

 The spent Ta#54 target has been moved from the south hot cell to the spent target vault. It was placed in Pail #157 and put in spot #5B of the vault.

Entry  Monday, November 13, 2017, 13:39, Travis Cave, South Hot-Cell, Standard Operation, TM2, Ta#54 and #55, Electrical Check TM2-Ta54-_Electrical_Check_SHC_Post_Beam.pdfTM2-no_target-_Electrical_Check_SHC_Nov_2017.pdfTM2-Ta55_Electrical_Check_SHC.pdf

 The results of the various electrical check done on the target module on November 7th and 8th of 2017. Checks were done with the old Ta#54 target without a target and finally with the new Ta#55 target. See the attached PDF for results.

Entry  Thursday, November 09, 2017, 10:39, Anders Mjos, Conditioning Station, Standard Operation, TM2, Ta#55, Conditioning Ta#55 

Thursday, November 09, 2017, 10:40: BIAS / EL to 30 / 15 kV. 400 uA on BIAS

Bias was stable for 1 hour. Handed over to RIB ops for heater conditioning.

Entry  Thursday, November 09, 2017, 09:35, David Wang, Conditioning Station, Standard Operation, TM2, Ta#55, TM2 has been connected at TCS 

TCS vacuum system and water system have been started as well. Everything looks fine.

Entry  Thursday, November 09, 2017, 09:34, David Wang, Conditioning Station, Standard Operation, TM2, Ta#55, Leak check on TM2 HS line at SHC and TCS. 

The TM2 HS line was leak checked at SHC yesterday . 0.9xE-9 atm.cc/sec.Helium sprayed by Chad, NO leak.  It was helium pressurized at TCS this morning. Leak rat:2.5 XE-7 atm.c/sec. The result  is same as last time check. No concern.

Entry  Thursday, November 09, 2017, 08:46, Anders Mjos, Conditioning Station, Repair, , , Communication fiber replaced for HV PLC 

 After extensive troubleshooting the communication fiber was found to be damaged and has been replaced by Gelo.

Entry  Tuesday, November 07, 2017, 10:11, Travis Cave, South Hot-Cell, Standard Operation, TM2, Ta#54, Module move 

 TM#2 with Ta#54 has been moved from the west target station to the south hot cell.

Entry  Thursday, October 26, 2017, 13:20, Travis Cave, Spent Target Vault, Standard Operation, , SiC#30,ZrC#7,Ta#44,TiC#4, and Ta#41, Targets moved to mini storage Mini_Vault_Storage_October_26_2017.pdf

SiC#30,ZrC#7,Ta#44,TiC#4, and Ta#41 have been moved from the spent target storage to the mini storage. See attached PDF for details of the orders of the pails in the mini vault.

Entry  Thursday, October 26, 2017, 09:56, Anders Mjos, ITE, Repair, TM4, SiC#37, Leak on multi pin connector feedthrough 

On maintenance day Tuesday, the roughing of the target station could not go below 1.5 Torr. A brief troubleshooting on Tuesday was unsuccessful in determining the cause. Leak checking continued on Wednesday by David and Anders. A leak was finally found on the multi pin connector feedthrough due to the seal between the connector and flange on top of the nylon insulator. Upon re-tightening the connector, the leak could be stopped and the module pumped down to allow starting of turbo pumps.

Entry  Tuesday, October 24, 2017, 11:58, Travis Cave, ITE, Standard Operation, TM4, SiC#37, Module move 

 TM#4 with SiC#37 has been moved from the conditioning station to the east target station. A measurement was taken on TM#4 as it was being removed from the conditioning station, the location was on the side of the service tray access panel approx one metre away and the cover fully exposed, the reading was 750uSV/hr.

Entry  Monday, October 23, 2017, 13:38, Travis Cave, Spent Target Vault, Standard Operation, , UC#21, Spent Target move Vault_Storage_October_23_2017.pdf

The spent UC#21 has been moved from the south hot cell to the spent target vault. See attached for details

Entry  Thursday, October 19, 2017, 14:20, Anders Mjos, Conditioning Station, Standard Operation, TM4, SiC#37, SiC#37 Conditioning SiC#37_BIAS_current_vs_voltage.xlsxSiC#37.docx

Thursday, October 19, 2017, 14:20: EE configured for conditioning. HV cage locked up

Thursday, October 19, 2017, 16:46: BIAS / EL / EE at 45 / 22.5 / 0 kV

Thursday, October 19, 2017, 17:16: 30 min without sparking. Lowering to 0. Continue conditioning tomorrow.


Friday, October 20, 2017, 08:22: Resuming HV conditioning

Friday, October 20, 2017, 08:44:  BIAS / EL / EE at 45 / 22.5 / 0 kV

Friday, October 20, 2017, 09:48: No sparking. Continue conditionoing

Friday, October 20, 2017, 10:40: BIAS / EL / EE at 50 / 22.5 / 0 kV

Friday, October 20, 2017, 11:30: HV spark (at 52.5 kV) tripped TP2 and TP1s resulting in IG1S and power supplies tripping.

Friday, October 20, 2017, 13:50: Gelo is troubleshooting flickering on/off of ANODE, TGHT and TBHT power supplies.

Friday, October 20, 2017, 13:51: BIAS / EL / EE at 50 / 25 / 0 kV

Friday, October 20, 2017, 14:26: BIAS / EL / EE at 55 / 28 / 0 kV

Friday, October 20, 2017, 14:37: TP2 tripped on spark

Friday, October 20, 2017, 14:51: Gelo has determined there is a communication problem with the PLC on the HV platform. Troubleshooting continues.

Friday, October 20, 2017, 19:02: Troubleshooting did not succeed. Not able to control power supplies. Troubleshooting continue on Monday.


Monday, October 23, 2017, 09:00: After starting the TCS again today communication has been reestablished. Started heater conditioning.

Monday, October 23, 2017, 14:03: Heater ramping previously aborted and ramp down started due to ongoing PLC communication issues. TGHT and TBHT power supplies tripped on timeout around 13:45. Gelo will continue the troubleshooting.

Monday, October 23, 2017, 19:55: Switching off source after operating for 5 hours without any communication glitches detected (fiber optic communication cables swapped between HV platform and BIAS/EZL PLCs)

Entry  Thursday, October 19, 2017, 14:20, Anders Mjos, Assembly/Bench Test, Standard Operation, , , Source tray inspection Left_Insulator.jpgRight_Insulator.jpg

 Two minor chips in the main 60 kV insulators on the source tray was inspected today by Anders, Tom and Aurelia. The chips are small enough that they should not be a problem. See photos for details.

Entry  Thursday, October 19, 2017, 10:11, David Wang, Conditioning Station, Standard Operation, TM4, , Leak check on TM4 HS line at SHC and TCS. 

Chad and I leak checked TM4 HS line after new target is installed yesterday. No leak has been found. Also, I helium pressurized the HS line at TCS this morning. TM4 HS line is good on this test. The TM4 gas line configuration on TM4 top is leak check as well. No problem.

Entry  Wednesday, October 18, 2017, 14:54, Anders Mjos, Assembly/Bench Test, Standard Operation, , , Source tray assembly electrical check Steerer_Connections_2017-10-18.pdf

Source tray meggered today by Anders and Keith

GND - MSP OL @ 1000V
MSP - EE OL @ 1000V
EE - GND OL @ 1000V
4x Steerers - GND OL @ 500V

Steerer continuity verified from socket to steerer plates
(looking in the direction of the RIB, labeled top to bottom on sockets)

1 - Top
2 - Left
3 - Right
4 - Bottom

Entry  Wednesday, October 18, 2017, 10:46, Travis Cave, Conditioning Station, Standard Operation, TM4, SiC#37, Module move 

 TM#4 with SiC#37 has been moved from the south hot cell to the conditioning station.

Entry  Wednesday, October 18, 2017, 10:45, Travis Cave, South Hot-Cell, Standard Operation, TM4, SiC#37, Electrical Check TM4_SIC37_elec_chk_SHC.pdf

 The results of the electrical check of TM#4 with SiC#37, see attached PDF.

Entry  Tuesday, October 17, 2017, 10:56, Travis Cave, South Hot-Cell, Standard Operation, TM4, UC#21, Module move 

 TM#4 with UC#21 has been moved from the east target station to the south hot cell.

Entry  Friday, October 13, 2017, 11:14, Keith C Ng, Assembly/Bench Test, Standard Operation, , , source tray alignment/build 20171013_sourcetray_P1030815.JPG20171013_sourcetray_P1030816.JPG20171013_sourcetray_P1030817.JPG20171013_sourcetray_P1030818.JPG

Source tray is complete for brazing, gas line bracket is currently missing but can be made in parallel with tube bending operations.

Source tray water lines to be fabricated according to ITA6144 drawing set.

- Alignment between target mounting plate and steerer cone is holding within .002"

- Aluminum soldering jigs are installed in place of the ceramics with fasteners only torqued just past "finger tight".

Entry  Thursday, October 12, 2017, 08:48, Travis Cave, Spent Target Vault, Standard Operation, , , Field measurements of the old source trays 

 Field measurements were taken of the old source trays. The old TM#2 source tray had a minimum field value of 0.50 mSv/hr and a maximum of 1.18 mSv/hr through 360 deg of rotation. The box was rotated around three times and put back in the vault. TM#1 old source tray was also removed and measured as well the field values for it were a minimum of 0.52 mSv/hr and a maximum of 1.15 mSv/hr through 360 deg of rotation. The box was rotated around three times and placed back in the vault. In both cases the box was roughly one metre from the radiation monitor.   

Entry  Wednesday, October 11, 2017, 15:50, Keith C Ng, Assembly/Bench Test, Standard Operation, , , spare source tray build alignment 

 

 

Spare source tray build continued.

 

Initial alignment check in the morning:

 

- Target mounting plate target: Horizontal: .002, Vertical: -.002

- Ground electrode (bore) target, with un-clamped target: H 0.0 V -.003

- Ground electrode target (with target clamped): H: 0.0, V: .010

 

 

@14:10: sighting Master target position WRT sighting axis, calculated using the edges of the brunson target center circle edges calculated to center. Target circle is .02" in diameter.

 

- Master target mounted with slight finger torque.

- Front of master target, H .002 V -.002

- Rear of master target, H: 0.0 V: .005 (circle target is .020" in diameter)

- Rear of ground electrode target, H: .002, V: 0.011

 

 

@14:49: Replace mount plate target.

 

- Target mounting plate target: H -.001, V .001

- Ground electrode target: H .002, V .011 (rear target was rotated 90 deg from in the morning as a check)

 

 

@15:21 Steerer cone re-alignment.

 

- Undid the six screws holding the steerer cone and steerers to the aluminum flange and adjusted cone tip to RIB axis. The ground electrode bore was deemed not to be adjustable to the RIB axis with the current build order.

*Steerer cone assembly torque is 23 in-lbs

- Steerer cone target, H: .001, V: 0.0

- Steerer cone target, H: .002, V: .002 (after rotating target 180 degrees)

 

 

@15:30 Replaced target mounting plate target.

 

- Mounting plate target, H: .001, V: -0.001


Will go ahead and finish mounting components to mounting plate and final check the alignment after.

Entry  Tuesday, October 10, 2017, 10:45, David Wang, Conditioning Station, Repair, , , Re-route TCS water lines. 8x

TCS  cooling polyurethane lines have been re-routed to solve to HV sparking issue on old configuration between lines and bais plate.  New re-routed system is tested to 70KV without spark. No leak has been found on new lines after the test.

ECO 4369, drawings and models IRH1715, IRH1716 have been issued and released for this job. Drawings and Models are located in PDM-ISAC1 -TCS polyurethane water lines re-route folder.

Entry  Tuesday, October 10, 2017, 10:38, David Wang, ITW, Standard Operation, , , 5 shielding blocks have been transferred from ITE to ITW . 

ITW is configured to take proton beam.

Entry  Friday, October 06, 2017, 13:25, Anders Mjos, Conditioning Station, Repair, , , HV Test 2017-10-06_HV_Water_Line_Test.xlsx

 HV was brought up to 70 kV for 1 h without sparks to test the new water installation.

Entry  Friday, October 06, 2017, 11:21, Isaac Earle, North Hot-Cell, Development, , , ISAC-1 active sump drain pipe modified IMG_0513.jpgIMG_0516.jpgIMG_0517.jpg

The 4" PVC drain line in the ISAC-1 active sump was modified so that the drain pipe terminates below the low level water line of the automatic pump-out system.  This will prevent backflow of sump gasses into the SHC, NHC, or TCS space if the air pressure in any of those rooms are lower than the sump air pressure.  The details of the modification were specified by Mechanical Services Group, and the work was done by Paul Jensen.  This system is defined in drawing IAM19183.

 

IMG_0513.jpg

 

IMG_0516.jpg

 

IMG_0517.jpg

Entry  Friday, October 06, 2017, 11:12, Isaac Earle, North Hot-Cell, Development, , , NHC module port shield block and TCS vessel shield block installed IMG_0472.jpgIMG_0476.jpgIMG_0479.jpgIMG_0481.jpgIMG_0486.jpg

 The NHC module port shield block (IRH1645) and the TCS vessel shield block (IRH1646) were installed yesterday in the target hall according to assembly drawing IRH1652.  No issues were encountered during installation.  Vacuum was pulled on the TCS and a leak check was performed on the shield: no leaks found.

 

IMG_0472.jpg

 

IMG_0476.jpg

 

IMG_0479.jpg

 

IMG_0481.jpg

 

IMG_0486.jpg

Entry  Thursday, October 05, 2017, 11:04, Anders Mjos, ITW, Maintenance, , , Installation of new valve for module move ventilation 

David installed the new ball valve and connections for the SAS project module move ventilation. SASP0482. Drawing reference ISK5029B.

Entry  Tuesday, October 03, 2017, 09:29, Travis Cave, ITW, Standard Operation, TM2, Ta#54, Module move 

 TM#2 with Ta#54 has been moved from the conditioning station to the west target station.

Entry  Thursday, September 28, 2017, 17:44, Anders Mjos, Conditioning Station, Standard Operation, TM2, Ta#54, Conditioning Ta#54 Ta#54.docxTa#54_BIAS_current_vs_voltage.xlsx

Thursday, September 28, 2017

Cooling water not yet connected to TM.

High leakage current still observed. 200 uA at 22 kV. Did not go past 25 kV. 


Friday, September 29, 2017, 14:05: Started heater ramping to 580 / 200 A at 1 A/min

Friday, September 29, 2017, 14:09: BIAS / EZL / EE at 20 / 10 / 1.5 kV. BIAS current at 90 uA


Monday, October 02, 2017, 10:29: Accidentally set BIAS current limit to 0 A (step size too large) at 28 kV. This also caused the TGHT to got to 0 A. Recovered to 580 A in 10 - 15 s.

Monday, October 02, 2017, 12:07: Ramping down heaters at 2 A / min

Entry  Thursday, September 28, 2017, 15:34, Anders Mjos, Conditioning Station, Development, TM2, , Changes to MP3 startup 

 Due to problems with the regulating valve WPV1, the VFD (Variable Frequency Drive) for the pump has been programmed to do a slow (2 min) ramp up. WPV1 has been bypassed and left fully opened. Work was done by Dave Morris

Entry  Thursday, September 28, 2017, 11:59, Travis Cave, Spent Target Vault, Standard Operation, , Ta#53, Spent Target move Vault_Storage_September_28_2017.pdf

The spent Ta#53 has been moved to the spent target vault. See attached file for details.

Entry  Thursday, September 28, 2017, 10:50, David Wang, Conditioning Station, Standard Operation, TM2, , Helium pressure test on TM2 window and HS water lines at TCS. 

  I did helium pressure test on TM2 containment box window and HS line at TCS. @ 70psi helium  for 3 minutes, HS:2.2XE-7 atm.cc/sec., Window:1.2XE-7 atm.cc/sec. There is no change on HS. But LR on window is bigger than before that was in E -9atm.cc/sec range.  

Entry  Wednesday, September 27, 2017, 09:02, Travis Cave, Conditioning Station, Standard Operation, TM2, Ta#54, Module move 

 TM#2 with Ta#54 has been moved from the south hot cell to the conditioning station.

Entry  Wednesday, September 27, 2017, 08:00, chad fisher, South Hot-Cell, Standard Operation, TM2, Ta#54, Ta#54 installed 

Containment box has been replaced onto TM2, interior of containment box vacuumed, and Ta#54 installed with new fasteners (high current torqued to 130 in lbs).

Entry  Tuesday, September 26, 2017, 14:27, Travis Cave, South Hot-Cell, Standard Operation, TM2, Ta#54, Electrical Check TM2_Ta54_elec_chk_SHC.PDF

Electrical check of TM#2 with Ta#54 at the south hot cell. See attached PDF for details.

Entry  Friday, September 22, 2017, 14:15, chad fisher, South Hot-Cell, Repair, TM2, , TM2 containment box off 20170922_140546.jpg20170922_140927.jpg

TM2 containment box has been removed. Found a piece of capton tape or tubing under table (see picture).

Entry  Friday, September 22, 2017, 12:13, David Wang, South Hot-Cell, Maintenance, TM2, , TM2 service cap inside inspection. TM2_serica_cap_inspection_002.JPGTM2_serica_cap_inspection_003.JPGTM2_serica_cap_inspection_004.JPGTM2_serica_cap_inspection_005.JPGTM2_serica_cap_inspection_008.JPG

Two side panels on TM2 service cap were removed for TM2 service cap inside inspection. A piece of cable tie was found inside cap closing to service tray entrance area. All blue nylon insulators are inspected. They look good. The broken cable tie is moved out of service cap.

 Panels are installed back after the inspection.

See attachments

Entry  Friday, September 22, 2017, 11:00, Travis Cave, South Hot-Cell, Standard Operation, TM2, no target, Electrical Check TM2_notgt_elec_chk_shc_09212017.PDF

Electrical check of TM#2 after the insulator change on thursday september 21.

Entry  Thursday, September 21, 2017, 16:26, Anders Mjos, South Hot-Cell, Standard Operation, TM2, , Inspection of Source Tray TM2_Source_Tray_EE_Insulator.pdf

Chad and Anders inspected the Source Tray today using the camera in the hot cell. A dark spot was observed on one of the four insulators separating the Extraction Electrode from the Ground Electrode. This could potentially influence the high leakage current. Some discolored areas were also observed in the Service Tray, but these was present when the module was built. See attachment for details.

Entry  Thursday, September 21, 2017, 12:07, chad fisher, South Hot-Cell, Repair, TM2, , Insulator Replacement 

Insulators ITD0053 and 54 have been replaced. All fasteners torqued to 56 in lbs.

 

Entry  Thursday, September 21, 2017, 10:48, Travis Cave, South Hot-Cell, Standard Operation, TM2, Ta#53, Electrical Check TM2_Ta53_elec_chk_shc.PDFTM2_Ta53_elec_chk_post_beam_shc.PDFTM2_notgt_elec_chk_shc_09202017.PDF

Electrical checks of TM#2 with Ta#53 and also with out a target.

Entry  Wednesday, September 20, 2017, 13:38, chad fisher, South Hot-Cell, Repair, TM2, , TM2 Insulator replacement 20170920_132813.jpg20170920_132820.jpg20170920_133244.jpg

Broken insulators ITD0053 and ITD0054 have been uninstalled from TM2.

Entry  Tuesday, September 19, 2017, 13:53, Travis Cave, South Hot-Cell, Standard Operation, TM2, Ta#53, Module move 

 TM#2 with Ta#53 has been moved from the west target station to the south hot cell.

Entry  Tuesday, September 19, 2017, 10:40, chad fisher, South Hot-Cell, Maintenance, , , South East Manipulator Maintenence 

Entered hot cell to preform replacement of slave tong cable. Existing cable shows no signs of wear so it has been re-installed. A spare tong cable has been loaded into a spare tong while in the hot cell in preparation for next time this cable needs to be replaced.

Entry  Friday, September 15, 2017, 14:12, Travis Cave, Conditioning Station, Standard Operation, TM3, no target, Module move 

 TM#3 has been moved back to the silo from the conditioning station.

Entry  Wednesday, September 13, 2017, 16:13, David Wang, Conditioning Station, Repair, TM3, , TCS turbo pumps are started.  

TCS and TM3 all vacuum pumps are started. Everything is fine.

Entry  Wednesday, September 13, 2017, 16:05, David Wang, Conditioning Station, Repair, TM3, , remove Tm3 service tray cover plate 

TM3 service tray cover plate has been removed. It is bagged and placed to TH b2 level south wall beside the silo.

Entry  Wednesday, September 13, 2017, 10:05, David Wang, Conditioning Station, Repair, TM3, , Switch off TCS water system and vacuums 

Preparing vent the TCS/TM3. We will remove TM3 service tray cover plate  after venting.

Entry  Friday, September 08, 2017, 14:08, David Wang, Conditioning Station, Repair, TM3, , TCS and TM3  

TM3 is located at TCS and it is pumping down now. TCS water system has been started.  All TCS water lines for TM3 module internal cooling are bypassed and looped at TCS top ground plate. Water only supply to TCS high  current conductors.

Entry  Friday, September 08, 2017, 11:20, Travis Cave, Conditioning Station, Standard Operation, TM3, no target, Module move 

 TM#3 has been moved from the north east silo to the conditioning station.

Entry  Tuesday, September 05, 2017, 10:25, Travis Cave, ITE, Standard Operation, TM4, UC#21, Module move 

 TM#4 with UC#21 has been moved from the conditioning station to the east target station.

Entry  Tuesday, September 05, 2017, 06:33, David Wang, Conditioning Station, Standard Operation, TM4, , Turned off TCS water system and vacuum system. 

Argon vent and disconnect TM4 at TCS.

Entry  Wednesday, August 30, 2017, 11:37, Travis Cave, Spent Target Vault, Standard Operation, , Ta#52, Spent Target move Vault_Storage_August_30_2017.pdf

The spent Ta#52 target has been moved from the south hot cell to the spent target vault. See attached PDF for details.

Entry  Tuesday, August 29, 2017, 09:01, David Wang, Conditioning Station, Standard Operation, TM4, , TM4 has been connnected at TCS. 

TM4 has been connected at TCS. TCS water system has been started for TM4. TM4 and TCS vacuum pumping down is good so far.

Entry  Tuesday, August 29, 2017, 08:59, David Wang, Conditioning Station, Standard Operation, TM4, , TM4 HS line leak checks 

TM4 HS line leak checks are done, at SHC and TCS. SHC: Helium spray. TCS: Helium  pressurize 70psi.  LD base LR 0.0 X E-9 atm.cc/sec.  No leak has been found on both leak checks. 

Entry  Monday, August 28, 2017, 14:40, Travis Cave, South Hot-Cell, Standard Operation, TM4, UC#21, Electrical Check TM4_UC21_elecchk_SHC.PDF

The results of the electrical check of TM#4 with UC#21 attached.

Entry  Monday, August 28, 2017, 14:34, Travis Cave, Conditioning Station, Standard Operation, TM4, UC#21, Module move 

 TM#4 with UC#21 has been moved from the south hot cell to the conditioning station.

Entry  Monday, August 28, 2017, 12:07, chad fisher, South Hot-Cell, Standard Operation, TM4, UCx#21, Ta#52 removed UCx#21 installed 

Ta#52 has been removed from TM$ and UCx#21 installed with new mounting and high current hardware. High current fasteners torqued to 130 in lbs.

Entry  Monday, August 28, 2017, 11:28, Travis Cave, ITE, Standard Operation, TM4, Ta#52, Module move 

 TM#4 with Ta#52 has been moved from the east station to the south hot cell.

Entry  Friday, August 25, 2017, 16:33, Anders Mjos, Conditioning Station, Repair, , , Testing HV after cooling line repair 2017-08-25_HV_Water_Line_Test.xlsx

 The BIAS voltage was brought up to 70 kV today and held there for 1h. No sparking observed.

Entry  Thursday, August 17, 2017, 14:38, Isaac Earle, North Hot-Cell, Development, , , 4/6 NHC roof blocks installed 7x

 Roof blocks IRH1641, IRH1642, IRH1643, and IRH1644 have been fully assembled, labeled, and installed as per drawing IRH1652.  Fabrication of TCS shield block (IRH1646) and NHC module port block (IRH1645) is still in progress.

 IMG_0381.jpg

 

IMG_0369.jpg

 

IMG_0368.jpg

 

IMG_0364.jpg

 

IMG_0362.jpg

 

IMG_0340.jpg

Entry  Tuesday, August 15, 2017, 12:10, Isaac Earle, North Hot-Cell, Development, , , ISAC Active Sump low water level measured 

The ISAC active sump in the Active Service Room (#002 on B2 level) was pumped out yesterday using the standard procedure (Section 5.5.2 of the ISAC Operators' Manual, V1.0).  The procedure makes use of the auto stop feature of the pump-out system which stops when a low level float switch is triggered.  The water level was measured after pumping stopped, and was found to be approximately 21" above the base of the sump.  A new section of pipe will be added to the 4" drain line in the sump to move the drain opening below the low level water line so that air in the sump is not pulled into the drain network (which could end up in the NHC or TCS space).

Entry  Tuesday, August 08, 2017, 13:26, Travis Cave, ITW, Standard Operation, TM2, Ta#53, module moved 

TM#2 with Ta#53 has been moved from the conditioning station to the west target station.

    Reply  Tuesday, August 15, 2017, 09:30, Anders Mjos, ITW, Standard Operation, TM2, Ta#53, TM2 radiation fields 

Travis Cave wrote:

TM#2 with Ta#53 has been moved from the conditioning station to the west target station.

 by Travis (measured at ~ 2' from module on service tray side):

at 3' 325 uSv/h

at 2' 640 uSv/h

Entry  Tuesday, August 01, 2017, 14:39, Travis Cave, South Hot-Cell, Standard Operation, TM2, SiC#36, Electrical Check TM2_SiC36_SHC_elec_chk.PDFTM2_SiC36_Postbeam_SHC_elec_chk.PDF

The electrical check of TM#2 with SiC#36 attached. Post beam at the south hot cell. See attached results allow the before beam electrical check results are posted here as well.

    Reply  Tuesday, August 15, 2017, 09:27, Anders Mjos, South Hot-Cell, Standard Operation, TM2, SiC#36, Electrical Check of target in SHC 

Travis Cave wrote:

The electrical check of TM#2 with SiC#36 attached. Post beam at the south hot cell. See attached results allow the before beam electrical check results are posted here as well.

by David and Chad after target removed from module:

Anode to target @500V - 65Kohm
Anode to HS - dead short
Target to HS@500V -62Kohm.

Entry  Wednesday, August 09, 2017, 16:39, Isaac Earle, North Hot-Cell, Development, , , NHC drain line into sump identified 

 The NHC drain line was tested by pouring approximately 10 gallons of water through the drain grate at the base of the NHC partition wall.  Water was seen a few minutes later pouring into the sump labeled "ACTIVE SUMP" from the light coloured pipe on the west side of the inside of the sump.  Rob Walker had previously said that the hot cells drain into the sump next to this one which is labeled "SANITARY SUMP", which appears to be incorrect.

Entry  Thursday, August 03, 2017, 17:08, Anders Mjos, Conditioning Station, Repair, TM2, , Power bump 

 Thursday, August 03, 2017, 17:08: Restarting vacuum and water system

Entry  Thursday, August 03, 2017, 15:02, Travis Cave, Spent Target Vault, Standard Operation, , SiC#36, Spent Target Move Vault_Storage_August_3_2017.pdf

 The spent SiC#36 has been moved from the south hot cell to the spent target vault.

Entry  Wednesday, August 02, 2017, 15:41, Keith C Ng, Assembly/Bench Test, Development, , , spare source tray build 20170802_sourcetray_RHB_8264.JPG20170802_sourcetray_RHB_8266.JPG

After re zeroing alignment telescope to master jig and adjusted parts into place:

 

Orientation: X = Left -, Right+; Y = Up +, Down -

 

Front wire target

X = 0.000, Y = 0.000

 

Rear wire target

X = 0.000, Y = +.008" (high)

 

All fasteners torqued to specification, steerer housing and assembly not installed yet. Weight of steerer assembly might cause rear to sag into place. Otherwise may attempt to split difference between the front and rear elements (alignment is on an angle in the horizontal vertical plane.)

Entry  Wednesday, August 02, 2017, 15:13, David Wang, South Hot-Cell, Standard Operation, TM2, , SHC, TM2 leak check on HS line. 

HS line is leak checked at SHC this afternoon by helium spay.  Leak detector base LR 0.0 XE-9atm.cc/sec. Base pressure 0.0Xe-4 torr. No leak has been found. This line will be helium pressured  at TCS. It had  a 1.7XE-7 atm.cc/sec leak rate on 70 psi helium at TCS  during last two target  checks.

 2017-08-03. Helium pressure test on TM2 HS line at TCS is done. 70psi helium, 3 minutes. base leak rate 0.0xE-7 atm.cc/sec. Result: 1.8XE-7atm.cc/sec leak which is almost same as before. This line has a very small leak on water block seal under helium pressure test  which we knew already. 

Entry  Wednesday, August 02, 2017, 15:09, David Wang, ITW, Standard Operation, TM2, , TM2 was disconnencted in ITW yesterday. 

Tm2 was disconnected in ITW yesterday. ITW EL cable crimp ring was broken. John Chow replaced this ring this afternoon.

Entry  Monday, July 31, 2017, 09:44, Travis Cave, Conditioning Station, Standard Operation, TM3, no target, Module move 

 TM#3 has been moved back to the NE silo from the conditioning station.

Entry  Tuesday, July 18, 2017, 16:53, Anders Mjos, Conditioning Station, Development, TM3, No target, Conditioning TM3 

Conditioning continues today with resistors removed from the HV cable

Tuesday, July 18, 2017, 16:53: BIAS / EZL 50 / 25 kV - no sparks

 Tuesday, July 18, 2017, 16:56: BIAS / EZL 55 / 27.5 kV - one spark


TM3 remained at 55 kV over night. Turbo pumps tripped twice and was restarted and HV recovered by RIB ops. Last recovery brought EZL to 16 kV (not 27.5 kV)

About 25 sparks over 15 h. No sparks for the last 3 h

Wednesday, July 19, 2017, 08:12: EZL to 27.5 kV

Wednesday, July 19, 2017, 08:38: BIAS to 57 kV

Wednesday, July 19, 2017, 08:46: BIAS to 57.5 kV

Wednesday, July 19, 2017, 09:05: BIAS to 59 kV

Wednesday, July 19, 2017, 09:19: BIAS to 60 kV

Wednesday, July 19, 2017, 09:28: EZL to 30 kV

Wednesday, July 19, 2017, 12:25: Heavy sparking. Lowered BIAS to 30 kV

Wednesday, July 19, 2017, 12:37: Increased BIAS again towards 50 kV, but heavy sparking again between 45 and 50 kV. Lowered back to 30 kV

Wednesday, July 19, 2017, 12:40: BIAS at 46 kV

Wednesday, July 19, 2017, 12:42: BIAS at 47 kV

Wednesday, July 19, 2017, 12:44: BIAS at 48 kV

Wednesday, July 19, 2017, 12:48: BIAS at 50 kV

Wednesday, July 19, 2017, 14:50: BIAS at 55 kV after ~2h without sparking at 50 kV

Wednesday, July 19, 2017, 15:12: Sparking. Lowered to 40 kV

Wednesday, July 19, 2017, 16:39: BIAS at 55 kV


Friday, July 21, 2017

Observed top of module inside target hall during HV sparks using crane cameras. No sparks observed, but some faint sound could be heard. Module still sparks at 60 and 55 kV. Have to lower to 40 kV to stop sparking.

Friday, July 21, 2017, 13:25: BIAS / EZL at 50 / 25 kV for without sparking for the last 90 min

Entry  Tuesday, July 18, 2017, 15:04, Travis Cave, Crane, Maintenance, , , Failure of the ISAC TH Crane Rotate. 

 Earlier in the day it was noted that the rotate function of the crane had creased operation. After David has finished the block moves. Don and I checked the Crane's control unit in the ISAC crane control room and found the breaker tripped for the rotation. The breaker was reset and the crane's rotation is now operational. If this occurs in the future only Travis Cave, Don Jackson or a TRIUMF Electrician are allowed in that control box as it is a 480Volt system. Don or I because we know what we are looking for and the Electrician because they are allowed to touch with and deal 480 V systems. 

Entry  Monday, July 17, 2017, 16:28, Anders Mjos, Conditioning Station, Development, TM3, No target, Conditioning TM3 TM3_HV_conditioning_2017-07-17.docx

50 kV stable with less than 1 spark/h during the weekend by RIB obs.

Today 57 kV reached, but observed sparking on the resistors of the new HV cable. The cable will be removed to take out the resistors, before reinstalling it.

The target hall was locked out, but has now been reopened. This was to avoid sparking to the HV cover.

    Reply  Monday, July 17, 2017, 17:50, Aurelia Laxdal, Conditioning Station, Development, TM3, No target, Conditioning TM3 2017-07-17-16_53_03.grab.LWYG0y.png

Anders Mjos wrote:

50 kV stable with less than 1 spark/h during the weekend by RIB obs.

Today 57 kV reached, but observed sparking on the resistors of the new HV cable. The cable will be removed to take out the resistors, before reinstalling it.

The target hall was locked out, but has now been reopened. This was to avoid sparking to the HV cover.

 EL was brought to 27.5kV.

Entry  Thursday, July 13, 2017, 10:53, Travis Cave, Conditioning Station, Standard Operation, TM3, no target, Module move 

 TM#3 has been moved from the north east silo to the conditioning station.

Entry  Wednesday, July 12, 2017, 11:05, Anders Mjos, Conditioning Station, Maintenance, , , Testing of new high voltage cable 2017-07-12_HV_Cable_Test.xlsx

The target hall has been locked-out as per Document-70039.

Forced IG1, IG1S and IG2 to switch on BIAS power supply

Wednesday, July 12, 2017, 11:53: 70 kV at 0.16 mA

2 sparks observed shortly after 70 kV was reached

Wednesday, July 12, 2017, 12:59: No sparks for the last hour.

BIAS power supply off. Forces removed.

Entry  Tuesday, July 11, 2017, 10:20, Travis Cave, ITE, Standard Operation, TM4, Ta#52, Module move 

 TM#4 with Ta#52 has been moved from the conditioning station to the east target station.

Entry  Monday, July 10, 2017, 10:19, David Wang, Conditioning Station, Standard Operation, TM4, , Turned off TCS water system 

Prepare for TM4 move tomorrow morning.

Entry  Monday, July 10, 2017, 09:09, Dan McDonald, North Hot-Cell, Repair, , , manipulator cart repair IMG_2955.JPG

A  hydraulic leak was found on the manipulator  install and repair cart, upon further investigation the cause was a faulty cylinder. Once the cylinder was removed and disassembled the inner bore was found to be scored beyond repair. Another point of interest was that the rod was painted to the point that when retracted it compromised the rod seal causing the cylinder to leak. attached are photos outlining the issues. new cylinders are being sourced and will be installed upon arrival. We have found that there is interaction between the tops of the cylinders and the bed of the cart when fully retracted and compressed, this might require some modifications to ensure proper operation in the future.

 

 

Entry  Thursday, July 06, 2017, 14:23, Isaac Earle, North Hot-Cell, Repair, , , Slave side Z motion tape snapped on NHC right side manipulator 

The NHC right side manipulator was evaluated today to check if operation was normal through all ranges of motion.  The manipulator was first moved through usual motions without the electric motion drives: the feel was fairly normal, a sound could be heard from the master side Z motion tapes rubbing on the sides of the pulleys, this problem had been identified a few weeks ago however it was significantly reduced since the master side upper and lower Z motion tapes were tensioned yesterday (using CRL repair manual)

The Y motion drive was then tested:  with the master arm close to the window we attempted to move the slave arm close to the slave side window using the Y motion drive; part way through travel the arm stopped moving and would not move any further towards the window.  At this point it was approximately 1 foot from the slave side window.  (I recall that when the manipulator was installed in the wall it was difficult to get the slave end fully horizontal, the arm would travel part way, then stop for seemingly no reason.  Eventually after multiple attempts I got it to reach the horizontal position)

The Z motion was then tested.  The slave end was moved to the fully extended position.  At this point when the Z drive was continued downwards the master side moved up.  Once it reached the upper limit the drive continued which caused the Z motion tape on the slave end to snap.  At this point testing was stopped.

 

Our plan is to assemble and test the left side manipulator after the manipulator handling cart repair is completed.  If the left side has the same problems it is likely a manufacturer defect.  If not, the problems with the right side may be due to a timing error introduced when we removed the slave end to fit the assembly and cart through the roof hatch from the ISAC-1 experimental hall.  In either case we plan to have  CRL technician come in to address the issues and tune-up both arms before use.

Entry  Wednesday, July 05, 2017, 15:36, Isaac Earle, North Hot-Cell, Development, , , NHC and SHC nuclear ventilation flow sensors installed IMG_0264.JPGIMG_0265.JPG

 Installation of new flow sensors and transmitters for the NHC and SHC duct lines was completed in the target hall today.  The sensors are Dwyer DS-300-8 in-line sensors for 8" pipe; The transmitters are Dwyer MS0121 magnesense differential transmitters with 4-20mA output.  The transmitters will be wired to the new PLC control system when the upgrade is done.

 

IMG_0264.JPG

 

IMG_0265.JPG

Entry  Wednesday, July 05, 2017, 11:18, Anders Mjos, Conditioning Station, Maintenance, TM4, Ta#52, Changed electrical configuration to cathode bias 

 John Chow configured TCS to cathode bias mode (IRH1538). The anode P/S is in positive mode.

Entry  Thursday, June 29, 2017, 14:42, Travis Cave, Spent Target Vault, Standard Operation, , UC#20, Spent Target Move Vault_Storage_June_29_2017.pdf

 The spent UC#20 has been moved from the south hot cell to the spent target vault. It was placed in pail #150 and spot 1B in the vault. See attached for details of the vault.

Entry  Thursday, June 29, 2017, 11:55, David Wang, Conditioning Station, Repair, , , TCS HV cable and feed through installation 

John Chow and I installed new TCS HV cable and feed through with their mounting panel back to TCS Faraday cage this Tuesday. ECO-4269 has been issued for the new cable feed through and mounting panel.

Entry  Thursday, June 29, 2017, 11:12, Anders Mjos, South Hot-Cell, Standard Operation, TM4, UC#20, Post Irradiation Examination (PIE) 

The target was inspected by Chad and Anders. Photos are available on DocuShare. It was noticed that the target tube heater terminals had lifted up from the insulator on the target assembly as seen in this Photo. This has later been detemined to be from the assembly, where additional clearance was required and achieved by installing washers.

Entry  Wednesday, June 28, 2017, 16:43, Anders Mjos, Conditioning Station, Standard Operation, TM4, Ta#52, Conditioning Ta#52 Ta#52.docx

NEW HV cable for BIAS installed earlier this week.

Wednesday, June 28, 2017, 16:42: BIAS at 20 kV

Wednesday, June 28, 2017, 16:46: BIAS at 30 kV, EZL at 15 kV

Wednesday, June 28, 2017, 17:00: BIAS at 35 kV, EZL at 17.5 kV


The voltage response on TBHT and TGHT changed as the target was heated up. This was later determined to be due to target shorting to heat shield and the grounding of the power supplies being achieved at the HV pedestal in the target hall and not in the HV enclosure as is done online. When this was changed, the target operated normally again.

Entry  Wednesday, June 28, 2017, 10:00, David Wang, Conditioning Station, Standard Operation, TM4, Ta#52, TM2 has been connected at TCS 

I started TCS water system.

Entry  Wednesday, June 28, 2017, 09:14, Travis Cave, Conditioning Station, Standard Operation, TM4, Ta#52, Electrical Check TM4_Ta52_Elec_chk_SHC_CSvac.PDF

Results of electrical check of TM#4 with Ta#52 at the south hot cell and the conditioning station under vacuum.

Entry  Tuesday, June 27, 2017, 14:34, David Wang, Conditioning Station, Standard Operation, TM4, , TM4 vacuum has been connected at TCS 

Turbo -pumps are started . The vacuum looks good so far.

Entry  Tuesday, June 27, 2017, 10:26, David Wang, South Hot-Cell, Standard Operation, TM4, Ta#52, Leak check on TM4 HS line at SHC 

LD base LR:0.0Xe-9 atm.cc/sec. No leak has been found during the check.  The HS line will be helium pressurized at TCS this week.

Helium pressurized the HS line at TCS. 70 psi 2 minutes, 0.0 x E-9 atm.cc/sec. No leak.

Entry  Tuesday, June 27, 2017, 09:14, Travis Cave, Conditioning Station, Standard Operation, TM4, Ta#52, Module move 

 TM#4 with Ta#52 has been moved from south hot cell to the conditioning station.

Entry  Monday, June 26, 2017, 11:47, chad fisher, South Hot-Cell, Standard Operation, TM4, Ta#52, UC#20 Removed Ta#52 installed 

UC#20 has been removed from TM4 and put in a bucket back-filled with argon. Ta#52 has been installed onto TM4 with new fasteners. High current torqued to 130 in lbs.

Entry  Monday, June 26, 2017, 11:42, Travis Cave, South Hot-Cell, Standard Operation, TM4, UC#20, Module move 

 TM#4 with UC#20 has been moved from the east target station to the south hot cell. Also the shield plug was remotely installed as well after David set it up.

Entry  Friday, June 23, 2017, 17:28, Isaac Earle, North Hot-Cell, Development, , , NHC module flange and cameras installed IMG_0231.jpgIMG_0234.jpgIMG_0240.jpgIMG_0245.jpgIMG_0240.jpg

 The North Hot Cell module support flange (IRH1152D) was installed on June 21, 2017 using 1/8" rubber sheet as a sealing gasket.  The rubber was glued at the seams with Loctite 495 instant adhesive.  Cameras with all required wiring and connectors were installed on the mounting bars (IGN0325D) and then aligned to provide the same view as at other module installation locations in the target hall.  A cable with 5 video signals, and a camera power cable was routed from the south wall in the target hall (where video line connections are), to the panduit on the north wall.  An additional section of cable will be installed to link to the flange cameras after cable covers are installed on the floor.

 

IMG_0231.jpg

 

IMG_0234.jpg

 

IMG_0245.jpg

 

IMG_0240.jpg

Entry  Friday, June 23, 2017, 12:08, David Wang, Crane, Repair, , , TH crane inspection and probem fixing by Gordon crane  

Gordon crane technician Peter came in today and checked TH crane. Maico and I were there with him. What he found is that brake gap on both side of main hoist decreased after months of using.  The solution is to lock the automatic self adjustment system so the gap will be fixed there. Each year during annual inspection, they will adjust the gap manually. After he locked both side of device, I tested the crane up and down couple of times. The brakes work fine. 

Entry  Thursday, June 22, 2017, 11:10, chad fisher, South Hot-Cell, Maintenance, , , In cell airline 

The in cell airline has preemptively been replaced. The hose was, as far as I know the original.

Entry  Monday, June 19, 2017, 07:29, David Wang, Conditioning Station, Standard Operation, TM2, , Update TH MS project schedule. Target_Hall_shedule_132_Apr_to_Sep.pdfTarget_Hall_shedule_132_Apr_to_Sep.mpp

Update TH MS project schedule. See attachment 1,2.

Entry  Thursday, June 15, 2017, 11:29, Isaac Earle, North Hot-Cell, Development, , , NHC inlet ducting installed IMG_0217.jpgIMG_0218.jpgIMG_0219.jpgIMG_0214.jpg

The North Hot Cell inlet ducting assembly was installed today in the target hall at the north end of the NHC roof block.  A small section of the perforated aluminum sheet on the TCS cage had to be trimmed for the assembly to fit (see IMG_0214).  At each end of the assembly it was fastened to the roof structure using a 1/4"-20 tapped hole in the steel roof, and a 1/4"-20 anchor in the north wall of the target hall.  The base flange of the assembly was sealed to the roof structure and TH wall using Sikaflex 1A polyurethane sealant on all sides.

 

IMG_0217.jpg

 

IMG_0218.jpg

 

IMG_0219.jpg

 

IMG_0214.jpg

Entry  Tuesday, June 13, 2017, 13:41, David Wang, ITW, Standard Operation, TM2, , TM2 has been connected in ITW. 

Yasmine and I connected TM2 in ITW today. the control page is set to febiad mode. Both gas line in ITW are opened for febiad run. All connections are double checked. Module connection checklist is finished.  All turbo pumps are started now. Everything is good so far. The TM2 is ready for conditioning when the ITW vacuum is good enough.

Entry  Tuesday, June 13, 2017, 11:10, Grant Minor, Crane, Maintenance, , , ISAC THall Crane 100% / 125% Load Test Documentation - 2011 ISAC_TH_Crane_Load_Test_Norelco_Sept_30_2011.pdfIMG_8722.JPGIMG_8752.JPGIMG_8735.JPGIMG_8745.JPG

The ISAC Target Hall Crane was load tested and re-certified in January 2011 prior to doing a near-capacity lift for the North Hot Cell roof structure (IRH1112E).

Photos and documentation from Norelco is attached.

- Grant

Entry  Tuesday, June 13, 2017, 09:57, Travis Cave, ITW, Standard Operation, TM2, SiC#36, module moved 

TM#2 with SiC#36 has been moved from the conditioning station to the west target station.

Entry  Monday, June 12, 2017, 13:51, Travis Cave, Spent Target Vault, Standard Operation, , , Spent Target move Vault_Storage_June_12_2017.pdf

The spent Ta#51 target has been moved from the south hot cell to the spent target vault. It was placed in pail#149 and put in spot 8B of the vault.

Entry  Friday, June 09, 2017, 11:21, chad fisher, North Hot-Cell, Maintenance, , , Model 'N' Slave Removal Through Roof 

Isaac and Chad disengaged the slave end of the manipulator and performed a slave removal through the slave removal roof hatch. This is part of investigation into a 'Z' motion tape that is "rubbing" on its drum on the master side of the manipulator during manual 'Z' retraction of 'Z' extension.

This also was the first test of the concept of removing the manipulator slave through the manipulator hatch that was built into the roof.

The lifting bail on the slave end of the manipulator was not centered to the hatch as per design but this did not compromise the procedure at all and the procedure otherwise followed the design intent.

Pictures can be located on Docushare  http://documants.triumf.ca/docushare/dsweb/View/Collection-20157

 

 

Entry  Thursday, June 08, 2017, 08:35, David Wang, Conditioning Station, Development, TM2, , TM2 gas line reconfiguration on the module top. TM2_gas_line_on_the_top_002.JPG

Reconfigured TM2 gas line on the module top. It matches with the febiad gas line we are using on service tray now. Facing the module, both of them should be that right side line of two SST lines on feed-through. The gas line on TM2 was leak checked with a blind cap installed on service tray side and LD connected on module top this Tuesday. It is leak free with helium spray on the top of module and service tray.

Entry  Thursday, June 08, 2017, 07:37, David Wang, Conditioning Station, Standard Operation, TM2, , Helium pressure test on TM2 water llines at TCS. TM2_helium_pressure_test..png
  The helium pressure test on HS line is done at TCS this morning. I got the same result as last time when we helium pressure it it with first target in April. The leak  rate on this line is 1.8 XE-7atm.cc/sec. So, we know this leak is mostly on the line, but not on the VCR joints connecting the target.  See attachment for last time(April) checking e-log. The leak could be from water block which is same as other lines. I do not think this leak rate will affect the operation.

The attachment can not be opened for some reasons. Please check TM2 leak check  2017-03-13 e- log for last time test result and comment.

Entry  Wednesday, June 07, 2017, 13:34, David Wang, Conditioning Station, Standard Operation, TM2, , TM2 and TCS vacuum system has been connected. 

I started all turbo pumps.

Entry  Wednesday, June 07, 2017, 13:33, David Wang, Conditioning Station, Standard Operation, TM2, , TM2 SiC#36 leakc check and electrical check. TM2_SiC_36#_leak_check_an_delectrical_check..pdf

The results  are good. See attachment.

Entry  Tuesday, June 06, 2017, 13:42, chad fisher, South Hot-Cell, Standard Operation, TM2, SiC#36, Ta#51 removed SiC#36 installed 

This afternoon Ta#51 was removed from TM2 and SiC#36 installed.

All new fasteners used. High current fasteners torqued to 130 in lbs.

 

 

Entry  Wednesday, May 24, 2017, 08:11, David Wang, ITW, Standard Operation, TM2, , TH schedule 132 update weekly Target_Hall_shedule_132_Apr_to_Sep.mppTarget_Hall_shedule_132_Apr_to_Sep.pdf

See attachments.

Entry  Tuesday, May 23, 2017, 14:10, David Wang, ITE, Standard Operation, , , ITE water interlock check is done. 

We do this check once a year now. Rene found a target oven reset issue during the check . He will consult with Friedhelm. The interlock check is good.

Entry  Tuesday, May 23, 2017, 13:30, David Wang, ITE, Standard Operation, TM4, , TM4 has been connected in ITE 

Yasmine and I connected TM4 in ITE . All turbo pumps are started.

Entry  Tuesday, May 23, 2017, 10:41, Travis Cave, ITE, Standard Operation, TM4, UC#20, Module move 

 TM#4 with UC#20 has been moved from the conditioning station to the east target station.

Entry  Friday, May 19, 2017, 13:49, David Wang, Conditioning Station, Repair, TM4, , TM4 TP1 at TCS 

TM4 TP1 is replaced. TCS and TM4 was argon vented before the job.The job took about 30minutes.  I started the all turbo pumps after job. All pumps work fine. The TCS vacuum is good.     

Entry  Friday, May 19, 2017, 12:25, David Wang, Conditioning Station, Standard Operation, TM4, , TCS and TM4 water flow measurement.  

 

 

  TCS(LPM) Freq(HZ) TCS+TM4(LPM) Freq(HZ)
Ta 5.5 106 3.7 68
Tu 5.6 107 4.3 79
Coil(RU only) 5.8 112 4.6 92
HS 7.0 13 6.6 12
MSP 6.4 21 5.8 21
EE 5.6 112 3.8 77
Window 4.5 81 4.3 78

 

Entry  Thursday, May 18, 2017, 11:36, Travis Cave, Conditioning Station, Standard Operation, TM4, UC#20, Electrical Check TM4_UC20_Elec_chk_CS_vac.PDF

Electrical check of TM#4 with UC#20 at the conditioning station under vacuum. See attached for details.

Entry  Thursday, May 18, 2017, 10:41, Travis Cave, Spent Target Vault, Standard Operation, , UC#19, Spent Target move Vault_Storage_May_18_2017.pdf

The spent UC#19 target has been moved from the south hot cell into the spent target storage. It was placed in pail #145 and put in tray one spot C. See attached PDF for all vault details.

Entry  Thursday, May 18, 2017, 10:08, David Wang, Conditioning Station, Standard Operation, TM4, , TM4 TP1 at TCS 

TM4 TP1 was found making some noise during operation this morning. The current draw was check then. It was 1.8 A which is higher than 1.0A normal range. The pump body temperature was higher by hand feeling. But,1.0 hour later when checking again, everything on the pump goes back to normal. It is still fine so far. I will watch on this pump closely.

 2017-05-19,morning.  The TM4 TP1 stopped running last night.  I tried to start it this morning. But, It can't pass 6KRMP even. I think we have to replace it.    E- fault will be issued as well.   

Entry  Wednesday, May 17, 2017, 08:35, David Wang, Conditioning Station, Standard Operation, TM4, , TCS turbo pumps was started yesterday 

Anders started TCS turbo-pumps yesterday. The TCS and TM4 pumping down is good so far. I started TCS water pumps this morning for TCS water flow check.

2017-05-17 morning:  Stopped the water pumps. The field around the TM4 is high because of spent target in SHC. The water flow measurement will be delayed to this Friday.

Entry  Wednesday, May 17, 2017, 08:31, David Wang, South Hot-Cell, Standard Operation, TM4, , Leak check on TM4 HS line at SHC 

Chad and I finished leak check on HS line with UCx target installed on it.  Base Leak rate:0.0X 10^-9 atm.cc/sec, Base pressure 0.0X 10 ^-4 torr.  Sprayed helium to VCR joints.   No leak has been found . The line will be pressurized with helium at TCS.

 Helium pressure test on TM4 HS line is done at TCS. BLR 0.0XE-9 atm.cc/sec. 70psi helium , 2 minutes. No response. The line is leak free.

Entry  Tuesday, May 16, 2017, 14:19, Travis Cave, Conditioning Station, Standard Operation, TM4, UC#20, module moved 

TM#4 with UC#20 has been moved from the south hot cell to the conditioning station.

Entry  Tuesday, May 16, 2017, 14:18, Travis Cave, South Hot-Cell, Standard Operation, TM4, UC#20, Electrical Check TM4_UC20_Elec_chk_SHC.PDF

TM#4 with UC#20 has had the electrical check done on it  at the south hot cell, see attached for details

Entry  Tuesday, May 16, 2017, 13:23, chad fisher, South Hot-Cell, Standard Operation, TM4, UC#20, UC#20 Installed 

UCx#19 has been removed from TM4 and UCx#20 installed.

UCx#19 still had water in it at pressure and sprayed when the VCR was undone. It was quickly re-tightened but not before significant water pooled beside the main Mykroy standoff and table. Contacted Anders would suggested to soak it up with some wipes and continue, which I did.

New target fasteners including high current. High current fasteners torqued to 130 in lbs.

Entry  Tuesday, May 16, 2017, 10:28, Travis Cave, South Hot-Cell, Standard Operation, TM4, UC#19, module moved 

TM#4 with UC#19 has been moved from ITE to the south hot cell.

Entry  Friday, May 12, 2017, 07:42, David Wang, Crane, Repair, , , TH crane burning smell, smoke, and big noise on east side main hoist brake assembly. 

This morning, when I prepare for today's crane check, The crane made a very strong noise without any load during the full speed up motion. I stopped the crane right away, and noticed that east side of main hoist motor area was smoking . The crane was moved to east end. And, I climbed up to the top, and found the smoke is coming form brake side, and should be produced by braking. The smell is same as before.Unless other thing is wrong,  I think Gordon crane technician has to adjust the gap to a proper distance on both side of the main hoist. I feel very uncomfortable by operating the crane this way. They have to figure out what is wrong on these new brake assembly installation.

2017-05-12. This morning , Crane technicians increased both side of main hoist brake gaps today. They found on east side brake assembly, The gap is automatically closed after some  jogging motions. Peter think this is caused by torque produced by automatic adjustment springs on brake. This torque rotate  the gap adjustment device and closed the gap.  We operate the crane for a while with 20000lbs load on it after gap adjustment. The rattling sound is still there at slow up motion.  But, The main hoist braking sound is softer and gentle comparing to past month.This sound is more close to the sound before we replaced the brake assembly. So, This adjustment could be right in my view.  They checked  gaps after 0.5 hours operation. Everything is still fixed there . No change. They suggest we keep operating the main hoist, and they will be back on next Monday check again.  I operated the main hoist up and down in different speed motion for 1 hour after they left. Everything works fine. Braking are gentle. No strange sound and smoke during up or down. I will do  more operation on Monday morning before they come. Lets see the result after their checking.  

2017-05-15 This morning, 20minutes of crane main hoist up and down test with lots jogging and braking. The braking sound is softer and gentle. Everything works fine.

2017-05-15.  Gordon crane technician Peter came in during lunch time. Both side main hoist brake gaps have been checked. They are still at the same position as last Friday. The gap is not changed after operation. Peter will be back on next Monday and check everything again.  

Entry  Thursday, May 11, 2017, 16:10, Isaac Earle, North Hot-Cell, Development, , , NHC roof block to TH north wall gap sealed 

 The gap between the north face of the NHC roof block and the target hall north wall in the area where the NHC inlet ducting will be installed has been sealed with Sikaflex 1a flexible polyurethane sealant applied over foam backer-rod.

Entry  Wednesday, May 10, 2017, 14:00, Anders Mjos, South Hot-Cell, Development, , ITE-Ta-LP-FEBIAD, Test target examination 

Chad and Anders inspected the test target in the hot cell today. The lid had been previously removed.

  • The EE looked to have performed well. 
  • A piece of Ta foil was found inside the heat shield. It is not clear if this has been there during operation or if it entered the heat shield while in the hot cell. The foil has markings which indicate that it has seen heat.
  • Travis measured 40 MOhm at 500V between heat shield and anode after the target was removed.

Photos are available on DocuShare

Entry  Wednesday, May 10, 2017, 13:42, Anders Mjos, Conditioning Station, Repair, , , Leaky gauge at TCS:TS2 (e-fault: 9609) IRH1056_-_Leaky_Gauge.pdf

 Neil Wong will fix this leak tomorrow Friday.  See attached schematics for location.

Entry  Tuesday, May 09, 2017, 12:45, David Wang, Conditioning Station, Repair, TM3, , TM3 service tray side panel is cleaned and installed back to TM3 TM3_service_tary_side_panel_005.JPGTM3_service_tary_side_panel_001.JPGTM3_service_tary_side_panel_004.JPG

TM3 service tray side panel is cleaned and installed back to TM3 this morning. I visually inspected service tray insulators. Nothing is changed comparing to inspection before.Nine screws are installed on  panel to hold it onto TM3.

Entry  Tuesday, May 09, 2017, 07:00, David Wang, Conditioning Station, Repair, TM3, , Follow up Aurelia's entry, TM3 and TCS current limits investigation.  

Aurelia and I investigated this current limit issue May 8th. First, By separating TM3 from TCS. we found the problem is on TCS side. We did a Megga test on TM3 as well. TM3 is good at 1KV megga test. After that, The insulators between TCS to ground is test. they are good which could hold 1G ohm at 1000V megga test. So the problem should be on power supply side  including power supply itself ,cables and transformer. Later, Tom and John found the TCS bias HV cable from power supply to HV chase top in faraday cage is broken down. It can not hold 5KV on HV test now. This cable should hold 100KV. But not this time. Tom also found  the adapter on Faraday cage could be designed in a better way. The broken cable was removed yesterday. John and Tom will order an exactly same cable from Glassmen.

Entry  Monday, May 08, 2017, 14:46, Travis Cave, Spent Target Vault, Maintenance, , , Mini Vault Door 

 Mini Vault Door as some difficulty over coming a small hump on its track. To open the door one needs to give the door  a slight tug while it is opening to over come this hump.

Entry  Monday, May 08, 2017, 09:49, David Wang, Conditioning Station, Standard Operation, , , TH schedule 132 update weekly Target_Hall_shedule_132_Apr_to_Sep.mppTarget_Hall_shedule_132_Apr_to_Sep.pdf

Update TH schedule weekly to show the job process.

Entry  Saturday, May 06, 2017, 13:30, Aurelia Laxdal, Conditioning Station, Repair, TM3, no target, TM3 current limiting  

Today the voltage was raised from 65kV to 65.7kV. After about 10min at this level TM3 started current limiting. TM3 was not sparking when this happened.

ISAC OPS turned it OFF and then tried to ramp it back ON, but could not do it due to the current limiting.

I turned OFF/ON the PS (locally) 20ming ago and and then tried to get it back from the Control Room, but around 4-5kV it started current limiting.

Turned everything OFF on EPICS for the time being. We'll investigate on Monday.

Over the night the sparking rate at 65kV was from 6 to 2 sparks per hour. It tripped OFF once over the night: backing valves closed, tripping the turbos, tripping IG1 and turning OFF the BIAS. At that time ISAC OPS got it back smoothly.

Entry  Friday, May 05, 2017, 19:36, Aurelia Laxdal, Conditioning Station, Repair, TM3, no target, TM3 HV test at TCS up to 65kV 

Today TM3 HV conditioning went up to 65kV. I'll leave it here over night. ISAC OPS have instructions to keep an alarm on the HV, and ion gauge and turbo pump (TP2 tripped 3 times due to sparking).

Entry  Friday, May 05, 2017, 11:53, David Wang, Conditioning Station, Repair, TM3, , sparking on TM3 serice cap top. 

Sparking was found this morning inside HV cover on TCS in TH while TM3 was HV conditioning at TCS. The TCS bias was set to 50KV when I found this spark. It sparks between HV cover front side wall to a KF 25 clamp on HS water terminal. The KF 25clamp is used in this situation on HS water line top because the HS line is opened inside module, and we need a vacuum seal on the top of this line.  Actually, The clap is much smaller than the corona ring on HS terminal, and the corona ring is more close to side wall. But there is a 90 degree straight corner on this clam. So the spark happened between the side wall and this 90degree corner on the clamp. We can not change the clap now since it will break vacuum. So, we decide to do HV test without HV cover installed onTM3 at TCS. A work permit is issued for  this. Lock out procedure: Document-70039 is clarified in WP.

Entry  Friday, May 05, 2017, 11:06, David Wang, Crane, Standard Operation, TM3, , TH crane is used for 5 shielding blocks transferring.  

  TH crane is used for transferring five shielding blocks(30000lbs) today. All brakes work fine. Mostly, I do not need crane slow up motion for this job so during 1 hour moving, no rattle sound and burning smell has been found.  I think TH crane is good to use as we decided. 

Entry  Thursday, May 04, 2017, 19:10, Aurelia Laxdal, Conditioning Station, Repair, TM3, no target, TM3 HV test at TCS up to 50kV 

Today TM3 was conditioned up to 50kV. At 50kV sparking started and to go higher in voltage it needs more conditioning time. Lowered it to 49kV for the night.

Entry  Thursday, May 04, 2017, 14:06, David Wang, Conditioning Station, Repair, TM3, , A vacuum to air leak on TM3 service cap round side panel was found and fixed..  

During TM3 roughing down yesterday afternoon,The vacuum gauges CG1 and CG1S stopped at 1.20 torr and refused to drop down. Leak detector was used to found where the problem was. LD was in rough detecting mode and showed 2.7xE-6 atm.cc/sec as base leak rate.  Spray medium amount of helium to TM3 service top, and found this leak was on round panel of TM3 side wall. LR climbed to E-4 atm.cc/sec range on helium spraying. In my vie,One 10# socket head screw was not tightened properly after cameras job and caused this.  The TCS was vented. The panel was took off and reinstalled. O-ring on the panel  was replaced by a new one as well. Then TCS was pumped down again. The leak disappeared .  All turbo pumps on TCS and TM3 were started successfully later.

Entry  Tuesday, May 02, 2017, 18:33, Aurelia Laxdal, South Hot-Cell, Repair, TM3, no target, TM3 HV tests at atmosphere for Each Line(s) after the Fiber Glass removal May 2, 2017 

Today a HV test at atmosphere was performed for Each Line(s), while floating the other lines. THIS TEST AT ATMOSPHERE IS THE FIRST ONE AFTER THE FIBER GLASS WAS REMOVED.

Please note:

a). the Einzel Lens line (Y) was grounded.

b). after the fiber glass was removed the "R-U COIL" line and the "(F) Plasma" (which is the Anode line) were shorted to the BIAS voltage.

Tests performed:

1. Applied up to 32kV to "(A) OVEN -"

Sparks occurred at 32kV between the Extraction Electrode holder and the Ground Electrode.

2. Applied up to 33kV to "(B) OVEN +"

Sparks occurred at 33kV but we could not identify the spark location.

3. Applied up to 31kV to "(C) TUBE -"

Sparks occurred at 31kV between the Extraction Electrode holder and the Ground Electrode, at the top and the bottom.

4. Applied up to 30kV to "(D) TUBE +"

Sparks occurred at 30kV between the Extraction Electrode holder and the Ground Electrode, 2 spots at the bottom.

5. Applied up to 30kV to "(P-Q) COIL +"

Sparks occurred at 30kV between the Extraction Electrode holder and the Ground Electrode, all around.

6. Applied up to 30kV to "(R-U) COIL -", to "(F) Plasma" the Anode, to "(E) Cavity" or MSP, "(G) Gas", and  "(J) Heat Shield" - all these are "connected" together at the BIAS voltage.

Sparks occurred around 29-30kV at the Extraction Electrode holder and the Ground Electrode, at the bottom.

8. Applied up to 23kV to "(I) EE" - this is for the Extraction Electrode.

Sparks occurred at 23kV again at the same spot near the bottom, between the Extraction Electrode holder and the Ground Electrode.

 

Entry  Tuesday, May 02, 2017, 13:49, Travis Cave, Spent Target Vault, Standard Operation, , , Spent Targets moved Mini_Vault_Storage_May_2_2017.pdfVault_Storage_May_2_2017.pdf

Five spent targets have been moved from the target storage vault to the mini vault in preparation for Thursdays loading of the F-308s. See attached for the list of targets in the mini vault, and the new status of the storage vault.

Entry  Tuesday, May 02, 2017, 09:48, Isaac Earle, North Hot-Cell, Development, , , NHC polycarbonate window cover panel installed IMG_0066.JPGIMG_0068.JPGIMG_0071.JPGIMG_0074.JPGIMG_0076.JPG

 The window cover panel has been installed on the hot side of the NHC shielding window according to drawing IRH1638.  It was necessary to drill and tap a hole in the steel frame first to achieve proper grounding for stud welding.  The strength of all studs were checked by installing a nut on the stud tightened against a block up against the steel frame, which was then torqued to a minimum of 10 ft*lbs.  For the final installation the nuts were each torqued to approximately 3 ft*lbs.  Visibility from the cold side of the cell was checked before and after installation by Chad Fisher and Isaac Earle:  no distortion was caused by the new cover panel and with the in-cell work lights aimed in a similar direction to how the permanent lights will be installed (shining down from the roof, and also aimed south from the periphery of the window) there was no significant decrease in visibility of the work space.  A couple of small scratches are visible on the panel surface - these were already there when the panel arrived at TRIUMF.  The panel has been installed in an orientation that will minimize the visibility of these scratches during normal work.  When the work lights were aimed at the window many imperfections in the panel were visible, however this is not expected to occur during normal operation.  After the cell lighting has been installed the visibility will be re-evaluated and a new panel can be procured if necessary.  

 

IMG_0076.JPG

 

IMG_0074.JPG

IMG_0071.JPG

 

 IMG_0068.JPG

IMG_0066.JPG

 

 

Entry  Monday, May 01, 2017, 13:11, David Wang, South Hot-Cell, Repair, TM3, , Electrical Check on TM3 after fibergalss is moved in SHC.  

RU( coil 1), F (anode), and 60kv bias(HS, Gasline, and MSP)  are shorted together. Other lines are good.  They are measured between  individual line each other  @500V. The megga showed OL. All of  them to ground are OL @500V as well. EL is grounded during check.

Entry  Monday, May 01, 2017, 12:32, David Wang, Crane, Repair, , , TH crane burning smell 

TH crane burning smell showed again this morning. It appeared after 1-1.5 hours of continuously using during the F308 flasks moving in TH.After a certain time of using I think the brake gap is reduced because of  thermal expansion. The main hoist and brakes work fine still. We knew these brakes gap are tight especially on west side. So, It is not surprised that this burning smell appeared again. It does not affect the safe of crane use in my view. But, The life of this brake assembly could be affected.  I would like everyone know this issue. We may need to consult Gordon crane as well. Maybe, The gap should be increased up a little bit.  On this Friday, I will use crane to transfer 30K lbs shielding blocks. It will be a good test on crane main hoist again. 

Entry  Monday, May 01, 2017, 08:53, chad fisher, South Hot-Cell, Repair, TM3, , Fiberglass removal 

Fiberglass, capton tape and tie straps have been removed from TM3.

Entry  Sunday, April 30, 2017, 20:57, Aurelia Laxdal, South Hot-Cell, Repair, TM3, no target, TM3 May 1-15, 2017 Tentative Schedule at the SHC and TCS May_2107_TM3_Schedule_at_the_South_Hot_Cell_and_TCS.docx

Please see attachment for TM3 May 1-15, 2017 Tentative Schedule at the SHC and TCS.

Entry  Friday, April 28, 2017, 12:04, Anders Mjos, Conditioning Station, Maintenance, , , MP1 problem 

TCS:MP1 was tripping of intermittently yesterday. It was found by Dave Morris that the current sensor was not set correctly causing the pump on status to flicker at times. Dave adjusted the settings yesterday. The system should be operational and is currently running normally.

Entry  Thursday, April 27, 2017, 19:59, Aurelia Laxdal, South Hot-Cell, Repair, TM3, no target, TM3 HV tests at atmosphere for Each Line(s) April 27, 2017 

Today a HV test at atmosphere was performed for Each Line(s), while floating the other lines.

Please note the Einzel Lens line (Y) was grounded.

Tests performed:

1. Applied up to 29kV to "(A) OVEN -"

Sparks occurred at 29kV at the Fiber Glass inside the Service Tray; and at the right side at the lines wrapped in Fiber Glass.

2. Applied up to 29kV to "(B) OVEN +"

Sparks occurred at 29kV at the Fiber Glass inside the Service Tray.

3. Applied up to 6-7kV to "(C) TUBE -"

Could not identify the sparks; it was a continuous discharge.

4. Applied up to 6-7kV to "(D) TUBE +"

Sparks/discharges occurred at 6-7kV at the Fiber Glass on the right side at the lines wrapped in Fiber Glass. We had to turn OFF the lights in the Hot Cell to identify the small sparks.

5. Applied up to 4kV to "(P-Q) COIL +"

Discharge occurred at 4kV. Could not identify it.

6. Applied up to 29kV to "(R-U) COIL -"

Sparks occurred around 27-29kV at the Fiber Glass inside the Service Tray; and at the right side at the lines wrapped in Fiber Glass.

Tom saw a spark at 27kV between the Extraction Electrode holder and the Ground Electrode.

Saw also a spark at the Ring Alumina insulator in the Service Tray, located on top of the second comb insulator with Epoxi.

7. Applied up to 27kV to "(E) Cavity or MSP, (G) Gas, (J) Heat Shield" - all these are connected together at the BIAS voltage.

Sparks occurred at 27kV at the Fiber Glass inside the Service Tray.

8. Applied up to 23kV to "(I) EE" - this is for the Extraction Electrode.

Sparks occurred at 23kV again at the same spot near the bottom screw hole, between the Extraction Electrode holder and the Ground Electrode.

9. Applied up to 27kV to "(F) Plasma"- this is for the Anode.

Sparks occurred at 26-27kV again at the same spot near the bottom screw hole, between the Extraction Electrode holder and the Ground Electrode.

Entry  Thursday, April 27, 2017, 16:58, Isaac Earle, North Hot-Cell, Development, , , Right side NHC manipulator installed IMG_0036.JPGIMG_0046.JPGIMG_0054.JPGCRLD-1046-B_rev_1_Installation_Removal_Manual_(July_2013).pdfManipulator_Cart_User_Manual__(CRLD-1003).pdf

 Installation of the NHC right side manipulator was completed yesterday.  The three piece manipulator was assembled in the module assembly area on the manipulator cart which was then craned through the hatch to the NHC service area (the slave end had to be removed for it to fit through the hatch).  The installation went relatively smoothly except for the second (cold side) piece of lead shielding around the thru tube which would not fit because the OD of the two halves were not concentric when assembled (arrived this way from CRL).  The shielding was removed and 0.070" was cut down on the lathe, after which installation could be completed.  The slave end lift bail and the pulley cover panel had to be removed for the manipulator to fit through the thru-tube.  Both these items were reinstalled after the manipulator was in the wall, and it was confirmed that the slave end lift bail aligns with the slave-end removal hatch in the NHC roof.  There was some difficulty getting the slave end to the horizontal position using the Y motion drive, also while preparing the manipulator for installation we noticed one of the Z motion tapes on the master side was sliding to the edge of one of the pulleys and rubbing - both these issues will be investigated at a later date.

We confirmed that it is possible to remove the master end using the manipulator cart.  We will practice doing this at some point before the cell is commissioned.  We will also do a run-through of slave end removal through the NHC roof.

Electronic copies of the Model-N installation and removal manual as well as the manipulator cart user manual are attached for future reference.

 

IMG_0036.JPG

 

IMG_0046.JPG

 

IMG_0054.JPG

Entry  Wednesday, April 26, 2017, 17:55, Aurelia Laxdal, South Hot-Cell, Repair, TM3, no target, TM3 Schedule updates at the South Hot Cell and CS April_–_May_2107_TM3_Updated_Schedule_at_the_SHC_and_TCS.docxApril_–_May_2107_TM3_Initial_Schedule_at_the_SHC_and_TCS.docx

Please see TM3's Updated Schedule (the current schedule) at the SHC and TCS.

For the record I am uploading TM3's Initial Schedule at the SHC and TCS.

Entry  Wednesday, April 26, 2017, 17:37, Aurelia Laxdal, South Hot-Cell, Repair, TM3, no target, TM3 HV tests at atmosphere Pictures from April 19-21, 2017 DSC_0950.JPGDSC_0899.JPGSparkMarkEETM3.jpg


Please see the first two pictures of the HV test at atmosphere done on April 19.

First picture shows a big spark between the Extraction Electrode mounting plate holder (at HV) to the Ground Electrode. Please note minimum gap between these electrodes is 7.8mm.

However the biggest visible spark was noticed at the bottom screw hole. (It is difficult to determine if at the 7.8mm gap were concomitant sparks occurring.)This spark started at 22kV and became stable above 24kV.

On April 20, 2017 Chad inspected this area with the Hot Cell camera and found a spark mark on the Extraction Electrode holder plate at the bottom screw hole. See the third picture.

Again it is very difficult with the existing Hot Cell cameras to inspect the areas where the gap is small (at 7.8mm gap between the conical surfaces of the Ground Electrode and Extraction Electrode holder)

In the second picture there are 2 small sparks: one on the top and another one on the right side at the lines wrapped in Fiber Glass. These sparks started at 20kV.

On April 21 the HV test was repeated with the Containment box ON and the sparks occurred again, at the same locations and at the same voltage.

Entry  Thursday, April 13, 2017, 10:32, chad fisher, South Hot-Cell, Repair, TM3, , TM3 Lower Service Tray Video Inspection 

A video inspection of the lower service tray was performed this morning. Camera was inserted upwards into the service tray/service chase from the containment box. One potential spark mark was identified as well as epoxy not flush with insulator. Fiberglass does not extend into service tray/chase much and does not look, from initial inspection that it will be too difficult to remove.

Video can be found in docushare Document-142295

    Reply  Wednesday, April 26, 2017, 16:52, Aurelia Laxdal, South Hot-Cell, Repair, TM3, , TM3 Lower Service Tray Video Inspection FiberGlassInST.tiff

chad fisher wrote:

A video inspection of the lower service tray was performed this morning. Camera was inserted upwards into the service tray/service chase from the containment box. One potential spark mark was identified as well as epoxy not flush with insulator. Fiberglass does not extend into service tray/chase much and does not look, from initial inspection that it will be too difficult to remove.

Video can be found in docushare Document-142295

 The attached picture is from the video: showing the fiber glass inside the Service Tray.

Entry  Wednesday, April 26, 2017, 13:35, chad fisher, South Hot-Cell, Repair, TM3, , TM3 containment box removed 

the containment box has been removed from TM3.

Entry  Wednesday, April 26, 2017, 10:40, Travis Cave, South Hot-Cell, Standard Operation, TM3, no target, Module move 

 TM#3 has been moved from the north east silo to the south hot cell.

Entry  Wednesday, April 26, 2017, 10:24, David Wang, ITW, Standard Operation, TM2, , TM2 ITW 

TM2 was moved and connected in ITW yesterday afternoon. After roughing down, ITW turbo pumps are started. ITW TP4 can not be started to full speed. ISAC ops kept it at low speed mode with less than 1.0A current draw on pump. ITW IG1s shows red as well. I will take a look on them today when beam is off.

 

Entry  Wednesday, April 26, 2017, 08:28, chad fisher, South Hot-Cell, Repair, TM3, , TM3 progress and manipulators 

containment box was re-installed onto TM3 on Monday, Left manipulator may be showing signs of eminent handle or tong cable failure.

Entry  Tuesday, April 25, 2017, 19:35, Grant Minor, Crane, Repair, , , ISAC Target Hall Crane - West Hoist Brake Rattle 

Below is a report on the ISAC Target Hall crane brake issue observed yesterday and addressed today:

 

- On April 13th, both the East and West hoist brake assemblies were replaced by Gordon Crane & Hoist, after David observed a burning smell

- The East assembly was replaced with a completely new brake assembly from Kone crane

- The West assembly was replaced with a refurbished assembly, which used the East assembly housing fitted with a rebuild kit by Gordon Crane

 

- Yesterday while preparing TM3 for a lift, David noticed a vibration / rattle sound coming from the West hoist brake

- This issue was only observed when starting the hoist from a complete stop, at the slowest possible upwards hoist speed

- Once the hoist speed increased, the sound went away, even after returning to a slower speed

 

- Tom from Gordon Crane & Hoist came in this morning at 7am and replaced the new West assembly with the original West assembly, which had at that point also been fitted with a rebuild kit at Gordon Crane’s shop

- Tom also inspected the East brake assembly again

- Tom commented that he had issues setting the right gap between the friction plates and the brake rotor – too close and the brake would not release properly, too far and the brake rattle issue would be observed

- He also commented that during this most recent repair of the West brake, he applied never seize to the shaft and spline to ensure that this friction point was not an issue

 

- After Tom finished his repair and inspection of the brakes, David attempted a test lift of an SEG block (10 ton) at the slowest lift speed

- The rattle noise coming from the West brake was still observed

- Travis also tested the slowest speed in Remote Test mode from the control room, with David and Grant present in the Target Hall, the rattle was also still observed

 

- Tom advised that the rattle would not affect the safety of the hoist, and no damage would be done to the brake assemblies by running the hoist normally with the rattle noise

- Tom ensured that he would consult with Aiden and they would likely order a brand new West brake assembly from Kone

- Tom called Aiden Gordon to confirm that it was ok to proceed

- Aiden called me around 1:30pm and left a message that the slow speed rattle sound was benign and that we could proceed with normal operations, but he would definitely address the problem moving forward, and we should standby for his report

 

Photos and video have been uploaded to Docushare.  The hoist noise before the repair and after the repair during the test lifts can be heard in the videos.

 

https://documents.triumf.ca/docushare/dsweb/View/Collection-19812

 

Thanks and regards,

 

Grant

 

--

Grant Minor, M.A.Sc., P.Eng.

TRIUMF Remote Handling Group Leader

Nuclear Engineer

4004 Wesbrook Mall, Vancouver

BC, Canada, V6T2A3

gminor@triumf.ca

(604) 222-7359

http://www.triumf.ca/profiles/4557

Entry  Monday, April 24, 2017, 16:11, David Wang, Conditioning Station, Standard Operation, TM2, , TCS TP1s is restarted. 

TCS IG1S  is switched on as well. The reason to start the pump is to prepare a possible extended TM2 conditioning at TCS caused by TH crane issue. TCS:TP1 and TP2 are not switched on for this.

Entry  Monday, April 24, 2017, 16:06, David Wang, South Hot-Cell, Repair, TM2, , Crane main hoist strane noise when lifting up TM2  

 When lifting up TM2 (20000lbs) this afternoon, TH crane has a strange noise on main hoist. The module was lift up less than 1 feet.when strange sound was noticed.  The module move was stopped right away,and module  was lowed back to SHC. The strange noise was confirmed later with SEG block six inches lifting up. Gordon crane technician will be here to tomorrow morning to investigate the problem.

Entry  Monday, April 24, 2017, 09:52, David Wang, Conditioning Station, Standard Operation, TM2, , Switch off TCS water system and vacuums 

The TCS bias was turn off before that. The TM2 and TCS are still under vacuum now.

Entry  Friday, April 21, 2017, 08:19, David Wang, Conditioning Station, Repair, , , Low frequency on TCS TGHT flow sensor. TCS_water_lines_001.JPGTCS_water_lines_002.JPGTCS_water_lines_003.JPG

Anders and I found a low frequency issue(13hz only) on TCS TGHT flow sensor when doing TM4 conditioning. By trouble shooting, We found the module water lines are good. the restriction cause this problem in on TCS supply or return water lines to TGHT.  I switched TGHT lines with MSP water lines. The wheel frequency on TGHT is 67.0hz which is pretty high. Now, MSP is using the original TGHT water line(flow sensor frequency 13hz). Flow sensors and thermocouples are switched as well so no control system change is needed on epic page. Everything are re-labeled in TH.  With less brazing joints closing to heater source, the MSP line should be ok. By further troubleshooting this issue, I think the problem on this low flow sensor frequency problem is on those 1/2" Parker gray water lines inside that big  6" white pipe.  See attachments. The lines are are twisted, and could be squeezed in my view. Since everything is enclosed in that big pipe, It is hard to tell where the lines are squeezed and cause this restriction. Comparing to an open guide chase, this round pipe makes everything  difficult. Hard to trouble shooting , hard to remove lines or add new lines. It only looks beautiful. I tried all I can do, But, I have no quick solution to solve this problem permanently.  Maybe, Rob walker and his technicians has better skill or more strength on removing old lines, or adding new lines to solve the problem. 

Entry  Wednesday, April 19, 2017, 08:29, David Wang, Conditioning Station, Standard Operation, , , TH schedule 132 update in first beam week  Target_Hall_shedule_132_Apr_to_Sep.pdfTarget_Hall_shedule_132_Apr_to_Sep.mpp

Update schedule to show job process in TH. See attachment 1,2.

Entry  Thursday, April 13, 2017, 14:16, David Wang, Crane, Repair, , , TH crane: east side main hoist brake assembly is replaced.  

Gordon Crane technician Tom Kauss finished the replacement of the east side main hoist brake assembly. A new set up is installed. he adjusted gap too close during first time try. So, the smell appeared when operate the brake. He increased the gap to a proper distance then. It looks like everything works fine now. Still, The brake need to be tested with 10K lBS load on it. We will do the load test on next Thursday when he come here to replace west side brake assembly.  Before that, No module move or other heavy lifting action should be fulfilled on TH crane.

2017-04-20. Tom Kauss finished the replacement of west side main hoist brake assembly. The old set up will be rebuilt, and stored as spare for the future. The load test is done.  10k lbs load was used for testing. Brakes work fine. No strange noise and smell has been found during the test. 

Entry  Thursday, April 13, 2017, 11:44, Anders Mjos, Conditioning Station, Standard Operation, TM2, Ta#51, Conditioning Ta#51 

 Thursday, April 13, 2017, 11:43: Water package started.

Entry  Thursday, April 13, 2017, 11:33, David Wang, Conditioning Station, Standard Operation, TM2, , Helium pressure test on TM2 water llines at TCS. 

LD  BLR :0.0 X E-9 atm.cc/sec. BP:0.0XE-4 torr. helium 70 psi. 3 minutes on each circuit

HS 1.8XE-7 ATM.CC/SEC
TA+ 1.4 XE-7
TA- 4.3XE-8
TUBE+ 1.0XE-7
TUBE- 5.9XE-8
COIL 1 2.2XE-9
COIL 2 0.0XE-9
EE 0.0XE-9
MSP 8.8XE-8
ALL TOGETHER 6.7XE-7
ALL TOGETHER WITHOUT HS 4.7XE-7

There is a smallleak HS which we did not see before. The HS is checked in SHC  with helium spray yesterday. We did not see the leak . We checked this HS line every time when new target was installed. So mostly, this small leak is from VCRs connected to new target. But, we can not confirm it.  Still this line will be checked on next new target. We should have a better understanding when checking next time.  Other line are almost same as we checked in last year November. I did not see essential change.

Entry  Wednesday, April 12, 2017, 16:39, Aurelia Laxdal, South Hot-Cell, Repair, TM3, no target, TM3 Inspection at the South Hot Cell DSC_0886.JPGDSC_0883.JPG

Found spark signs on TM3's containment on the side of the water blocks. They may be OLD or/and NEW sparking signs, but this in not determined at this moment. Please see picture: first attachment. First and second attachment show the profiles of water block and HV lines.

Entry  Wednesday, April 12, 2017, 13:03, Travis Cave, South Hot-Cell, Standard Operation, TM3, no target, Electrical Check TM3_elec_chk_no_tgt.PDF

Electrical check of TM#3 with no target at the south hot cell

Entry  Wednesday, April 12, 2017, 12:51, David Wang, South Hot-Cell, Repair, TM3, , TM3 Ram readings @ SHC 

 We have a ram installed on SHC pole which is 0.5 meter to  module shielding block surface. the readings we got today during TM3 move:
at containment box center (highest reading): 3.14 msv/hr.
at bottom  of shielding blocks: 960 usv/hr.
at 1/4  of  shielding blocks height from  bottom :700usv/hr.
at 1/2 of shielding blocks height from bottom: 340usv/hr.
at 3/4 of shielding blocks height from bottom:140u/sv/hr.
   The Ram is behind the pole and measured the surface which is 90 degree right side of that opened service tray side. 

Entry  Wednesday, April 12, 2017, 09:20, Travis Cave, South Hot-Cell, Repair, TM3, no target, Module move 

 TM#3 is now in the south hot cell.

Entry  Wednesday, April 12, 2017, 07:26, David Wang, Conditioning Station, Standard Operation, TM2, , TM2 and TCS vacuum system has been connected. 

Roughing down overnight. Turbo pumps are started this morning. Everything looks good so far.

Entry  Tuesday, April 11, 2017, 14:06, David Wang, Conditioning Station, Standard Operation, TM4, , SHC, TM2 leak check on HS line. 

Chad and I did leak check on TM1 HS line at SHC. 0.0XE-9 atm.cc/sec.  No leak.

Entry  Tuesday, April 11, 2017, 14:02, Travis Cave, Conditioning Station, Standard Operation, TM2, Ta#51, module moved 

TM#2 with Ta#51 has been moved from the south hot cell to the conditioning station.

Entry  Tuesday, April 11, 2017, 11:30, Travis Cave, South Hot-Cell, Standard Operation, TM2, Ta#51, Electrical Check TM2_Ta51_SHC_elec_chk.PDF

Electrical check performed on TM#2 with Ta#51, see attached PDF.

Entry  Monday, April 10, 2017, 11:23, Travis Cave, Conditioning Station, Standard Operation, TM1, no target, Module move 

 TM#1 has been moved from the conditioning station to the north west silo.  There was a slight delay in the move as the limits for the hoist drum got way out of whack and had to be adjusted.

Entry  Friday, April 07, 2017, 09:53, Travis Cave, Conditioning Station, Maintenance, TM1, no target, Electrical Check and TM1 other checks TM1_elec_chk_no_tgt.PDF

Results of an electrical check on TM#1 with no target attached to it.

 I use this e-log entry for TM1 notes as well  1. TM1 IG1 is a dual filament gauge . Its filament is very close to grid now. It shorted one time during the pumping down. It still works fine so far . But, we may need to change it if we use this module in TS again.

TCS 1G1 and 1G1S are pumped to 5Xe-6 torr. IG2 stayed at 2.5XE-5 torr. Since no target is installed on module , I capped top of HS water line. Maybe, the small o-ring seal in cap is too old, I found a big leak on this seal when i use LD check it. That is the reason IG2 stayed too high. Still, Leak check and helium presuure test are fulfilled on TM1. Leak detector BLR 5XE-7 atm.cc/sec, BP 0.0XE-4 torr9.  Back up pressure is 51 mtorr which is high because of leak on HS line cap seal so LD BLR is high. At this level, Ta+-, Tube +-, MSP,  EE are good.  Other air to vacuum seal are good as well at this leak rate.  I will check and change small o-ring seal in HS cap. The TM1 is functional basically.

Entry  Thursday, April 06, 2017, 15:16, Anders Mjos, Conditioning Station, Maintenance, , , Installation of new break out box to accommodate both ITM:MP2 and TCS:MP1 

Installation by Marshall. Dave M from controls adjusted circuitry to get TCS:MP1 to start.

Work is being done in preparation for the Module Move Ventilation SAS project

Entry  Thursday, April 06, 2017, 15:11, Grant Minor, Crane, Maintenance, , , Target Hall Crane 20 ton hoist - Report by Gordon Crane 5-Apr-2017 

-------- Forwarded Message --------

Subject:

ISAC Hoist Brake Repair

Date:

Wed, 05 Apr 2017 20:42:49 -0700

From:

Aidan C. Gordon <aidan@gordoncrane.com>

To:

Curtis Ballard <ballard@triumf.ca>, Neil Wong <nwong@triumf.ca>

CC:

Peter Neumann <peter@gordoncrane.com>, Shelley Cherkowski <Shelley@gordoncrane.com>

 

Hi Curtis

 

Further to the emergency service call at the Isac Target Hall on Thursday March 23rd, we advise as follows:

 

It was reported that the hoist was making an unusual noise and that there was a strong brake odour during operation.

The lift was completed using the auxiliary hoist.

 

A man-lift was arranged and Senior Service Technician Tom Kauss attended site the next morning to troubleshoot.

He determined that one of two hoist brakes (walkway side) had a strong odour and on closer examination it appeared that the 

brake lining material was breaking down and particulate lining material was getting caught between the lining and the discs.

These lining fragments were rubbing and burning off during the hoist operation.

The end cover of the brake had an accumulation of brake lining fragments 

The lining was not overly worn, but appears to be becoming friable, perhaps with age or exposure to radiation.

 

The brake was cleaned with compressed air to remove the friable material and thoroughly tested. 

A test load of approximately 10 tons was lifted and the hoist handled the load without issue

The brake fragment issue did not recur while we on site and the hoist was recommissioned for use.

 

To guard against the likely recurrence of this condition on this critical application crane, and as both brakes have seen identical conditions in operation, 

we recommend that both brake assemblies be replaced.

The brake assembly would include the brake coil, friction discs, steel brake discs and the brake springs

TRIUMF does not have a spare brake on hand, therefore one of the removed brakes could be rebuilt and kept on hand. 

 

Two (2) each  XL-60009637 Complete Brake Assemblies   $ 5,706.00  Each

 

One (1) only XL-60009674 Brake Repair Kit $ 2,435.00

            For Rebuild

 

One (1) only XL-52272125 Brake Spring Kit $     59.72 For Rebuild

Installation & Testing of New Brakes estimated at: $ 1,250.00 Lot

We have one brake in stock in our Vancouver Service Depot. A second brake is available Ex-Ontario

FOB Site

Applicable Taxes Extra

Quote Valid for 30 days, subject to prior sale.

 

We are available next week to perform this work on site.

Please let us know if you have any questions or if you would like us to proceed.

 

Best Regards

          Aidan

 

------------------

Aidan C. Gordon

General Manager

aidan@gordoncrane.com

Gordon Crane & Hoist Inc.

Celebrating 34 years of Excellence (1983-2017)


www.gordoncrane.com

Toll Free 1-866-HOIST-IT

              (1-866-464-7848)

Tel:  (604) 324-2441

105-8475 Ontario St

Vancouver BC  V5X 3E8


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Entry  Thursday, April 06, 2017, 12:33, David Wang, Conditioning Station, Repair, TM1, , TM1 rust inpsection and removal 

TM1 inside service cap surface and shielding plug surface are visually inspected yesterday. No rust has been found. I cleaned all rust on top of TM1  today.  Rust on TM1 silo  top plate are cleaned as well.

Entry  Wednesday, April 05, 2017, 14:13, David Wang, Conditioning Station, Maintenance, TM1, , TM1 and TCS vacuum system are connected together 

I started two turbo-pumps on TM1 and one small TP on TCS. They are work fine. 

Entry  Wednesday, April 05, 2017, 11:57, David Wang, ITE, Maintenance, , , ITE target module flange o-ring repalcement 

ITE target module tank flange o-ring was replaced yesterday before TM4 moving. ITE: IG1S reading looks fine so far. 

Entry  Wednesday, April 05, 2017, 09:46, Travis Cave, Conditioning Station, Standard Operation, TM1, no target, module moved 

TM#1 has been moved from the North West silo to the conditioning station.

Entry  Tuesday, April 04, 2017, 14:40, David Wang, ITE, Standard Operation, TM4, , TM4 has been connected in ITE 

all turbo-pumps are started. Everything looks fine so far.

Entry  Tuesday, April 04, 2017, 14:39, David Wang, Crane, Standard Operation, , , Crane check main hoist on jogging with shielding plug lifted.  

Today, I checked TH crane main hoist  when shielding plug is installed into ITE pit. I did  some jogging actions on main hoist during the operation. Everything looks fine. No burning smell, no strange noise. An outside crane expert suggest that jogging is the worst working situation for crane. We have to use jogging actions during our crane operation. But, we could try to use less jogging when operate the crane.

Entry  Tuesday, April 04, 2017, 10:24, David Wang, Conditioning Station, Standard Operation, TM4, , Stopped TCS pumps this morning 

 Argon vented TCS and TM4 after pumps are stopped.

Entry  Tuesday, April 04, 2017, 10:23, David Wang, Conditioning Station, Standard Operation, TM4, , Helium pressure leak check on TM4 Ta(-) water lines  

This morning, The helium pressure leak check on TM4 Ta(-) is done after TM4 finished conditioning yesterday.  LD base LR:8.0XE-9 atm.cc/sec, base pressure: 0.0XE-4 torr. Applied 70 psi helium to TM4 TA(-) water line. The LR slowly climbed to 2.2XE-7 atm.cc/sec, and stopped there. Waited for 5 minutes and change at 2.2 X E-7 atm.cc/sec.

Entry  Tuesday, April 04, 2017, 09:29, Travis Cave, ITE, Standard Operation, TM4, UC#19, module moved 

TM#4 with UC#19 has been moved from the conditioning station to the east target station.

Entry  Thursday, March 30, 2017, 11:21, David Wang, Conditioning Station, Repair, TM4, , Leak check on TM4 Ta(-) water lines in service cap 

Leak check on TM4 Ta(-) water lines in service cap is done. LD base LR after 50minutes pumping down:0.0xE-9 atm.cc/sec. base pressure: 0.0XE-4 torr. I sprayed lots helium on welding stems on Ta(-) line in service cap including stems in blue nylon insulator and stems to service tray.  no any response has been foun on LD. The Ta(-) line in service cap is leak free.

 Totally panel open and leak check time is about 12minutes. Argon vented TCS before leak check this morning. 

Entry  Wednesday, March 29, 2017, 14:11, David Wang, Conditioning Station, Standard Operation, TM4, , small leak on TM4 Ta(-) water line. TM4_2017_leak_check_in_ITE.png

A small leak has been found on TM4 Ta(-) which is marked as "B" on terminal blocks. The LD base Leak rate is 1.2XE-8 atm.cc/sec. 70psi helium has been applied to Ta(-) water line for 3minutes. The leak rate went up to 2.5xE-6 atm.cc/sec and stabilized there. Anders found a helium response on RGA helium reading during the same time. This confirms the leak is real. Other lines are leak checked today also. They are good still. All TM4 water lines were leak checked in ITE in 2017 January. They  were all good at 0.0 X E-9 atm.cc/sec. See attachment e-log.

Entry  Wednesday, March 29, 2017, 11:42, Anders Mjos, Conditioning Station, Standard Operation, TM4, UC#19, Conditioning UC#19 UC#19.docxTCS-2017-03-29_UC#19.rgaTCS-2017-03-30_UC#19.rgaTCS-2017-04-03_UC#19.rga

 Wednesday, March 29, 2017, 11:37: RGA on

Wednesday, March 29, 2017, 13:51: Water package on


Thursday, March 30, 2017, 08:50: Restarted chiller. OP3 fault on both VFDs.

Thursday, March 30, 2017, 10:18: Roughing

Thursday, March 30, 2017, 16:02: Configured EE to conditioning mode. All power supplies for SIS operation was checked to be working earlier.

Thursday, March 30, 2017, 16:06: BIAS / EL 10 / 5 kV and 0.02 / 0.04 mA

Thursday, March 30, 2017, 16:10: BIAS / EL210 / 10 kV and 0.03 / 0.06 mA

Thursday, March 30, 2017, 16:11: IG1 at 7.8E-7 T, IG2 at 2.3E-6 T

Thursday, March 30, 2017, 16:21: No sparking. Ramping down for the day


Friday, March 31, 2017, 08:32: BIAS / EL 20 / 10 kV and 0.03 / 0.06 mA

Friday, March 31, 2017, 08:32: IG1 at 4.2E-7 T, IG2 at 1.4E-6 T

Friday, March 31, 2017, 08:45: BIAS / EL 25 / 12.5 kV and 0.04 / 0.08 mA. Some minor vacuum responses around 24 kV

Friday, March 31, 2017, 10:03: BIAS current was limiting at 26 kV after EPICS restart. Updated limit

Friday, March 31, 2017, 10:10: BIAS / EL 30 / 15 kV and 0.04 / 0.09 mA. Vacuum and current responses when increasing BIAS.

Friday, March 31, 2017, 10:54: BIAS / EL 35 / 17.5 kV and 0.05 / 0.10 mA.

Friday, March 31, 2017, 11:24: BIAS / EL 40/ 20 kV and 0.05 / 0.11 mA.

Friday, March 31, 2017, 11:43: BIAS / EL 45/ 22.5 kV and 0.06 / 0.13 mA.

 Friday, March 31, 2017, 13:47: No sparks for ~90 min. Ramping down HV

Friday, March 31, 2017, 13:58: Starting auto-ramping heaters to 100 / 100 A at 1 A/min. Good/bad vacuum at 3E-6 and 5E-6 T on IG2. EE to 1500 V

Friday, March 31, 2017, 14:03: BIAS / EL / EE at 30 / 15 / 1.5 kV and 0.04 / 0.09 / 1.5 mA


Saturday, April 01, 2017, 10:58: Continue auto-ramping to 440 A / 200 A.

Saturday, April 01, 2017, 17:17: IG1 / IG2 to 1.7E-6 and 3.6E-6 T at 440 A. Reduced manually to 430 A to limit outgassing.

Saturday, April 01, 2017, 18:03: Discovered TP2 had tripped off. Likely causing "increased outgassing" above.

Saturday, April 01, 2017, 18:12: TP2 back at speed.

Saturday, April 01, 2017, 23:25 : TP2 fault from spark. Restarting. Ramping down heaters.


Sunday, April 02, 2017, 06:45: Found source to be tripped on water flow TGHT at around 1:15 am. Vacuum and water flow otherwise ok. Set source to 0. To be investigated Monday. 


Monday, April 03, 2017, 11:05: The paddle wheel on the TGHT line was not turning this morning. After running water through a bypass an reconnecting to the module, flow was restored, but it appeared to be at a relatively low rate.

Monday, April 03, 2017, 12:00: BIAS / EL / EE at 30 / 15 / 1.5 kV and 0.03 / 0.09 / 1.5 mA

Monday, April 03, 2017, 12:18: Tested TGHT / TBHT to 20 / 10 A.

Monday, April 03, 2017, 12:18: Increased EE to 2 kV and 2.0 mA

Entry  Tuesday, March 28, 2017, 10:44, chad fisher, South Hot-Cell, Standard Operation, TM4, UCx#19, UCx#19 Installed 

UCx#19 has been installed onto TM4. High current fasteners torqued to 130 in lbs. Has been leak and electrical checked and is ready to leave hot cell.

Entry  Tuesday, March 28, 2017, 10:30, Travis Cave, South Hot-Cell, Standard Operation, TM4, UC#19, Electrical Check TM4__UC19_SHC.PDF

Electrical check done on TM#4 with UC#19. See attached PDF for results.

Entry  Tuesday, March 28, 2017, 09:18, Travis Cave, South Hot-Cell, Standard Operation, TM4, no target, module moved 

TM#4 has been moved from the conditioning station to the south hot cell.

Entry  Monday, March 27, 2017, 13:40, Travis Cave, South Hot-Cell, Standard Operation, TM2, no target, Electrical Check TM2__No_Tgt.PDFTM4__No_Tgt.PDF

Did the start of the running year electrical checks of both TM#2 and TM#4 with no target attached to either module. TM#2 was in the south hot cell and TM#4 is in the conditioning station under vacuum.

Entry  Monday, March 27, 2017, 12:55, David Wang, Spent Target Vault, Repair, , , S/W silo rust clean up rust_removal_at_sw_silo_001.JPGrust_removal_at_sw_silo_002.JPGrust_removal_at_sw_silo_003.JPGrust_removal_at_sw_silo_004.JPGrust_removal_at_sw_silo_005.JPG

Rust on S/W silo and cover plate stored at silo area are cleaned up.

Entry  Monday, March 27, 2017, 06:33, David Wang, ITE, Standard Operation, , , ITE clean up 

ITE clean up is done.  HV cage inside is wiped.

Entry  Friday, March 24, 2017, 13:21, Travis Cave, Spent Target Vault, Standard Operation, , 2A window, 2A window has been removed from the vault. Vault_Storage_March_24_2017.pdf

2A window has been removed from the vault and moved over the cyclotron vault tunnels.  Attached is the updated storage vault list.

Entry  Wednesday, April 30, 2014, 12:03, Travis Cave, Spent Target Vault, Standard Operation, , 2A3 window, Window now in vault Vault_Storage_April_30_2014.pdf

The 2A3 window now has a lid, and lift yolk on it and it has been installed in the spent target vault in spot 2A. The lid is a normal unmodified and has no sealant on it.

    Reply  Friday, March 24, 2017, 11:19, Keith C Ng, Spent Target Vault, Standard Operation, , 2A3 window, Window now in vault 2017mar24_vault_tunnel_storage_form(1).pdf

Travis Cave wrote:

The 2A3 window now has a lid, and lift yolk on it and it has been installed in the spent target vault in spot 2A. The lid is a normal unmodified and has no sealant on it.

The pail containing window was transferred from the Storage Vault to the Cyclotron Vault Tunnel Storage 2017 Mar 24. It was placed in a brick bunker along the north wall and marked with item #1434. RPG storage form is attached.

Highest field measured at 0.5 m was 3000 uSv/h with an estimate of 4000 uSv/h on contact with the pail. Pail exterior was not contaminated. See attached storage form for details.

 

Entry  Friday, March 24, 2017, 11:12, Keith C Ng, Spent Target Vault, Standard Operation, , , 2A window transfer 2017mar24_vault_tunnel_storage_form(1).pdf

Transfered the 2A window from the ISAC Storage Vault to the Cyclotron Vault Tunnel Storage area. RPG storage form attached.

Entry  Thursday, March 23, 2017, 11:42, David Wang, Conditioning Station, Maintenance, TM4, , TM4 Sevice cap rust are cleaned out. TM4_clean_up_at_TCS_006.JPGTM4_clean_up_at_TCS_007.JPGTM4_clean_up_at_TCS_002.JPGTM4_clean_up_at_TCS_008.JPGTM4_clean_up_at_TCS_005.JPG

TM4 service cap rust are cleaned out at TCS. All top surface of TM4 are wiped and cleaned . The module looks good now. see attachments

Entry  Thursday, March 23, 2017, 11:22, Grant Minor, Crane, Maintenance, , , Target Hall crane 20 ton hoist noise / smell - inspection by Gordon Crane & Hoist Target_Hall_crane_main_hoist_problem_-_A_Mjos_-_22_Mar_2017.pdfUpdate_-_Target_Hall_20T_Hoist_Inspection_-_G_Minor_-_23_Mar_2017.pdfRe__Update__Target_Hall_20T_Hoist_Inspection_-_David_Wang_-_23_mar_2017.pdf

Strange noise and a burning brake type smell was observed yesterday by David and Anders when running the main 20 ton hoist locally.  A service call was arranged today with Gordon Crane.  No major issues were found.  A more detailed summary is in the attached e-mail correspondence.  Gordon Crane will issue a formal report, but they recommend replacing both sets of brake disks and brake calipers. - Grant

Entry  Thursday, March 23, 2017, 09:30, Travis Cave, South Hot-Cell, Standard Operation, TM2, test target, Electrical Check TM2_Ta_Dummytgt_Preandpost.PDF

Electrical check of the Ta test target on TM#2

Entry  Wednesday, March 22, 2017, 14:05, Travis Cave, South Hot-Cell, Standard Operation, TM2, test target, module moved 

TM#2 has been moved from the east target station to the south hot cell.

Entry  Tuesday, March 21, 2017, 11:59, David Wang, Conditioning Station, Repair, TM4, , Rust inpsection on TM4 service cap inside surface and shielding plug surface.  11x

Yasmine and I did a rust inpsection on TM4 service cap inide surface and shielding plug surface. No rust has been found. Also, all steel bolts on this surface look fine. The inside of silo held this module are rust free as well.  See attachments

Entry  Tuesday, March 21, 2017, 10:06, Travis Cave, Conditioning Station, Standard Operation, TM4, no target, module moved 

TM#4 has been moved from the SW Silo to the conditioning station.

Entry  Tuesday, March 21, 2017, 10:05, Travis Cave, Spent Target Vault, Standard Operation, , , Spent target assay. Vault_Storage_March_20_2017.pdf

All target in the ISAC spent target vault have been either assayed or had their fields measured or both.

Entry  Thursday, March 16, 2017, 12:24, chad fisher, South Hot-Cell, Maintenance, , , West 'Z' motion cable replacement 

The west 'Z' motion cable on the east manipulator has successfully been replaced. The job took slightly less than an hour (including inspection of the scissor table hoses) and I received 0.075mSv. Scissor table hoses appear to be fine and also didn't "shed" or flake at all when checked by hand.

Entry  Thursday, March 16, 2017, 10:32, David Wang, Spent Target Vault, Repair, TM4, , TM4 and its silo rust photos 13x

I watched rust on TM4 and its silo. Most of rust are on est side of module and silo. See attachments

Entry  Wednesday, March 15, 2017, 07:45, chad fisher, South Hot-Cell, Maintenance, , , South Hot Cell Fields 

I have moved the suspected "hot" items in the hot cell and placed them under some lead bricks. I have re-measured the fields and it has been reducded to 90 uSv\h at the manipulator repair area and 110 uSv/h at the previous 1.82 mSv\h area.

Entry  Tuesday, March 14, 2017, 11:46, chad fisher, South Hot-Cell, Maintenance, , , 'Z' motion cable dry run 

Did a dry run with the latest procedure with Dan Mcdonald. Elapsed time was approximately 30 min.

Entry  Tuesday, March 14, 2017, 07:34, chad fisher, South Hot-Cell, Maintenance, , , Hot Cell Fields 

I have re-measured the fields in the hot cell. Fields at shield door Al cover are 101 uSv\h, in cell at the east manipulator are 245 uSv\h, and the largest field is 1.84 mSv\h...this appears to be the high current fasteners removed from the last target.

Entry  Friday, March 10, 2017, 09:19, chad fisher, South Hot-Cell, Standard Operation, , , South Hot Cell Field Measurements 

The fields in the hot cell have been measured by means of a pole monitor through the tool port. Field was measured to be 25 uSv/h.

Entry  Wednesday, March 08, 2017, 14:09, David Wang, ITE, Maintenance, TM2, , ITE IG1S increasing. ITE_IGIS_surge.pngITE_IG1S_and_PNG4.pngITE_IG1S_back_to_normal_overnight.pngITE_IG1S_behavior_from_Feb_08th_to_Mar_10th.png

By retrieving data further, It has been found no directly relationship between IG1S surging and dump plug water opening. Vacuum surging is 10minutes ahead dump water supply to circuit. SEE attachment 1. Also, The ITE IG1S start to behavior unusual in middle of Feburary. See attachment 2. Today,  ITE IG1S is still slowly climbing up. I decide to leak check ITE vacuum vessel. Before  leak check, for more information and trouble shooting. I closed water supply to ITE to see if vacuum has response on it. I will return water supply to ITE  tomorrow morning.

Water supply to ITE is returned this afternoon at 2: 10 PM.  Everything works fine so far

I leak checked ITE secondary vessel vacuum. A leak have been found in March 09th noon which is located between entrance module and TM2 top tank flange o-ring seal( on tank flange). It could not be confirm on which side of the o-ring the leak is from.

During last night, ITE IG1S reading went back to normal low E-7 range and stays in this range now. So I leak checked same area again this morning. The leak disappeared now. The o-ring works sometime , but not all the time. The plan for this issue: Change ITE target module side o-ring when TM2 is move out., and watch on the ITE IG1s when TM4 is moved back to ITE and pumped down.

Entry  Tuesday, March 07, 2017, 14:41, David Wang, ITE, Maintenance, , , ITE dump plug water circuit is closed for ITE IG1S small surge. 

It is closed @ 2:35PM by closing supply side valve first , the return side valve of ITE dump plug .

Opened ITE dump plug circuit valves @4:28PM. ITE IG1S still at 1XE-6. No change before and after of circuit closing and reopeneing.

Entry  Tuesday, March 07, 2017, 09:25, David Wang, ITW, Repair, , , ITW HALCW 2" return line ball valve seals replacement. 

Leaking seals on ITW HALCW 2" return line ball valve have been replaced. 8 liter waters are drained out for this job. Water are drained into a thick plastic bag.  The bag is tie strapped , labeled, and put into a yellow garbage bin in MAA. Water sample is given to RPG. After analyzing, RPG will give instruction on how to deal with it. Since we just refilled NALCW to system before this job, the active level on sample is very low. We may dump them into active sump.  After seals change, The system is refilled . I started pump and set everything back to normal configuration. NO leak has been found on new seals. The HALCW system is operating good so far.

Entry  Monday, March 06, 2017, 08:01, David Wang, Cooling, Repair, , , HALCW resin tank replacement. 11x

HALCW resin tank has been replaced. The old tank is stored in middle-west silo now. The field on old resin tank bottom is about 3.5 msv/ hr(on contact). By shielding it into silo and putting two lead blankets on the top cover of the silo,The general field 1 feet above this silo is 25usv/hr. And, The field around the silo area are less affected. This old tank will stay there as long as possible.  For the new resin tank during preparation, It was found that on return line side, the 1.25" pipe thread plug with return line tube  was very difficult to be installed onto the female thread adapter which is welded onto to tank body. It was jammed in half way of threading onto tank at manufacturer. This plug was removed out first and inspected. The first and second male threads were galled.  Maico repaired the thread on a lathe. The female thread on the tank was tapped. A tight spot was found during the tap. After that, the return line plug could be installed onto the tank properly.  The new tank was installed into the vessel and connected back to HALCW system. Water are refilled into new tank. During refill air were trapped into the system. This caused  pump restarting problem. By Several times of starting up the pump, stopping the pump and venting,  Most air were breathed out of  system. Finally,The system was restarted by supply water to ITW( without module) only. ITE and resin can circuits were brought back to system after that without problem.

 Before removing the old tank, We drained water out of old tank to decay tank. Since the resin tank is largely filled with  resin, and water are soaked into resin, we only can drain out less than 10 liters water out of tank. Also, The drain caused some part of return line on pumps have to been drained. This is the main reason air was trapped in system during the new resin tank water refilling. For the future replacement, we should not drain water in old tank. It does not worth to do it. 

Attach TH HALCW resin tank replacement procedure here.

2022-02-17 reload replacement procedure and draining schematic.

Entry  Thursday, March 02, 2017, 15:02, Isaac Earle, North Hot-Cell, Development, , , NHC roughing filter installed IMG_8014.JPGIMG_8018.JPGIMG_8019.JPG

 The roughing filter assembly (RFM0001D) has been installed at the ventilation exhaust hole on the NHC partition wall.  The filter used is Model # 332-528-002 supplied by BGE Service & Supply Ltd (see PO # TR123998).  Installation and removal of the filter using the manipulators will be tested after they have been installed.

 

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Entry  Tuesday, February 28, 2017, 17:51, Isaac Earle, North Hot-Cell, Development, , , NHC flanged ducting connection sealed IMG_8012.JPG

 The North Hot Cell ducting (IRH1617) has been sealed with a bead of Sikaflex 1a polyurethane construction sealant where the flanged connection bolts to the NHC/TCS partition wall.  When this sealant shows signs of aging it may be cut away and re-applied without unbolting the flange.

 

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Entry  Monday, February 27, 2017, 14:23, chad fisher, South Hot-Cell, Repair, , , Manip. 'Z' motion cable run through 

Aaron and I successfully completed a run through on the procedure to replace the 'Z' motion cable. I will be writing up the procedure for review and we will be performing more run through-s for practice before the actual job.

Entry  Friday, February 24, 2017, 15:12, Isaac Earle, North Hot-Cell, Development, , , NHC interior walls/floor/ceiling re-finished, sealed, and painted 8x

The North Hot Cell interior walls, floor, and ceiling were re-finished, sealed, and painted by Omni Coating from Feb 6 - 17 under PO #3036471.  This job required 2-3 people for 4-6 hours per day over the 2 week period.  First the existing surfaces were ground and/or sanded to remove existing coatings and protrusions/sharp edges.  This was followed by a coat of primer to highlight uneven surfaces and improve adhesion of following fillers and coatings.  Metal shims between the cell walls and roof were cut away where they protruded into the cell.  Loose steel cylinders between SHC and NHC spaces were fixed in place using epoxy filler. Epoxy or polyurethane fillers were used to fill all gaps, cracks, holes, etc, as detailed below.  Foam backer rod and polyurethane filler were used to seal all large wall-to-wall and ceiling-to-wall gaps.  An approximate 2cm radius rounded corner was formed at all wall-to-wall and floor-to-wall corners using polyurethane sealant.  The interior of the tool-port, personnel access hatch, as well as the north roof hatch were also re-finished with the same procedure.  After all sealing and finishing work the surfaces were coated with "Mill White"  Macropoxy 646 Fast Cure Epoxy Paint as per manufacturer instructions.  Note:  this paint is recommended by the manufacturer for nuclear applications and has been tested for decontaminability:  99% water wash; 95% overall as per ASTM D4256/ANSI N 5.12 as well as for radiation tolerance:  Passed ASTM D4082 / ANSI 5.12 with a 525 micron thick coating.

 

The following products were used as described (data sheets attached):

Sanitile 120 Universal Acrylic Primer - 50-75 micron dry film thickness coat applied over all existing ceiling, walls, and floor surfaces after preparation by sanding

Sika Duochem 8107 Epoxy Paste - Used for filling voids and cracks in concrete surfaces

Sikaflex 291 Polyurethane Elastomeric Adhesive and Sealant - used for caulking joints and cracks in the concrete walls and aluminum panel wall and for creating radiused corners in wall-to-wall and wall-to-floor corners

Macropoxy 646 Fast Cure Epoxy Paint - 4 coats applied on all surfaces using rollers or brushes to create a total thickness of 525 microns as per data sheet

 

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Entry  Wednesday, February 15, 2017, 12:07, chad fisher, South Hot-Cell, Maintenance, , , Manipulator 'Z' motion cable replacement preparation status 20170215_113609.jpg

Aaron and I completed assembling (re-assembling) the clean spare on Tuesday, February 14th to assist in determining a procedure for replacement of the 'Z' motion cable on the south hot cell manipulators.

 

The anchor point in the slave end of the clean manipulator could not be found as the manipulator stand is too low and does not allow full extension of the slave end.

 

Did some poking around on the in-situ manipulator in the south cell and was able to find the anchor point viewing it with the in cell camera (see blurry attached photo).

 

Was able to then find reference to the "cable clamp" in the parts list and drawing for the slave end. Also, confirmed there is not a procedure in the manual for a CABLE 'Z' motion system as we have, only a tape driven system. The procedure should however be very similar safe this mystery anchor point I discovered today and how readily this anchor point can be worked in.

Entry  Friday, February 10, 2017, 09:56, David Wang, Conditioning Station, Standard Operation, , , water has been refilled to TCS:TK2  

TCS:TK2 , Water has been refilled to 28.5" level. It was 15.1". Fall protection equipment  are used during the job.

Entry  Thursday, February 09, 2017, 14:07, Isaac Earle, North Hot-Cell, Development, , , North Hot Cell Shielding Window Gaskets Changed 23x

 The North Hot Cell shielding window gaskets have been changed and the window has been filled with new oil.  Although there was no noticeable oil leaks before starting the job, the gaskets had not been changed since initial installation approximately 15 years ago, so they were done now as part of construction of the new  cell.  The work took place between January 26 – Feb 8, 2017 following the attached PDF “Full procedure for NHC shielding window gasket change” which references “Gasket change procedure from Hot Cell Services” (also attached).

To drain the window a 1/2”polyethylene hose was attached to the drain line using  a Swagelok fitting and routed into a 55 gallon drum.  A vent valve on the expansion tank was opened to allow air to enter  the window.  It took approximately 5 hours to drain the window using this method.  Approximately 50 US gallons were drained from the window, agreeing with the amount specified on Hot Cell Services drawing #96173-100 (attached).

After draining, the window was purged with helium then pressurized to approximately 13” WC with helium.  A pressure drop of 0.6” WC was observed over a 2 hour period.  While pressurized, a Varian G8601-60001 leak detector was  used to sniff for helium around the perimeter of the gaskets on both the hot and cold  sides – no helium leaks detected.  A small leak was found on the pressure gauge used to monitor helium pressure.

The cold side cover panel assembly was  then removed  following the HCS procedure.  From HCS Drawing #96173-100, the weight  of the cold side glass cover panel was estimated to be  approximately 50lbs.  The guide  pins used were McMaster-Carr PN# 93460A385.  The trim frame could be easily removed, however the glass panel was stuck to the window housing.  A putty knife and isopropyl alcohol were used to cut through the gasket to separate the window from the housing.  The alcohol did not damage the paint of the housing – acetone was also tested on a small area and did not cause damage  to the paint.  Two suction cup handles were used to transport the glass panel, and it was easily lifted by two people.  Various methods were attempted to remove old gasket material and gasket adhesive  from the trim frame and housing surfaces – the most successful was using a razor blade scraper to remove the majority of the material, followed by an acetone wipe to remove the remainder of the stuck-on gasket adhesive.  The panel was reinstalled with new gaskets following the attached  procedures - no issues encountered.  After torqueing the trim frame bolts the window was leak checked as before.  A drop of 0.8” WC was observed over two hours, and no helium could be detected around  the perimeter of the new cold side gasket.

The hot side cover panel assembly was changed using the same method as for the cold side.  The glass panel was estimated to be 150lbs.  A small amount of oil (< 0.5 L) remained behind the hot side glass panel after draining which spilled out after removal of the glass. Four suction cup handles were used, and four people were required to remove and reinstall the panel.  After installation the leak check was repeated with a drop of 0.3” WC observed over two hours, and no helium detectable around the perimeter of the hot side gasket.

The replacement gaskets were ordered from Hot Cell Services under PO# 3033973 matching the material and sizes specified on  HCS drawing #96173-100.

The window was filled with Drakeol 10B LT MIN OIL NF, Product  code: PEN1550-00-C-DR, PO #3034657.  The window was filled by lifting the drum onto the walkway leading  to the target hall entrance, and siphoning the oil out of the drum with a 1/2” polyethylene tube connected to the drain fitting, and an air vent open on the expansion tank.  Oil was added until the expansion tank was approximately 80% full.

After filling was complete, the cold side housing was repainted using Macropoxy 646 epoxy paint, 4019 Flint Gray.  When the inside of the NHC is next accessible the hot side trim frame bolts will be re-painted to protect the bare metal exposed from removing and reinstalling them.

Note that a quote for $74,313 ($56,823 USD) (PDF attached) was received from Hot Cell Services for them to do this job.  We were able to  successfully complete this ourselves with approximately $4500 required for the gaskets, $200 for other materials, and roughly 8 FTE days of work.

 

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Entry  Thursday, February 09, 2017, 09:24, David Wang, Conditioning Station, Development, , , Target module window cooling lines at TCS. 

Target module window  cooling lines at TCS has been modified to use spare 2 channel in TCS: WFB1. The old cooling lines used a spare channel in TCS WFB2(HVC channel) are removed and capped. After change, TCS window cooling lines will be interlocked with heaters. The test run on new lines are good. No leak  on all fittings, and signals on flow and temperature are good.   Control people will be noticed on this change for their following up job.

Entry  Tuesday, February 07, 2017, 15:57, Isaac Earle, North Hot-Cell, Development, , , Ventilation Ducting Gasket Installed 

 Lead gasket IRH1633 was installed today according to assembly drawing IRH1618 Rev B.

Entry  Tuesday, February 07, 2017, 10:34, David Wang, ITW, Maintenance, , , ITW clean up 

ITW has been cleaned up today.  All station are vacuum cleaned. I wiped all HV cover and HV area including conductors and insulators. The black foams which are used to wrap around TP back up line are degrading now. I removed most of these foams. Also, Some obsolete  water lines  are moved our of station. All waste are bagged . they will be surveyed and  stored(or disposed) according to radio-active level.

Entry  Friday, February 03, 2017, 11:49, David Wang, Conditioning Station, Standard Operation, , , Update 2017 winter shutdown TH schedule. 2017_Winter_Shut_Down_Target_Hall_Schedule.mpp2017_Winter_Shut_Down_Target_Hall_Schedule.pdf

Update 2017 winter shut down target hall schedule. See attachments

Entry  Wednesday, February 01, 2017, 12:23, David Wang, ITE, Standard Operation, TM2, , TM2 has been connected in ITE. 

TM2 has been connected in ITE. The SST window water lines in ITE can not be connected properly to TM2. The water line connector on TM2 window is 90 degree CCW installed in direction comparing to TM4.This caused the problem. Solution: Two piece of flexible lines and extra male QC adapters have been used to fix this issue.  HV cover and HV fence in ITE work  with TM2. Other connections are good as well.

Entry  Friday, January 27, 2017, 10:52, David Wang, Conditioning Station, Standard Operation, TM2, , TM2 has been moved from TCS to ITE 

The move is successful.

Entry  Friday, January 27, 2017, 08:50, chad fisher, South Hot-Cell, Standard Operation, , , UCx#18 and Ta#50 autopsy and spent target move 

On Thursday, January 26th UCx#18 and Ta#50 were inspected and packaged into spent target pails, move to storage vault.

Entry  Friday, January 27, 2017, 08:46, chad fisher, South Hot-Cell, Standard Operation, TM4, Ta#50 , Ta#50 Removed 

Ta#50 has been was removed from TM4 on Wednesday, January 25th.

Entry  Friday, January 27, 2017, 08:44, chad fisher, South Hot-Cell, Standard Operation, TM2, Ta#50, UCx #18 - Ta Feibiad Dummy installed. Target Change Waterline interference TM2_Waterline_interference.jpg

On Tuesday, January 24th UCx#18 was removed from TM2 and Ta febiad dummy installed. I encountered the same issue mounting the new target as last time. Was able to determine that the issue is the routing of the waterlines to the right-hand (as viewed from the operator) high current tube heater. The lines interfer the the target mounting plate (bottom right hand corner).

Entry  Tuesday, January 24, 2017, 15:32, David Wang, ITW, Standard Operation, TM2, , TM2 was moved from ITW to SHC this morning. 

The move is smooth. Yasmine and Travis did the move.

Entry  Tuesday, January 24, 2017, 15:29, David Wang, Conditioning Station, Standard Operation, TM2, , TM2 has been moved to TCS . 

I connected TCS vacuum system to TM2. The station is under roughing now. All turbo pumps will be started soon.

Entry  Tuesday, January 24, 2017, 15:24, David Wang, Conditioning Station, Standard Operation, TM2, , TM2 electrical check and leack check. 

I did electrical check before and after Fefiad target installation on TM2. The RU (coil) Is till short to 60KV as before. Other result are good. After Febiad target is installed, Tm2 HS line is leak checked. On leak detector, base leak rate pumping down is much slow  than before.  The base pressure still could be pumped down to 0.0XE-4 torr.  After a long time wait, Chad and I leak checked at 2.2XE-8 atm.cc/sec base leak rate. Chad sprayed lots helium around the fittings and target. No any response has been found on LD. At this leak rate, the target and HS line is leak tight.  The Tm2 has been moved to THC so a heium pressure check will be fulfilled on HS line at TCS to confirm this leak check result.  

TM2 HS line is pressurized with 70 psi helium at TCS. LD base leak rate: 0.0 X E-9 atm.cc/sec. Base pressure 0.0XE-4 torr. 5 minutes test time. The leak rate slowly climed to 3.3XE-9 atm.cc/sec and stabled there( 3minutes). base pressure no change. The leak is too small to be concern. We will run this target as this condition.

 

Entry  Thursday, January 19, 2017, 10:15, David Wang, Conditioning Station, Standard Operation, , , Target Hall schedule for 2017 winter shut down 2017_Winter_Shut_Down_Target_Hall_Schedule.mpp2017_Winter_Shut_Down_Target_Hall_Schedule.pdf2017_Winter_Shut_Down_Target_Hall_Schedule.mpp2017_Winter_Shut_Down_Target_Hall_Schedule.pdf

Updated target hall schedule for 2017 winter shut down. See attachments 1,2

Update schedule after Febiad beam schedule changed to ITE. See attachments 3,4

Entry  Wednesday, January 18, 2017, 11:53, Isaac Earle, North Hot-Cell, Development, , , NHC partition wall installation complete IMG_7728.JPG

 The final panels of the partition wall were installed today as per drawing IRH1609.  Sealing, finishing, and painting of the NHC walls and floor can now commence.

 

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Entry  Wednesday, January 18, 2017, 09:55, David Wang, ITE, Standard Operation, TM4, , ITE and TM4 2017 winter shut down leak check. 

ITE and TM4 2017 winter shut down leak check are finished. All ITE primary, secondary vacuum vessel and TM4 water lines are good. No any leak has been found.

Entry  Tuesday, January 17, 2017, 13:45, Isaac Earle, North Hot-Cell, Development, , , NHC ducting installed IMG_7688.JPGIMG_7716.JPGIMG_7723.JPGIMG_7721.JPG

 The new ducting section connecting the existing duct termination in the TCS space to the NHC partition wall has been installed by Smith Sheet Metal contractors.  The installation drawing is IRH1618.  There was not enough clearance between the duct pipe and the TCS vessel to butt weld the new ductwork as originally intended.  Instead a flange was welded to the existing pipe and also to the new section and the two were bolted together.  Drawings of the modifications have been provided by the contractor, and as-built drawings will be completed at a later date.  There was not time for the contractor to fabricate a gasket for the flanged joint, so one will be installed by TRIUMF at a later date and included in the as-built drawing package.

Entry  Monday, January 16, 2017, 09:32, David Wang, ITW, Standard Operation, TM2, , Helium pressure test on TM2 water llines at ITW 

TM2 helium pressure test result at ITW. 70 psi helium 3 minutes on each circuit. LD base LR0.0XE-9atm.cc/sec  BP 0.0XE-4torr.  ITW IG1 1.22Xe-7 torr, ITW IG1S 1.31XE-7torr, ITW PNG4 2.66XE-6Torr(ITW TP4 off).

 

  2017-01-13 (atm.cc/sec) 2017 mini shut down
HS 0.0 x E-9  
Window 0.0 x E-9  
EE 2.7 x E-9  
Ta+ 2.2 x E-9  
Ta- 6.6 x E-9  
Tube- 1.3 x E-8  
Tube+ 2.8 x E-8  
Coil 2 2.8 x E-9  
coil 1 7.1 x E-9  
MSP 6.7 x E-8  
GE leak , no test  

All number are getting better comparing to last time check. All ITW vacuum readings are very good. ITW PNG4 was in low E-7 torr range also. At present, it is in low E-6 range due to ITW TP4 switching off.  The TM2  water line seals  are stable and reliable for 2017 beam run. The same check will be repeated  in 2017 mini shut down.

Entry  Thursday, January 12, 2017, 14:24, David Wang, ITW, Standard Operation, TM2, , ITW primary and secondary vacuum vessel winter shut down leak check. 

TM2 is located in ITW for this leak check. Leak detector is installed between ITW BV2s as before. LD base leak rate 0.0XE-9atm.cc/sec, base pressure 0.0XE-4 Torr. First , I leak checked dump module top flange seal which a small leak was found in last year winter shut down. This time,all ITW  turbo-pumps cooling fans are switched off during the check. Lots helium are sprayed around the dump module top flange this time. I did not see any response on LD.  The check is repeated 3 times. The results are same. There is no leak has been found on ITW dump module top flange seal at this moment. The  further confirming check will be repeated  when TM2 is moved back to ITW with dummy Febiad target  at the end of this month. The rest check result:  1 small leak(1.2 xE-8 atm.cc/sec) is found on one TM2 blue nylon bottom o-ring. This o-ring will be replaced when module is moved out of ITW.  It will be an easy job. Another small leak( 1.1XE-8 atm.cc/sec) is found on exit module 1 service cap top plate to frame o-ring seal. Its location is on east-south side of the exit module 1.This side is close and parallel to exit module 2 west-south side. Vacu- seal sprayer is used to fix this problem.  After two times spray, the leak is disappeared. This is not a permanent fix. The big top plate o-ring replacement is a complicate and dose taking job. It need to be well planned. The leak rate is small, and the leak source is close to ITW TP3 so there is no rush to replace the big o-ring on exit 1 service cap top plate at this moment. But, we need to close watching on this issue and have a job plan for this o-ring replacement since it could get worse in the future. There is no leak has been found on big T tank seal this year as well. All other primary and secondary vacuum seals  in ITW are good. TM2 water lines helum pressurize will be fulfilled In ITW or at TCS later. I will update this e-log when further test are finished.

 2017-01-25:  The O-ring on 60KV bias blue nylon stand is replaced at TCS. I leak check it. It is perfectly good now.

Entry  Wednesday, January 04, 2017, 14:27, David Wang, Conditioning Station, Standard Operation, , , started TCS vacuum pump 

TCS TP1S has been started.

2017-01-23 afternoon: Stopped TP1S. We will use TCS to take TM2 tomorrow afternoon.

Entry  Wednesday, November 30, 2016, 16:31, David Wang, Conditioning Station, Repair, TM3, , TM3 vacuum system have been connected at TCS. 

All water circuits are by passed on the top of TM3. Water pumps and vacuum turbo- pumps are started. Everything is ready for TM3 camera sparking check.

    Reply  Monday, December 05, 2016, 10:04, Aurelia Laxdal, Conditioning Station, Repair, TM3, , TM3 vacuum system have been connected at TCS. 

David Wang wrote:

All water circuits are by passed on the top of TM3. Water pumps and vacuum turbo- pumps are started. Everything is ready for TM3 camera sparking check.

 Wednesday November 30st: <br>

- 3 cameras (1 UV and 2 regular cameras)  were installed in the Service cap and the module was pumped down.  1 UV and 1 regular were placed on the East side of the module, aiming to water lines entering the Service Tray; 1 regular camera was placed on the South side of the module, aiming at the bottom of the blue insulators.

- started pumping down. <br>

Thursday, December 1st: <br>

- 1st HV test done. TM3 started sparking above 20kV. The cameras responses were consistent with the sparks. However, the screens were flickering and it was not clear if the responses were due to electromagnetic interferences; or due to cameras' gain change caused by high intensity light due to sparking.<br>

- added helium using the regulating valve. same results were found; <br>

Friday, December 2nd: <br>

- vented the module. <br>

- shielded the cameras' cables with aluminum tape. <br>

- removed 2 blue insulator (EE and HS) and shortened them by 1". They were found too long: HS blue insulator touching the horizontal HV water line; and the EE blue insulator at 2-3mm far from the HV water line; re-installed both shortened blue insulators.<br>

- changes the location of the cameras: 1 regular camera taped to the UV camera were placed South, aiming at the bottom of the blue insulators; 1 regular camera was kept on the East side of the module, also aiming at the bottom of the blue insulators. <br>

- started pumping down. <br>

Saturday, December 3rd: <br>

- 2nd HV test was done, with cameras' installed as mentioned above. results were consistent with the first test results. <br>

- added helium. results were the same. <br>

- vented and changed the location of the cameras: 1 regular camera taped to the UV camera were placed at the top of the Service Tray (South-West corner) aiming down the Service Tray; 1 regular camera was kept (its setup was not touched at all) on the East side of the module, aiming at the bottom of the blue insulators. <br>

- attempted to pump down, but the module was leaking. reopened the flanges, cleaned them, attempted again to pump down, but it showed a bigger leak. <br>

Sunday, December 4th: <br>

- the third attempt to pump down was successful (without reopening the module!). <br>

Monday, December 5th: <br>

- did the 3rd HV test with the cameras installed as described on December 3rd. same results as before were seen. <br>

- again helium was added and same results were noticed. <br>

- stopped pumps and prepared for venting to relocate the cameras lower in the Service Tray.

 

 

 

       Reply  Friday, December 09, 2016, 18:05, Aurelia Laxdal, Conditioning Station, Repair, TM3, , TM3 vacuum system have been connected at TCS. 

Aurelia Laxdal wrote:

David Wang wrote:

All water circuits are by passed on the top of TM3. Water pumps and vacuum turbo- pumps are started. Everything is ready for TM3 camera sparking check.

 Wednesday November 30st: <br>

- 3 cameras (1 UV and 2 regular cameras)  were installed in the Service cap and the module was pumped down.  1 UV and 1 regular were placed on the East side of the module, aiming to water lines entering the Service Tray; 1 regular camera was placed on the South side of the module, aiming at the bottom of the blue insulators.

- started pumping down. <br>

Thursday, December 1st: <br>

- 1st HV test done. TM3 started sparking above 20kV. The cameras responses were consistent with the sparks. However, the screens were flickering and it was not clear if the responses were due to electromagnetic interferences; or due to cameras' gain change caused by high intensity light due to sparking.<br>

- added helium using the regulating valve. same results were found; <br>

Friday, December 2nd: <br>

- vented the module. <br>

- shielded the cameras' cables with aluminum tape. <br>

- removed 2 blue insulator (EE and HS) and shortened them by 1". They were found too long: HS blue insulator touching the horizontal HV water line; and the EE blue insulator at 2-3mm far from the HV water line; re-installed both shortened blue insulators.<br>

- changes the location of the cameras: 1 regular camera taped to the UV camera were placed South, aiming at the bottom of the blue insulators; 1 regular camera was kept on the East side of the module, also aiming at the bottom of the blue insulators. <br>

- started pumping down. <br>

Saturday, December 3rd: <br>

- 2nd HV test was done, with cameras' installed as mentioned above. results were consistent with the first test results. <br>

- added helium. results were the same. <br>

- vented and changed the location of the cameras: 1 regular camera taped to the UV camera were placed at the top of the Service Tray (South-West corner) aiming down the Service Tray; 1 regular camera was kept (its setup was not touched at all) on the East side of the module, aiming at the bottom of the blue insulators. <br>

- attempted to pump down, but the module was leaking. reopened the flanges, cleaned them, attempted again to pump down, but it showed a bigger leak. <br>

Sunday, December 4th: <br>

- the third attempt to pump down was successful (without reopening the module!). <br>

Monday, December 5th: <br>

- did the 3rd HV test with the cameras installed as described on December 3rd. same results as before were seen. <br>

- again helium was added and same results were noticed. <br>

- stopped pumps and prepared for venting to relocate the cameras lower in the Service Tray.

 

 

 

 Monday, December 5th (Con't): <br>

- vented and changed the location of the cameras;<br>

- the UV camera was placed (tapped on an aluminum spacer and on the grounded water lines) at the middle of the Service Tray (right below the first Mykroy insulator-plate) aiming down the Service Tray (at the second Mykroy insulator-plate and water lines) ; <br>

- 1 regular camera was placed right below the UV camera, also using a spacer (taped with the camera on grounded water lines) and also aiming down the Service Tray (at the second Mykroy insulator-plate and water lines);  The spacer for this camera had 300counts on it after it was removed from TM3, after the test;<br>

- NOTE: when installing the 1st regular camera: dropped a small allen key in the Service Tray. It landed on last insulator with the epoxi and water lines, between the first HV line and the wall of the grounded Service Tray.  This insulator is down below in the Service tray. Used a magnet stick to recuperate the allen key. <br>

- the 2nd regular camera was placed at the top of the Service Tray (tapped on the grounded water lines) looking down at the first Mykroy insulator-plate and water lines. NOTE: this camera had a filter applied to its lens. <br>

- pumped down <br>

Tuesday, December 6th:<br>

- did the 4th HV test with the cameras installed as described on December 5rd Tuesday morning very early . Same results as before were seen, except that the top camera (2nd regular camera) with the filter applied to its lens was flickering less than the other 2 cameras, and for small sparks this camera was not reacting at all. <br>

- vented shortly after the 4th test and relocated the cameras for the 5th HV test (last test); <br>

- placed only 2 regular cameras in the Service Tray;<br>

- 1 regular camera was placed right below the 2nd Mykroy insulator-plate, aiming down the Service Tray at the last insulator with the epoxi and water lines (this insulator is down below in the Service tray); <br>

- the 1st regular camera was placed a level up in the Service Tray, right below the 1st Mykroy insulator-plate, aiming down the Service Tray at the 2nd Mykroy insulator-plate; <br>

- NOTE: no spacers were used<br>

- pumped down and did the 5th HV test with the cameras installed as described above in the evening; <br>

- again same results as before were seen: the camera with the filter applied to its lens was flickering less than the other camera, and for small sparks this camera was not reacting at all. <br>

- NOTE: for this last test heard sparks outside (at atmosphere) when the HV was pushed at 26kV; <br>

Wednesday, December 7th:<br>

- vented and removed the cameras from TM3. No contamination was found on the cameras and wires. <br>

- TM3 was moved to the silo.<br>

Entry  Friday, December 09, 2016, 14:58, Isaac Earle, North Hot-Cell, Development, , , NHC service area floor and top of roof block painted NHC_SA_before_and_after.jpgNHC_roof_before_and_after.jpg

 The concrete floor in the North Hot Cell service area and the top of the NHC roof block in the target hall have been painted with Macropoxy 646 oil based epoxy paint, colour Flint Grey.  Two coats were used for the NHC roof, and one for the service area floor.

 

NHC_SA_before_and_after.jpg

 

NHC_roof_before_and_after.jpg

Entry  Monday, December 05, 2016, 10:10, David Wang, ITW, Standard Operation, TM2, , Five shielding blocks have been transferred from ITE to ITW.  

The ITW is configured to take proton beam.

Entry  Saturday, December 03, 2016, 10:01, David Wang, ITW, Repair, TM2, , venting ITW and TM2 with argon. 

A short between TM2 EE and bias is produced yesterday during tube heater ramp up.  Alex asked for an argon venting on ITW to see if the problem could be solved by venting and pumping down yesterday.  I set up argon venting system in electrical room and started the venting at 8:30 AM this morning.  It will take 5 hours to vent the ITW to 760 torr(mechanical gauge reading).  The venting system pressure is set as 2 torr. A pressure relieve valve is installed into ITW venting line to prevent station over venting. The argon bottle  valve in electrical room will be closed by isac opps after 5 hours venting.

Entry  Tuesday, November 29, 2016, 14:50, Travis Cave, ITW, Standard Operation, TM2, UC#18, module moved 

TM#2 with UC#18 has been moved to ITW from the conditioning station.

Entry  Tuesday, November 29, 2016, 12:57, David Wang, ITW, Standard Operation, TM2, , TM2 is connected in ITW 

All turbo pumps are started. Water system and water signals have been checked. Pumping down on ITW and TM2 is good so far.

Entry  Tuesday, November 29, 2016, 07:50, David Wang, Conditioning Station, Standard Operation, TM2, , TM2 is disconnected at TCS. 

Argon venting is done.

Entry  Tuesday, November 29, 2016, 06:27, David Wang, Conditioning Station, Standard Operation, TM2, , TCS water pumps are stopped 

Argon venting on TCS and TM2 is processing

Entry  Friday, November 25, 2016, 09:04, Travis Cave, Spent Target Vault, Standard Operation, , SiC#35, Spent Target move Vault_Storage_November_24_2016.pdf

On November 24th 2016 the spent SiC#35 was moved from the south hot cell to the spent target vault. see attached pdf for details.

Entry  Thursday, November 24, 2016, 10:30, David Wang, Conditioning Station, Standard Operation, TM2, , HV cover is installed on TM2 at TCS 

Interlock key  are returned back to B2 level.TM2 is ready for HV conditioning and heating up at TCS.

Entry  Thursday, November 24, 2016, 09:33, Anders Mjos, Conditioning Station, Standard Operation, TM2, UC#18, Conditioning UC#18 

Thursday, November 24, 2016, 09:33: Water package on

Thursday, November 24, 2016, 09:43: TCS:WPV1 shows only 12% open. A visual inspection confirms the valve is fully opened. Controls will be contacted to troubleshoot

 

Entry  Wednesday, November 23, 2016, 16:21, David Wang, Conditioning Station, Standard Operation, TM2, , TM2 and TCS vacuum system has been connected. 

All vacuum pumps have been started. Air ballast 50seconds on roughing pump. Everything is good  so far.

Entry  Wednesday, November 23, 2016, 16:10, David Wang, South Hot-Cell, Standard Operation, TM2, , SHC, TM2 leak check on HS line. 

Chad and I leak checked TM2 HS line with new UCx target installed. Helium spray  2 seconds on each joint and 10seconds flushing around target in SHC. LD base LR: 0.0XE-9atm.cc/sec, base pressure:0.0XE-4 torr. No response has been found on LD during check. The line is leak free.

Entry  Wednesday, November 23, 2016, 14:25, Travis Cave, South Hot-Cell, Standard Operation, TM2, UC#18, Electrical Check TM2_elechk_UC18_SHC.PDF

Results of TM#2 with UC#18 electrical at the south hot cell. See attached PDF for details.

Entry  Wednesday, November 23, 2016, 14:21, Travis Cave, Conditioning Station, Standard Operation, TM2, UC#18, module moved 

TM#2 with UC#18 has been moved from the south hot cell to the conditioning station.

Entry  Tuesday, November 22, 2016, 14:26, David Wang, Conditioning Station, Standard Operation, , , TCS vacuum pumps are switched off 

TCS will be vented tomorrow morning for TM2 moving.

Entry  Tuesday, November 22, 2016, 11:56, Travis Cave, South Hot-Cell, Standard Operation, TM2, SiC#35, Electrical Check TM2_elechk_SiC35_postbeam.PDF

Electrical check of TM#2 with the SiC#35  post beam run. See attached PDF for details.

Entry  Tuesday, November 22, 2016, 10:45, Travis Cave, South Hot-Cell, Standard Operation, TM2, SiC#35, module moved 

TM#2 with the old SiC #35 has been moved from ITW to the south hot cell.

Entry  Tuesday, November 15, 2016, 07:53, David Wang, Conditioning Station, Standard Operation, TM4, , Target Hall schedule for beam schedule 131(Sep-Dec, 2016) Target_Hall_shedule_131_Sep_to_Dec.pdfTarget_Hall_shedule_131_Sep_to_Dec.mppTarget_Hall_shedule_131__Sep_to_Dec_2016.pdf

Update TH schedules . See attachments

Entry  Tuesday, November 08, 2016, 14:45, David Wang, ITE, Maintenance, TM4, , TM4 has been moved to ITE and connected there. 

All ITE and TM4  turbo pumps are started. The east station pumping down is good so far.

Entry  Tuesday, November 08, 2016, 14:04, Isaac Earle, North Hot-Cell, Development, , , Interference check with TCS turbo pump and proposed NHC duct routing IMG_7577.JPGIMG_7583.JPGIMG_7582.JPG

David Wang and I accessed the NHC today to check if the proposed duct routing (IRH1618) will interfere with servicing or replacement of the TCS turbo pump.  A piece of plywood was placed in the future position of the NHC/TCS partition wall (IRH1609), and a ducting elbow was placed at the approximate position of the nearest elbow to the turbo pump.

David concluded that the ducting in the proposed location will not have any significant effect on replacement of the turbo pump, and he does not expect replacement will be difficult to perform after installation of the wall and NHC ducting.  Standing at floor level towards the east side of the TCS space and reaching upwards seemed to be the best way to reach the turbo pump flange bolts.  It was also noted that there was sufficient room in the TCS space for two workers to be in the area.

 

IMG_7577.JPG

 

IMG_7583.JPG

 

IMG_7582.JPG

Entry  Tuesday, November 08, 2016, 10:23, Travis Cave, ITE, Standard Operation, TM4, Ta#50, module moved 

TM#4 with Ta#50 has been moved to the east target station.

Entry  Tuesday, November 08, 2016, 07:47, David Wang, Conditioning Station, Standard Operation, TM4, , TCS water and vacuum pumps are switched off 

TCS is vented. TM4 is disconnected and TCS.

Entry  Monday, November 07, 2016, 10:35, Travis Cave, Spent Target Vault, Standard Operation, , SiC#34, Spent Target move Vault_Storage_November_3_2016.pdf

Spent SiC#34 was moved on the 3rd of November and  placed in the spent target vault. See attached pdf for details.

Entry  Thursday, November 03, 2016, 09:01, David Wang, Conditioning Station, Standard Operation, TM4, , TCS water system has been started for TM4. 

The system works fine. All water signals to TM4 at TCS are normal. HV cover is installed on to TM4 at TCS.

Entry  Thursday, November 03, 2016, 08:57, David Wang, Conditioning Station, Standard Operation, TM4, , Helium pressure test on TM4 HS line at TCS 

70 psi helium ,2minutes to  TM4 HS line. LD base leak rate 0.0xE-9 atm.cc/sec. No leak.

Entry  Wednesday, November 02, 2016, 13:41, David Wang, Conditioning Station, Standard Operation, TM4, , TM4 has been connected at TCS.  

All turbo-pumps are started. The pumping down is good so far.

Entry  Wednesday, November 02, 2016, 09:12, Travis Cave, Conditioning Station, Standard Operation, TM4, Ta#50, module moved 

TM#4 with Ta#50 has been moved from the south hot cell to the conditioning station.

Entry  Tuesday, November 01, 2016, 14:58, David Wang, South Hot-Cell, Standard Operation, TM4, , SHC, TM4 leak check on HS line. 

Chad and I did a leak check on TM4 HS line with new Ta target installed. Base leak rate 0.0xE-9 atm.cc/sec. base pressure 0.0XE-4.   splayed 2 helium to each VCR joints and did 10 seconds helium flush. No response on LD during the test. The HS line is leak free so far. It will be helium pressurized at TCS later.

Entry  Tuesday, November 01, 2016, 14:54, David Wang, ITE, Standard Operation, TM4, , TM4 was disconnected at ITE 

TM4 was disconnected at ITE this morning. It was moved to SHC  after. No alpha alarm issue has been happened during and after move. The ventilation pumping down procedure on ITE was fulfilled during the move.

Entry  Tuesday, November 01, 2016, 14:53, David Wang, ITE, Standard Operation, TM4, , TM4 was disconnected at ITE 

TM4 was disconnected at ITE this morning. It was moved to SHC  after. No alpha alarm issue has been happened during and after move. The ventilation pumping down procedure on ITE was fulfilled during the move.

Entry  Wednesday, October 26, 2016, 12:33, David Wang, Conditioning Station, Standard Operation, TM2, , Target Hall schedule for beam schedule 131(Sep-Dec, 2016) Target_Hall_shedule_131__Sep_to_Dec_2016.pdfTarget_Hall_shedule_131_Sep_to_Dec.mppTarget_Hall_shedule_131_Sep_to_Dec.pdf

Update TH schedule after job delay on TM2 Febiad target. Everything should be back to schedule on last two targets. See attachments.

Entry  Tuesday, October 25, 2016, 15:10, David Wang, ITW, Standard Operation, TM2, , TM2 has been connected at ITW 

All turbo pumps are started. Two gas valves for Febiad run are opened. Pumping down is good so far.

Entry  Monday, October 24, 2016, 14:56, Travis Cave, South Hot-Cell, Standard Operation, TM2, SiC#35, Electrical Checks TM2_elechk_notgt_SHC_repair.PDFTM2_elechk_SiC35_SHC.PDF

Results of the electrical check of TM#2 with no target after the repair and with the SiC#35 mounted on the module.

Entry  Monday, October 24, 2016, 14:54, David Wang, South Hot-Cell, Standard Operation, TM2, , SHC, TM2 leak check on HS line. 

Chad and I did the leak check on TM2 heat shield line. LD base leak rate:0.0xE-9atm.cc/sec. Base pressure:0.0X E-9 torr. The line is leak free.

Entry  Monday, October 24, 2016, 14:44, chad fisher, South Hot-Cell, Standard Operation, TM2, SiC#35, SiC#35 installed 20161024_141155.jpg

Sic#35 has been installed onto TM2. High current fasteners torqued to 130 in lbs.

Mating of the 9 pin connector was extremely problematic but in the end I was able to get it to mate properly. Noticed left (when facing module in hot cell) febiad coil left twisted a bit when torqued up.

Entry  Monday, October 24, 2016, 12:22, chad fisher, South Hot-Cell, Repair, , , TM2 Insulator replacement 

conductor insulators itd0053 and 54 have been replaced on TM2. All fasteners (1/4-20 x 1 1/4 vented) torqued to 60 in lbs.

Entry  Monday, October 24, 2016, 11:34, Travis Cave, South Hot-Cell, Standard Operation, TM2, no target, module moved 

TM#2 has been moved from the south west silo to the south hot cell.

Entry  Monday, October 24, 2016, 10:10, chad fisher, South Hot-Cell, Repair, , , Manipulator Repair Complete 

Maico entered the hot cell and re-strung the skipped cable back onto the pulleys this morning. Manipulator is now operational.

Entry  Friday, October 21, 2016, 15:10, Anders Mjos, South Hot-Cell, Repair, TM2, Ta#49, Stuck TGHT clamp bolt removal 

During target removal on Wednesday October 12th, the left target heater conductor bolt (ITD0058) could not be removed. The bolt was found to be stuck in the threads (keensert) of the TGHT conductor block (ITA0583). In the process of attempting to remove the bolt, the conductor insulator (ITD0054) cracked (ref assy ITD0052). To allow increased torque to be applied and support the conductor block, a clamping jig (ITD0612) was designed and fabricated. The jig was assembled and it's function tested on the ISAC Test Stand on Friday 14th. On Monday 17th the bolt could be removed using the clamping jig and a socket wrench with an extended handle.

The threads on the removed bolt was damaged. A new set of bolts were therefore prepared and a tap was run through the keensert to restore the threads. The threads in the conductor block was tested and found to be OK using a new bolt.

The spent target could now be removed. Unfortunately the right manipulator failed during installation of a new conductor insulator, which forced the repair of the insulator and installation of the new target (SiC#35) to be postponed until the manipulator can be repaired.

Photos are available on DocuShare

Entry  Friday, October 21, 2016, 12:51, chad fisher, South Hot-Cell, Repair, , , Manipulator Repair 

Broken cable has been replaced however a cable has hopped some pulleys inside. After two hours in cell the job was stopped with cables still off pulleys. Alternate tooling will have to be made and the job will continue Monday.

Entry  Thursday, October 20, 2016, 14:17, Anders Mjos, ITE, Repair, TM4, SiC#34, HV enclosure inspection SiC#34_Dose_Map_Target_Pit.pdfSiC#34_Dose_Measurements.xlsx

 The HV enclosure and module connections were inspected by David and Anders on Wednesday 19th in an attempt to find any HV problems causing the high leakage current. One cable was cable tied to a copper conductor in the chase. Some small pieces of loose material were removed. No obvious problems could be detected.

Entry  Thursday, October 20, 2016, 10:45, Travis Cave, Spent Target Vault, Standard Operation, , Ta#49, Spent Target move 

Ta#49 has been removed from the south hot cell and placed in the storage vault. It is in pail 146 and in spot 6A.

Entry  Wednesday, October 19, 2016, 11:46, Travis Cave, South Hot-Cell, Standard Operation, TM2, no target, module moved 

TM#2 has been moved from the south hot cell to the south west silo.

Entry  Wednesday, October 12, 2016, 10:01, David Wang, Conditioning Station, Standard Operation, , , TCS pumps are stopped 

Argon venting is started

Entry  Wednesday, October 12, 2016, 10:00, David Wang, ITW, Standard Operation, TM2, , TM2 was disconnected at ITW 

TM2 was disconnected at ITW. 3 water circuits in ITW gave been looped to keep 75 GPM water flow to ITW. HS line was purged at HS. RPG got the water sample.

Entry  Tuesday, October 11, 2016, 10:36, Travis Cave, ITW, Standard Operation, TM2, Ta#49, module moved 

TM#2 with Ta#49 has been moved from the west target station to the south hot cell.

Entry  Tuesday, October 04, 2016, 09:18, David Wang, ITE, Standard Operation, TM4, , 5 Shielding blocks have been transferred from ITW to ITE. 

The ITE is configured to take proton beam.

Entry  Friday, September 30, 2016, 14:34, David Wang, Conditioning Station, Standard Operation, , , Target Hall schedule for beam schedule 131(Sep-Dec, 2016)  Target_Hall_shedule_131_Sep_to_Dec.mppTarget_Hall_shedule_131_Sep_to_Dec.pdf

Weekly update TH schedule for beam schedule 131. See attachments 1,2

Entry  Wednesday, September 28, 2016, 13:47, David Wang, Conditioning Station, Standard Operation, , , TCS pumping down during mini-shut down. 

A steel plate  is covered on TCS. TCS roughing pump  is started now. The TCS will be pumping down during mini-shut down.

Entry  Wednesday, September 28, 2016, 13:43, David Wang, ITE, Standard Operation, TM4, , TM4 has been connected at ITE 

All ITE turbo pumps have been started since yesterday afternoon. The ITE and TM4 pumping down is good so far.

Entry  Tuesday, September 27, 2016, 09:13, Travis Cave, ITE, Standard Operation, TM4, SiC#34, module moved 

TM#4 with SiC #34 has been moved to the east target station.

Entry  Tuesday, September 27, 2016, 07:30, David Wang, Conditioning Station, Standard Operation, TM4, , TM4 has been disconnected at TCS 

TCS water system and vacuum system are turned  off this morning. The TCS and TM4 are vented.

Entry  Monday, September 26, 2016, 13:59, Travis Cave, Spent Target Vault, Standard Operation, , UC#17, Spent Target move Vault_Storage_September_26_2016.pdf

The spent UC#17 has been moved from the south hot cell to the spent target vault. See the attached pdf for details.

Entry  Saturday, September 24, 2016, 11:23, Anders Mjos, Conditioning Station, Standard Operation, TM4, SiC#34, Conditioning SiC#34 SiC#34.docxTCS-2016-09-22_SiC#34.rgaTCS-2016-09-24_SiC#34.rga

Conditioning by ISAC operations

Saturday, September 24, 2016, 11:15: RGA on for heater conditioning. (kept off during HV conditioning)


Sunday, September 25, 2016, 07:44: TGHT and TBHT voltage jumps during heater ramping. Likely contact between target and heat shield. Contacted ISAC operations and asked to abort ramping at current values. TGHT/TBHT 500 /270 A


Monday, September 26, 2016, 08:22: ISAC operations resuming ramping to 550 A. Corrected TGHT voltage at ISAC TS was ~6.2 V at 580 A. Expected voltage at TCS would then be 6.2 + (3.4+2.9)E-3*580 = 9.9 V. Limit set at 9.5 V.

Monday, September 26, 2016, 09:09: Increased TGHT voltage limit to 9.6 V to allow it to reach 550 A.

Monday, September 26, 2016, 10:17: Voltage limit increased to 10.2 V which allowed the current to go to 575 A


Tuesday, September 27, 2016, 08:08: Conditioning complete. Ran at 575 / 270 A and 47 kV for about 1 hour. Conditioned cold to 49 kV.

Entry  Friday, September 23, 2016, 08:55, Travis Cave, Conditioning Station, Standard Operation, TM4, SiC#34, Electrical Checks TM4_elechk_SiC34_SHC.PDF

The bundle of electrical checks, first one is the Iglis that failed, the second is the everything passed at the hot cell and the third is a the conditioning station under vacuum.

Entry  Friday, September 23, 2016, 07:49, David Wang, Conditioning Station, Standard Operation, TM4, , TM4 has been moved and connected at TCS 

All TCS and TM4 turbo-pumps were started yesterday. Overnight pumping down is good so far.

Entry  Thursday, September 22, 2016, 13:04, David Wang, South Hot-Cell, Standard Operation, TM4, , SHC, TM4 leak check on HS line. 

Chad and I leak checked the TM4 HS line after new target installation. base leak rate:0.0Xe-9 atm.cc/sec.  No response on LD during the leak check. The line is leak free so far. It will be helium pressurized at TCS  late.

Entry  Tuesday, September 20, 2016, 11:48, David Wang, Assembly/Bench Test, Development, , , A silo and blue steel frame are removed out of TH  

A silo and blue steel frame are removed out of TH this morning. They are transferred  through ante room, and moved to experimental hall TM assembly area for a long term storage. Swipes are done on the silo and frame before and during move. No contamination has been found .

Entry  Tuesday, September 20, 2016, 11:41, David Wang, ITE, Standard Operation, TM4, , TM4 has been disconnected in ITE. 

TM4 has been disconnected in ITE. No water line purge on HS and 3 water circuits are looped after disconnection. The HALCW system resistivity is stable before and after this disconnection.

Entry  Tuesday, September 20, 2016, 10:32, Travis Cave, South Hot-Cell, Standard Operation, TM4, UC#17, module moved 

TM#4 has been moved from the east target station to the south hot cell

Entry  Monday, September 19, 2016, 08:28, David Wang, Conditioning Station, Standard Operation, , , Target Hall schedule for beam schedule 131(Sep-Dec, 2016) Target_Hall_shedule_131__Sep_to_Dec_2016.pdfTarget_Hall_shedule_131__Sep_to_Dec_2016.xlsxTarget_Hall_shedule_131_Sep_to_Dec.mppTarget_Hall_shedule_131_Sep_to_Dec.pdf

Post new  target hall Excel sheet schedule for beam schedule 131. See attachment 1,2

Post new target hall  MS project schedule for beam schedule131. See attachment 3,4

Entry  Thursday, September 15, 2016, 11:05, Isaac Earle, North Hot-Cell, Development, , , NHC / SHC feedthrough panel removed original_panel.JPGpanel_removed.JPGtemp_panel.JPG

The sheet metal panel covering the NHC/SHC feedthrough port was removed today using a slide-hammer to pull out the concrete anchors (this oversized panel would have interfered with the NHC partition wall).  50cpm was found on the inside of the panel, 100cpm on the NHC side lip of the feedthrough, and 350cpm on the face of the shielding bricks in the feedthrough.  Various dimensional measurements of the feedthrough were taken which will be added to the partition wall Solidworks model (IRH1609).  The panel was bagged for disposal and a temporary 20"x20" panel was put over the feedthrough and secured with duct tape.  A permanent panel with anchored supports that is compatible with the NHC partition wall will be designed and installed at a later date.  A swipe of the NHC walls and floor picked up 30cpm after completion of the job.  

Entry  Wednesday, September 14, 2016, 13:53, Travis Cave, Conditioning Station, Standard Operation, TM3, no target, Module move 

TM#3, no target, has been moved from the conditioning station to the north east silo.

Entry  Wednesday, September 14, 2016, 11:54, David Wang, Conditioning Station, Repair, TM3, , TM3 is disconnected at TCS. 

 TM3 is disconnected at TCS and ready to be moved to silo.

Entry  Tuesday, September 13, 2016, 13:52, Anders Mjos, Conditioning Station, Standard Operation, TM3, , HV Test with new insulators on Service Cap (vacuum to air) TM3_HV_conditioning_2016-09-13.docxTCS-2016-09-11_TM3_New_Blue_Insulators.rga

Tuesday, September 12, 2016, 10:00: RGA on


Tuesday, September 13, 2016, 13:52: Source on

Tuesday, September 13, 2016, 13:55: BIAS / EL at 10 / 5 kV

Tuesday, September 13, 2016, 13:59: BIAS / EL at 18 / 9 kV

Tuesday, September 13, 2016, 14:06: BIAS / EL at 20 / 10 kV. Minor sparking

Tuesday, September 13, 2016, 14:25: Sparking at about 1 spark/min for the last 10 min

Tuesday, September 13, 2016, 15:38: ~10 sparks for the last 60 min.

Tuesday, September 13, 2016, 15:41: BIAS / EL 22 / 11 kV

Tuesday, September 13, 2016, 15:57: Heavy sparking at 24 kV. Lowered to 21 kV. EL at 12.5 kV

Tuesday, September 13, 2016, 16:00: BIAS / EL at 22 / 12.5 kV

Tuesday, September 13, 2016, 16:05: Trip on resistivity caused by spark

Tuesday, September 13, 2016, 16:07: BIAS / EL at 10 / 5 kV

Tuesday, September 13, 2016, 16:14: BIAS / EL at 20 / 10 kV

Tuesday, September 13, 2016, 16:25: BIAS / EL at 22 / 11 kV

Tuesday, September 13, 2016, 17:00: Sparking at about 1 spark/min for the last 30 min

Tuesday, September 13, 2016, 17:02: Source off.


Wednesday, September 14, 2016, 08:22: BIAS / EL at 20 / 10 kV

Wednesday, September 14, 2016, 08:33: BIAS / EL at 22 / 11 kV

Wednesday, September 14, 2016, 08:35: Trip on resistivity caused by spark

Wednesday, September 14, 2016, 08:38: BIAS / EL at 20 / 10 kV

Wednesday, September 14, 2016, 08:41: BIAS / EL at 21.5 / 11 kV

Wednesday, September 14, 2016, 08:45: BIAS / EL at 22 / 11 kV

Wednesday, September 14, 2016, 09:06: Sparking at about 1 spark/min for the last 20 min

Wednesday, September 14, 2016, 10:17: Sparking rate somewhat reduced. BIAS / EL at 23 / 11 kV

Wednesday, September 14, 2016, 10:23: BIAS / EL at 24 / 12 kV

Wednesday, September 14, 2016, 10:31: BIAS / EL at 25 / 12 kV.

Wednesday, September 14, 2016, 10:32: Trip on resistivity caused by spark

Wednesday, September 14, 2016, 10:36: BIAS / EL at 20 / 10 kV

Wednesday, September 14, 2016, 10:40: BIAS / EL at 23 / 12 kV

Wednesday, September 14, 2016, 10:51: BIAS / EL at 24 / 12 kV

Wednesday, September 14, 2016, 10:57: BIAS / EL at 25 / 12 kV

Wednesday, September 14, 2016, 11:01: Heavy sparking at 25 kV (>15 /min). Trip on resistivity caused by spark

Wednesday, September 14, 2016, 11:10: RGA off.

Entry  Monday, September 12, 2016, 09:25, David Wang, Conditioning Station, Repair, TM3, , TM3 leak checked at TCS 

After blue insulators replacement, TM3 service cap are leak checked. LD base leak rate 0.0xe-9 atm.cc/sec. I sprayed lots helium on all blue insulator seals. No leak has been found. Double checked them again, and got same result. All other seals on top of TM3 also have been checked. They are leak free. OVEN, TUBE, MSP, COIL, and EE water lines are pressurized with 70 psi helium for 3minutes each. They are good also.

Entry  Thursday, September 08, 2016, 16:30, David Wang, Conditioning Station, Repair, TM3, , TM3 vacuum system have been connected at TCS. 

start of roughing now.

 start of TCS and TM3 turbo-pumps. Everything is good so far.

Entry  Thursday, September 08, 2016, 16:28, David Wang, Conditioning Station, Repair, TM3, , TM3 blue insulators have been replaced. 

All TM3 blue insulators except Gas,EL, and 60 KV common  on top of the module have been replaced with new designed insulators. The new blue insulator for gas line need to be modified to fit for the bent on the gas  line.   EL, and 60KV common blue insulators were replaced during last time TM3 refurbishment so they are relative new, and  not replaced this time. All seals related to the blue insulators are changed to new seals. The o- r-ing surfaces  for o-ring 221 inside the  new insulators  are rougher than old parts. The module top need to be leak checked.

Entry  Wednesday, September 07, 2016, 11:44, Travis Cave, Conditioning Station, Standard Operation, TM3, no target, module moved 

TM#3 has been moved from the NE Silo to the conditioning station.

Entry  Wednesday, September 07, 2016, 11:39, Isaac Earle, North Hot-Cell, Development, , , NHC North / South Wall Gap Measurements 

 Measurements were taken today of the NHC north/south wall gap at the location where the NHC/TCS partition wall will be installed (43.375" from the NHC west wall).  A HILTI PD40 laser range meter was used for the measurements.  They were taken at 10", 34", 62", 90", 118", and 142" from the floor which matches the top of each cross-beam.  The results are below:

10" from floor:  102.44"
34" from floor:  102.40"
62" from floor:  102.48"
90"  from floor:  102.63"
118" from floor:  102.28"
142" from floor:  102.24"

 

Based on these results a partition wall plate width of 102.00" will be used for the bottom two plates, and 102.25" for the upper three plates in order to keep the gap on each side approximately 1/8"

Entry  Tuesday, September 06, 2016, 10:05, David Wang, ITW, Standard Operation, TM2, , 5 Shielding blocks have been transferred from ITE to ITW. 

5shielding blocks have been transferred from ITE to ITE. ITW is configured to take proton beam.

Entry  Tuesday, August 30, 2016, 13:17, David Wang, ITW, Standard Operation, TM2, , TM2 has been connected at ITW 

  ITW turbo pumps  have been started.

Entry  Tuesday, August 30, 2016, 10:35, Travis Cave, ITW, Standard Operation, TM2, Ta#49, module moved 

TM#2 with Ta#49 has been moved to the west target station from the conditioning station.

Entry  Monday, August 29, 2016, 13:34, David Wang, Conditioning Station, Standard Operation, TM2, , TM2 has been disconnected at TCS 

I stopped TCS water pumps and vacuum pumps also.   TM2 and TCS will be vented tomorrow morning.

Entry  Thursday, August 25, 2016, 14:25, Travis Cave, Spent Target Vault, Standard Operation, , SiC#33, Spent Target move Vault_Storage_August_25_2016.pdf

SiC#33 was placed into pail #141 which in turn was placed into slot 2B of the vault. I was 295mS/hr upon removal from the south hot cell.

Entry  Thursday, August 25, 2016, 13:59, David Wang, Conditioning Station, Standard Operation, , , Target Hall schedule for beam schedule 130 (Apr- Sep, 2016) Target_Hall_shedule_130_Apr_to_Sep.pdfTarget_Hall_shedule_130_Apr_to_Sep.mpp

Weekly update schedule.  See attachment 1,2.

Entry  Thursday, August 25, 2016, 08:43, David Wang, Conditioning Station, Standard Operation, TM2, , All TM2 connections to TCS are done. 

The HV cover is installed. The Faraday cage at B2 level is locked also.The TCS and TM2 are still pumping down. Everything is good so far.

Entry  Thursday, August 25, 2016, 08:36, David Wang, Conditioning Station, Standard Operation, TM2, , Helium pressure test on TM2 HS water lline  

I did a helium pressure test on TM2 HS water line at TCS. Leak detector base leak rate only could get to 1.8x e-8 atm.cc/sec at this moment. Applied 5 minutes 70psi helium on it. No leak has been found at this level. I connected water to this circuit after the test for weekend TM2 conditioning at TCS.

I will do another helium pressure test after the conditioning. The LD base leak rate should be 0.0Xe-9 atm.cc/sec at that time.

2016-08-29: LD Base leak rate 0.0xe-9atm.cc/sec.TM2 HS line helium pressure check again after conditioning. 70psi helium 5minutes. no response on LD. HS line is perfectly sealed.

Entry  Wednesday, August 24, 2016, 14:42, Anders Mjos, Conditioning Station, Standard Operation, TM2, Ta#49, Conditioning TCS-2016-08-24_Ta#49.rgaTa#49.docx

Wednesday, August 24, 2016, 14:42: RGA on

Wednesday, August 24, 2016, 20:27: IG2 and IG1S on. Checked on water system.


Conditioning by ISAC operations. Water flow tripped power supplies after a few hours of conditioning at 580 / 230 A and 30 kV. See operations e-log for details.

Entry  Wednesday, August 24, 2016, 14:37, Anders Mjos, South Hot-Cell, Standard Operation, , SiC#33, PIE 

 The target was inspected by Anders and Chad. The target was in good condition as can be seen on the photos on DocuShare. Only minor accumulation of material on the EE.

Entry  Wednesday, August 24, 2016, 11:06, Travis Cave, South Hot-Cell, Standard Operation, TM2, Ta#49, module moved and electrical check TM2_elechk_SiC34_SHC.PDF

TM#2 with Ta#49 has had its electrical check and was moved to the conditioning station. see the attached pdf for the electrical check details.

The electrical check has been edited to reflect that well the original has been just not the PDF.

Entry  Wednesday, August 24, 2016, 10:45, David Wang, Conditioning Station, Standard Operation, TM2, , TM2 vacuum system has been connected at TCS 

Start of roughing now.

Entry  Wednesday, August 24, 2016, 10:44, David Wang, South Hot-Cell, Standard Operation, TM2, , SHC, TM2 leak check on HS line. 

Chad and I leak checked Tm2 Hs line with new target installed. Base LR 0.0Xe-9 atm.cc/sec.   No leak has been found. This line will be helium pressured at TCS later.

Entry  Wednesday, August 24, 2016, 10:41, David Wang, ITW, Standard Operation, TM2, , TM2 was disconnected in ITW yesterday. 

TM2 was disconnected in ITW yesterday and moved to SHC.

Entry  Wednesday, August 24, 2016, 09:19, chad fisher, South Hot-Cell, Maintenance, , , Anteroom Clean -up paint prep 

Remaining items from anteroom have been bagged and removed (save the boot boxes, 1 garbage can and 1 coverall garbage can).

Room is ready to be surveyed so it can be deemed a non-boot box area for painting.

Entry  Wednesday, August 24, 2016, 09:17, chad fisher, South Hot-Cell, Standard Operation, TM2, , Ta#49 

Ta#49 has been installed on TM2 and tested. All high current fasteners torqued to 130 in lbs.

Entry  Tuesday, August 23, 2016, 13:31, chad fisher, South Hot-Cell, Standard Operation, TM2, SiC#33, SiC#33 Removed 

SiC#33 has been removed from TM2.

Entry  Tuesday, August 23, 2016, 10:39, Travis Cave, South Hot-Cell, Standard Operation, TM2, SiC#33, module moved 

TM#3 with SiC#33 has been moved from the west station to the south hot cell.

Entry  Tuesday, August 23, 2016, 08:05, chad fisher, South Hot-Cell, Maintenance, , , Post Hot Cell Entry Clean-up 

Plastic has been removed from the floor and any known active items in the hot cell moved to the south east corner in an attempt to shield the anteroom. Fields at the aluminum panel were reduced from 66 uSv/h to 58.8uSv\h. No contamination found on walls, floor, tacky mats, or standard aluminum cover. The aluminum cover with breathable air line hole did have 400 counts on 44-2, 1200 on ludlum.

 

Entry  Thursday, August 18, 2016, 14:19, Travis Cave, Conditioning Station, Standard Operation, TM3, no target, module moved 

TM#3 is now back in the the north east silo.

Entry  Thursday, August 18, 2016, 13:57, chad fisher, South Hot-Cell, Maintenance, , , Manipulator maitenance 

South hot cell was entered to check to replace cable if needed. Wrist cable showed no signs of fraying or broken strands.

A tong with new cable pre-installed is now in the hot cell for next time this job needs to be done. There is also another spare tong cable not installed in a tong located in the box of manipulator repair equipment located inside the hot cell.

Both manipulator slave ends were lubricated whilst inside.

Entry  Friday, July 08, 2016, 16:56, Anders Mjos, Conditioning Station, Repair, , , VFD21 OL1 fault on Chiller 

Plant Services group (Tony) will contact a service tech on Monday.

Water system will be switched off over the weekend.

    Reply  Thursday, July 14, 2016, 13:25, Anders Mjos, Conditioning Station, Repair, , , VFD21 OL1 fault on Chiller 

Anders Mjos wrote:

Plant Services group (Tony) will contact a service tech on Monday.

Water system will be switched off over the weekend.

Thursday, July 14, 2016, 13:24: Claus from Daikin is on site to troubleshoot.

The VFD driven fan motor has failed. Temporarily blocked air-flow through failed fan to improve air-flow to radiator. A new motor will be ordered (Curtis).

Thursday, July 14, 2016, 15:39: Stopped cooling system for the day


Friday, July 15, 2016, 08:16: Cooling system started

Friday, July 15, 2016, 15:00; Cooling system stopped.

       Reply  Thursday, August 18, 2016, 10:35, Anders Mjos, Conditioning Station, Repair, , , VFD21 OL1 fault on Chiller 

Anders Mjos wrote:

Anders Mjos wrote:

Plant Services group (Tony) will contact a service tech on Monday.

Water system will be switched off over the weekend.

Thursday, July 14, 2016, 13:24: Claus from Daikin is on site to troubleshoot.

The VFD driven fan motor has failed. Temporarily blocked air-flow through failed fan to improve air-flow to radiator. A new motor will be ordered (Curtis).

Thursday, July 14, 2016, 15:39: Stopped cooling system for the day


Friday, July 15, 2016, 08:16: Cooling system started

Friday, July 15, 2016, 15:00; Cooling system stopped.

 Thursday, August 18, 2016, 10:34: The motor was replaced today by Claus from Daikin. System is running normally again.

Entry  Tuesday, August 16, 2016, 12:35, David Wang, Conditioning Station, Repair, TM3, , CS vacuum pumps have been stopped 

The TCS is venting now. The TM3 blue insulator replacement job will be started soon.

Entry  Tuesday, August 16, 2016, 11:27, chad fisher, South Hot-Cell, Maintenance, , , South Cell Field Readings 

Field readings have been taken at the south hot cell in preparation for entry into the cell to fix manipulator.

Field on contact at aluminum cover is 66 uSv/h, and a pole monitor into the cell through the tool port read 297 uSv/h.

Entry  Monday, August 15, 2016, 10:15, David Wang, Conditioning Station, Standard Operation, TM4, , Target Hall schedule for beam schedule 130 (Apr- Oct, 2016) Target_Hall_shedule_130_Apr_to_Sep.pdfTarget_Hall_shedule_130_Apr_to_Sep.mpp

Weekly update target hall schedule. Everything on schedule are finished  on time.   See attachment.  

Entry  Monday, August 15, 2016, 10:08, David Wang, ITE, Standard Operation, TM4, UC#17, 5 Shielding blocks have been transferred from ITW to ITE. 

Dan and I transferred 5 shielding blocks from ITW to ITE. The ITE is configured to take proton beam.

Entry  Friday, August 12, 2016, 10:59, Anders Mjos, Conditioning Station, Development, TM3, , HV Test with Service Chase Panel removed TM3_HV_conditioning_2016-08-12.docxTCS-2016-08-11_TM3_Service_Chase_Panel_Removed.rga

Water cooling is performed manually with CP1. RGA is ON since yesterday. EE is not connected and in conditioning mode.


Friday, August 12, 2016, 10:43: BIAS at 10 kV, EL at 0.5 kV. IG1 at 1.8E-6 T

 Friday, August 12, 2016, 11:04: BIAS at 20 kV

Friday, August 12, 2016, 11:10: Sparking at 21 kV

Friday, August 12, 2016, 11:29: BIAS at 22 kV. Many small sparks/current excursions.

Friday, August 12, 2016, 11:32 : BIAS at 23 kV

Friday, August 12, 2016, 11:37: BIAS at 24 kV

Friday, August 12, 2016, 11:43: BIAS at 25 kV. Heavy sparking. Lowered to 24 kV to reduce spark rate.

Friday, August 12, 2016, 11:52: Increased sparking rate. Lowered to 23 kV.

Friday, August 12, 2016, 12:05: Lowered to 20 kV

Friday, August 12, 2016, 12:21: Back to 23 kV

Friday, August 12, 2016, 12:28: Heavy sparking between 23 and 24 kV. Lowered to 22 kV

Friday, August 12, 2016, 12:29: More sparking. Lowered to 21 kV.

Friday, August 12, 2016, 13:02: Increased back up to ~25 kV while Aurelia was listening for sparks in the Target Hall.

Friday, August 12, 2016, 13:03: EL to 10 kV

Friday, August 12, 2016, 13:06: BIAS / EL to 23 / 12.5 kV

Friday, August 12, 2016, 13:34: Repeated sparking at 24.5 kV. Ramping down

Friday, August 12, 2016, 15:33: Stopped water package. RGA off

Entry  Friday, August 12, 2016, 09:58, chad fisher, South Hot-Cell, Maintenance, , , Manipulator Maitenance 

Disassembled the master side of the right manipulator this morning to check the wrist cable. The cable on the master side shows no sign of wear or fraying suggesting that the slave side cable may be the item that is wearing. during disassembly of the master I did notice some loose parts that could have been the source of the audible concern but should not have contributed to the slippage felt in the gripper. I will try and schedule Tuesday for entry into the hot cell to address the slave cable.

Entry  Thursday, August 11, 2016, 10:37, David Wang, Conditioning Station, Repair, TM3, , TM3 service tray cover plate ITA2108 has been removed. 

Requested by Aurelia, and approved by Friedhelm, TM3 service tray cover plate ITA2108 has been remove out of the module. The plated is checked for active and contamination after removal. Then,It is double bagged, sealed ,  tagged, and placed downstairs in TH between south wall and green block . The ram contact reading on the plate is about 10 usv/hr.  We will do anther TM3 HV test at TCS without this cover plate.

Entry  Wednesday, August 10, 2016, 14:38, Isaac Earle, North Hot-Cell, Development, , , North Hot Cell Ventilation Test Results 

Testing was performed on August 9th on the ISAC nuclear ventilation system to determine if the existing ventilation system can achieve the required cell depressions for both SHC and NHC under all expected configurations and if a proposed modification to the DDC control system can provide acceptable stability and response time for the system.  The proposed control system observes the lower of the SHC depression or the NHC depression + 10% (to avoid stability issues), and adjusts the dampers to try to achieve 250Pa (1.00" WC) depression in the area it is observing.  With the proposed control system the SHC and NHC dampers are programmed to be at the same position, but can be tuned with a bias between them if required to achieve all ventilation requirements. The NHC and SHC dampers are programmed with a limit at 90% of the fully-open position.  There is a damper in the ducting system in the section of duct after the SHC and NHC legs join together;  this is set at 50% open, and was not adjusted during the the tests.  Test summary and results are listed below:

1.  Prior to switching to SHC+NHC control mode, the flow rate and depression of the SHC was measured with the lid on:  266Pa cell depression, damper 47% open, duct flow 417cfm.  The lid was opened and the measurements repeated:  35Pa, damper 90% open, duct flow 630cfm (results in 83ft/min, 0.42m/s average flow velocity across HC module opening)

2. The control system was switched to the new SHC+NHC single control loop system. Measurements were taken with both hot cell lids closed.  SHC:  246Pa, damper 72% open, 350cfm flow rate.  NHC: 257Pa, damper 72% open, 510cfm flow rate.  The ventilation fan speed was then increased from 53Hz to 57Hz (maximum speed is 60Hz).  Measurements were taken with both hot cell lids closed.  SHC:  257Pa, damper 51% open, 353cfm flow rate.  NHC: 257Pa, damper 51% open, 515cfm flow rate.

3. The SHC module port lid was opened and the NHC lid left closed.  SHC: 37Pa, damper 90% open, 462cfm (results in 61ft/min, 0.31m/s average flow velocity across HC module opening).  NHC: 249Pa, damper 90% open, 551cfm.

4. The NHC module port lid was opened and the SHC lid closed.  SHC: 203Pa, damper 90%, 360cfm.  NHC: 33Pa, damper 90%, 648cfm (results in 85ft/min, 0.44m/s average flow velocity across HC module opening).  The fan speed was then increased to 60Hz (max speed) to see if the depression setpoint for the SHC could be achieved in this configuration.  SHC: 231Pa, damper 90%, 389cfm.  NHC: 29Pa, damper 90%, 705cfm (results in 93ft/min, 0.47m/s average flow velocity across HC module opening)

5. Both SHC and NHC module port lids were opened and the fan was left at 60Hz.  SHC: 31Pa, damper 90%, 448cfm (results in 59ft/min, 0.30m/s average flow velocity across HC module opening).  NHC: 29Pa, 90% damper, 669cfm (results in 88ft/min, 0.45m/s average flow velocity across HC module opening)

 

For all tests the control system arrived at a stable depression value in less than 5 minutes, and thereafter exhibited only minor fluctuations.

It was observed that when the fan speed was increased to 57Hz, and for the duration of the tests, there was negligible change in the depression and damper positions for the mass separator room and target pit area.
 
The HEPA filter in the SHC leg of ducting has not been changed since commissioning of the facility (~15 years), and the SHC charcoal filters have not been changed since installation approximately 5 years ago.  The SHC pre-fitler located inside the cell was changed in January 2016.  When these are changed (which should be done before commissioning of the NHC ventilation system), the difference between SHC and NHC flow rates should decrease, and the SHC depression with NHC open should increase (likely up to the 250Pa setpoint).
 
Conclusion: The new SHC+NHC single control loop system effectively controls the system under all conditions tested.  The existing ventilation system achieved the required NHC depression (250Pa, from RS 50, Document #131915) with both cells closed, and with SHC open only.  The same depression for SHC with both cells closed was achieved with both cells closed, but only reached 231Pa w/ NHC open (203Pa at 57Hz fan speed).  It is expected that 250Pa can be easily achieved in the final system because the NHC will be better sealed than in its current condition, the damper in the shared SHC/NHC leg can be opened further, there will be greater flow through the SHC leg after changing the HEPA and charcoal filters, and the system can be tuned to better balance the SHC and NHC flow rates.  RS51 states "the ventilation system should maintain an average air flow velocity of 0.5m/s across the opening into the hot cell".  This is almost achieved with the NHC open, but SHC only had 0.3m/s average flow velocity.  It should be possible to increase both to > 0.5m/s by further opening the shared leg damper and tuning the system to have more balanced flow rates.  At the very least, both SHC and NHC should have > 0.42m/s average flow velocity to match what is currently achieved in SHC only mode (measured in test step #1), which to date has not allowed contamination to escape out the top of the hot cell.  Depending on what flow velocity is deemed acceptable, after commissioning it may be possible to have both the SHC and NHC open concurrently based on the results of Test 5.  At the time of commissioning, the SHC/NHC damper bias and NHC air inlet damper should both be tuned to achieve as similar depression and flow rate conditions as possible for both cells, and to meet all requirements in the RS document.

 

Notes:

Duct flow rate was calculated assuming that measured flow velocity at the center of the duct is 90% of average duct velocity.  The duct ID at the sample location is 7.75", the hot cell opening size used for SHC and NHC module opening flow velocity calculations was 33" x 33".

Duct flow velocity measurements were taken using a thermal anemometer (Model number: 9555-P, Serial number: 9555:1108059 Rev. 2.11.0, Last calibrated by Rob Walker on April 29, 2016).

After completion of the tests the system was restored to it's original configuration and the ISAC target hall was swiped for contamination: none found.  No EF12 trips occurred during these tests.

Entry  Wednesday, August 10, 2016, 12:18, chad fisher, South Hot-Cell, Maintenance, , , Anteroom clearing 

Black "radio active" materials cabinet has been emptied, items bagged and removed from the anteroom. Cabinet itself has been swiped inside and out and also been removed from the anteroom. Most items have been removed from the anteroom now save some cardboard, rolls of plastic etc.

Entry  Wednesday, August 10, 2016, 11:30, David Wang, ITE, Standard Operation, TM4, UC#17, TM4 has been connected at ITE 

Dan and I connected TM4 in ITE yesterday. It is pumping down at ITE now. Everything is fine so far.

Entry  Wednesday, August 10, 2016, 09:44, Travis Cave, Conditioning Station, Standard Operation, TM3, no target, module moved 

TM#3 has been moved from the north east silo to the conditioning station.

Entry  Tuesday, August 09, 2016, 11:36, Anders Mjos, Conditioning Station, Maintenance, , , RGA and CG1S moved Old.JPGNew.JPG

 The locations (ports) for the RGA and CG1S was swapped today by Anders and Isaac to provide clearance for the North Hot Cell ventilation. Attached photos show old and new locations.

Entry  Tuesday, August 09, 2016, 10:05, Travis Cave, ITE, Standard Operation, TM4, UC#17, module moved 

TM#4 with UC#17 is now in the east target station.

Entry  Tuesday, August 09, 2016, 07:15, David Wang, Conditioning Station, Standard Operation, TM4, UCx17, TM4 has been disconnected at TCS 

I stopped TCS water pumps this morning . The argon venting for TCS is in processing.

Entry  Monday, August 08, 2016, 11:24, chad fisher, South Hot-Cell, Maintenance, , , Anteroom Clean-up - Waveguide 

The wave guide from TM3 has been surveyed, swiped and removed from the anteroom and transported to rad waste for disposal. The wave guide has been stored in the anteroom since its removal.

Entry  Friday, August 05, 2016, 14:13, Isaac Earle, North Hot-Cell, Development, , , Preparations for NHC Ventilation Test 

A hole was drilled in the NHC exhaust duct in the east end of the target hall above the hatch to the Ante Room.  This will be used for measuring NHC exhaust flow rate with a thermal anemometer.  The hole was tapped and plugged with an NPT tap.

Flow was measured in the existing hole in the SHC exhaust duct in approximately the same location.  Flow velocity was measured to be 1415 ft/min with the lid on the SHC.  Using duct ID 7.75", and assuming the average flow velocity is 90% of the flow at duct center, the flow rate was found to be 417cfm.  We will attempt to match this figure for the NHC when the ventilation tests are performed.  The tests have been scheduled for the maintenance day on Tuesday August 9th.

The anemometer probe and SHC test port plug were checked for contamination: none found.

Entry  Friday, August 05, 2016, 13:50, chad fisher, South Hot-Cell, Maintenance, , , Anteroom clean out 

Some items have been removed from the anteroom in preparation for painting. Items have been placed on plastic in the south hot cell service area. No contamination found so far.

Entry  Thursday, August 04, 2016, 08:56, Travis Cave, Spent Target Vault, Standard Operation, , UC#16, Spent Target move Vault_Storage_August_3_2016.pdf

The spent UC #16 have been moved from the south hot cell to the storage vault see attached PDF for details.

Entry  Wednesday, August 03, 2016, 10:02, Travis Cave, South Hot-Cell, Standard Operation, TM4, UC#17, Electrical Check TM4_elechk_UC17_SHC.PDF

The result of yesterdays electrical check on TM#4 with UC#17.

Entry  Wednesday, August 03, 2016, 09:56, David Wang, Conditioning Station, Standard Operation, , , Target Hall schedule for beam schedule 130 (Apr- Oct, 2016) Target_Hall_shedule_130_Apr_to_Sep.mppTarget_Hall_shedule_130_Apr_to_Sep.pdf

Update schedule weekly. See attachments 1,2

Entry  Wednesday, August 03, 2016, 09:49, David Wang, Conditioning Station, Standard Operation, TM4, , TM4 is ready for conditioing at TCS. 

I started TCS water system and installed HV cover onto TM4.  The TM4 containment box is supplied with water also. TM4 is ready for conditioning at TCS.

Entry  Wednesday, August 03, 2016, 09:45, David Wang, Conditioning Station, Standard Operation, TM4, UC#17, Helium pressure test on TM4 HS line at TCS  

Helium pressure test on TM4 HS line at TCS  is done.Leak detector 0.0X E-9atm.cc/sec.  5minutes, 70psi helium.    No response on LD.

Entry  Wednesday, August 03, 2016, 09:15, chad fisher, South Hot-Cell, Repair, , , Manipulator 

East manipulator on the south hot cell is showing signs of eminent wrist/tong cable failure. Some slight slippage was noted yesterday and confirmed by a snapping sound and more slippage tomorrow.

Entry  Wednesday, August 03, 2016, 08:08, Anders Mjos, Conditioning Station, Standard Operation, TM4, UC#17, Conditioning UC#17 UC#17.docxTCS-2016-08-03_UC#17.rgaTCS-2016-08-08_UC#17.rga

Wednesday, August 03, 2016, 08:08: RGA on

Wednesday, August 03, 2016, 11:25: Configured EE to be connected to EE PS (not grounded)

Wednesday, August 03, 2016, 11:25: PS on

Wednesday, August 03, 2016, 11:32: BIAS / EL / EE to 20 / 10 / 1 kV

Ramping set to 40 / 20 A at 1 / 0.5 A/min. Good / bad vacuum at 2.0 / 2.2 E-6 T (IG2). Vacuum too high.

Wednesday, August 03, 2016, 13:02: BIAS / EL / EE to 30 / 15 / 1.5 kV

Wednesday, August 03, 2016, 15:59: BIAS / EL / EE to 35 / 17.5 / 1.5 kV. Some conditioning from 30 kV


Chiller staging stopped working around midnight. TGHT and TBHT ramped down by ISAC operators.

Thursday, August 04, 2016, 08:14: Ramping target to 50 / 25 A

Thursday, August 04, 2016, 08:22: Cycled power on chiller to reset alarm. Repeated again 5 min later

Thursday, August 04, 2016, 08:37: BIAS / EL / EE to 30 / 15 / 1.5 kV

Thursday, August 04, 2016, 09:36: Continue ramping to 100 / 50 A

Thursday, August 04, 2016, 11:32: Continue ramping to 120 / 60 A

Thursday, August 04, 2016, 14:50: ramping down


Friday, August 05, 2016, 07:09: Started cooling system

Friday, August 05, 2016, 07:56: Started ramping to 100 / 50 A

Friday, August 05, 2016, 14:27: TGHT / TBHT at 253 / 126 A.

Friday, August 05, 2016, 14:30: Ramping down at 2 / 1 A/min

Friday, August 05, 2016, 15:27: BIAS / EL / EE off


Monday, August 08, 2016, 08:15: Continue ramping. : BIAS / EL / EE to 30 / 15 / 1.5 kV

Monday, August 08, 2016, 14:36 TGHT / TBHT at 260 / 130 A. Ramping down at 2 / 1 A/min

Monday, August 08, 2016, 15:30: BIAS / EL off. EE remains at 1 kV.

Monday, August 08, 2016, 22:56: RGA off. Water system fault. Running CP1 manually

Monday, August 08, 2016, 22:57: EE off.

Monday, August 08, 2016, 22:58: Vacuum off

Entry  Tuesday, August 02, 2016, 15:22, David Wang, Conditioning Station, Standard Operation, TM4, UC#17, TM4 with new target has been connected at TCS 

It is being pumped now at TCS.

Entry  Tuesday, August 02, 2016, 14:52, Travis Cave, South Hot-Cell, Standard Operation, TM4, UC#17, module moved 

TM#4 with UC#17 is now in the conditioning station.

Entry  Tuesday, August 02, 2016, 13:32, chad fisher, South Hot-Cell, Standard Operation, TM4, UC#16, UC#16 Removed #17 installed 

UCx#16 has been removed from TM$ and UCx#17 installed, high current conductors toqued to 130 in lbs.

 

UCx#16 did not show the standard arcing marks on the 9 pin connector.

In regards to the 9 pin connector on number 17, it was by far the best fitting TM4 target with 9 pin as it required no "fiddling" during installation.

Entry  Tuesday, August 02, 2016, 11:02, Travis Cave, ITE, Standard Operation, TM4, UC#16, module moved 

TM#4 with UC#16 has been moved from the east station to the south hot cell. The shield plug was also install remotely once it was hooked up due to alphas.

Entry  Friday, July 29, 2016, 14:27, Isaac Earle, North Hot-Cell, Development, , , North Hot Cell Measurements & Cleanup 

 The North Hot Cell was accessed today via the Ante Room for inspection, measurements, and clean-up.  There were no modules in the SHC or TCS, and no spent targets in the SHC.  Under these conditions the maximum field in the NHC was approximately 2μSv/hr.  The inside of the cell was cleaned and swept, followed by a floor swipe to check for contamination (none found).  All areas of the ante room floor were also swiped:  no contamination found.

 


The following measurements were taken in the NHC for comparison with the Soldiworks model:

SHC/NHC feedthrough panel fastener size:  1/4"-20,  1/2" long
NHC west wall to east edge of SEG block:  33-1/4" on south side, 33" on north side
NHC west wall to furthest extent of TCS (IRH1170): 40"
NHC west wall to wall indentation for viewing window: 46-7/8"
NHC west wall to end of existing ventilation duct: 4-1/8"

 

Entry  Thursday, July 28, 2016, 11:27, Travis Cave, Conditioning Station, Standard Operation, TM3, no target, module moved 

TM#3 with no target has been moved from the conditioning station to the NE silo.

Entry  Tuesday, July 26, 2016, 11:22, chad fisher, South Hot-Cell, Maintenance, , , Soth Hot Cell Waste Storage Vault Tunnel 

The two 45 gal (m) drums of waste removed from the south hot cell in December 2015 and January 2016 were transferred from the north hot cell to the shaft of the east vault tunnel on Monday, July 25th 2016 and subsequently to the east tunnel bunker in the vault tunnel on Tuesday, July 26th, 2016.The first drum (removed from the hot cell in December) containing both activated and contaminated metals was measured at 900 uSv/hr @ .5 m and the second drum (removed from the hot cell in January 2016) containing compressible items such as tank suits and plastic was measured at 150 uSv/hr @ .5 m.

Items were filed for storage/disposal with RPG under item number 1395 on the radioactive storage form.

Drums were transported to the vault tunnel using the 500 Mev Shield Flask (Drawing E-7097) with some minor modifications, namely a 1/4" thick Aluminum plate with four holes that line up with the holes in the bottom flange of the flask. This plate provided a bottom for the flask so that a drum could be contained within the flask during craning. Holes in the plate where countersunk for a 1/2" flat head bolt. Four bolts were also modified to accept 3/16 hair pins. 3 plates with clearances holes for the bolts were also manufactured to act as washers.

Procedure was as follows: With plate, washers and pins installed onto the flask, a modified drum dolly (5" spacers added to the casters) was placed inside the flask. Drum was craned into the flask using the automatic drum lifter. Flask with drum loaded was moved to the Meson Hall loading bay then craned to the B2 level of the Meson hall. Hair pins were pulled from the flask and the flask was then craned up leaving the drum (which was on the dolly firstly installed into the flask) and the plate. Drum on dolly was rolled to vault access shaft where it was craned off the modified dolly using the automatic drum lifter and down the access shaft to the vault tunnel level.  A second drum dolly was waiting at the bottom level and drum lowered onto it. Procedure was repeated for the second drum

Was vault was open , drums were wheeled into the vault tunnel and into a bunker that had been modified to accept these drums. Drums were lifted off dollies and put in place in bunker which had blocks installed to cover the entrance provided for installation.

 

Pictures can be found on docushare http://documents.triumf.ca/docushare/dsweb/View/Collection-18072  (collection 18072)

 

 

Entry  Monday, July 25, 2016, 08:15, Anders Mjos, Conditioning Station, Repair, TM3, , HV Test TM3_HV_conditioning_2016-07-25.docxTCS-2016-07-25_TM3_no_target.rgaTCS-2016-07-26_TM3_no_target.rga

 Monday, July 25, 2016, 08:14: Enabled staging for chiller

Monday, July 25, 2016, 08:33: Disabled staging. Fault 2. Staging does not work at this point.

Monday, July 25, 2016, 08:34: Running CP1 manually to cool down water.

Monday, July 25, 2016, 09:15: Bias current limiting at 150 V. Investigating short.

Monday, July 25, 2016, 09:51: EE cable was shorting the BIAS on the TCS side.

Monday, July 25, 2016, 09:57: BIAS/ / EL at 20 / 10 kV

Monday, July 25, 2016, 10:08: Sparking at 24 kV. Lowered to 22 kV

Monday, July 25, 2016, 10:44: BIAS at 25 kV

 Monday, July 25, 2016, 11:00: Sparking at 25.5 kV. Lowered to 25 kV

Monday, July 25, 2016, 12:03: 25.5 kV. No sparking for 10 min. Lower to 20 kV for lunch break.

Monday, July 25, 2016, 12:51: 26 kV

Monday, July 25, 2016, 13:00: Sparking at 27.3 kV. Lowered to 27 kV. EL at 14 kV

Monday, July 25, 2016, 13:04: More sparking. Lowered to 25 kV

Monday, July 25, 2016, 13:39: 25 kV

Monday, July 25, 2016, 14:21: A spark tripped the PS on water resistivity

Monday, July 25, 2016, 14:31: 25 kV

Monday, July 25, 2016, 15:34: ~20 sparks for the last 60 min

Monday, July 25, 2016, 16:28: ~10 sparks for the last 60 min. BIAS an EL off

Monday, July 25, 2016, 16:36: Stopped water cooling system.


Tuesday, July 26, 2016, 08:20: Started water cooling system.

Tuesday, July 26, 2016, 08:24: Ran CP1 manually for 3 min. Enabled staging.

Tuesday, July 26, 2016, 08:31: BIAS / EL at 25 / 0 kV

Tuesday, July 26, 2016, 08:39: EL float to 300 V. Set to 500 V

Tuesday, July 26, 2016, 08:45: BIAS to 25.5 kV

Tuesday, July 26, 2016, 09:07: 26 kV

Tuesday, July 26, 2016, 09:12: Lost contact with EPICS. Scheduled maintenance

Tuesday, July 26, 2016, 10:26: 6 sparks for the last 60 min

Tuesday, July 26, 2016, 10:33: BIAS to 27 kV

Tuesday, July 26, 2016, 10:43: Sparking at 27.8 kV. Lowered to 23 kV

Tuesday, July 26, 2016, 10:51: BIAS back at 27 kV. A spark tripped the BIAS on water resistivity

Tuesday, July 26, 2016, 11:08: BIAS at 27 kV

Tuesday, July 26, 2016, 11:22: BIAS at 28 kV

Tuesday, July 26, 2016, 11:42: BIAS at 27 kV after trip due to water resistivity (spark)

Tuesday, July 26, 2016, 12:00: BIAS / EL off for lunch break

Tuesday, July 26, 2016, 14:10: EL to 10 kV

Tuesday, July 26, 2016, 14:14: El to 20 kV

Tuesday, July 26, 2016, 14:20: EL to 25 kV

Tuesday, July 26, 2016, 14:27: First spark at 27.6 kV

Tuesday, July 26, 2016, 14:29: EL to 28 kV (BIAS at 0 kV)

Tuesday, July 26, 2016, 14:43: RGA on

Tuesday, July 26, 2016, 14:49: No sparking for 20 min

Tuesday, July 26, 2016, 16:02: No sparks for 90 min.

Tuesday, July 26, 2016, 16:06: PS and water off.


Wednesday, July 27, 2016, 09:14: BIAS at 24 kV

Wednesday, July 27, 2016, 09:19: Lowered to 20 kV due to sparking

Wednesday, July 27, 2016, 09:28: BIAS at 22 kV

Wednesday, July 27, 2016, 15:30: BIAS and water off


Thursday, July 28, 2016, 08:43: RGA off

Entry  Friday, July 22, 2016, 10:57, David Wang, Conditioning Station, Repair, TM3, , TM3 has been moved and connected at TCS 

I started vacuum system.

I started TCS water system. The chiller does not work properly still. But, It will not affect the TM3 HV conditioning.  HV cover is installed on TM3 in TH. The module is ready for HV conditioning.

Entry  Monday, July 18, 2016, 14:14, David Wang, Conditioning Station, Repair, TM3, , TM3 leak checked at TCS 

Last Friday July-15, TM3 was leak checked at TCS. All air to vacuum seals on service cap are good.  Helium pressure test on  TM3 water lines(except GE, HS, and Window) were done. Leak detector has no response at 0.0xE-9 atm.cc/sec. They are leak free.

    Reply  Tuesday, July 19, 2016, 14:35, Aurelia Laxdal, Conditioning Station, Repair, TM3, , TM3 leak checked at TCS 

David Wang wrote:

Last Friday July-15, TM3 was leak checked at TCS. All air to vacuum seals on service cap are good.  Helium pressure test on  TM3 water lines(except GE, HS, and Window) were done. Leak detector has no response at 0.0xE-9 atm.cc/sec. They are leak free.

Friday July 15: did HV tests (with no target installed and with the anode wire removed ). <br>

TM3 went up to 22.5kV. At this voltage it started sparking. The EL was kept at 1/2 with respect to the HV BIAS. <br>

Also HV tests were done while the EL was kept at zero V. In this case, the EL voltage was once in a while spiking  up (up to 4kV). <br>

During sparking we saw responses in the vacuum. Checked the Service Cap (with the HV Cover) in the Target Hall: we couldn't hear/see sparks there.  <br>

The HV was turned off in the same day, after 5:30pm.

Entry  Monday, July 18, 2016, 13:56, Travis Cave, South Hot-Cell, Standard Operation, TM3, no target, module moved 

TM#3 is now in the south hot cell.

Entry  Thursday, July 14, 2016, 10:54, David Wang, Conditioning Station, Standard Operation, TM2, , Target Hall schedule for beam schedule 130 (Apr- Oct, 2016) Target_Hall_shedule_130_Apr_to_Sep.pdfTarget_Hall_shedule_130_Apr_to_Sep.mppTarget_Hall_shedule_130_Apr_to_Sep_2016.pdfTarget_Hall_shedule_129_Sep_to_Dec.xlsx

Update TH schedule 130 according to mini-shut down change.See attachment 1,2,3,4

Entry  Wednesday, July 13, 2016, 08:47, Travis Cave, Conditioning Station, Standard Operation, TM3, no target, module moved 

TM#3 has been moved from the north east silo to the conditioning station.

Entry  Tuesday, July 12, 2016, 12:42, David Wang, Conditioning Station, Standard Operation, , , Target Hall schedule for beam schedule 130 (Apr- Sep) Target_Hall_shedule_130_Apr_to_Sep.pdfTarget_Hall_shedule_130_Apr_to_Sep.mpp

Update schedule weekly.Attachment 1,2

Entry  Tuesday, July 12, 2016, 12:40, David Wang, ITW, Standard Operation, TM2, , TM2 has been connected in ITW 

All turbo-pumps are started. Everything is good so far.

Entry  Tuesday, July 12, 2016, 09:59, Travis Cave, ITW, Standard Operation, TM2, SiC#33, module moved 

TM#2 with SiC#33 has been moved from the conditioning station to the west target station.

Entry  Monday, July 11, 2016, 10:59, Travis Cave, Spent Target Vault, Standard Operation, , Ta#48, Spent Target move Vault_Storage_July_11_2016.pdf

The spent Ta#48 was moved from the south hot cell to the spent target vault. I was placed in pail 139 and is in spot 6C in the vault. It was 201mSv/hr when measured at the hot cell. See the attached PDF for the latest results.

Entry  Friday, July 08, 2016, 08:20, David Wang, Conditioning Station, Standard Operation, TM2, , TM2 has been connected at TCS 

I connected TM2 to TCS and started water system.

Entry  Wednesday, July 06, 2016, 15:23, Anders Mjos, Conditioning Station, Standard Operation, TM2, SiC#33, Conditioning SiC#33 SiC#33.docxTCS-2016-07-06-SiC#33.rga

 Wednesday, July 06, 2016, 15:23: RGA on. IGs on


Friday, July 08, 2016, 17:07: Stopped cooling system due to a problem with the chiller. Will continue with HV conditioning on Monday.


Monday, July 11, 2016, 08:08: Cooling system started. Operating CP1 manually to control temperature

Monday, July 11, 2016, 09:38: BIAS / EL / EE to 10 / 5 / 1 kV

Monday, July 11, 2016, 09:41: BIAS / EL / EE to 20 / 10 / 1.5 kV

Monday, July 11, 2016, 09:47: BIAS / EL / EE to 30 / 15 / 1.5 kV

Monday, July 11, 2016, 10:01: BIAS / EL / EE to 40 / 20 / 2.0 kV - one spark at 40 kV

Monday, July 11, 2016, 10:38: BIAS / EL / EE to 45 / 22.5 / 2.0 kV - conditioning from 40 kV

Monday, July 11, 2016, 10:40: BIAS / EL / EE to 45 / 22.5 / 2.3 kV

Monday, July 11, 2016, 12:21 : No sparks for the last 60 min.

Monday, July 11, 2016, 12:21: BIAS / EL / EE off to investigate TGHT / TBHT PS problem (power surge this morning)

Monday, July 11, 2016, 13:07: Power cycled TGHT / TBHT PS. Alarm cleared. Tested both to 10 A

Entry  Wednesday, July 06, 2016, 14:25, David Wang, Conditioning Station, Standard Operation, TM2, , TCS and TM2 turbo-pumps have been started. 

The TCS and TM2 are pumping down.

Entry  Wednesday, July 06, 2016, 13:38, Travis Cave, Conditioning Station, Standard Operation, TM2, SiC#33, module moved 

TM#2 with SiC#33 has been moved from the south hot cell to the conditioning station.

Entry  Wednesday, July 06, 2016, 09:59, Travis Cave, South Hot-Cell, Standard Operation, TM2, Ta#48 and SiC#33, Electrical Check TM2_elechk_Ta48_SHC_postbeam.PDFTM2_elechk_SiC33_SHC.PDFTM2_elechk_notgt_SHC.PDF

Electrical check done on TM#2 with Ta#48, no target and SiC#33 the short on the coils to 60kV is still present it is on the R-U coil line. See attached PDFs for details.

Entry  Wednesday, July 06, 2016, 09:16, chad fisher, South Hot-Cell, Standard Operation, TM2, SiC#33, Ta#48 removed SiC#33 installed 

Ta#48 has been removed from TM2 and SiC#33 installed.

Entry  Wednesday, July 06, 2016, 07:06, David Wang, Conditioning Station, Standard Operation, , , venting TCS with argon. 

I switched off the vacuum pumps and vented TCS with argon. The TCS will be ready to accept TM2 this afternoon.

Entry  Wednesday, July 06, 2016, 07:03, David Wang, ITW, Standard Operation, TM2, , TM2 was connected in ITW. 

TM2 was disconnected in ITW and moved to SHC.

Entry  Thursday, June 30, 2016, 13:33, Dan McDonald, Spent Target Vault, Maintenance, , , F308's 

The five spent target F308  flasks where gone through in accordance with Nordion guidelines, the sixth spare is remains in the Hot Cell area. All flasks where in reasonable shape with two needing weld repairs on the pallets. I replaced all the 3/4" pallet to flask fasteners with new Grade 8 bolts nut and washer combo. Flasks have been moved into the Hot Cell area awaiting movement into the Target Hall.

Entry  Tuesday, June 28, 2016, 14:42, Travis Cave, Spent Target Vault, Standard Operation, , Many, Spent target assay. Vault_Storage_June_30_2016.pdfMini_Vault_Storage_June_30_2015.pdf

The spent target assay were finally started or re-started today. Four targets were done today.

June 29 2016 another four targets were done today.

June 30 2016 all targets have assayed and measured. see the attached PDFs for the results.

Entry  Monday, June 27, 2016, 13:45, David Wang, ITE, Standard Operation, , , 5 Shielding blocks have been transferred from ITW to ITE. 

ITE is configured to take proton beam.

Entry  Tuesday, June 21, 2016, 13:47, Travis Cave/ Dan McDonald, Spent Target Vault, Repair, , , Spent Target Vault Door 

The spent target vault door does not open or close. The emergency door closing did have to be used to close the door as it was locked in an open position, the door stopped just off the open override limit. The door was closed and the spent target that was being assayed was placed into the mini storage. The problem with the door appears to be related to the motor itself, as all the controls to the motor appear to be in working order. Also it was noticed on the emergency door closing winch the wire rope has a kink in it from sitting in open position for so long this can cause the wire rope to jump from the pulleys.

 

6/27/2016  Dan McDonald. Replacement motor was ordered from Beaver Industries Friday the 24th received this morning the 27th. Once received Travis wired the motor to its proper operating orientation. Once the motor was wired  it was  set it up and plugged it in to test rotation and control function, at this point we disconnected the motor and re installed it to the gear box. Ran three open close sequences to ensure all was well. In the case of the emergency cable system a plan is being developed to correct the cable slack and kinking problem. We went ahead and ordered a spare  vault motor which is located in the RH Machine Shop 

Entry  Wednesday, June 15, 2016, 09:39, Travis Cave, Spent Target Vault, Standard Operation, , Ta#47, Spent Target move Vault_Storage_June_15_2016.pdf

The spent Ta#47 target has been moved from the south hot cell to the spent target vault. It was placed in pail #137 in spot 4C of the vault. It was 114mSv/hr upon removal from the vault.

Entry  Tuesday, June 14, 2016, 11:20, David Wang, ITE, Standard Operation, TM4, , TM4 has been connected in ITE 

TM4 and ITE are under roughing now.

Entry  Tuesday, June 14, 2016, 10:51, Travis Cave, ITE, Standard Operation, TM4, UC#16, module moved 

TM#4 with UC#16 has been moved from the conditioning station to the east target station.

Entry  Tuesday, June 14, 2016, 08:04, David Wang, Conditioning Station, Standard Operation, TM4, UC#16, TM4 has been disconnected at TCS 

The TM4 and TCS are vented with argon. 

Entry  Thursday, June 09, 2016, 10:04, David Wang, Conditioning Station, Standard Operation, , , Target Hall schedule for beam schedule 130 (Apr- Sep) Target_Hall_shedule_130_Apr_to_Sep.mppTarget_Hall_shedule_130_Apr_to_Sep.pdf

Weekly update .

Entry  Thursday, June 09, 2016, 09:44, David Wang, Conditioning Station, Standard Operation, TM4, UC#16, TM4 has been connected at TCS 

It is ready for HV conditioning/ heating. 

Entry  Thursday, June 09, 2016, 08:37, David Wang, Conditioning Station, Standard Operation, TM4, UC#16, TM4 with UCx16 helium pressure test at TCS TM4_withUCx16_helium_pressure_test_at_TCS.pdf

I did a helium pressure test on TM4 at TCS with UCX16 target installed on the module. No leak has been found on all using water lines in TM4. See attachment for detail.

Entry  Wednesday, June 08, 2016, 08:25, Anders Mjos, Conditioning Station, Standard Operation, TM4, UC#16, Conditioning UC#16 UC#16.docxTCS-2016-06-08_UC#16.rga

 Wednesday, June 08, 2016, 08:15: RGA on


Thursday, June 09, 2016, 09:00: Water on by David. TK2 level dropped by about 1.5 in.

Thursday, June 09, 2016, 10:30: BIAS / EL / EE to 10 / 5 / 0.5 kV

Thursday, June 09, 2016, 10:44: Started heater ramp. TGHT / TBHT to 40 / 20 A at 1 / 0.5 A/min. IG2 vacuum limits 2E-6 / 3E-6 T

Thursday, June 09, 2016, 11:59: Continue ramping to 100 / 50 A.


Friday, June 10, 2016, 08:04: Continue ramping to 300 / 150 A IG2 vacuum limits 1.9E-6 / 2.3E-6 T

Friday, June 10, 2016, 21:32: Stopped ramping at 275 A /  138.5 A


Saturday, June 11, 2016, 11:40: Ramped to 281 A / 140 A


Sunday, June 12, 2016, 08:31: Ramped to 290 A / 145 A

Sunday, June 12, 2016, 08:49: Ramped to 300 A / 150 A


Monday, June 13, 2016, 08:06: Continue ramping to 400 / 200 A

Monday, June 13, 2016, 17:00: TGHT / TBHT at 390 A / 195 A.

Monday, June 13, 2016, 17:17: BIAS / EL / EE to 30 / 15 / 1.5 kV

Monday, June 13, 2016, 18:02: Ramping down TGHT / TBHT at 2 / 1 A/min

Monday, June 13, 2016, 21:39: Source off. Water, RGA, vacuum off.

Entry  Tuesday, June 07, 2016, 18:17, David Wang, Conditioning Station, Standard Operation, TM4, UC#16, TM4 and TCS turbo pumps are started. 

TM4 and TCS vacuum system are connected.   Turbo pumps are started.  Everything is fine so far.

Entry  Tuesday, June 07, 2016, 17:14, David Wang, Conditioning Station, Standard Operation, TM4, UC#16, TM4 with UCx16 target has been moved from SHC to TCS. 

Bill and Yasmine did the move remotely this afternoon. The move is successful.

Entry  Tuesday, June 07, 2016, 17:11, David Wang, Conditioning Station, Standard Operation, TM4, UC#16, TM4 UCx16 electrical check and leak check at SHC UCX_16_electrical_test.pdfelectrical_check._TM4_UCx16_at_TCS..pdf

Chad and I finished the TM4 UCx6 electrical check and leak check at SHC. Leak check result on HS line is good. There is a dead short between "Z" repellor and HS during the first time electrical check. The dead short disappeared after re- installation of UCx 14 target onto TM4. See attachment

 Anders and I did another electrical check on TM4 at TCS under vacuum. See attachment 2

Entry  Tuesday, June 07, 2016, 11:42, David Wang, South Hot-Cell, Standard Operation, TM4, Ta#47, electrical check on TM4 with old Ta target at SHC. electrical_check_2016-06-07._TM4_with_old_Lp_Ta_target..pdfelectrical_check_2016-06-07._TM4_with_old_Lp_Ta_target..pdf

I did an electrical check on TM4 with the old target still installed. The number is a little bit low on 500V mega check between chassis and 60KVbias which is 146Mohm. Others are good.    See attachment

I wrote all OL to 0  in attachment 1 ohmmeter check. Please See attachment 2 for correction.

Entry  Tuesday, June 07, 2016, 11:37, David Wang, ITE, Standard Operation, TM4, Ta#47, TM4 has been moved from ITE to SHC 

Bill and Yasmine did the move. Everything is good.

Entry  Tuesday, June 07, 2016, 11:36, David Wang, ITE, Standard Operation, TM4, Ta#47, TM4 has been disconnected in ITE. 

Dan and I disconnected TM4 in ITE. HS water lines has been purged.

Entry  Thursday, June 02, 2016, 11:59, David Wang, South Hot-Cell, Repair, TM3, , 5K mega test on TM3 5K_mega_check_on_TM3.pdf

I did a 5KV mega test on TM3.  Only5Mohm @5kV between coli line PQ and chassis(ground). It confirmed the close gap between P,Q and GE. Other lines are ok. See attachment.

    Reply  Thursday, June 02, 2016, 18:04, Aurelia Laxdal, South Hot-Cell, Repair, TM3, , 5K mega test on TM3 DSC_0821.JPGDSC_0822.JPG

David Wang wrote:

I did a 5KV mega test on TM3.  Only5Mohm @5kV between coli line PQ and chassis(ground). It confirmed the close gap between P,Q and GE. Other lines are ok. See attachment.

See attachment for sparking signs of the water lines mentioned  above (Coil and Ground Electrode lines) in TM3 Source Tray.

       Reply  Friday, June 03, 2016, 16:04, Aurelia Laxdal, South Hot-Cell, Repair, TM3, , 5K mega test on TM3 

Aurelia Laxdal wrote:

David Wang wrote:

I did a 5KV mega test on TM3.  Only5Mohm @5kV between coli line PQ and chassis(ground). It confirmed the close gap between P,Q and GE. Other lines are ok. See attachment.

See attachment for sparking signs of the water lines mentioned  above (Coil and Ground Electrode lines) in TM3 Source Tray.

PLEASE NOTE: the resistance values for A and B on David's attachment are not correct since these measurements were done after Chad removed the target and the heat-shield bracket was moved, so consequently the water lines were not at their nominal locations. Once they were back in plac,e David took another measurement and the resistance values for A and B showed also 3,000 MOhm (as it was for most of the lines). The only lines that still showed a low resistance were the Coil lines. 

Entry  Friday, June 03, 2016, 11:35, Travis Cave, South Hot-Cell, Standard Operation, TM3, no target, module moved 

TM#3 has been moved back to the north east silo.

Entry  Thursday, June 02, 2016, 08:44, Travis Cave, South Hot-Cell, Standard Operation, TM3, no target, Electrical Check TM3_elec_chk_no_tgt.PDF

Electrical check of TM#3 no target at the south hot cell. see attached for results.

Entry  Tuesday, May 31, 2016, 09:45, Travis Cave, South Hot-Cell, Standard Operation, TM3, no target, module moved 

TM#3 has been moved from the NE Silo to the south hot cell.

Entry  Wednesday, May 25, 2016, 14:08, David Wang, ITW, Standard Operation, TM2, Ta#48, TM2 has been connected in ITW 

TM2 has been connected in ITW by Dan.M and David.W. All turbo-pumps have been started. Everything is good so fine.

Entry  Wednesday, May 25, 2016, 10:57, Travis Cave, ITW, Standard Operation, TM2, Ta#48, module moved 

TM#2 with Ta#48 has been moved from conditioning station to the west target station.

Entry  Tuesday, May 24, 2016, 10:52, Travis Cave, Spent Target Vault, Standard Operation, , UC#15, Spent Target move Vault_Storage_May_24_2016.pdf

Spent UC#15 has been moved from the south hot cell to the spent target storage. It was placed in pail number 136, and placed in spot C of tray one. It was 14.1mSv/hr upon removal from the south hot cell.

Entry  Tuesday, May 24, 2016, 10:42, David Wang, Conditioning Station, Standard Operation, TM2, , Target Hall schedule for beam schedule 130 (Apr- Sep) Target_Hall_shedule_130_Apr_to_Sep_2016.xlsxTarget_Hall_shedule_130_Apr_to_Sep.mppTarget_Hall_shedule_130_Apr_to_Sep.pdf

Weekly update the TH schedules. See attachments 1, 2,3.

Entry  Tuesday, May 24, 2016, 10:39, David Wang, Conditioning Station, Standard Operation, TM2, Ta#48, TM2 and TCS turbo-pumps have been switched off this morning. 

The TCS and TM2 are still under vacuum without venting

Entry  Friday, May 20, 2016, 10:38, David Wang, Conditioning Station, Standard Operation, TM2, Ta#48, Helium pressure test on TM2 with new Lp Ta target 

LD base LR: 0.0 X E-9. Base pressure:0.0 X E-4. 70 psi helium. 5 minutes each circuit.

window 0.0X E-9  
HS 0.0X E-9  
EE 0.0X E-9  
Ta+ 0.0X E-9  
Ta- 0.0X E-9  
coil1 R-U 0.0X E-9  
Coil2 P-Q 5.0X E-9  
Tube- 5.1X E-9  
Tube+ 1.1X E-8  
MSP 3.5X E-9  

The bigger leak found on MSP before was gone. Leak rate are smaller on all circuits  comparing to before. 

The leak rate on 1 hour total lines test at 70 psi is better also which is 6.6 XE-8 atm.cc/sec this time. 

Entry  Friday, May 20, 2016, 08:13, David Wang, Conditioning Station, Standard Operation, TM2, Ta#48, I switched off TCS and TM2 water system 

Disconnected  TM2 at TCS(vacuum system still on). Purged all TM2 water lines for helium pressure test.

Entry  Thursday, May 19, 2016, 10:35, Travis Cave, South Hot-Cell, Standard Operation, TM1, no target, module moved 

TM#1 has been moved from the south hot cell to the north west silo.

Entry  Wednesday, May 18, 2016, 11:42, Travis Cave, South Hot-Cell, Standard Operation, TM1, UC#15, module moved 

TM#1 with  UC#15 has been moved from the west target station to the south hot cell. The target shield plug was also remotely installed as well.

Entry  Tuesday, May 17, 2016, 14:15, Travis Cave, ITW, Standard Operation, TM1, UC#15, module moved 

TM#1 with UC#15 was moved back to the west station due to alpha concerns.

Entry  Tuesday, May 17, 2016, 11:47, Travis Cave, South Hot-Cell, Standard Operation, TM1, UC#15, module moved 

TM#1 has been moved from the west target to the south hot cell. The target on TM#1 is UC#15.

Entry  Monday, May 16, 2016, 13:26, Anders Mjos, Conditioning Station, Standard Operation, TM2, Ta#48, Conditioning Ta#48 Ta#48.docx

 Monday, May 16, 2016, 13:20: BIAS/EL/EE 30 / 15 / 1.5 kV

Monday, May 16, 2016, 13:20: Ramping TGHT / TBHT to 580 / 220 A at 2 A/min. IG2 1E-6 / 2E-6 T

Monday, May 16, 2016, 15:45: Paused ramping.

Monday, May 16, 2016, 15:00: Resumed ramping

Monday, May 16, 2016, 16:23: Stopped ramping for the day. TGHT / TBHT at 310 / 220 A. FC at 6.2E-7 A


Tuesday, May 17, 2016, 08:00: Continue ramping.


Wednesday, May 18, 2016, 09:40: BIAS / EL / EE to 35 / 17.5 1.7 kV


Thursday, May 19, 2016, 04:07: BIAS dropped to 0. Likely caused by a power bump.

Thursday, May 19, 2016, 08:05: BIAS returned to 35 kV. Increased EL to 22 kV to maximize FC current.

Thursday, May 19, 2016, 08:11: TBHT to 230 A

Thursday, May 19, 2016, 08:22: Ramping down TGHT / TBHT

Thursday, May 19, 2016, 10:41: BIAS / EL / EE off

Thursday, May 19, 2016, 14:00: TGHT / TBHT off


Friday, May 20, 2016, 14:39: RGA off.

Entry  Monday, May 16, 2016, 11:16, David Wang, ITW, Standard Operation, TM1, , ITW, TM1 turbo-pumps are swithched off 

I let isac opp switched off ITW turbo-pumps. The argon vent valve in electrical room is opened. The ITW argon venting will be started  soon.

Entry  Monday, May 16, 2016, 10:48, Anders Mjos, Conditioning Station, Maintenance, , , Topped up water in TCS:TK2 

 Filled from 15 to 25 in

Entry  Friday, May 13, 2016, 10:12, David Wang, Conditioning Station, Standard Operation, TM2, , TM2 water lines, heaters, EE, and EL are connected at TCS. 

The HV  cover is installed on to TM2 after the connections. The HV key is returned back to B2 level. The TCS Faraday cage is locked.

Entry  Friday, May 13, 2016, 10:08, David Wang, Conditioning Station, Standard Operation, TM2, , Helium pressure test on TM2 HS and window line at CS with new Lp Ta target 

These two lines are passed helium pressure test this morning. The LD base leak rate 0.0 X E-9 atm.cc/sec. The base pressure 0.0 X E-4 torr. Helium pressure 70 psi. applied helium to both line for 5minutes each. No response on LD during the test.

Entry  Wednesday, May 11, 2016, 13:16, David Wang, Conditioning Station, Standard Operation, TM2, , TM2 and TCS vacuum system has been connected. 

TM2 and TCS vacuum system has been connected. I started all turbo pumps. Everything is good so far.

Entry  Wednesday, May 11, 2016, 13:15, David Wang, Conditioning Station, Maintenance, TM2, , TCS tank top flange seal is changed this morning 

I changed TCS tank top flange seal(o-ring 42.00"ID X 0.275" DIA) this morning before TM2 was moved to TCS.

Entry  Wednesday, May 11, 2016, 09:44, Travis Cave, Conditioning Station, Standard Operation, TM2, Ta#48, module moved 

TM#2 with Ta#48 has been moved from the south hot cell to the conditioning station.

Entry  Tuesday, May 10, 2016, 14:27, Travis Cave, South Hot-Cell, Standard Operation, TM2, Ta#48, Electrical Check TM2_elec_chk_Ta48_SHC.PDF

Electrical check of TM#2 with Ta#48 attached. See the attached PDF for details.

Entry  Tuesday, May 10, 2016, 13:54, David Wang, South Hot-Cell, Standard Operation, TM2, , SHC, TM2 leak check on window line and HS line. 

Chad and I leak checked the TM2 HS and window lines after new target installation.  The window line was very easy pumped down on LD. But, The HS line only could pumped to 2-3 torr at first. Chad changed the VCR gaskets on HS line(target). It solved the problem. The LD could pumped  both of Window and HS lines to the bottom scale. Chad sprayed lots helium around the VCR joints.  No leak has been found. WE will do helium pressurizing test on them at TCS.

Entry  Tuesday, May 10, 2016, 13:37, chad fisher, South Hot-Cell, Standard Operation, TM2, Ta#48, Ta#48 Installation 

Ta#48 has been installed onto TM2. Also new window gaskets were installed.

High current fasteners were torqued to 130 in lbs. Shutter side of the containment box recieved new fasteners.

Entry  Monday, May 09, 2016, 10:13, Travis Cave, South Hot-Cell, Standard Operation, TM2, no target, module moved 

TM#3 was moved from the conditioning station to the NE Silo. TM#2 was moved from the SW Silo to the South hot cell.

Entry  Monday, May 09, 2016, 08:43, David Wang, Conditioning Station, Repair, TM3, , I reinstalled all the side panel on TM3 service cap. 

They were moved for TM3 inspection job last week. All the bolts on the panel are hand tight only now since they will be removed out for camera installation during next stage inspection.

Entry  Wednesday, May 04, 2016, 12:01, David Wang, Conditioning Station, Standard Operation, , , Target Hall schedule for beam schedule 130 (Apr- Sep) Target_Hall_shedule_130_Apr_to_Sep_2016.pdfTarget_Hall_shedule_130_Apr_to_Sep.mppTarget_Hall_shedule_130_Apr_to_Sep.pdf

Update schedule weekly. See attachment 1,2,3.

Entry  Wednesday, May 04, 2016, 11:14, Isaac Earle, North Hot-Cell, Development, , , North Hot Cell Scope Decision 

A meeting was held on May 4, 2016 to determine the scope of the North Hot Cell project.  The following was agreed upon by those in attendance:

The NHC will be a designated target change hot cell.  It will be capable of performing all routine target operations (target removal/installation, leak check, electrical check, video inspection, post irradiation examination, target waste packaging and removal) using the same method currently used in the south hot cell.  Provisions will be included for the ability to perform target waste separation in the future unless a significant obstacle is encountered in which case the meeting attendees will be consulted.  Target waste separation involves separating the internal target heater from the target heat shield, then combining multiple target heaters in a single F-308 shipment.  Neither an inert gas atmosphere nor a double-door waste transfer system will be part of the NHC scope.

 

The following people were in attendance:  Bob Laxdal, Anders Mjos, Don Jackson, Joe Mildenberger, Friedhelm Ames, Alex Gottberg, Grant Minor, Yasmine Saboui, Peter Kunz

The following people were invited, but were unable to attend:  Chad Fisher, Pierre Bricault

The project will begin immediately, with Isaac Earle as the project leader.  The first steps will be to submit a Project Initiation Sheet, then to write and release the Requirements Specification document.

Entry  Monday, May 02, 2016, 11:33, Travis Cave, Conditioning Station, Standard Operation, TM2, no target, module moved 

TM#2 was moved to the SW Silo from the Conditioning Station. TM#3 was from from the NW Silo to the Conditioning Station.

Entry  Friday, April 29, 2016, 10:06, David Wang, Conditioning Station, Standard Operation, TM2, , I switched off TCS and TM2 vacuum pumps. 

  I switched off TCS and TM2 vacuum pumps. The TM2 will be disconnected at TCS today and moved to silo on next Monday.

Entry  Friday, April 29, 2016, 08:01, David Wang, Conditioning Station, Maintenance, TM2, , TM2 leak check at TCS, helium pressure test 

Anders and I finished the most part of TM2 water lines helium pressure test yesterday.I list the system parameters and test result as below:

TCS  IG1: 9.8XE-8 torr,  TCS IG2: 9.6Xe-7 torr, TCS IG1S: 3.5XE-9 torr, TCS CG1A: 10 m torr

Helium pressure: 70 psi. Test time: 5 minutes for each individual circuit.  1 hour for all  lines together test.

 Leak detector base leak rate:0.0 X E -9 atm.cc/sec, base pressure 0.0X E-4 torr. LD was always restored or closely restored to the bottom  scale after each individual test.

 

Circuit Result (atm.cc/sec)
EE 0.0X E-9
Target Oven + 0.0X E-9
Coil 1   P-Q 0.0X E-9
Target Oven - 1.0X E-9
Tube Heater- 4.1X E-9
Tube heater+ 1.6X E-8
Coil 2    R-U 6.6X E-9
MSP 1.4X E-7
All above together (1 hour) 2.3X E-7
HS Open circuit . No test
Window Open circuit.  No test.
GE  7.2X E-7

The HS and Window lines will be tested later with new target installed and  window line gaskets restored.

Entry  Thursday, April 28, 2016, 06:28, David Wang, Conditioning Station, Maintenance, TM2, , TCS water system are turned off. 

 TCS water system worked fine overnight. I turned off TCS water system at 6:16 AM this morning. Start of purging TM2 water lines for helium pressure test again this morning.

2016-4-28 7:58AM. Disconnected TM2 water lines at TCS. Purged them with compression air each for 5 minutes. 

Entry  Tuesday, April 26, 2016, 10:47, David Wang, Conditioning Station, Repair, TM2, , TM2 leak check at TCS, water test. 

The following water circuits in TM2 are connected at TCS and running with water now : target oven+ - ( one circuit), tube heater+ -( one circuit), coil1 and 2(one circuit), MSP, and EE. The HS and window are open circuits now so they can not be supplied with water.  During the check before we knew HS and window circuit were close to perfectly sealed. So, The test result should not be affected without them

The TCS water pumps are started at 8:28 AM. All TCS high vacuum gauge readings are getting slight better after that.

Entry  Monday, April 25, 2016, 12:18, David Wang, Conditioning Station, Standard Operation, , , Target Hall schedule for beam schedule 130 (Apr- Sep) 7x

Post MS project and Excel    target hall schedule for beam schedule 130 see attachments 1,2

Update TH schedule 130 with TM3 jobs involved in.see attachments 4,5.

2016-04-29.  Weekly update schedule according to changes. See attachments 6,7.

Entry  Friday, April 22, 2016, 14:07, David Wang, Conditioning Station, Standard Operation, TM2, , 2016 Winter Shut Down Target Hall Schedule 2016_winter_shut_down__target_hall_schedule.pdf2016_winter_shut_down__target_hall_schedule.mpp

Weekly update.This is the last update on 2016 winter shut down schedule. The new TH schedule for beam130  will be posted weekly after this. All jobs in winter shut down schedule were finished on time.

 

Entry  Monday, April 18, 2016, 09:07, David Wang, Conditioning Station, Repair, TM2, , venting TCS with argon. 

Anders reported a possible air leak on TM2 and TCS by watching RGA  this morning. I found the quick connector on F terminal on the top of the module is leaking air. It is only used as "X" terminal for Febiad without  water. So, it should be blind capped instead of installing a quick connector. It was installed with a  blind cap before. I borrowed it for leak check on coil lines at SHC, but forgot to put it back right away. Instead, I put a quick connector on it later. This caused the problem. Anyway The TCS need to be vented , and a blind cap  will be installed on the F terminal.

2014-04-18, 9:24AM, I changed the quick connector with a blind cap on F terminal. the rough pump is started now.

Entry  Thursday, April 14, 2016, 12:56, David Wang, ITW, Standard Operation, TM1, , 5 shielding blocks have been moved to ITW. 

The ITW is configured to take proton beam.

Entry  Thursday, April 14, 2016, 09:46, Anders Mjos, Conditioning Station, Standard Operation, TM2, , TM2 water leak test 2016-04-15_RGA.png

 Thursday, April 14, 2016, 07:50: RGA on


Friday, April 15, 2016, 08:09 : Ratio between water and air is higher than normal (indicating possible air leak). See attachment. 3.5 more H2O than N2.  (Ratio in TM3 Nov 2015 was 82:1)


 

A leak was found on the o-ring between the module flange and TCS. This could be fixed by cleaning the o-ring and sealing surface. The Window line is not closed and was accidentally pressurized with He on April 25


Tuesday, April 26, 2016, 08:47: David started the water package.


Wednesday, April 27, 2016, 08:15: Switched off chiller / water cooling.

Wednesday, April 27, 2016, 14:41: Switched chiller / water cooling back on.

Entry  Wednesday, April 13, 2016, 10:46, David Wang, Conditioning Station, Standard Operation, TM2, , TM2 and TCS vacuum system has been connected.  

TCS is under roughing now.

2016-04-14, Started TCS and TM2 turbo-pumps yesterday afternoon. Overnight pumping down is fine.

Entry  Wednesday, April 13, 2016, 10:46, David Wang, Conditioning Station, Standard Operation, TM2, , TM2 and TCS vacuum system has been connected.  

TCS is under roughing now.

Entry  Wednesday, April 13, 2016, 10:14, Travis Cave, Conditioning Station, Standard Operation, TM2, no target, module moved 

TM#2 has been moved from the south west silo to the conditioning station.

Entry  Tuesday, April 12, 2016, 11:41, David Wang, ITE, Standard Operation, TM4, , TM4 has been connected in ITE. 

Tm4 has been connected in ITE. The ITE and TM4 is under roughing now. ITE

Turbo-pumps have been started. Everything is fine.

Entry  Tuesday, April 12, 2016, 09:08, Travis Cave, ITE, Standard Operation, TM4, Ta#47, module moved 

TM#4 with Ta#47 has been moved from the conditioning station to the east target station.

Entry  Monday, April 11, 2016, 13:44, David Wang, Conditioning Station, Standard Operation, TM4, , I stopped TCS and TM4 vacuum pumps. 

The TM4 is still under vacuum at TCS. It will be vented tomorrow morning.

I disconnected TM4 vacuum system at TCS.

Entry  Monday, April 11, 2016, 10:07, Travis Cave, Spent Target Vault, Standard Operation, , UC#14, Spent Target move Vault_Storage_April_11_2016.pdf

The spent UC#14 target has been moved into the ISAC spent target vault. See the attached PDF for the details.

Entry  Monday, April 11, 2016, 09:42, David Wang, Conditioning Station, Standard Operation, TM4, , Helium pressure test on TM4 HS line at CS with new Lp Ta target 

70 psi helium , 2 minutes. Base leak rate 0.0x E-9 atm.cc/sec. base pressure 0.0XE-4 torr. no response on LD.The line is good.

Entry  Friday, April 08, 2016, 13:16, David Wang, Conditioning Station, Standard Operation, , , 2016 Winter Shut Down Target Hall Schedule 2016_winter_shut_down__target_hall_schedule.mpp2016_winter_shut_down__target_hall_schedule.pdf

Update schedule weekly .see attachment 1,2

Entry  Friday, April 08, 2016, 08:48, David Wang, ITW, Standard Operation, , , ITW water signal interlock check. 

I did a ITW water signals interlock check with ISAC opp. They are checked once a year before first beam on.

2016-04-13 Same test is done on ITE also. Everything is good.

Entry  Friday, April 08, 2016, 08:13, Anders Mjos, ITE/ITW Cooling, Maintenance, , , High Active Water Resistivity 2016-04-08_ISAC_High_Active_Water_Resistivity.png

The high active water resistivity took a long time to recover after the upgrade to the water cooling circuit. The system needed about a month (from end February to end March) to recover to nominal values. See attached plot of archiver data.

TM1 has now been connected in ITW and the water resistivity remains > 8 MOhm cm, which should allow normal operation. However, the resin is suspected to be approaching end of life. Work is ongoing to get a new replacement resin tank.

Entry  Friday, April 08, 2016, 07:13, David Wang, ITW, Standard Operation, TM1, UCx15, TM1 has been connected in ITW. 

After ITW HV test is done, TM1 has been connected to ITW. Water signals are checked in electrical room. They are good.

Entry  Friday, April 08, 2016, 07:10, David Wang, Conditioning Station, Standard Operation, TM4, , TM4 vacuum has been connected in ITE. 

All turbo pumps are started yesterday. The pumping down is good over night.

Entry  Thursday, April 07, 2016, 09:24, Travis Cave, Conditioning Station, Maintenance, TM4, Ta#47, module moved 

TM#4 has been moved from the south hot cell to the conditioning station.

Entry  Wednesday, April 06, 2016, 14:52, Travis Cave, South Hot-Cell, Standard Operation, TM4, UC#14, No Target, Ta#47, Electrical Check TM4_elec_chk_notgt_SHC.PDFTM4_elec_chk_Ta47_SHC.PDFTM4_elec_chk_UC14_SHC_postbeam.PDF

Various electrical checks done on TM#4, one of post beam UC#14, of no target and with Ta#47. See PDFs for details.

Entry  Wednesday, April 06, 2016, 14:03, chad fisher, South Hot-Cell, Standard Operation, TM4, Ta#47, UCx#14 removed Ta#47 installed 

UCx#14 has been removed from TM4 and Ta#47 installed. No marks on 9 pin connector on UCx#14.

Entry  Wednesday, April 06, 2016, 09:37, Travis Cave, South Hot-Cell, Standard Operation, TM4, UC#14, module moved 

TM#4 with UC#14 has been moved from the east target station to the south hot cell.

Entry  Tuesday, April 05, 2016, 12:40, David Wang, ITE, Standard Operation, TM4, , I stopped ITE turbo pumps this morning 

The ITE and TM4 have been vented with Argon . TM4 vacuum system is disconnected in ITE.

Entry  Tuesday, April 05, 2016, 12:36, David Wang, ITW, Standard Operation, TM1, , TM1 vacuum system has been connected in ITW. 

 All turbo -pumps are started.

Entry  Tuesday, April 05, 2016, 09:33, Travis Cave, ITW, Standard Operation, TM1, UC#15, module moved 

TM#1 with UC#15 have been moved from the conditioning station to the west target station.

Entry  Tuesday, April 05, 2016, 07:12, David Wang, Conditioning Station, Standard Operation, TM1, UC#15, stop CS vacuum pumps. 

Stop TCS vacuum pumps . Preparing argon venting on TM1 and TCS.

7:34 AM, Disconnected TM1 at TCS, argon venting now.

Entry  Monday, April 04, 2016, 11:14, David Wang, Conditioning Station, Standard Operation, TM1, , Helium pressure test on TM1 HS line at CS 

New UCx target is installed on the module. 70psi helium,3 minutes. NO response on LD.  LD is pumped to bottom LR and LP during test.

Entry  Friday, April 01, 2016, 14:41, David Wang, Conditioning Station, Standard Operation, TM1, , TM1 and TCS vacuum system has been connected. TCS control page white out. 

I can not start the TCS pumps due to control page white out. Control group is working on this issue.

Control group fixed the white out problem. I started all turbo-pumps. The pumping down is good so far. The TM1 IG1 is broken. I will check it on next Monday. It could be a broken filament. Then, the filament will be replaced.

Entry  Friday, April 01, 2016, 13:58, Travis Cave, Conditioning Station, Standard Operation, TM1, UC#15, module moved 

TM#1 has been moved from the conditioning station to the south hot cell, had UC#15 installed and then moved back to the conditioning station.

Entry  Friday, April 01, 2016, 11:41, Travis Cave, South Hot-Cell, Standard Operation, TM1, UC#15, Electrical Check TM1_elec_chk_UC#15_SHC.PDF

Electrical check of the target on TM#1, target in question is UC#15. See PDF for details.

Entry  Wednesday, March 30, 2016, 15:49, David Wang, Assembly/Bench Test, Repair, TM2, , TM2 Helium spray leak check on solder stems inside service cap on the top of SW silo. 7x

On each water circuit in side the service cap, there are 4 soldering stems which two of them are inside blue nylon insulator and other two are connected to service tray. Each stem has two soldering spots. See attachment pictures for detail location. I sprayed 15 psi helium on each soldering spots on stems  for 20second on each circuit. I sprayed tons of helium inside each blue nylon.No any leak has been found during the check. The leak detector base leak rate:0.0 XE-9 atm.cc/sec, base pressure:0.0X E-4 torr. The circuit which I checked are :TA+, Ta-, Tube+, Tube-, PQ (coil 2), RU( coil1), EE, MSP, GE. The HS and window circuit are opened at this moment so they can not be checked.

Entry  Wednesday, March 30, 2016, 11:00, Travis Cave, Conditioning Station, Standard Operation, TM1, no target, Electrical Check TM1_elec_chk_notgt.PDF

The results of the TM#1 electrical check from the 29th of March 2016

Entry  Wednesday, March 30, 2016, 08:40, David Wang, Conditioning Station, Standard Operation, , , 2016 Winter Shut Down Target Hall Schedule 2016_winter_shut_down__target_hall_schedule.pdf2016_winter_shut_down__target_hall_schedule.mpp

update the schedule according to changes.See attachment1, 2.

Entry  Tuesday, March 29, 2016, 08:38, David Wang, Conditioning Station, Standard Operation, TM1, , TM1 water lines helium pressure check at TCS TM1_PNG1_panel_o-ring_replacement_001.JPGTM1_PNG1_panel_o-ring_replacement_002.JPGTM1_PNG1_panel_o-ring_replacement_004.JPGTM1_PNG1_panel_o-ring_replacement_005.JPGTM1_PNG1_panel_o-ring_replacement_006.JPG

TM1 water lines helium pressure check at TCS is done. 70 psi helium was applied to water circuits. Leak detector base leak rate 0.0 x E-9 atm.cc/sec, base pressure 0.0 x E-4 torr. The result shows as below:

 

 

Ta+   0.0 X E-9 atm.cc/sec 3minutes stabilizing
Ta-  0.0 X E-9 atm.cc/sec 3minutes stabilizing
Tube-  0.0 X E-9 atm.cc/sec 3minutes stabilizing
Tube+  0.0 X E-9 atm.cc/sec 3minutes stabilizing
MSP   0.0 X E-9 atm.cc/sec 3minutes stabilizing
EE   0.0X E-9 atm.cc/sec 3minutes stabilizing
HS  not tested without caps.  
Window  E-5 range,leak on stem as we knew before.  10seconds to E-5

The results is good so far as we know the window line is leak on stem in service cap. The HS will be tested later with target on.

 The service cap air to vacuum seals also have been checked. The PNG1 panel and side round panel close to shutter are leak. The o-rings on them need to be replaced.

On March 30th -2016, I doubled checked the air to vacuum seal on the TM1 service cap. The side round panel is leak free actually. The PNG1 panel is leak at the bottom side. Confirmed.

On march 31th-2016, The o-ring(1-1/ 2275) on TM1 PNG1 side panel has been replaced today. The o-ring slot and mating surfaces are cleaned, and new  o-ring is installed. The panel is put back to TM1 and all bolts are tightened.

See attachments.

Entry  Thursday, March 24, 2016, 13:55, Travis Cave, Conditioning Station, Standard Operation, TM1, no target, module moved 

TM#2 has been moved from the south hot cell to the south west silo and TM#1 was moved from the north east silo to the conditioning station. All done by 10AM.

Entry  Thursday, March 24, 2016, 13:15, David Wang, Conditioning Station, Standard Operation, TM1, , TM1 and TCS vacuum system has been connected  

TM1 and TCS vacuum system have been connected. All turbo-pumps are started. The pumping down is fine.

Entry  Wednesday, March 23, 2016, 11:32, David Wang, South Hot-Cell, Repair, TM2, , TM2 Helium spray leak check on GE and MSP lines at SHC 

  Chad and I did the helium spray leak check on TM2 GE and MSP water lines at SHC this morning. We confirmed the GE leak on water blocks. We can not found the MSP leak by using the helium spray since its leak rate in TCS is much smaller than GE leak.  The leak check process are as below:
Leak detector are calibrated before the check.
GE lines : Base leak rate 0.0 X E-9 atm.cc/sec, base pressure 0.0 XE-4 torr.
Chad sprayed 5 psi helium to GE lines soldering joints  for 5 second, no response on leak detector.
Chad sprayed 5 psi helium to GE lines water blocks( between blocks seal surface) for 5 seconds, Leak detector response to 8 XE-9 atm.cc/sec right away.
Chad sprayed  5 psi helium to GE lines soldering joints for 5 seconds again, No response on leak detector.
Chad sprayed 5 psi helium around the source tray and to vacuum duct for 5 seconds more, No response on leak detector.
MSP lines: Base leak rate 0.0X E-9 atm.cc/sec, base pressure 0.0 X E-4 torr.  Chad did same thing as he did on GE lines. no response on LD. Chad repeated the test and prolonged the spray time to 10 seconds, No response.
The conclusion: It is pretty clear we have a leak on GE line water blocks seal.  MSP lines leak could not be found by helium spray in SHC since it is a small leak.
 

Entry  Wednesday, March 23, 2016, 11:00, Travis Cave, South Hot-Cell, Standard Operation, TM2, no target, module moved 

TM#2 was moved into the south hot cell by 08:30.

Entry  Tuesday, March 22, 2016, 10:27, Travis Cave, Spent Target Vault, Standard Operation, , SiC#32, Spent Target move Vault_Storage_March_22_2016.pdf

SiC#32 has been moved from the south hot cell to the spent target storage. See attached PDF for details.

Entry  Monday, March 21, 2016, 15:27, David Wang, Conditioning Station, Repair, TM2, , TM2 has been disconnected at TCS 

TM2 vacuum system has been disconnected at TCS. Venting is in process now.

Entry  Monday, March 21, 2016, 11:30, David Wang, Conditioning Station, Repair, TM2, , TM2 and TCS vacuum pumps are stopped 

I stopped TM2 and TCS vacuum pumps. It will be vented and disconnected this afternoon for tomorrow  moving.   

Entry  Monday, March 21, 2016, 10:25, David Wang, Conditioning Station, Repair, TM2, , TM2 Helium pressure Test Result in TCS and ITW 

TM2 has been helium pressure tested in ITW and TCS. They are both tested with 70psi helium, each circuit for 3minutes. 

The leak detector base leak rate: 0.0X E-9 atm.cc/sec, base pressure 0.0 xE-4 torr  for both ITW and TCS. The test results are:

 

 

 

 

circuit TCS Test Result (atm.cc/sec) 2016-03-021  ITW Test Result (atm.cc/sec) 2016-03-02

TCS Test Result (atm.cc/sec)

2116-11-24

Target Oven + 5.2 X E-9 1.7 X E-8 2.0 X E-9
Target Oven - 5.6 X E-9 8.7 X E-9 2.2 X E-8
Tube Heater + 3.7 X E-8 1.7 X E-8 2.3 X E -8
Tube Heater - 1.9 X E-8 1.5 X E-8 8.2 X E-8
Coil 2 (P-Q) 7.2 X E-8 6.7 X E-8 5.4 X E-9
Coil 1 (R-U) 1.4 X E-8 1.3 X E-8 2.4 X E-9
MSP 2.3 X E-7, SECOND TIME 2.5 X E-7 4 X E-9 2.4 X E-7
HS NO TEST, LINE IS OPEN TO VACUUM. GOOD, NO RESPONSE ON LD Good, 0.0 X E-9
EE 4.3 X E-9 GOOD, NO RESPONSE ON LD

3.7 X E-8

 

window 4.5 X E-9 GOOD, NO RESPONSE ON LD Good , 0.0 X E-9
GE NO TEST, CONFIRMED IN SHC MIDDLE OF E-6 RANGE No test. Blanked
       

 2016-11-24: Checked again and added result into this elog.  No essential change has been found. MSP still has the biggest leak rate. David

Entry  Friday, March 18, 2016, 13:13, Travis Cave, Conditioning Station, Standard Operation, TM2, SiC#32, Electrical Check TM2_SiC32_postbeam.PDFTM2_elec_chk_notgt_CS.PDF

Electrical checks of the TM#2 with the old SiC#32 and without the target. See attached PDFs.

Entry  Friday, March 18, 2016, 11:43, chad fisher, South Hot-Cell, Standard Operation, , , SiC#32 dissection 20160318_105519_1.jpg20160318_105311.jpg20160318_105248.jpg20160318_105428.jpg

SiC#32 has been open for inspection.

Entry  Friday, March 18, 2016, 09:42, David Wang, Conditioning Station, Standard Operation, TM2, , TM2 vacuum sysytem has been connected at TCS 

TM2 vacuum system has been connected at TCS. Started roughing pump. Everything is good so far.

Entry  Friday, March 18, 2016, 09:34, David Wang, Conditioning Station, Standard Operation, TM2, , Target Hall schedule for beam schedule 130 (Apr- Sep) Target_Hall_shedule_130_Apr_to_Sep_2016.xlsxTarget_Hall_shedule_130_Apr_to_Sep_2016.pdf

I would like to post the spreadsheet of target hall schedule for beam schedule 130(Apr to Sep) first. The MS project of TH schedule for  beam schedule 130 is under construction, and will be posted later.

Entry  Friday, March 18, 2016, 08:34, Travis Cave, Conditioning Station, Standard Operation, TM2, no target, module moved 

TM#2 with no target has been moved to the conditioning station from the south hot cell.

Entry  Thursday, March 17, 2016, 14:57, David Wang, South Hot-Cell, Repair, TM2, , TM2 first round leak check in SHC 

Chad and I finished the first round check on Tm2 water lines. The lines and spots checked are: Target oven + and - (front side braze joints) , Tube heater+and -(front side braze joints and water blocks), coil2 and coil 1(front side braze joints and area close to water blocks),. No leak has been found on all above of them.  The last, we checked   the GE which has the biggest leak so far. The leak detector base leak rate only can get to 4XE-9 atm.cc/sec. Chad sprayed helium very close to GE water block, and I got a quick response on leak detector. The leak rate climbed from 4Xe-9 atm.cc/sec to 1.4 atm.cc/sec. We confirmed the GE is leaking now. The exact location need to be pinpointed later once the containment box is out after the module is back to SHC. The module will be moved to TCS tomorrow morning and pressurized again there. Anders will use RGA to monitor the helium response during the check.  

Entry  Wednesday, March 16, 2016, 14:23, chad fisher, South Hot-Cell, Standard Operation, TM2, SiC#32, SiC#32 removal Target Module Inspection 20160316_141127.jpg20160316_141146.jpg

SiC#32 has been removed from TM2. Quick inspection shows some troubling discoloration on the water cooled connection blocks of C and D as well as the left target heater A.

As for the target, both legs are broken and is has the normal "charge up" marks on the 9 pin connector.

Entry  Wednesday, March 16, 2016, 09:20, Travis Cave, ITE, Standard Operation, TM2, SiC#32, module moved 

TM#2 with SiC#32 has been moved from the west station to the south hot cell.

Entry  Monday, March 14, 2016, 15:22, David Wang, Conditioning Station, Standard Operation, TM2, , 2016 Winter Shut Down Target Hall Schedule 2016_winter_shut_down__target_hall_schedule.pdf2016_winter_shut_down__target_hall_schedule.mpp

update schedule according to change. See attachment 1,2

 

Entry  Monday, March 14, 2016, 11:24, David Wang, ITE/ITW Cooling, Maintenance, , , HALCW resin tank filter cartridges are changed today 002.JPG003.JPG006.JPG

Two of resin tank filter cartridges(supply and return) are changed today. Old cartridges and bagged and tagged. The contact field on them are 650usv/hr. The new cartridges are fiber-glass, Triumf store item. After replacement, the field on contact with the filter case are about 10 usv/hr. But the field on contact with top resin tank  has been increased from 45usv/hr  to 225 usv/hr

 The flow rate is relatively stable before and after change. See attachment

Entry  Friday, March 04, 2016, 13:58, David Wang, Conditioning Station, Standard Operation, , , 2016 Winter Shut Down Target Hall Schedule 8x

Update Schedule according to changes.See attachment1, 2.

 Re-post it after some minor correction See attachment 3,4.

Update schedule according changes. See attachments 5,6

 update schedule according to changes. See attachment 7,8

Entry  Friday, March 04, 2016, 12:34, David Wang, ITE, Standard Operation, TM4, , TM4 ITE annual leak check 

Dan and I finished TM4 and ITE annual leak check on primary and secondary vacuum vessel. We found one leak on a KF25  blank off which is located on the top of the service cap. It is a low E-7 atm.cc/sec range leak. But, it is very close to turbo-pumps so ITE IG1 and other gauges are not affected by it very much. It is an easy fix. TheKF -25 center ring on the blank off  will be replaced  after vent . It be will leak checked again at CS after replacement.  That is only leak we found on TM4 and ITE primary and secondary vessel air to vaccum leak check.

Dan and I also finished the helium pressure test on all TM4 using water circuits. 70 psi helium. base LR 0.0xE-9 atm.cc/sec. All of them are leak free. No any response has been found on leak detector during test.

Entry  Wednesday, March 02, 2016, 10:04, David Wang, ITW, Standard Operation, TM2, , Leak check on ITW and TM2. 

Dan and I leak checked TM2 and ITW primary vacuum vessel. It was found a 1X E-7 atm.cc/sec leak on top T flange seal between TM2 and dump module in first time check. But it is not a repeatable leak. I checked the same spot and around area two more times with increased helium volume.It did not show up again. The first response could  be a helium drift to dry scroll pump. I will check it again later. The primar vacuum vessel on ITW and TM2 are leak free. 

Dan and I found a small  leak on ITW dump module  top flange seal. The leak detector got a response  to 7xE-9 atm.cc/sec when I spray the helium to west side of dump module top flange. We tested again, and got same result. The o-ring which seals ITW dump module top flange is deteriorating. It need to be replaced at a proper time. This is the only air to vacuum leak we confirm so far on primary and secondary vacuum vessel on TM2 and ITW. The module and station no other air to vacuum leak.

The TM2 water lines helium pressure tested started in ITW. The helium pressure 70psi. The result so far is: Window: good, GE: huge leak directly shoot over E-7 atm.cc/sec( need to be confirmed tomorrow), HS: good, EE: good, MSP: tiny leak which is response to 3-4xE-9 atm.cc/sec. Coil 1 : small leak which is response to 1.3XE-8 atm.cc/sec. Tomorrow, We will test the rest water lines on TM2which are TA+, TA-, Tube+, Tube-, and coil 2. And We will confirm the GE huge leak at the last.

Finished the helium pressure test on TM2 water line.70 psi helium, The result of the rests 5 circuits: coil 1: leak 7.2xE-8atm.cc/sec,Ta(+): small leak 1.7XE-8 atm.cc/sec, Ta(-) small leak 8.7xE-9atm.cc/sec,Tube(-) 1.5 x E-8 atm.cc/sec. Tube(+)small leak 3.7xE-8 atm.cc/sec.    We repeated the helium pressure test on GE. There is a huge leak on TM2 GE circuit. The leak detector shoot up to E-7  atm.cc/sec right after the helium was applied.It went up to E-6 range in less than 1 minutes.

 

 

Entry  Wednesday, March 02, 2016, 09:51, David Wang, ITW, Standard Operation, TM2, , all water lines on TM2 and TM4 are purged. 

All water lines on TM2 and TM4 are purged for upcoming water lines helium pressure test.

Entry  Thursday, February 25, 2016, 09:29, David Wang, ITE, Standard Operation, TM4, , TM4 has been disconnected in ITE. 

TM4 has been disconnect in ITE(except  vacuum lines). The ITE vacuum system is still operating.

Entry  Thursday, February 25, 2016, 09:27, David Wang, ITW, Standard Operation, TM2, , TM2 has been disconnected in ITW 

TM2 has been disconnected in ITW (except vacuum lines). The vacuum system is still operating.

Entry  Thursday, February 25, 2016, 06:52, David Wang, Conditioning Station, Standard Operation, , , stop CS vacuum pumps. 

I stopped the conditioning station vacuum pumps. The CS is still under vacuum without venting.

Entry  Thursday, February 25, 2016, 06:48, David Wang, ITE, Standard Operation, , , 4 Shielding blocks have been transferred from ITE to block storage area. 

Dan and I transferred 4 shielding blocks from ITE to block storage area. The ITE pit is opened now.

Entry  Friday, February 19, 2016, 06:58, maicodallavalle, Spent Target Vault, Maintenance, , , F-308's serviced/loaded/ bolts torqued 

Five F-308's were loaded with spent ISAC targets. All five F-308's were serviced two weeks ago. All bolts were torqued and security  cables were installed  for shipment.

Entry  Friday, February 12, 2016, 13:00, David Wang, Conditioning Station, Standard Operation, , , 2016 Winter Shut Down Target Hall Schedule  6x

2016 Winter shut down target hall schedule. See attachments1,2.

 update the schedule weekly. Everything is on time so far. see attachment 3,4.

Update the schedule according to beam new beam schedule and target process. see attachment 5,6

Entry  Friday, January 22, 2016, 14:24, David Wang, South Hot-Cell, Standard Operation, , , 2016 Winter Shut Down Target Hall Schedule (sketch) 2016_winter_shut_down__target_hall_schedule.pdf2016_winter_shut_down__target_hall_schedule.mpp2016_winter_shut_down__target_hall_schedule.pdf2016_winter_shut_down__target_hall_schedule.mpp

Post a sketch of 2016 winter shut down target hall schedule. see attachment 1,2

 UPDATE THE SCHEDULE ACCORDING TO CYCLOTRON SIDE JOB. SEE ATTACHMENTS 3,4

Entry  Wednesday, January 13, 2016, 09:57, Travis Cave, Spent Target Vault, Standard Operation, , Ta#35, Ta#39, SiC#27, UC#12, ThO#1, Spent targets moved to mini storage. 

Five spent targets have been moved from the Spent Target Vault to Mini Storage in preparation for transfer to F-308s in February. The following targets were moved Ta#35, Ta#39, SiC#27, UC#12, ThO#1

Entry  Friday, January 08, 2016, 09:29, chad fisher, South Hot-Cell, Repair, , , Window Decon 

Entered the hot cell to perform final decon on the window. Initial swipes this morning were 11000 c.p.m. on 44-2. After decon approximately 100 counts.

Entry  Friday, December 18, 2015, 11:42, Anders Mjos, Conditioning Station, Repair, , , Vacuum gauges not reading correctly 

 It was found that the conversion from voltage to vacuum (Torr) in EPICS is not correct for the XGS-600 controllers in use at the TCS. EPICS did not correspond to local values displayed on the controller. An e-fault has been submitted.

    Reply  Monday, December 21, 2015, 13:27, Anders Mjos, Conditioning Station, Repair, , , Vacuum gauges not reading correctly 

Anders Mjos wrote:

 It was found that the conversion from voltage to vacuum (Torr) in EPICS is not correct for the XGS-600 controllers in use at the TCS. EPICS did not correspond to local values displayed on the controller. An e-fault has been submitted.

 EPICS conversion updated and corrected by Mike Rowe.

Entry  Thursday, December 10, 2015, 13:17, Anders Mjos, Conditioning Station, Standard Operation, , , Blank off flange TCS_Blank_Off.png

Thursday, December 10, 2015, 13:17: Roughing

Thursday, December 10, 2015, 14:56: Started TP1S

Thursday, December 10, 2015, 15:59: Bypass applied on IG2

Thursday, December 10, 2015, 15:59: IG2 / IG1S 5.5E-5 T

Thursday, December 10, 2015, 16:01: RGA ON


Friday, December 11, 2015, 09:24 : IG2 / IG1S 7.5E-6 / 5.4E-6 T

Friday, December 11, 2015, 16:54: IG2 off for the weekend. Vacuum at 6.5 and 4.4E-6 Torr


Monday, December 14, 2015, 08:57: IG2 switched on.


Friday, December 18, 2015, 11:40: IG2 off for the weekend. Vacuum at 2.0E-6 and 8.9E-7 Torr 


Tuesday, December 22, 2015, 15:11: RGA off


Monday, January 11, 2016, 10:13: RGA on

Monday, January 11, 2016, 12:50: RGA off

Entry  Wednesday, December 02, 2015, 10:41, chad fisher, South Hot-Cell, Repair, , , Drum Clean-up #2 

Another drum of waste was removed from the south hot cell this morning. This drum contained one 5 gal steel pail (damaged), two sodium light bulbs, airlines, and tank suits. Upon removal the drum was/is 1.5 mSv/h on contact. there was 200 counts of contamination found on the lid...easily removed. It will be moved to the north hot cell at 11am.

Entry  Tuesday, December 01, 2015, 14:30, David Wang, ITE, Standard Operation, TM4, UCx 13, TM4 has been connected in ITE 

TM4 has been connected in ITE. All turbo-pumps are started. Everything is good so far.

Entry  Tuesday, December 01, 2015, 11:47, Anders Mjos, Conditioning Station, Maintenance, TM4, UC#14, Short on Extraction Electrode 

 After conditioning over the weekend the EE developed a short. This was confirmed by measuring the resistance between EE and Heat Shield on the module yesterday.

Entry  Tuesday, December 01, 2015, 11:26, Travis Cave, ITE/ITW Cooling, Standard Operation, TM4, UC#14, Module moved 

TM#4 with UC#14 has been moved from the conditioning station to the east target station.

Entry  Tuesday, December 01, 2015, 06:41, David Wang, Conditioning Station, Standard Operation, TM4, UC#14, Turned off TCS all vacuum pumps and water pumps. 

I turned off TCS vacuum and water pumps. The TSC and TM4 are still under vacuum condition.

Entry  Monday, November 30, 2015, 11:46, David Wang, Conditioning Station, Standard Operation, , , Target Hall schedule from Sep 08th 2015 to Dec 25th 2015 Target_Hall_Scheduled_Activities__Sep_09_to_Dec_30.pdfTarget_Hall_Scheduled_Activities__Sep_09_to_Dec_30.mppTarget_Hall_Scheduled_Activities__Sep_09_to_Dec_30.pdfTarget_Hall_Scheduled_Activities__Sep_09_to_Dec_30.mpp

Weekly update TH schedule according to changes. see attachment 1,2 .

Update TH schedule before the weekend. see attachment 3,4

Entry  Thursday, November 26, 2015, 08:52, Travis Cave, Spent Target Vault, Standard Operation, , Ta#46, Spent Target move Vault_Storage_November_26_2015.pdf

Ta#46 was placed in the ISAC spent target vault yesterday. See attached PDF for details.

Entry  Thursday, November 26, 2015, 07:37, David Wang, Conditioning Station, Standard Operation, TM4, UC#14, TM4 has been connected at CS 

TM4 has been connected at TCS. The water system is started. The TCS HV cover for TM4 is installed also. Basically, The TM4 is ready for conditioning.

Entry  Thursday, November 26, 2015, 07:34, David Wang, Conditioning Station, Standard Operation, TM4, UC#14, Helium pressure test on TM4 HS line at CS  

I did helium pressure test on TM4 HS line at TCS this morning.  70psi helium 3 minutes, 0.0xE-9 atm.cc/sec base leak rate. No response. No leak.

Entry  Thursday, November 26, 2015, 06:25, David Wang, Conditioning Station, Standard Operation, TM4, UC#14, TM4 vacuum has been connected in TCS. 

TM4 vacuum has been connected in TCS. All vacuum pumps were started yesterday. The pumping down of TM4 and TCS are good so far.

Entry  Wednesday, November 25, 2015, 15:37, Anders Mjos, Conditioning Station, Standard Operation, TM4, UC#14, Conditioning 

 Wednesday, November 25, 2015, 15:36: RGA on


Thursday, November 26, 2015, 09:55: PS energized. EE connected to power supply.

Thursday, November 26, 2015, 11:41: Applied some current and voltage to all power supplies. All looks good.

Some sparking around 5 kV. Turned out to be a bad cable connection. Fixed with David W.

Thursday, November 26, 2015, 15:04: BIAS/EL/EE 20 / 15 1.5 kV

Thursday, November 26, 2015, 15:43: Handed TCS over to ISAC operations


 Target heated over the weekend. EE went into current limiting (down to ~100 V) a while after the target was at temperature.


Monday, November 30, 2015

Target conditioned by ISAC operators to 30 kV without any problems.

EE current limit increased to about 26 mA in an attempt to recover. Cooling down target to investigate.

Entry  Wednesday, November 25, 2015, 14:16, chad fisher, South Hot-Cell, Repair, , , Cell Decon 20151125_100512.jpg20151125_101620.jpg

Cell (table) was systematically cleaned with a swiffer and resulting piles of contaminated waste placed in pail with spent Ta target.

Entry  Wednesday, November 25, 2015, 14:13, chad fisher, South Hot-Cell, Standard Operation, TM4, UC#14, UCx#14 

UCx#14 installed onto TM4. High current fasteners torqued to 130 in lbs.

Entry  Wednesday, November 25, 2015, 11:55, Travis Cave, Conditioning Station, Standard Operation, TM4, UC#14, Module moved and electrical check. TM4_UC14_elecchk_SHC.PDF

TM#4 with UC#14 was moved from the south hot cell to the conditioning station.  Here are the results of the electrical check of the module with the UC#14 target while at the hot cell.

Entry  Wednesday, November 25, 2015, 11:52, Travis Cave, South Hot-Cell, Standard Operation, TM4, Ta#46, Module moved 

Yesterday TM#4 with Ta#46 was moved from the east station to the south hot cell.

Entry  Tuesday, November 24, 2015, 14:03, chad fisher, South Hot-Cell, Standard Operation, TM4, , Ta#46 

Ta#46 has been removed from TM4.

Entry  Tuesday, November 24, 2015, 14:02, chad fisher, South Hot-Cell, Repair, , , Left Manip repair 

electronics package on left manip died completely yesterday (it has been going for a while).

Disconnected entire package and replaced with package from "spare" manipulator.

everything is back up and working.

Entry  Tuesday, November 24, 2015, 14:00, chad fisher, South Hot-Cell, Repair, , , Compressible waste sorting. 20151124_101547.jpg

Residual fields from the remaining compressible waste were still too high (as far as I'm concerned) so I have unpacked all compressible waste looking for a "hot" item that has snuck into these items.

I have a hand full of small bolts (possible target components), a hand full of target material/dust (including an entire target disc), and some cloths that had clearly been used to wipe the table (they are black with target dust).

These items will be disposed of with the next spent target.

Entry  Tuesday, November 24, 2015, 13:54, chad fisher, South Hot-Cell, Repair, , , Cell Decon 

Decon/removal of large solid waste was performed on Wednesday November 18th."Hot" activated items included containment box cover from TM2, Febiad coil line remnants from TM4 (the hottest ends were previously cut off and disposed of), some target conductor bolts, steerer plugs from TM2, target material remn.

Drum containing these solid items is 2.5mSv/hr at 1/2m.

Drum is stored in the north hot cell temp.

Compressible waste will require another drum.

Swipes were taken of the window... 170k counts per minute of cont.

Entry  Monday, November 16, 2015, 13:59, Travis Cave, Conditioning Station, Maintenance, TM3, no target, Module moved 

TM#3 has been moved back to the NW silo.

Entry  Monday, November 16, 2015, 10:37, David Wang, Conditioning Station, Repair, TM3, , TM3 has been disconnected at TCS. 

I stopped the TM3 and TCS vacuum pumps and water system. The TM3 is disconnected and vented. It will be moved to silo this afternoon.

Entry  Monday, November 16, 2015, 10:33, Anders Mjos, Conditioning Station, Standard Operation, , FEBIAD Test Target, HV conditioning by ISAC operators 

ISAC operators attempted HV conditioning over the weekend.

https://web.accel.triumf.ca/isac_elog/Elog_show_result.pl?inid=218447&style=entry

 

Entry  Monday, November 16, 2015, 10:09, Anders Mjos, Conditioning Station, Standard Operation, TM3, FEBIAD Test Target, Electrical check after HV conditioning 2015-11-16_TM3_Electrical_Test.pdf

 Problem found between ANODE (F) and chassis 90 kOhm. See attachment for details.

Entry  Monday, November 16, 2015, 08:04, David Wang, Conditioning Station, Standard Operation, , , Target Hall schedule from Sep 08th 2015 to Dec 25th 2015 Target_Hall_Scheduled_Activities__Sep_09_to_Dec_30.pdfTarget_Hall_Scheduled_Activities__Sep_09_to_Dec_30.mppTarget_Hall_Scheduled_Activities__Sep_09_to_Dec_30.pdfTarget_Hall_Scheduled_Activities__Sep_09_to_Dec_30.mpp

Update TH schedule according to changes. See attachment 1,2 .

update TH schedule weekly. See attachments 3,4

Entry  Thursday, November 12, 2015, 13:25, Anders Mjos, Conditioning Station, Standard Operation, TM3, FEBIAD Test Target, Electrical check and leak check TM3_iwth_FEBIAD_in_TCS_Electrical_Check.pdf

Target to Anode and target to Common showed ~ 500 kOhm values. No leaks above 3E-9 atm-cc/s seen. See attached.  

Entry  Tuesday, November 10, 2015, 10:23, Anders Mjos, Conditioning Station, Maintenance, TM3, , Air to vacuum leak on service cap TM3_Service_Cap_Leak.pdf

Conducted a more thorough leak check this morning with Edi. He found a leak on the base of the  blue F/T insulator for the multi-pin connector (see attachment). I discovered that all the bolts could rotate freely in the threads as they were too small. The bolts were replaced. The leak rate was reduced but still significant. The o-ring will likely need to be replaced.

Tuesday, November 10, 2015, 17:00: Could not find new o-ring. Cleaned groove and o-ring and applied o-ring grease. Re-attached F/T.

    Reply  Thursday, November 12, 2015, 10:18, Anders Mjos, Conditioning Station, Maintenance, TM3, , Air to vacuum leak on service cap 

Anders Mjos wrote:

Conducted a more thorough leak check this morning with Edi. He found a leak on the base of the  blue F/T insulator for the multi-pin connector (see attachment). I discovered that all the bolts could rotate freely in the threads as they were too small. The bolts were replaced. The leak rate was reduced but still significant. The o-ring will likely need to be replaced.

Tuesday, November 10, 2015, 17:00: Could not find new o-ring. Cleaned groove and o-ring and applied o-ring grease. Re-attached F/T.

Tuesday

Steerer wire had disconnected again. See DocuShare for photos.


Thursday, November 12, 2015

Leak checked the fixed F/T and the panel for steeerers. No leaks found.

Entry  Friday, November 06, 2015, 14:36, Anders Mjos, Conditioning Station, Development, TM3, FEBIAD test target, Testing TM3 

Friday, November 06, 2015, 14:35: Roughing

Turbos was started around 4pm. Later it was found that the manual valve for the two turbo pumps on the service cap was closed. The valve was open and pumping resumed. The roughing vacuum was high and increased into Saturday morning. The vacuum system was switched off on Saturday.


Purged MP1 using the purging function. Performance recovered. Started rouging.

Monday, November 09, 2015, 09:18: Started TP1S

Monday, November 09, 2015, 09:22: Started TP1 and TP2

Monday, November 09, 2015, 09:33: All 3 turbos at speed


Leak found on F/T for multipin connector

Tuesday, November 10, 2015, 09:53: stopped turbos

    Reply  Tuesday, November 10, 2015, 16:53, Anders Mjos, Conditioning Station, Development, TM3, FEBIAD test target, Testing TM3 2015-11-13_TCS_TM3_FEBIAD_Test_Target.docx

Tuesday, November 10, 2015, 16:53: Roughing

Tuesday, November 10, 2015, 18:24: TP1S started

Tuesday, November 10, 2015, 18:30: TP1 and TP2 started

Tuesday, November 10, 2015, 18:41: All 3 turbos at speed.


Thursday, November 12, 2015, 08:30: Purged backing pump using purging function. Vacuum in backing line recovered to previous value. 


Module connected for HV testing. No target heating possible. All F/Ts tied together to HV common. EZL connected.

Friday, November 13, 2015, 11:20: Started water package

Friday, November 13, 2015, 11:52: 1kV on BIAS and 1 kV on EL

Friday, November 13, 2015, 12:54: BIAS/EL 10 / 5 kV

Friday, November 13, 2015, 12:59: BIAS/EL 15 / 7.5 kV

Friday, November 13, 2015, 13:04: BIAS/EL 20 / 10 kV

Friday, November 13, 2015, 13:08 : BIAS/EL 22 / 11 kV. Some sparks.

Friday, November 13, 2015, 13:17: Sparking at 22.5 kV. Had to return to 20 kV to recover. Back at 22.5

Friday, November 13, 2015, 13:21 : BIAS/EL 24 / 12 kV. 

 Friday, November 13, 2015, 13:27: Heavy spakring around 24.5 kV. Had to return to 20 kV to recover.

Friday, November 13, 2015, 13:31: Attempted to increase voltage again. Sparking started around 23 kV. Had to lower to 20 kV.

Friday, November 13, 2015, 13:36: 9 sparks for the last 5 min.

Friday, November 13, 2015, 13:45: Spark rate reduced, but multiple sparks encountered again at 20.5 kV. Reduced back to 20 kV

Friday, November 13, 2015, 13:50: Increased sparking at 20 kV. Had to lower to 18 kV

Friday, November 13, 2015, 14:07: Back at 20 kV

Friday, November 13, 2015, 14:13: BIAS and EL off


Monday, November 16, 2015, 08:18: Fault on chiller. Reset chiller unit on the roof.

Entry  Monday, November 09, 2015, 16:47, Anders Mjos, Conditioning Station, Maintenance, TM3, FEBIAD Test Target, Leak check of Service Cap 

Service cap leak checked this afternoon. Found multiple leaks of 10E-8 to 10E-7 range. Connected to the backing line with IG1 at ~4E-6 T, CG1A around 40 mT. Got responses around large round flange on top, rectangular side panels, water f/t on GND and water f/t on HV. Will resume leak checking tomorrow to attempt to pinpoint sources of leak more accurately.

Entry  Friday, November 06, 2015, 14:44, Anders Mjos, Conditioning Station, Repair, TM3, , O-rings replaced on service cap 

O-rings were replaced on the service cap by Anders, Maico, Aurelia and Keith under work permit  I2015-11-05-5    


 

 One of the wires for the steerers had come loose and was reattached by Maico. Photo on DocuShare

 

 

 

 

 

 

 

 

 

 

 

 

 

 

 

 

Entry  Thursday, November 05, 2015, 09:57, Travis Cave, Conditioning Station, Maintenance, TM3, no target, Module moved 

TM#3 has been moved from the north west silo to the conditioning station.

Entry  Thursday, October 29, 2015, 13:59, Travis Cave, Spent Target Vault, Standard Operation, , , Filling F-308s 

Five F-308s have been filled with the spent targets. The F-308s have been moved to the hall way between the north and south hot cell areas.

Entry  Friday, October 23, 2015, 11:40, Travis Cave, Spent Target Vault, Standard Operation, , ZrC #7, Spent target moved Vault_Storage_October_23_2015.pdf

The spent ZrC#7 target has been moved from the south hot cell to the spent target vault. The target was placed in pail #129 and then placed in slot 3B of the vault, it was 157mSv/hr upon removal from the south hot cell.

Entry  Friday, October 23, 2015, 11:30, chad fisher, South Hot-Cell, Standard Operation, , ZrC#7, ZrC#7 Spent Move and Febiad Coil 

ZrC#7 was transfered to a spent target disposal pail today and removed from the hot cell. The "hot" end of the TM4 coil end was also disposed of in the same pail (#129)

Entry  Friday, October 23, 2015, 07:41, Dan McDonald, Spent Target Vault, Maintenance, , , F-308's 

Six F-308's where received from Nordion #6,#15,#13,#16 all contained contamination. Loose contamination was removed with some fixed contamination remaining levels are low enough to allow the transport of spent targets. flasks where serviced as per Nordion Document IS/PP 0009 F308, IS/PP 0981 F308. Flasks are now located in the north hot cell area.

Entry  Wednesday, October 21, 2015, 11:58, Anders Mjos, South Hot-Cell, Development, TM2, ZrC#7, Extraction Electrode inspection 

The failed extraction electrode was inspected in the hot cell this morning by Anders and Chad. The following electrical measurements were taken

  • EE on target assembly as recieved from TM after online operation. 14 Ohm
  • EE removed from target assembly and placed on conductive flat surface. ~1 G-Ohm at 1kV
  • EE installed back onto target assembly (fasteners not tightened).~ 0.8 G-Ohm at 1 kV

There was some material deposited on the EE. Some of which has fallen off - possibly during removal of the electrode from the target assembly. It seems the cause of the short was material build up between plasma electrode and extraction electrode. See photos.

The heat shield lid was removed after lunch. This revealed a broken target. The target may have broken after operation (in hot cell).

Photos are available on DocuShare

 

Entry  Wednesday, October 21, 2015, 09:49, chad fisher, South Hot-Cell, Repair, , , Manipulator handle repair 

Rebuild handle of manipulator serial 7986 (currently in the east position) and replaced broken snap ring 5555-18h on west side of the handle underneath motion switch.

Entry  Tuesday, October 20, 2015, 13:52, chad fisher, South Hot-Cell, Maintenance, , , TM4 Febiad coil line disposal 20151020_133045.jpg20151020_134303.jpg

The febiad coil line removed from TM4 has been cut into pieces small enough to be disposed of in a 5 gal pal. The line was cut with a Ridgid Model 104 manual pipe cutter (using the manipulators of course).

This pieces constitute the bulk of the field in the hot cell and will be disposed of with the next spent target.

Entry  Tuesday, October 20, 2015, 12:49, Dan McDonald, ITW, Standard Operation, , SiC#32, Tm2 hook up In ITW 

Lower and disconnect TM2 from crane in ITW, proceed with hooking up TM2 as per checklist with Anders. Double check flow meters and coils, reset TP1 and TP2

Entry  Tuesday, October 20, 2015, 10:18, Travis Cave, ITW, Standard Operation, TM2, SiC#32, Module moved 

TM#2 with SiC#32 has been moved from the south hot cell to the west target station.

Entry  Monday, October 19, 2015, 15:52, Anders Mjos, South Hot-Cell, Standard Operation, TM2, SiC#32, Electrical and leak check ITW-TM2-SiC#32-HP-FEBIAD_Electrical_Check_SHC_(pre).pdf

 An electrical check was completed by Travis C and Anders M. Note ~250 kOhm between Target and 60 kV common. Leak check was done by Dan M and Chad F on HS and Window circuits. No leaks found

Entry  Monday, October 19, 2015, 11:53, chad fisher, South Hot-Cell, Standard Operation, TM2, SiC#32, SiC#32 installed on TM2 

SiC#32 has been installed on TM2. High current fasteners torqued to 130 in lbs.

Entry  Thursday, October 15, 2015, 14:17, chad fisher, South Hot-Cell, Repair, TM2, , Anode Connector Install and adjustment 20151015_085914.jpg

The TM2 containment box was removed this morning for installation of the 9 pin connector...connection.

The 9 pin connector copper tube connection was made and Anders advised on routing of the cable to the banana plug water block connection.

Short was diagnosed (short disappeared when water block was pushed slightly towards center of module) and thicker Ultem spacer installed and tested again. All good.

Entry  Thursday, October 15, 2015, 08:07, David Wang, South Hot-Cell, Standard Operation, TM2, no target, TM2 no target electrical check at SHC. TM2_electrical_check_2015-10-16_no_target.pdf

I did a TM2 no target electrical check at SHC this morning. A to RU at 500v  is 250K which is low.   anode- x pin is dead short to 60kv bias. RU is dead short to 60kv bias( as before).   see attachment

Entry  Wednesday, October 14, 2015, 14:49, David Wang, South Hot-Cell, Standard Operation, TM2, , Install new high current cables to TM2 TM2_Febiad_High_current_cables_047.JPGTM2_Febiad_High_current_cables_048.JPGTM2_Febiad_High_current_cables_049.JPG

I installed a set of new high current cables for TM2 Febiad run. The top of TM2  is configured to Febiad mode. See attachments

Entry  Wednesday, October 14, 2015, 14:03, chad fisher, South Hot-Cell, Standard Operation, TM2, ZrC#7, ZrC#7 removed 20151014_134022.jpg20151014_135127.jpg

ZrC#7 has been removed from TM2. Everything looks good.

Entry  Wednesday, October 14, 2015, 12:48, David Wang, South Hot-Cell, Standard Operation, TM2, ZrC#7, TM2 ZrC#7 after run electrical check at SHC. ZrC_#7_after_run_electrical_check.pdf

I did an electrical check on TM2 with ZrC #7 on it. The EE is short to 60KV bias. See attachment

Entry  Wednesday, October 14, 2015, 12:44, David Wang, ITW, Standard Operation, TM2, ZrC#7, TM2 has been moved from ITW to SHC 

Bill and I remotely removed TM2 from ITW to SHC. The move is smooth.

Entry  Wednesday, October 14, 2015, 12:42, David Wang, ITW, Standard Operation, TM2, ZrC#7, TM2 has been disconnected in ITW  

Dan and I disconnected TM2 in ITW this morning.

Entry  Tuesday, October 13, 2015, 10:53, David Wang, Conditioning Station, Standard Operation, , , Target Hall schedule from Sep 08th 2015 to Dec 25th 2015 Target_Hall_Scheduled_Activities__Sep_09_to_Dec_30.mppTarget_Hall_Scheduled_Activities__Sep_09_to_Dec_30.pdfTarget_Hall_Scheduled_Activities__Sep_09_to_Dec_30.pdfTarget_Hall_Scheduled_Activities__Sep_09_to_Dec_30.mpp

Weekly update schedule. TM3 evaluation schedule in Nov is added.  

update the schedule after  the cancellation of TM2 from SHC to CS trip.see attachments 3,4

Entry  Thursday, October 08, 2015, 14:08, David Wang, South Hot-Cell, Standard Operation, TM3, Dummy target febiad., TM3 has been moved from SHC to NW silo 

Bill and I moved TM3 from SHC to NW silo with a dummy febiad target installed on it. The move is smooth.

Entry  Tuesday, October 06, 2015, 21:12, Aurelia Laxdal, South Hot-Cell, Repair, TM3, , TM3 service cap inspection in target hall Pic1.jpg

David Wang and I did the service cap inspection in target hall: see WP I2015-10-06-10.<br>

Signs of sparking were seen underneath 3 insulators: E ("Cavity"), A ("Oven+") and B ("Oven -") at the pair water lines coming out of the  feed-through and going to the HV chase. Specifically one water line of E is very close to the feed-through insulator (2-3mm gap) and here the sparking sings are more prominent: see picture.

Entry  Tuesday, October 06, 2015, 13:25, David Wang, ITE, Standard Operation, TM4, , Target Hall schedule from Sep 08th 2015 to Dec 25th 2015 Target_Hall_Scheduled_Activities__Sep_09_to_Dec_30.mppTarget_Hall_Scheduled_Activities__Sep_09_to_Dec_30.pdf

Weekly update target hall schedule. See attachment 1,2.

Entry  Tuesday, October 06, 2015, 13:00, David Wang, ITE, Repair, TM4, , spark on top of TM4 in ITE 

During the weekend condition The TM4 spark at 30KV without vacuum response. It is confirmed the spark is from the top TM4 this morning.The flexible cables in a  black wire sleeve which is used for febiad X pin connection drooped too close to the TM4 surface plate, and caused the sparking. The problem is fixed by Anders and David. The cables is put back where it should stay.  After test, no sparking on the top.

Entry  Tuesday, October 06, 2015, 12:50, David Wang, ITE, Standard Operation, TM4, Ta#46, 5 Shielding blocks have been transferred from ITW to ITE. 

The ITE is configured to take proton beam.

Entry  Tuesday, October 06, 2015, 12:50, David Wang, ITE, Standard Operation, TM4, Ta#46, 5 Shielding blocks have been transferred from ITW to ITE. 

The ITE is configured to take proton beam.

Entry  Monday, October 05, 2015, 10:19, Anders Mjos, Conditioning Station, Maintenance, , , Chiller maintenance 

 will be performed Tuesday October 6th

Tuesday, October 06, 2015: Maintenance re-schedlued for Wednesday October 7th

Entry  Thursday, October 01, 2015, 09:18, Travis Cave, Spent Target Vault, Standard Operation, , , Targets transfered to mini storage. 

In preparation for shipping of the spent targets five have been moved to the mini storage. The following target were moved to the mini storage, SiC#26, Ta#36, UC#9,10,11.

Entry  Wednesday, September 30, 2015, 11:14, Travis Cave, South Hot-Cell, Repair, TM3, no target, Electrical Check TM3_elecchk_notgt_shc.PDF

TM#3 electrical check at the south hot cell, no target, all value are done at 1000Volts. See the attached PDF for the results.

Entry  Wednesday, September 30, 2015, 08:50, Travis Cave, South Hot-Cell, Maintenance, TM3, no target, Module moved 

TM#3 is in the south hot cell it was moved from the north west silo.

Entry  Tuesday, September 29, 2015, 12:31, David Wang, ITE, Standard Operation, TM4, Ta#46, TM4 has been connected in ITE 

Dan and I connected TM4 in ITE. The turbo- pumps are started. Water supply to TM4 only at this stage. Everything is good so far.

Entry  Tuesday, September 29, 2015, 09:38, Travis Cave, ITE, Standard Operation, TM4, Ta#46, Module moved 

TM#4 with Ta#46 has been moved to ITE from the conditioning station.

Entry  Monday, September 28, 2015, 10:10, David Wang, Conditioning Station, Standard Operation, TM4, Ta#46, Switched off CS vacuum pumps and water system 

I switched off CS vacuum pumps and water system after Isac opps finished the TM4 conditioning at CS.

Entry  Friday, September 25, 2015, 08:21, Travis Cave, South Hot-Cell, Standard Operation, , UC#13, Spent Target move Vault_Storage_September_24_2015.pdf

The spent UC#13 target has been moved from the south hot cell to the ISAC spent target vault. It was placed pail #128 and in tray spot 1A. It was 21.5mSv/hr upon removal from the hot cell. See attached PDF for details.

Entry  Friday, September 25, 2015, 07:56, David Wang, Conditioning Station, Standard Operation, , , Target Hall schedule from Sep 08th 2015 to Dec 25th 2015 Target_Hall_Scheduled_Activities__Sep_09_to_Dec_30.pdfTarget_Hall_Scheduled_Activities__Sep_09_to_Dec_30.mpp

weekly update see attachment

Entry  Thursday, September 24, 2015, 14:59, Friedhelm Ames, Conditioning Station, Standard Operation, TM4, Ta#46, start high voltage conditioning 
 
Entry  Thursday, September 24, 2015, 07:00, David Wang, Conditioning Station, Maintenance, TM4, Ta#46, Turned off TCS all vacuum pumps and water pumps. 

TCS:MP1 back up pressure went up too high (700mtorr).I turned off all the pumps.The TCS is under vacuum still. TCS water  package cooling fans showed error on control page.The water pumps are stopped  also.

Restarted the vacuum pumps 40 minutes after stopping. Everything is back to normal. The MP1 back up pressure need to be monitored frequently before we have a final solution on this issue.

Reset the CS cooling package on roof and restarted the water  pumps. The system is running good so far.

Entry  Wednesday, September 23, 2015, 14:35, David Wang, Conditioning Station, Standard Operation, TM4, Ta#46, TM4 has been connected at CS 

TM4 has been connected at CS. Turbo- pumps and water system are started and running . The HV cover has been installed on the module. Everything is good so far.

Entry  Wednesday, September 23, 2015, 14:32, David Wang, Conditioning Station, Standard Operation, TM4, Ta#45, Helium pressure test on TM4 HS line at CS 

Helium pressure test HS line at CS with 70 psi for 2 minutes. Base  leak rate 0.0xE-9atm.cc/sec. No response. The line is leak tight.

Entry  Wednesday, September 23, 2015, 13:56, Travis Cave, Conditioning Station, Standard Operation, TM4, Ta#46, Electrical Check TM4Ta46elecchkCS.PDF

TM#4 electrical check at the conditioning station with Ta#46 target.

Entry  Wednesday, September 23, 2015, 08:38, Travis Cave, Conditioning Station, Standard Operation, TM4, Ta#46, Module moved 

TM#4 with Ta#46 has been moved from the south hot cell to the conditioning station.

Entry  Tuesday, September 22, 2015, 13:15, David Wang, South Hot-Cell, Standard Operation, , Ta#46, Leak check on TM4 HS water line with new Ta#46 target. at SHC 

Chad and I leak checked the HS line at SHC. No leak. Leak rate 0.0xE-9atm.cc/sec.

Entry  Tuesday, September 22, 2015, 11:39, Travis Cave, South Hot-Cell, Standard Operation, TM4, Ta#46, Electrical Check TM4Ta46elecchkSHC.PDF

TM#4 electrical check with Ta#46 attached.

Entry  Tuesday, September 22, 2015, 11:35, Travis Cave, South Hot-Cell, Standard Operation, TM4, UC#13, Electrical Check TM4elecchkUC13postbeamSHC.PDFTM4_elecchk_totgt_with_IGLISline.PDF

TM#4 with UC#13 post beam electrical check. Also and electrical check was done without the target on.

Entry  Tuesday, September 22, 2015, 11:12, Travis Cave, ITE, Standard Operation, TM4, UC#13, Module moved 

TM#4 with UC#13 has been moved from the east target station to the south hot cell.

Entry  Thursday, September 17, 2015, 11:50, David Wang, Spent Target Vault, Repair, TM1, , TM1 window circuit leak check TM1_leak_soldering_stems_001.JPGTM1_leak_soldering_stems_003.JPG

 Leak check TM1 window circuit soldering stems inside service cap when module is located at NE silo. LD base LR 0.0xE-9atm.cc/sec.  Only 1 second tiny amount  helium sprayed on stems soldering joints . LD got a quick response to high E-7 atm.cc/sec.Test is repeated again with same result.  See attachments

Entry  Thursday, September 17, 2015, 09:01, Travis Cave, South Hot-Cell, Standard Operation, TM1, no target, Module moved 

TM#1 has been moved from the south hot cell to the north east silo.

Entry  Tuesday, September 15, 2015, 11:06, chad fisher, South Hot-Cell, Repair, TM1, , TM1 Window Gasket Replacement 

Replaced the custom silver gaskets on the entrance window panel of TM1 this morning...this has eliminated an sign of leak at this joint, however there appears to still be a leak somewhere...a good distance from the vcr joints of the window as we are getting a drift response.

Chad sprayed helium to soldering stems in containment box which we suspected with leak last week. With 1second click  on helium, after 80 seconds waiting time , the LD started to show leak up to 3xe-9atm.cc/sec.

Chad sprayed helium close to service tray and vacuum chase. with 1second click on helium , after 30 seconds waiting time, the LD started to show leak up to 2Xe-8 atm.cc/sec.

After this test, we knew the leak is somewhere in service tray or service cap, but not the soldering stems in containment box we suspected before.The further investigation is needed.

Entry  Tuesday, September 15, 2015, 08:24, David Wang, South Hot-Cell, Repair, TM1, UCx 13, Leak check on TM1 window circuit soldering stems in service cap. 

I did a leak check on TM1 window circuit  2 soldering  stems in service cap.The round side panel was opened for the job. I sprayed helium on the stems for 10 seconds. The leak detector got a tiny response(from 0.0xE-9 atm.cc/sec to 2.0xE-9 atm.cc/sec). The test  repeated again. The second time, LD climbed  to 1.2xE-9atm.cc/sec. It looks like there is a very tiny leak on the stems soldering spots. But , this is not the same leak we found from SHC helium spray which LD climbed to 1.4xE-8atm.cc/sec with only one click helium spray by Chad.

 Because of the high air flow at SHC when the round panel is removed, The result is not conclusive. The same test is done at silo without  airflow. We found a big leak on this soldering stems . See later e-log.

Entry  Friday, September 11, 2015, 14:31, Anders Mjos, Conditioning Station, Maintenance, TM2, ZrC#7, Vacuum gauge and EPICS read back calibration 

The corelation betwenn the local value on the gauge controllers and the read back valiues in EPICS was compared. Data can be found in a previous  e-log

Entry  Thursday, September 10, 2015, 08:59, chad fisher, South Hot-Cell, Repair, , , Manipulator Mait. and field check Sept. 4 

Hot cell was entered for preventative mait. on left manip. field measurements around the cell were taken in prep. for window removal in January and left/south light bulb changed.

Hottest item in the cell was the conductor block end of the TM4 febiad coil line. It was 70 mSv/H on contact and seemed to be the major source of field in the hot cell. The waterblock end of this line did not apper to be hot.

Entry  Thursday, September 10, 2015, 08:55, chad fisher, South Hot-Cell, Repair, TM1, , TM1 Window Leak Diag. P0000122.JPG

Vacuum leak check on the window line circuit of TM1 took place yesterday and again to confirm this morning. Both days the response to helium is in the area of a soldered reduction fitting at the top of the containment box above and to the shutter side of the extraction column (see attached picture). To verify this morning each joint in the system had a 1 second shot of helium and then timed for 1 minute to wait for a response. This area responded both times tested at about 40 seconds...no response at any of the other locations.

Entry  Wednesday, September 09, 2015, 09:59, Travis Cave, South Hot-Cell, Standard Operation, TM1, no target, Module moved 

TM#1 has been moved from the south west silo to the south hot cell.

Entry  Tuesday, September 08, 2015, 10:11, David Wang, ITW, Standard Operation, TM2, ZrC, 5 Shielding blocks have been transferred from ITE to ITW. 

Maico and Dan moved 5 shielding blocks from ITE to ITW. The ITW is configured to take proton beam.

Entry  Wednesday, September 02, 2015, 09:26, David Wang, ITE, Standard Operation, , , Target Hall schedule from Sep 08th 2015 to Dec 25th 2015 Target_Hall_shedule_129_Sep_to_Dec.xlsxTarget_Hall_Scheduled_Activities__Sep_09_to_Dec_30.pdfTarget_Hall_Scheduled_Activities__Sep_09_to_Dec_30.mppTarget_Hall_Scheduled_Activities__Sep_09_to_Dec_30.pdfTarget_Hall_Scheduled_Activities__Sep_09_to_Dec_30.mpp

I attach new Target Hall schedules here for 2015 fall and winter runs (beam schedule 129). The TH excel sheet schedule for beam 129 is included also.

Weekly update of Target Hall Schedule.See Attachments 3,4

Entry  Tuesday, September 01, 2015, 16:55, Anders Mjos, Conditioning Station, Maintenance, , , TBHT power supply remvoed 

 The power supply is needed as a spare for the failed TGHT p/s in ITW

Entry  Tuesday, September 01, 2015, 16:03, Grant Minor, ITW, Standard Operation, TM2, ZrC #7, Photos of TM2 Connection Procedure on Docushare 1Sept2015 

https://documents.triumf.ca/docushare/dsweb/View/Collection-15323

Entry  Tuesday, September 01, 2015, 14:54, David Wang, ITW, Standard Operation, TM2, , TM2 has been connectec in ITW. 

TM2 has been connected in ITW. During the connection, Anders and I  found the TM2  high current cables used in ITE and CS are short in ITW.  Anders and Grant found the original TM2 ITE high current cables in target hall. We replaced them. They works fine. But, a little bit longer on cable length would be easy to connect them. All other connections and HV cover in ITW work for the TM2 so far.

Entry  Tuesday, September 01, 2015, 10:38, David Wang, ITW, Maintenance, TM2, , ITW top tank flange clean up and r-ring replacement. ITW_o-ring_replacement_2015-09-01_008.JPGITW_o-ring_replacement_2015-09-01_007.JPGITW_o-ring_replacement_2015-09-01_006.JPG

During last run, ITW dump circuit had a water leak on an adaptor below the pressure gauge. The top tank flange, slot, and O-ring were water contaminated by the leak. I removed the old o- ring, cleaned up the flange and o-ring slot, and put a new o-ring into the flange. Some  pictures will be attached in this mail later.

Entry  Tuesday, September 01, 2015, 10:32, Travis Cave, ITW, Standard Operation, TM2, ZrC #7, Module moved 

TM#2 with ZrC#7 has been moved from the conditioning station  to the west target station.

Entry  Tuesday, September 01, 2015, 06:25, David Wang, Conditioning Station, Standard Operation, TM2, ZrC, Argon venting TM2 at CS 

Argon venting TM2 at CS.

Entry  Thursday, August 27, 2015, 10:10, Anders Mjos, Conditioning Station, Standard Operation, TM2, ZrC#7, Conditioning new Source Tray 2015-08-31_Service_Cap_Sparking_on_Rubber_Plug.pdfTM2_Source_Tray_with_ZrC#7.docxVacuum_gague_calibration.xlsx

Thursday, August 27, 2015, 10:10: Started water system. TK2 level reduced from 24.9 to 23.5 in. 

IG2 not working. Force is ON.


EE in conditioning mode.

 Friday, August 28, 2015, 08:39: BIAS/EL 10 / 5 kV

Friday, August 28, 2015, 08:49: BIAS/EL 20 / 10 kV

Friday, August 28, 2015, 09:18 BIAS OFF. Ramping to 200/100 A at 2/1 A/min

Friday, August 28, 2015, 15:46: Target at 76 / 38 A. Changed ramping to 100/40 at 1/0.5 A/min

Friday, August 28, 2015, 22:20: Ramping down heaters.


Saturday, August 29, 2015, 09:50: RGA off. PNG1 7.85E-6 / 5.0E-6 T (EPICS / local)

Saturday, August 29, 2015, 10:11: BIAS/EL 20 / 10 kV

Saturday, August 29, 2015, 10:28: BIAS/EL 30 / 15 kV. Some sparking around 29 kV

Saturday, August 29, 2015, 10:43: 10 min w/o sparking

Saturday, August 29, 2015, 10:55: BIAS/EL 32 / 15 kV. Small vacuum responses for every 100 V increase

Saturday, August 29, 2015, 11:03: Sparking at 33 kV

Saturday, August 29, 2015, 11:12: BIAS/EL 34 / 15 kV

Saturday, August 29, 2015, 14:22: Power has returned after site-wide power outage, but no communication with IOC yet.

Saturday, August 29, 2015, 15:13: IOC restarted.

Saturday, August 29, 2015, 15:14: Starting turbos

Saturday, August 29, 2015, 15:22: Turbos at speed.

Saturday, August 29, 2015, 15:22 : MP3 not running. Investigating

Saturday, August 29, 2015, 15:47: Reset MP3 breaker (wait 5 min for capacitors to empty)

Saturday, August 29, 2015, 15:48: Water system running


Sunday, August 30, 2015, 09:38: BIAS/EL 10 / 5 kV

Sunday, August 30, 2015, 09:54: BIAS/EL 20 / 10 kV 

Sunday, August 30, 2015, 10:01: BIAS/EL 30 / 15 kV 

Sunday, August 30, 2015, 10:12: No sparking

Sunday, August 30, 2015, 10:27: BIAS/EL 35 / 15 kV 

Sunday, August 30, 2015, 10:37: No sparking

 Sunday, August 30, 2015, 10:52:  BIAS/EL 37.5 / 15 kV 

Sunday, August 30, 2015, 11:00:  BIAS/EL 37.5 / 20 kV. No sparks

Sunday, August 30, 2015, 11:22:  BIAS/EL 40 / 20 kV 

Sunday, August 30, 2015, 11:34: No sparks

Sunday, August 30, 2015, 12:00: BIAS/EL 42 / 21 kV

Sunday, August 30, 2015, 12:32: Sparking at 43.5 kV. Tripped off PS on conductivity (spark response)

Sunday, August 30, 2015, 12:44:  BIAS/EL 40 / 20 kV. ISAC Ops will monitor over lunch

Sunday, August 30, 2015, 14:20: BIAS/EL 43 / 20 kV

Sunday, August 30, 2015, 14:41: Sparking at 43.5 kV. lowered to 43 kV

Sunday, August 30, 2015, 15:56: Sparking every 5-10 min at 43.4 kV not able to increase to 43.5 kV. Sparking is causing signal response on water conductivity and drop in IG1 and IG1S readings during sparking.


Monday, August 31, 2015, 08:33: BIAS/ EL to 40 / 20 kV in 9 min w/o any sparking

Monday, August 31, 2015, 08:44: No sparking

 Monday, August 31, 2015, 08:46: BIAS/ EL to 42 / 20 kV

Monday, August 31, 2015, 08:53: BIAS/EL 43 / 20 kV. Two vacuum/current responses

Monday, August 31, 2015, 09:47: BIAS off to investigate spakring.

David observed sparking coming from under the HV cover on TM2 twice. When the cover was removed, spark marks on a rubber plug for the water lines was observed. The plug with marks and one more plug was removed from the service cap as it is not used. See attached PDF.

Monday, August 31, 2015, 10:09: BIAS/ EL to 40 / 20 kV in 8 min w/o any sparking

Monday, August 31, 2015, 10:15 BIAS/EL 43.5 / 22 kV. One small spark

Monday, August 31, 2015, 10:30: No sparks

Monday, August 31, 2015, 10:35: BIAS/EL 44 / 22 kV.

Monday, August 31, 2015, 11:00: BIAS/EL 45 / 22 kV.

Monday, August 31, 2015, 11:31: PNG1 taken out by a spark

Monday, August 31, 2015, 12:04: Reset power to PNG1 controller. PNG1 back online.

Monday, August 31, 2015, 12:25: BIAS tripped on IG1 after a spark at 47.1 kV

Monday, August 31, 2015, 12:39: BIAS/EL 47 / 24 kV. No sparks for 5 min

Monday, August 31, 2015, 12:54: PNG1 taken out by spark at 47.7 kV

Monday, August 31, 2015, 13:02: BIAS/EL 48 / 24 kV

Monday, August 31, 2015, 13:07: No sparks

Monday, August 31, 2015, 13:25: BIAS/EL 49 / 24 kV

Monday, August 31, 2015, 13:30: No sparks

Monday, August 31, 2015, 13:37: PNG1 returned after a spark

Monday, August 31, 2015, 14:06: BIAS/EL 50 / 25 kV

Monday, August 31, 2015, 14:45: No sparks.

Monday, August 31, 2015, 15:15: BIAS/EL 51 / 25 kV

Monday, August 31, 2015, 15:38: BIAS/EL 51 / 30 kV

Monday, August 31, 2015, 16:01: Tested XCB0 and YCB0 to 5 kV. Some sparking. Tested CCB0 to 4 kV. No sparking.

Monday, August 31, 2015, 16:50: No sparks for 1 hour at 51 / 30 kV.

Monday, August 31, 2015, 17:00: HV off.

 Monday, August 31, 2015, 17:07: EE at 2 kV, R= 1 MOhm

Monday, August 31, 2015, 17:08 : EE off.

Monday, August 31, 2015, 17:10: Water off.

Monday, August 31, 2015, 17:12 : Vacuum gauges off. Turbos off. Roughing pump off.

Entry  Thursday, August 27, 2015, 08:43, Travis Cave, Conditioning Station, Standard Operation, TM2, ZrC #7, Electrical Check TM2_elec_chk_ZrC7_CS.PDF

Electrical check of TM#2 at the conditioning station under vacuum. The resistance value of the target to 60kV common is a bit lower then what it was at the south hot cell.

Entry  Wednesday, August 26, 2015, 14:52, David Wang, Conditioning Station, Standard Operation, TM2, ZrC, Helium pressure test on TM2 HS and window lines at CS 

LD base LR 0.0xE-9 atm.cc/sec , 80 psi helium 2 minutes on HS and window circuits. No leak. Also, the reinstalled(after rewiring job) TP2 and PNG1(steers) side panel have been leak checked. No leak.

Entry  Wednesday, August 26, 2015, 14:30, David Wang, Conditioning Station, Standard Operation, TM2, ZrC, TM2 and Cs vacuum sysyem has been connected at CS. 

Turbo-pumps are started . The pumping down is good so far.

Entry  Wednesday, August 26, 2015, 14:28, David Wang, Conditioning Station, Standard Operation, TM2, ZrC, Leak check on TM2 HS and windowwater line with new ZrC target at SHC 

Chad and I leak checked TM2 HS and window circuit VCR joints with ZrC target and containment box installed at SHC. No leak has been found. They will   be helium pressurized  at CS later.

Entry  Wednesday, August 26, 2015, 11:12, Travis Cave, Conditioning Station, Standard Operation, TM2, ZrC #7, Module moved 

TM#2 with ZrC#7 has been moved to the conditioning station from the south hot cell.

Entry  Wednesday, August 26, 2015, 10:55, chad fisher, South Hot-Cell, Repair, TM2, ZrC#7, New wiring and target 20150826_090047.jpg

New wiring was installed yesterday as well as ZrC#7 which had its high current fasteners torqued to 130 in lbs.

 

Entry  Wednesday, August 26, 2015, 09:54, Anders Mjos, Conditioning Station, Maintenance, , , Topped up water in TCS:TK2 

 Filled to 24.9 in

Entry  Wednesday, August 26, 2015, 09:20, Travis Cave, South Hot-Cell, Standard Operation, TM2, ZrC #7, Electrical Check TM2_elec_chk_ZrC7_SHC.PDF

Electrical check of TM#2 with ZrC #7 installed

Entry  Tuesday, August 25, 2015, 13:54, Grant Minor, South Hot-Cell, Repair, TM2, ZrC#7, TM2 - Electrical / HV Short Repair and Current Status (ZrC target) TM2_Loose_Wires_Touching_Febiad_Gas_Line_notes_21Aug2015.jpgTM2_Wire_Bundle_Clear_of_Febiad_Gas_Line_notes_25Aug2015.jpg

Hello all,

TM2's first performance in the Conditioning Station with the new source tray was not great, with sparking and HV degradation beginning to occur at 30kV:
https://elog.triumf.ca/TIS/RH-ISAC/1039

This is perplexing, because the module without the source tray performed well at the TCS:
https://elog.triumf.ca/TIS/RH-ISAC/829

AND the new source tray performed well at the test stand (i.e. not inside the module):
https://elog.triumf.ca/TIS/Test-Stand/447

Upon inspection back at the Hot Cell last week after the failure, David Wang was observant enough to notice that one of the steerer coax wires (ground plane) was essentially touching one of the FEBIAD gas lines (HV plane) in the new source tray installation (photo attached).  Closer inspection by a group consisting of Anders, Alex, and myself revealed some apparent tracking and damage to the wire sheath.
https://elog.triumf.ca/TIS/RH-ISAC/1045

We believed at this point that the bad HV performance of TM2 was due to this problem.  The wires were originally arranged loose as it was believed it would be easier to install them in the Hot Cell this way.  However, it turned out to be a bad decision, as the wires at ground ended up becoming stray and touching the HV surface.

To correct the problem, the old wires were removed, and a new steere wire bundle was made using a PEEK material sheath.  This new sheath bundle was installed over the last day or so.  The penning gauge wire was kept separate from the steerer wire bundle.  You can see the new wire bundle and penning gauge wire in the attached photo, now with a healthy clearance to the FEBIAD gas lines.

Chad has been instructed to re-install the Einzel lens wire, install the new ZrC target, and replace the containment box in preparation for transport back to the TCS for another HV test.  If anybody would like to see the source tray today before ~3pm, I have asked Chad to wait for my final OK to put the containment box back on the module.

I apologize for this problem.  We are hopeful the solution we have installed will improve the HV performance.  Much work over the last 2+ years was put into building and installing this source tray by many contributors inside and outside of Remote Handling, and we want this module to succeed more than anybody!

Thanks and best regards,

Grant

Entry  Friday, August 21, 2015, 11:38, Anders Mjos, South Hot-Cell, Repair, TM2, FEBIAD Test Target, Steerer wires found to be touching the gas lines 

Yesterday TM2 was inspected in the SHC. Spark marks were found both on the steerer wires and on the ANODE wire. The steerer wires (GND)  were touching the gas lines (60kV). This is likely the cause of the sparking observed at the Conditioning Station (e-log).

Photos are available on DocuShare

Entry  Thursday, August 20, 2015, 13:48, David Wang, Conditioning Station, Standard Operation, TM2, , Target Hall Scheduled Activities April 07 - Sep 08 2015 Target_Hall_Scheduled_Activities__Apr_07_to_Sep_08.pdfTarget_Hall_Scheduled_Activities__Apr_07_to_Sep_08.mppTarget_Hall_Scheduled_Activities__Apr_07_to_Sep_08.mppTarget_Hall_Scheduled_Activities__Apr_07_to_Sep_08.pdf

 Weekly update target hall schedule.See attachment 1,2

Spring and summer run is close to the end. This will be the last update on this old schedule. See attachment3,4.    A new schedule for TH activities after mini shut down will be posted next time.

Entry  Thursday, August 20, 2015, 11:00, Travis Cave, Conditioning Station, Standard Operation, TM2, Dummy Target, Electrical Check TM2_elecchkdummytgtatCS.PDF

TM#2 electrical check at the conditioning station. All pumps were off but the module was not vented.

Entry  Thursday, August 20, 2015, 10:15, Travis Cave, South Hot-Cell, Standard Operation, TM2, Dummy Target, Module moved 

TM#2 is now in the south hot cell.

Entry  Thursday, August 20, 2015, 09:38, David Wang, Conditioning Station, Repair, TM2, , TM2 was disconnected at CS 

TM2 was disconnected at CS. Travis and I did  electrical check before the venting. After,The module was vented and moved to SHC. The moving is smooth.

Entry  Wednesday, August 19, 2015, 14:52, David Wang, Conditioning Station, Repair, TM2, , TM2 at CS 

During the TM2 HV test at CS, It failed. In order to confirm there is no any water leak inside the module after the heaters and beam extraction test, I disconnected all the water lines on the TM2, and purged the water lines with pressure air. Leak detector was reconnected back to the TM2 service cap, and all water lines are pressurized with 80psi helium again each for 2 minutes.No any leak had been found during the test. All the water lines are still perfectly sealed. Also, I checked all the vacuum to air seals on the top of the module.They are good either.  Anders used the RGA  tracking the helium during the test. No leak.

Entry  Monday, August 17, 2015, 10:44, Anders Mjos, Conditioning Station, Development, TM2, LP-FEBIAD Test Target (empty), Conditioning TM2 Source Tray with FEBIAD test target FirstBeamTM2SourceTray2015-08-17.pngTM2_Source_Tray_with_FEBIAD_test_target.docx

TGHT, TBHT, ANODE and COIL power tested (some amps/volts)

Monday, August 17, 2015, 10:43: BIAS/EL/EE to 15/7.5/1.5 kV

Monday, August 17, 2015, 10:45 : COIL 20A, ANODE 200V

Keiko fixed the auto-ramping program and access rights to it.

Monday, August 17, 2015, 13:06: Auto-ramping at 2/1 A/min. Good/bad vacuum at 6E-6 and 8E-6 T

Monday, August 17, 2015, 13:24 : ANODE current limit set incorrectly. Corrected and 200V (9 mA)

Monday, August 17, 2015, 15:28: COIL to 50 A

Monday, August 17, 2015, 15:43: Reduced ANODE to 100 V

Monday, August 17, 2015, 16:56 : Increased EL to 8.3 kV to increase FC current.

Monday, August 17, 2015, 17:04 : FC0 current at 1.5E-8 A

Beam ionized and accelerated on the new TM2 source tray

Monday, August 17, 2015, 17:12 : TGHT / TBHT at 500 / 250 A. Will leave over night to outgas. ISAC ops are monitoring the source.


Tuesday, August 18, 2015, 08:07: Everything stable overnight. Continue ramping heaters.

Tuesday, August 18, 2015, 08:48: TBHT voltage limited by EPICS (hardcoded) at 273 A.

TGHT/TBHT at 600 / 273 A 

Tuesday, August 18, 2015, 09:52: Adjusted COIL current down to 0 and back up. Response seen on FC0.

Tuesday, August 18, 2015, 22:29 : Starting cool down.


 Wednesday, August 19, 2015, 08:26: Source and HV off. EE configured to conditioning mode. RGA off.

Wednesday, August 19, 2015, 08:42: BIAS/EL at 15 / 7.5 kV. PNG1 at 3.5E-6 T, IG1 at 3.9E-7 T

Wednesday, August 19, 2015, 08:53: BIAS/EL 20 / 10 kV. 2 sparks.

Wednesday, August 19, 2015, 09:54: BIAS/EL 30 / 15 kV. Some sparking around 28 kV required BIAS voltage to be reduced momentarily. 

Wednesday, August 19, 2015, 10:04: Sparking at 30 kV. Reduced BIAS to 13 kV to get spar rate to less than 10/min

Wednesday, August 19, 2015, 10:19 : BIAS current limiting. Switch off BIAS and EL

Wednesday, August 19, 2015, 12:04: Water off for purging and leak test.

Wednesday, August 19, 2015, 12:52: Vacuum response observed while David was working on purging the water lines. This turned out to be when the valve to the leak detector was opened.

Entry  Friday, August 14, 2015, 10:00, David Wang, Conditioning Station, Repair, TM2, , Started CS water package for TM2  

I finished the rest TM2 connections to CS, and started CS cooling package. Everything works fine so far.

Entry  Thursday, August 13, 2015, 17:17, David Wang, Conditioning Station, Repair, TM2, Dummy target, TM2 at CS 

TM2 has been moved to CS. All turbo-pumps have been started. The pumping down is good so far.  I connected the leak detector to service cap, and finished the leak check today.  The LD base LR:0.0Xe-9atm.cc/sec. 80psi helium were applied to coil1, coil 2. HS and window circuits, each for 2minutes. No any response has been found on LD. So all water lines are leak tight now. I also sprayed   helium to top service cap checking all air to   vacuum seals. They are all good either. But, The new installed PGN1 does not work. Other thing need to mention is The TP2 is running at 2.45A which is 1A higher comparing to TP1. It need to be monitored to see if we have to replace it or not. The high current cables and water lines will be connected tomorrow morning.

Entry  Thursday, August 13, 2015, 14:36, Travis Cave, Conditioning Station, Standard Operation, TM2, Dummy Target, Module moved 

TM#2 with the dummy target has been moved to the conditioning station.

Entry  Thursday, August 13, 2015, 13:46, chad fisher, South Hot-Cell, Repair, TM2, , TM2 Status 

As previously mentioned, dump target installed with new mounting and high current fasteners.

Leak Check complete and ready to move to CS at 1:30

Entry  Thursday, August 13, 2015, 11:34, Travis Cave, South Hot-Cell, Standard Operation, TM2, Dummy Target, Electrical Check TM2_elechknotgtafterwidget.PDFTM2_elechknotgtshunt.PDFTM2_elecchkdummytgt.PDF

Electrical check of TM2 without target after that widget has installed, electrical check with the shunts on, electrical check with the dummy target installed.

Entry  Thursday, August 13, 2015, 09:17, chad fisher, South Hot-Cell, Repair, TM2, , TM2 status 20150811_132709.jpg20150813_083255.jpg20150813_090814.jpg

Tuesday, August 11,  insulator ITA6272 was installed onto the "pin x" line (unused plasma electrode) and tested; it seems to have successfully eliminated the shorts on that line.

Wednesday, August 12  "shunts" installed on tube heater and oven circuit and electrically  tested.

Thursday , August 13, dummy target installed.

 

Entry  Monday, August 10, 2015, 14:07, Isaac Earle, South Hot-Cell, Repair, TM2, , TM2 Containment Box Removed 

The containment box was taken off TM2 in preparation for installation of a new coil line isolator.

ITA6272 and ITA6273 have been received from the Scintillator Shop.  ITA6274 should be ready by the end of today.

Entry  Friday, August 07, 2015, 10:01, David Wang, ITE, Standard Operation, , , Target Hall Scheduled Activities April 07 - August 19 2015 Target_Hall_Scheduled_Activities__Apr_07_to_Aug_19.pdfTarget_Hall_Scheduled_Activities__Apr_07_to_Aug_19.mppTarget_Hall_Scheduled_Activities__Apr_07_to_Sep_08.mppTarget_Hall_Scheduled_Activities__Apr_07_to_Sep_08.pdf

Weekly update target hall schedule and activities. See attachment 1,2

Update and extend Target Hall schedule to Sep 08.  See attachment 3,4

Entry  Thursday, August 06, 2015, 11:40, Travis Cave, South Hot-Cell, Standard Operation, TM2, no target, Module moved 

TM#2 is now in the south hot cell

Entry  Thursday, August 06, 2015, 10:26, Travis Cave, Spent Target Vault, Standard Operation, , , Spent Target Measurments and Assays Vault_Storage_August_6_2015.pdf

All targets but one ( SiC#31 went in last week) have been measured or assayed. See attached PDF for the details.

Entry  Friday, July 31, 2015, 09:47, David Wang, ITE, Standard Operation, , , Target Hall Scheduled Activities April 07 - August 019 2015 Target_Hall_Scheduled_Activities__Apr_07_to_Aug_19.pdfTarget_Hall_Scheduled_Activities__Apr_07_to_Aug_19.mpp

Weekly update of Target Hall schedule after so many jobs have been finished in this week.  See attachment 1, 2

Entry  Thursday, July 30, 2015, 14:05, Travis Cave, Spent Target Vault, Standard Operation, , SiC#31, Spent target moved Vault_Storage_July_30_2015.pdf

SiC#31 has been moved to the spent target vault. It is in pail #127 and placed in spot 3C of the vault is was 489mSv/hr when removed from the south hot cell. See attached pdf for vault status

Entry  Wednesday, July 29, 2015, 10:14, David Wang, ITE, Standard Operation, TM4, , TM4 has been connected in ITE 

Dan and I connected TM4 in ITE. We checked all water signals on ITE cooling circuits. Everything is good.

Entry  Wednesday, July 29, 2015, 08:59, Travis Cave, ITE, Standard Operation, TM4, UC#13, Module moved 

TM#4 with UC#13 has been moved from the conditioning station to the east target station.

Entry  Wednesday, July 29, 2015, 06:24, David Wang, Conditioning Station, Standard Operation, TM4, UCx 13, Stopped the CS and TM4 pumps and vent with argon. 

Dan and I stopped the CS and TM4 pumps. We are venting the CS with argon for UCX13 target.

Entry  Tuesday, July 28, 2015, 14:40, chad fisher, South Hot-Cell, Standard Operation, TM4, SiC#31 UCx#13, SiC#31 removed UCx#13 installed 20150727_115314.jpg

SiC#31 has been removed from TM4 and UCx#13 installed. UCx#13 connection to the 9 pin connector was VERY VERY tight to the tube heater insulator on both the test jig and module.

 

 

Entry  Tuesday, July 28, 2015, 14:36, chad fisher, South Hot-Cell, Standard Operation, TM4, SiC#31, SiC#31 Autopsy 

Extraction electrode was removed from SiC#31 and target inspected.

Pictures of findings can be found at          https://documents.triumf.ca/docushare/dsweb/View/Collection-15131

 

 

 

Entry  Tuesday, July 28, 2015, 14:31, Travis Cave, Conditioning Station, Standard Operation, TM4, UC#13, Electrical Check TM4UC13IGLISelecchkCS.PDF

TM#4 with UC#13 electrical check at the conditioning station under vacuum. See attached PDF.

Entry  Tuesday, July 28, 2015, 10:17, David Wang, ITE, Repair, , , ITE TP4 has been replaced 

Tony and I replaced the ITE TP4 turbo pump today. The pumping time on controller has been reset to 0. The replaced broken  pump is bagged and stored at west end of TH.

Entry  Tuesday, July 28, 2015, 10:12, David Wang, Conditioning Station, Standard Operation, TM4, UCx 13, Helium pressure test on TM4 HS line at CS 

I did the helium pressure test on TM4 HS line at CS. Applied 70 psi helium  2 minutes. base leak rate0.0x E-9 atm.cc/sec.  No response during the test. No leak.

Entry  Monday, July 27, 2015, 17:03, David Wang, Conditioning Station, Standard Operation, TM4, UCx 13, UCx13 and TM4 under vacuum at CS. 

I connected the CS  vacuum system  to TM4. The CS and TM4 turbo pumps are started. Everything is good so far. The HS line will be pressured with helium tomorrow for leak checking. The CS and TM4 will be vented with Argon on Wednesday morning as planned before moved to ITE.

Entry  Monday, July 27, 2015, 15:46, David Wang, South Hot-Cell, Standard Operation, , , The yellow steel plug is put on SHC in TH 

The yellow steel plug is put on SHC in TH. The spent target is inside the SHC.The field around the SHC area in TH is so high that we have put it on. It will be moved out on this Thursday just before the spent target move. 

Entry  Monday, July 27, 2015, 15:34, David Wang, ITE, Standard Operation, TM4, , Leak check on TM4 HS water line with new UCX target. at SHC 

Chad and I leak checked the HS line at SHC after UCX target installation. On first round helium spray, one of VCR fitting has a leak to E-6 atm.cc/sec range. Chad tightened the fitting, and solved the problem. We leak checked both VCR fittings twice. No leak. The line will be helium pressured at CS tomorrow.

Entry  Monday, July 27, 2015, 14:37, Travis Cave, South Hot-Cell, Standard Operation, TM4, UC#13, Module moved 

TM#4 has been moved from the east target station (morning with SiC#31), and moved to the conditioning station from the south hot cell with UC#13 on it.

Entry  Monday, July 27, 2015, 13:38, Travis Cave, South Hot-Cell, Standard Operation, TM4, UC#13, Electrical Check TM4UC13IGLISelecchkSHC.PDF

Electrical check of TM#4 with UC#13 at the south hot cell. See PDF for details.

Entry  Monday, July 27, 2015, 12:12, Travis Cave, South Hot-Cell, Standard Operation, TM4, SiC#31, Electrical Check TM4_elecchk_notgt.PDFTM4SiC31postbeamelecchk_.PDF

Electrical check of TM#4 post beam with target (SiC#31) on and module without target on. There is a short between the target and EE when the target is on and when the target was removed short went away. See the PDF for details.

Entry  Friday, July 24, 2015, 14:41, Travis Cave, South Hot-Cell, Standard Operation, TM2, no target, Module moved 

TM#2 has been moved from the south hot cell to north east silo.

Entry  Friday, July 24, 2015, 10:04, David Wang, ITE, Standard Operation, , , 5 Shielding blocks have been moved from ITE to block storage area. 

Dan and I moved 5 shielding blocks from ITE to block storage area. The move is smooth.

Entry  Thursday, July 23, 2015, 10:23, David Wang, ITE, Standard Operation, , , Target Hall Scheduled Activities April 07 - August 019 2015 Target_Hall_Scheduled_Activities__Apr_07_to_Aug_19.pdfTarget_Hall_Scheduled_Activities__Apr_07_to_Aug_19.mpp

Update Target Hall schedule after the changing on TM2 process. See attachment 1,2

Entry  Wednesday, July 22, 2015, 12:13, chad fisher, South Hot-Cell, Repair, TM2, , TM2 Short Findings TM2_Short_July_22.jpg

Pin X was unplugged, short remained, however any slight pressure on the block towards the source tray makes the short go away.

Confirmed clearance between the EE and thr R / U coil lines as well as MSP of coil line.

Camera inspection would seem to indicate that ALL issues stem from a common location...there is a spot where both the pin X waterline and the one of the R / U waterline  contact the heat shield waterline...one on one side of the heat shield line and the other on the other side.

 

 

Entry  Wednesday, July 22, 2015, 11:31, Travis Cave, South Hot-Cell, Standard Operation, TM2, no target, Electrical Check TM#2elecchksourcetraynotgt62515.PDF

Electrical check done on TM#2 around the 25th of June 2015, this was before the coil line leak was found.

Entry  Tuesday, July 21, 2015, 12:38, David Wang, ITW, Repair, , , ITW external water leak on dump circuit has been fixed. 

The leaking 1/8 NPT(M)-1/4NPT(F) adapter on the ITW dump circuit is replaced.

Entry  Tuesday, July 21, 2015, 12:29, David Wang, ITE, Maintenance, , , target pit Hepa filter 

Target pit Hepa filter has been replaced today. There is 500 counts on swipe which is taken inside of the replaced filter. The field measurement on the filter wood box  is less than 0.5 usv/hr on contact. Right now,The outlets of the old filter are sealed with thick plastic and duct tape. The whole filter is wrapped with plastic sheet and tape. It has been moved to SHC ante room.  It will be moved out of there by Tony.N soon with RPG help.

Entry  Tuesday, July 21, 2015, 10:40, Grant Minor, Assembly/Bench Test, Repair, TM2, , TM2 - bench inspection photos from 6-June-2015 TM2_Source_Tray_Bench_Inspection_6-June-2015_04.JPGTM2_Source_Tray_Bench_Inspection_6-June-2015_13.JPGTM2_Source_Tray_Bench_Inspection_6-June-2015_11.JPG
 
Entry  Tuesday, July 21, 2015, 09:21, Travis Cave, South Hot-Cell, Standard Operation, TM2, no target, Electrical Check Failed TM#2_elec_chk_source_tray_no_tgt.PDF

TM#2 has failed the electrical check see attached pdf for details.

Entry  Monday, July 20, 2015, 17:11, Grant Minor, South Hot-Cell, Repair, TM2, , TM2 New Source Tray - additional photos 20 July 2015 3-8ths_gap_check_15July2015.JPGTM2_New_Source_Tray_20July2015.JPGTM2_Spacer_ITA6270_and_copper_ground_clip_detail_20July2015.JPG

A few additional higher-resolution photos of the TM2 source tray with new spacer ITA6270, and bent copper ground line clip.

Also attached is a photo of a 3/8" copper line placed in between the loose ECR line and the Mounting Support Plate line, for dimensional reference.

Entry  Monday, July 20, 2015, 14:12, chad fisher, South Hot-Cell, Repair, TM2, , TM2 Status 20150720_134819.jpg20150720_135747.jpg20150720_140100.jpg

Ultem high voltage spacer installed and 9 pin banana plug plugged in. Target has been inserted into the hot cell and will be installed after base-line electrical checks...probably first thing in the morning.

Entry  Friday, July 17, 2015, 13:51, chad fisher, South Hot-Cell, Repair, TM2, , TM2 Status 20150717_134123.jpg

Gas lines extensions installed yesterday were too long and gas lines touched top inside of containment box. They have been removed and the gas lines re-installed in their original manner. Gas lines have been "adjusted" as to clear the tube heater lines, which was the original issue.

Entry  Thursday, July 16, 2015, 14:36, chad fisher, South Hot-Cell, Repair, TM2, , TM2 Status 20150716_110247.jpg20150716_142818.jpg

IMG gauge, clip for ground to window lines and gas line extensions were installed today.

David and I also tried to locate the short between the coil line and MSP/Heat Shield...it went away for a bit...but is back.

Entry  Thursday, July 16, 2015, 07:38, David Wang, ITE, Standard Operation, , , Target Hall Scheduled Activities April 07 - August 07 2015 Target_Hall_Scheduled_Activities__Apr_07_to_Aug_07.pdfTarget_Hall_Scheduled_Activities__Apr_07_to_Aug_07.mppTarget_Hall_Scheduled_Activities__Apr_07_to_Aug_19.pdfTarget_Hall_Scheduled_Activities__Apr_07_to_Aug_19.mpp

Update the TH schedule according to present TM2 refurbishment process. See attachments 1,2

2015-07-20 , Update the TH schedule after some changes on TM2 and TM4 arrangement. See attachments 3,4

Entry  Wednesday, July 15, 2015, 11:18, David Wang, South Hot-Cell, Repair, TM2, , leak check coil line(R,U) on TM2 at SHC 007.JPG008.JPG

Chad and I leak checked the coil 1 circuit(R,U) after rebuilt coil line is installed on TM2 source tray. The pumping down on the circuit is very quick and smooth. The LD base lake rate 0.0xE-9 atm.cc/sec. Base pressure0.0xE-4 torr.

Chad sprayed lots helium on the R( coil 1+)and U(coil 1 -) water blocks. During  1 minute waiting time, there is no any response on LD. The R and U water blocks and C-seals are leak tight.

Entry  Wednesday, July 15, 2015, 11:02, chad fisher, South Hot-Cell, Repair, TM2, , TM2 Coil Line Vacuum Leak Check 

TM2 coil line R,U has been vacuum leaked check at the hot cell and has passed with no response from the leak detector.

Entry  Wednesday, July 15, 2015, 09:44, chad fisher, South Hot-Cell, Repair, TM2, , Coil Line replacement TM2_20150715_093157.jpgTM2_20150715_094745.jpg

water block jig installed, module side sealing surfaces re-polished and cleaned. Coil line inserted into the hot cell and installed onto the module. Bolts torqued to 90 in.lbs. Received .13mSv.

Entry  Tuesday, July 14, 2015, 12:56, chad fisher, South Hot-Cell, Repair, TM2, , TM2 containment box removed 

Containment box was removed from Tm2 this morning  in preparation for installation of coil line and all the trimmings.

Entry  Tuesday, July 14, 2015, 08:42, Travis Cave, South Hot-Cell, Standard Operation, TM2, no target, Module moved 

TM#2, no target, has been moved from the north east silo to the south hot cell.

Entry  Monday, July 13, 2015, 11:31, Travis Cave, Conditioning Station, Standard Operation, TM1, no target, Module moved 

TM#1 has been moved back to the south west silo from the conditioning station.

Entry  Friday, July 10, 2015, 14:41, Anders Mjos, Conditioning Station, Maintenance, TM1, , Replaced roughing pump 

 The roughing pump was replaced with a more leak tight pump due to the discovery of Rn-220 migration while roughing on TM1 in TCS

Entry  Friday, July 10, 2015, 09:33, chad fisher, South Hot-Cell, Repair, TM2, , Coil Line Decon 

Coil line has been in RPG's ultrasonic decon over night. Initial swipes this morning picked up 5000 counts. It has been decontaminated to the point no more contamination is being found and nothing can be found with the frisker...so...it's ready for Maico and Dan?

Entry  Thursday, July 09, 2015, 14:02, David Wang, Conditioning Station, Development, TM1, , TM1 is pumping down at CS 

TM1 and CS  vacuum system are connected. All turbo-pumps are started. The new TP1S works fine also. The pumping down looks good so far. During the TM1 and CS roughing down time, Joe .M noticed a Rn-220 level surge up in TH . Then,the Rn220  level slowly dropped back. Anders suspected this Rn-220 surging is related to the TM1 roughing down at CS. We decided we will stop the pumps , vent the CS , and roughing  again tomorrow. During the same time Joe will monitor  Rn-220 level in TH to see if the surging is repeatable. We want to learn more on this TH Rn-220 issue.

Entry  Thursday, July 09, 2015, 13:51, chad fisher, South Hot-Cell, Repair, TM2, , Coil line removal hot cell 

coil line has been removed from the hot cell. Initial decon was performed...after it still appears to have approximately 200 counts. It will now be transfered to the rad waste decon facility for further decon.

Entry  Thursday, July 09, 2015, 13:17, Anders Mjos, Conditioning Station, Standard Operation, TM1, , TM1 in TCS for alpha contamination test 

 Thursday, July 09, 2015, 13:17: Water package started.

Thursday, July 09, 2015, 15:20: Water package stopped.


Friday, July 10, 2015, 14:15: Roughing with new pump

Entry  Thursday, July 09, 2015, 09:55, Travis Cave, South Hot-Cell, Standard Operation, TM2, no target, Module moved 

TM#2 has been moved from the south hot to the north east silo. TM#1 has been moved from the south west silo to the conditioning station.

Entry  Wednesday, July 08, 2015, 14:48, chad fisher, South Hot-Cell, Repair, TM2, , TM2 Status 

Water block jig has been removed. Stuck source tray side water block jig component has been removed. An attempt was made to connect the gas lines to there bracket however they contact/interfer with the tube heater lines...Anders is looking into a solution.

Containment box and front cover have been replaced and TM2 is ready to move to the silo.

Entry  Wednesday, July 08, 2015, 14:24, David Wang, South Hot-Cell, Repair, TM2, , TM2 pressure bubble test on RU water blocks. 

July-06, 2015. Chad , Grant and I did the bubble test on R,U water blocks. We suspected the leak on the R,U circuit is from C seals on the water blocks so we did this test first. I applied both air and helium to R,U circuit , Chad applied snoop soap on the R,U water blocks.The air and helium pressure was increased from 40 psi to 90 psi Max step by step.Chad did not see any bubbles on the water blocks during the test. Since we did not find the leak source, we decided to do vacuum helium check on the all joints and c-seals of the R,U lines later.  Finally, We found the leak by vacuum helium spray the day after this bubble test. See other e-log.

Entry  Wednesday, July 08, 2015, 14:05, David Wang, South Hot-Cell, Repair, TM2, , leak check coil line(R,U) on TM2 at SHC  

Chad and I leak checked coil line(R,U) on TM2 at SHC yesterday. The leak detector was pumped down to 0.0Xe-9 atm.cc/sec before the check. Chad sprayed helium on the soldering joints connecting the cooling copper lines to the small holding blocks for the coil terminal(R,U).  After sprayed helium 2 seconds, I saw the leak rate on LD started to climbed up. The highest leak rate is 4.0xE-8 atm.cc/sec. It is a very positive response. We waited the leak detector pumped back to 0.0xE-9am.cc/sec, and tested again on the same joints. The result is same. Chad also sprayed helium on the R,U water blocks to check the C-seal. I saw a delayed tiny response on LD ( from 0.0 to 1.3xE-9atm.cc/sec). We think this tiny response is caused by the helium drifting to the leak soldering joint, but not a real C seal leak.

Entry  Wednesday, July 08, 2015, 12:18, chad fisher, South Hot-Cell, Repair, TM2, , R U Coil line Removal TM2_20150708_coil_line_leak.jpg

R U coil line removal started at 11:30. Water block jig installed and coil line disconnected from module.

Entry  Tuesday, July 07, 2015, 12:12, David Wang, Conditioning Station, Repair, , , CS TP1S replacement 

CS TP1S had been replaced with a new TP-301 pump this morning.The old pump was broken last week.

Entry  Tuesday, July 07, 2015, 10:50, Anders Mjos, Conditioning Station, Development, , , EPICS migration update - archiver 
  • The archiver is now merged with ISAC - data available under Utilities - Archiver Retrieval
  • Old archiver data is available under Utilities -> Archiver Retrieval - old
  • Strip tool save/load and export files under /data/tcsdata
  • Login via isacepics1.triumf.ca. TCS button on ISAC menu
Entry  Friday, July 03, 2015, 13:29, chad fisher, South Hot-Cell, Repair, TM2, , Hot Cell/ Module Fields 

Field measured at block "R" through tool port with pole monitor is 6.65 mSv/H.

There are three air hoods and two air lines currently available.

Entry  Friday, July 03, 2015, 11:33, chad fisher, South Hot-Cell, Repair, TM2, , TM2 Coil Leak Progress TM2_coil_leak_20150703_11.jpg20150703_111248.jpg

First thing this morning the hot cell was "cleaned up" in preparation for the return of TM2 for attempted verification and locating of leak on R/U coil circuit.

Containment box has been removed and front cover reinstalled to provide some modicum of shielding form the entrance and exit windows. Box was placed at an angle in the corner to try and minimize line-of-sight with potential worker(s).

Did notice some funny discoloration of both sides of coil water block "R" as seen in attached picture.

Entry  Friday, July 03, 2015, 09:41, David Wang, Conditioning Station, Standard Operation, TM2, , Target Hall Scheduled Activities April 07 - July 24 2015 Target_Hall_Scheduled_Activities__Apr_07_to_July_24_2015.pdfTarget_Hall_Scheduled_Activities__Apr_07_to_July_24_2015.mppTarget_Hall_Scheduled_Activities__Apr_07_to_Aug_07.pdfTarget_Hall_Scheduled_Activities__Apr_07_to_Aug_07.mpp

Updated the schedule before the weekend 2015-07-03. See attachment 1,2

Updated the schedule according to present TM2 refurbishment process. See attachment 3,4

Entry  Friday, July 03, 2015, 09:27, Anders Mjos, Conditioning Station, Development, , , Controls working on access control in EPICS 

 Some reboots will be done.

Entry  Friday, July 03, 2015, 09:11, Travis Cave, South Hot-Cell, Standard Operation, TM2, no target, Module moved 

TM#2 has been moved from the conditioning station to the south hot cell.

Entry  Thursday, July 02, 2015, 11:51, Travis Cave, Spent Target Vault, Standard Operation, , UC#12, Spent target moved Vault_Storage_July_2_2015.pdf

UC#12 has been moved from the south hot cell and placed into storage. It is in pail #125 and in spot 1C of the vault it had a reading of 25.1mSv/hr upon removal from the south hot cell. See PDF for vault details.

Entry  Thursday, July 02, 2015, 11:49, Travis Cave, South Hot-Cell, Standard Operation, TM1, no target, Module moved 

TM#1 has been moved from the south hot cell to the south west silo.

Entry  Thursday, July 02, 2015, 10:22, Anders Mjos, Conditioning Station, Maintenance, TM2, , TP1S failed 

 See e-fault 8233. Edi assisted in diagnosing the problem. The pump will have to be replaced.

Entry  Tuesday, June 30, 2015, 15:53, David Wang, Conditioning Station, Development, TM2, , leak on TM2 at CS TM2_leak_check_2015-06-30.pdfleak_check_2015-06-30_007.JPGleak_check_2015-06-30_009.JPG

 I leak checked TM2 at CS this afternoon which including air to vacuum check on service cap and helium pressure test on water lines. There is a small leak on water line R ,U (COIL1) during the helium pressure test.. Below 20 psi helium, there is no leak on it. But , once the helium pressure is increased over 20 psi, it showed up on Leak Detector. At 60 psi helium, the leak rate is 9.4xE-9 atm.cc/sec. For detail information, See attachment.  All other water lines and air to vacuum seals are good.

Entry  Tuesday, June 30, 2015, 15:41, David Wang, ITW, Standard Operation, TM1, , TM1 was disconnected in ITW this morning. 

TM1 was disconnected in ITW  this morning. The ITW was vented with argon last night.

Entry  Tuesday, June 30, 2015, 12:37, chad fisher, South Hot-Cell, Standard Operation, TM1, UCx#12, UCx #12 Removal 

UCx#12 has been removed from TM1 and placed in a pail with argon.

Right leg (B) of target is clearly broken.

Containment Box cover re-installed and module ready to move.

Entry  Tuesday, June 30, 2015, 11:27, Travis Cave, ITW, Standard Operation, TM1, UC#12, Module moved 

TM#1 with UC#12 has been moved from the west station to the south hot cell.

Entry  Tuesday, June 30, 2015, 09:47, chad fisher, South Hot-Cell, Repair, , , manipulator repair 

The right hand manipulator has been repaired. It took 43 minutes and I received ~ 0.56 mSv

Entry  Monday, June 29, 2015, 10:51, David Wang, Conditioning Station, Repair, TM2, , leak on TM2 side panel 

There is an air to vacuum leak on TM2 service cap side panel which we moved out during the TM2 wiring job. The CS pumps are stopped now. The CS will be vented soon. The seal on this panel has to been changed.

2016-06-30.  The o-ring seal on this panel(PNG1 and steerers)  is replaced and leak checked. No leak now.

Entry  Friday, June 26, 2015, 15:38, Anders Mjos, Conditioning Station, Development, TM2, , Leak check and HV test 

Roughing started by David.

Friday, June 26, 2015, 15:31: Started TP1S

Friday, June 26, 2015, 15:38: Started  TP1 & TP2

Friday, June 26, 2015, 15:47: TPs timed out. Restarted

Friday, June 26, 2015, 15:49: TP2 at speed

Friday, June 26, 2015, 15:49: TP1 at speed.

Friday, June 26, 2015, 15:54: IG1 on. 4.7E-5 T.

Friday, June 26, 2015, 15:56: IG2 on.  9.8E-5 T

Friday, June 26, 2015, 15:59: IG1S on. 2.9E-4 T


Leak found on service cap panels (David W)

Monday, June 29, 2015, 10:29: Stopped turbo pumps.

Entry  Friday, June 26, 2015, 14:33, David Wang, Conditioning Station, Standard Operation, TM2, , TM2 have been moved from SHC to CS 

Bill and I mover TM2 from SHC to CS. The move is smooth. I connected the CS vacuum system after the move, and started the roughing.

Entry  Friday, June 26, 2015, 09:45, chad fisher, South Hot-Cell, Repair, TM2, , TM2 Status 

Containment box window waterlines have been connected and leak checked and new containment box cover installed.

Module ready for transport just before 9am.

Entry  Friday, June 26, 2015, 09:44, chad fisher, South Hot-Cell, Repair, TM2, , TM2 Retrofit Status 20150625_075616_1.jpg20150625_083457.jpg20150625_105735.jpg20150625_110053.jpg

On June 25th the following work was completed:

Optics tray was installed into TM2. The lower fastener on the vertical cable tray (IRH1585) needed to be removed and vertical cable tray rotated upwards as optics tray would not clear cable tray. Optics tray was intstaled, cable tray repositioned and screw re-inserted.

Modified water block for 9 pin connector was installed.

Steerers connected.

Ground Electrode water blocks were "repositioned" closer to there specified position to attempt eliminating the short between the ground electrode line and coil 1 circuit. This was successful but could still use a clamp or other method of ensuring the ground electrode line is in its "proper" place.

9 pin connector line was rerouted to ensure it does not contact anything it is not suppose to (Rerouting directions provided by Anders).

Enzel lens cable was installed.

Blank offs removed from window water lines and new gaskets installed in preparation for installation of the containment box.

 

Entry  Friday, June 26, 2015, 08:27, David Wang, Conditioning Station, Standard Operation, TM2, , Target Hall Scheduled Activities April 07 - July 24 2015 Target_Hall_Scheduled_Activities__Apr_07_to_July_24_2015.pdfTarget_Hall_Scheduled_Activities__Apr_07_to_July_24_2015.mppTarget_Hall_Scheduled_Activities__Apr_07_to_July_24_2015.pdfTarget_Hall_Scheduled_Activities__Apr_07_to_July_24_2015.mpp

Update the Target hall Schedule after some changes on TM2 refurbishment. See attachment 1,2

2015-06-30, updated the schedule after some jobs have been finished before Canada day. See attachment 3,4.

Entry  Wednesday, June 24, 2015, 13:49, David Wang, South Hot-Cell, Repair, TM2, , TM2 new source tray vacuum leak check. TM2_new_source_tray_water_block_leak_check_at_SHC.pdf

All water blocks seals and joints have been leak checked. No leak has been found on any of them. See attachment

Entry  Wednesday, June 24, 2015, 10:16, chad fisher, South Hot-Cell, Repair, TM2, , TM2 Vacuum Leak Check 

The following circuits have been vacuum leak checked and have not registered any leaks:

Circuit D, C, B, A, Coil2, EE, Ground Electrode, Mounting Support plate, Coil 1.

Left are Heat Shield and Window circuits which will be checked after blank offs are installed on the vcr terminations.

Entry  Tuesday, June 23, 2015, 16:49, Anders Mjos, Conditioning Station, Development, , , TCS is beeing migrated to ISAC 

by controls group (Dave Morris).


Friday, June 26, 2015

TCS has been migrated to ISAC controls. Access is possible on a per user basis from isacepics1.triumf.ca

Entry  Tuesday, June 23, 2015, 14:19, chad fisher, South Hot-Cell, Repair, TM2, , TM2 Water Block Jigs Removed 20150623_140917.jpg

Both halves of the water block jigs have been removed and the module is now ready for base vacuum leak and electrical checks.

During removal of the jigs the fiberglass that had been "shoved" by hand in between two of the lines in the early 2000's fell out again.

Entry  Tuesday, June 23, 2015, 10:55, chad fisher, South Hot-Cell, Repair, , , Left Manipulator Repair 

The master wrist/tong cable has been replaced on the left manipulator. Everything appears to function well so far.

Entry  Friday, June 19, 2015, 13:00, chad fisher, South Hot-Cell, Repair, TM2, , TM2 Source Tray Install Status 

Left manipulator now broken. Master side however, so repair can take place Monday or Tuesday.

Entry  Friday, June 19, 2015, 11:57, chad fisher, South Hot-Cell, Repair, TM2, , TM2 Source Tray Progress 

Window waterline has been successfully connected using 1 1/2 inch long non-blunt start 1/4-28 bolts.

All bolt torques have been checked with dial torque wrench and are confirmed to be tight to 90 in lbs.

Entry  Friday, June 19, 2015, 11:52, David Wang, ITE, Standard Operation, TM4, SiC #31, 5 Shielding blocks have been transferred from ITW to ITE. 

5 shielding blocks have been transferred from ITW to ITE. The ITE is configured to take proton beam.

Entry  Friday, June 19, 2015, 11:43, David Wang, ITW, Repair, TM1, , ITW external water leak on dump circuit 6x

There was an external water leak in ITW during the last beam running time. The leak started after the shielding blocks transfer(May 22). It cause a constantly water level drop on S-tank(0.5 "/day average). Today , after the blocks are moved , the leak source has been found. Water seeped through a fitting on ITW dump circuit pressure gauge. The leak water slowly flow around the TM1 on the tank flange. most of them are dried out, but left some stain on dump module and tank flange. By closing the supply and return water valves on the ITW dump circuit, the leak is stopped now. We will fix this problem after the module is moved out and the radioactive field is low.  See attachments.

Entry  Friday, June 19, 2015, 09:37, Isaac Earle, South Hot-Cell, Repair, TM2, , TM2 Source Tray Installation - June 18, 2015 

 The following work was done on June 18 2015:

- Finished cleaning and polishing all water blocks on module side (white felt with isopropyl, then buffing material with isopropyl, then canned air).  Heat shield waterblock re-done because water marks visible (white scotchbrite, white felt w/ isopropyl, buffing material w/ isopropyl, then canned air).  All surfaces looked very good, no lint or scratches visible.  
- Tray installed using installation jig (jig was very difficult to slide on hot cell table).  Window circuit waterline bracket tube retaining screws had to be removed for the sourcetray to clear the module frame.  Optics tray locating mushroom on source tray rubbed against the module side waterblock jig and was pushed past.  Gas lines were held clear of the source tray with the manipulator as the it went in.  The nut on the source tray side water block guide pin had to be loosened to facilitate complete insertion of the source tray.
- Connection of waterblocks for circuits D, C, B, A, Febiad Coil 2 were done in the sequence listed with no issues
- Extraction electrode and heat shield water blocks could not be done up initially because the locking tabs could not be undone (interference with module side jig bracket)
- Ground electrode waterblock connected without issue
- Window waterblock attempted: screws would not engage
- Febiad coil 1 negative waterblock source tray side locking tab had to be re-inserted into block, then waterblock was connected
- Febiad coil 1 positive connected without issue (failed initially due to shorter screw)
- Mounting support plate waterblock alignment pins did not engage initially, rotated source tray side waterblock using polishing tool.  Then was connected without issue.
- Extraction electrode waterblock revisited: pulled together with 1-5/8" screw, then connected (with 1-3/8" screws in both holes as per ITA6144)
- Heat shield waterblock revisited: installed without issue (as the jig had been pulled together by the previous step)
- Attempted window water block again.  Right side manipulator wrist tong cable broke while using camera.  Waterblock could not be connected (holes look concentric, pins engaged, blocks together and almost flush)
- All waterblocks except window waterblock torqued (tool did not slip properly, so torque will be re-checked)

Plan for Friday June 19:
- Put blank-offs and various fasteners in hot cell through tool port
- Check torque of all waterblocks with dial torque wrench
- Attempt window water line again with different fasteners (non-blunt start), try removing both sides of waterblock alignment jigs
- Install blank-offs on window and heat shield lines (VCRs)
- Perform preliminary leak check

Entry  Thursday, June 18, 2015, 08:03, chad fisher, South Hot-Cell, Repair, TM2, , TM2 Optics Tray Transfer 20150618_075326_1.jpg

The TM2 optics tray has been transferred from the source tray to the transfer fixture in preparation for installation of the source tray into the module.

Entry  Wednesday, June 17, 2015, 14:21, chad fisher, South Hot-Cell, Repair, TM2, , TM2 Waterblock Clean Polish 20150617_080236_1.jpg20150617_081538_1.jpg20150617_083830.jpg

Fiberglass that fell out yesterday was put back in place (as well as possible).

Cleaning took place this morning with excellent results. Cleaning was performed with red scotch brite on the cleaning tool, air pressure at 40 psi while running, with one 60 second cycle. Three blocks (EE, HS and Window) needed a second pass to remove the indium.

Polishing commenced with 2000 grit wet sand paper. Paper was wet with isopropynol. 60 second cycles for double seal blocks, 30 second for singles. The 2000 grit pass was completed.

Polishing will finish tomorrow morning as well as removal of optics tray from source tray in preparartion for insertion of the source tray into the module tomorrow afternoon or Friday morning.

First picture is Tube heater Circuit D block before cleaning and second picture is after cleaning.

 

 

Entry  Tuesday, June 16, 2015, 14:28, chad fisher, South Hot-Cell, Repair, TM2, , TM2 Source Tray Installation/Water Block Sealing Surface Clean 20150616_104240.jpg20150616_140505.jpg20150616_140506.jpg

Today cleaning and polishing pads were inserted into the hot cell.

Module side waterblock jig installation was attempted however one of the locking tabs/latches (ITA2405?) came undone/fell off. Luckily, I had old, obsolete jigs in the hot cell so I was able to remove parts I needed from an old one and rebuild the current one.

Jig was installed on module to retain module side waterblocks.

Blank-off remove was commenced, however due to and large amount of water coming out of the line to have the blank-off removed work had to stop till the water evaporates.

Waterblock sealing surface cleaning and polishing will continue tomorrow.

Also, upon installing the jig a piece of fiberglass that had previously been manual inserted between two of the water lines (early to mid 2000's) fell out.

Entry  Monday, June 15, 2015, 14:14, David Wang, South Hot-Cell, Standard Operation, , , Target Hall Scheduled Activities April 07 - July 21 2015 Target_Hall_Scheduled_Activities__Apr_07_to_July_21_2015.pdfTarget_Hall_Scheduled_Activities__Apr_07_to_July_21_2015.mppTarget_Hall_Scheduled_Activities__Apr_07_to_July_21_2015.mppTarget_Hall_Scheduled_Activities__Apr_07_to_July_21_2015.pdf

Weekly update Target Hall schedule 2015-06-15. See attachment 1,2

 2015-06-19, Update the schedule on  the end of the week. See attachment 3,4

Entry  Monday, June 15, 2015, 10:16, chad fisher, South Hot-Cell, Repair, TM2, , C.B. off 20150615_101043_1.jpg

As per scedule TM2 containment box has been removed.

 

Entry  Monday, June 15, 2015, 09:42, Travis Cave, South Hot-Cell, Standard Operation, TM2, no target, Module moved 

TM#2 is now in the south hot cell.

Entry  Friday, June 12, 2015, 13:27, David Wang, South Hot-Cell, Standard Operation, , , TM2 new source tray has been remotely transferred from TH into SHC successfully. 

TM2 new source tray has been remotely transferred into SHC successfully. The transfer table has been moved back to TH within 1 hour.  I swiped the table and found about 150counts contamination. It is much better comparing to last time using since we removed this table out of SHC as quick as we can. The table will be cleaned with windex  after Target Hall is surveyed.

Entry  Friday, June 12, 2015, 07:49, chad fisher, Assembly/Bench Test, Repair, TM2, , New TM2 Source Tray Ground to HV Measurements 

After bending and leak checking the new measurements from ground to HV on the TM2 source tray are:

Ground to C1+ 0.6645"

ground to heat shield 0.506

Window to mounting support plate - unchanged - over 0.80"

Entry  Thursday, June 11, 2015, 13:43, Dan McDonald, Assembly/Bench Test, Repair, TM2, , Leak check following tweaking of cooling line gaps 

Maico, Chad and I conducted a leak check on all affected lines following tweaking of cooling line gaps. All lines pumped down to a level of 10-9 torrliter/sec with no leaks detected with Helium.

Entry  Thursday, June 11, 2015, 13:11, chad fisher, Assembly/Bench Test, Repair, TM2, , Measurements beyween ground Plane and HV TM2 Source tary 

I've taken measurements between HV and ground circuit on TM2 source tray as instructed.

At their closest points:

Heat Sheild to Ground Electrode 0.445"

Ground Electrode to C1+ 0.281"

Window to Mounting Support Plate 0.858"

 

Entry  Wednesday, June 10, 2015, 16:49, Grant Minor, Assembly/Bench Test, Repair, TM2, , TM2 New Source Tray - *HOLD* on installation into Hot Cell until HV approval ITA6144_RevC_markup_10Jun2015.pdfTM2_cooling_lines_too_close_GE_HS_10June2015.jpgTM2_cooling_lines_too_close_Window_MSP_10June2015.jpg

Don Jackson brought to my attention some potential HV minimum spark gap issues with the source tray cooling lines.  It appears:

- The gap between the Ground Electrode cooling lines (ground) and Heat Shield cooling lines (HV) does not meet the spec of 0.668" MIN called out on the print

- The gap between the Window cooling lines (ground) and the Mounting Support Plate cooling lines (HV) does not meet the spec of 0.668" MIN called out on the print.

A copy of the tube bending drawing is attached with the spec highlighted in green.

The 0.668" MIN gap spec came from a check I asked Mark Llagan to perform to find the minimum gap when he was preparing the model for the tube bending drawing.  This gap was approved Jan 28th, 2015 by Friedhelm Ames on ECO-3587.

The source tray with the tubes bent as it is currently has been tested to 55 kV at the test stand by Anders, see:
https://elog.triumf.ca/TIS/Test-Stand/447

I am away June 12th to June 24th on vacation inclusive.  Isaac Earle is in charge of Remote Handling in my absence.

I am delegating Don Jackson responsible for resolving this TM2 HV issue, collecting and documenting the approval to proceed from the T/IS group leader with the source tray as-is, or to try to re-work the cooling lines and delay the project.

The source tray is NOT to be installed in the Hot Cell until this issue has been resolved.

Regards,

Grant

-- 
Grant Minor, M.A.Sc., P.Eng.
TRIUMF Remote Handling Group Leader
Nuclear Engineer
4004 Wesbrook Mall, Vancouver
BC, Canada, V6T2A3
gminor@triumf.ca
(604) 222-7359(604) 222-7359
http://www.triumf.ca/profiles/4557
Entry  Wednesday, June 10, 2015, 13:17, David Wang, ITE, Standard Operation, TM1, , Target Hall Scheduled Activities April 07 - July 26 2015 Target_Hall_Scheduled_Activities__Apr_07_to_July_21_2015.pdfTarget_Hall_Scheduled_Activities__Apr_07_to_July_21_2015.mpp

Weekly update the schedule after some jobs have been finished in this week.

Entry  Wednesday, June 10, 2015, 11:49, David Wang, ITE, Standard Operation, TM4, SiC #31, TM4 has been connected in ITE 

Dan and I connected TM4 in ITE. At this stage, water is supplied to TM4 only. We checked the TM4 water signals from electrical room.They are good. The turbo-pumps will be started today once the roughing is done.

Entry  Wednesday, June 10, 2015, 10:02, Travis Cave, ITE, Standard Operation, TM4, SiC#31, Module moved 

TM#4 has been moved from the conditioning station to the east target station.

Entry  Tuesday, June 09, 2015, 14:36, chad fisher, Assembly/Bench Test, Repair, TM2, , TM2 Source Tray Final Inspection 20150609_132818.jpg20150609_132825.jpg20150609_132833.jpg20150609_132839.jpg20150609_132851.jpg

Final inspection took place with Pierre, Grant, Friedhelm and Anders present.

Two action items were raised:

1) check routing of 9 pin connector line

2) Check orientation of 9 pin water block

Chad pointed out concerns on clearances between a target and conductor block waterlines, possible optics tray alignment issues (that it had changed slightly from the initial alignment), and gap between steerer housing and ground electrode due to alignment.

Entry  Tuesday, June 09, 2015, 09:49, chad fisher, Assembly/Bench Test, Repair, TM2, , TM2 Source Tray Final Alignment Check 

Final alignment continued this morning.

Steerers have been aligned to 0.001 low, 0.000 left/right wrt master jig.

Optics tray required some adjustment as well and is now at:

Front 0.000 left/right, .001 high wrt master jig

Back 0.001 high, 0.000 left/right wrt master jig

Febiad coil conductor blocks have been reset with the master target jig as well...as they have been on and off during the test stand test.

A few components have been removed during the test stand test (such as feet required for tranfser jig) which I will now hunt down.

Otherwise i believe we are ready.

Entry  Monday, June 08, 2015, 14:40, chad fisher, Assembly/Bench Test, Repair, TM2, , TM2 Source Tray Final Alignment Check 

Final Alignment checks of the TM2 source tray took place today.

Mater Jig: Front - 0,0 Back - 0 left, right, .005 low

Tray: Front .001 High, .001 right Back - .001 right, .008 low

Which equals  Tray: front .001 high, .001 right back: .001 right, .003 low in comparison to the master jig which is both within spec and within reason to pre-soldering numbers.

Steerer was out significantly and currently sits at .003 high, .002 right wrt. master jig.

More refinement on the steerer tomorrow and check on the optics tray as well.

Entry  Thursday, June 04, 2015, 08:27, chad fisher, Assembly/Bench Test, Repair, TM2, , TM2 Source Tray C-seal removal and inspection TM2_20150604_01.jpgTM2_20150604_02.jpgTM2_20150604_03.jpgTM2_20150604_04.jpgTM2_20150604_05.jpg

Source tray for TM2 has been moved to the alignment area by Dan and co.

This morning Dan removed the c-seals used during the test and he and I inspected the sealing surfaces to determine if they need to be cleaned...they do..trace indium was present on all blocks.

Surfaces will be cleaned before final alignment check.

 

Entry  Thursday, June 04, 2015, 07:44, Dan McDonald, Assembly/Bench Test, Development, TM2, , Movement of TM2 source tray to alignment area in ISAC 

Once the test stand was vented and all lines purged Anders Mjos and myself jigged up the water blocks and proceeded to remove the TM4 SiC#31 target used during the testing, Einso lens and steerer.  Once these components where removed we transferred the source tray to the transport plate and moved it to the alignment area.

Entry  Wednesday, June 03, 2015, 13:51, David Wang, Conditioning Station, Standard Operation, TM4, SiC #31, TM4 is connected at CS 007.JPG009.JPG008.JPG010.JPG

TM4 has been connected at CS. CS HV cover is installed.I made a pair of new cooling lines for TM window cooling at CS. The TM4 containment box window cooling line is connected to the HVC spare circuit now. I checked water flow visually, and it is good. The TM4 is ready for conditioning.See attachment for window cooling modification.

 

Entry  Wednesday, June 03, 2015, 13:01, Anders Mjos, Conditioning Station, Standard Operation, TM4, SiC#31, Conditioning SiC#31 SiC#31_Conditioning.docx

PNG1 connected to PNG in service cap (as per David W)

 Wednesday, June 03, 2015, 12:59: Water on

Wednesday, June 03, 2015, 13:04: Staging enabled.

Wednesday, June 03, 2015, 14:02: Auto-ramping to 580 and 200 A at 2 and 1 A/min.

Wednesday, June 03, 2015, 14:03 : BIAS/EL/EE to 20/10/1.5 kV


ISAC operations monitored TCS from Wednesday to Monday


Monday, June 08, 2015, 08:55 : Started cool-down of target

Monday, June 08, 2015, 09:19: BIAS/EL/EE off

Monday, June 08, 2015, 09:32: EE configured to conditioning mode

Monday, June 08, 2015, 10:12 : TGHT and TBHT off

Monday, June 08, 2015, 10:25: BIAS/EL to 20/10 kV

Monday, June 08, 2015, 10:32: BIAS/EL to 30/15 kV

Monday, June 08, 2015, 10:45: BIAS/EL to 40/20 kV. Some bias sparking from ~39 kV

Monday, June 08, 2015, 13:40: BIAS/EL to 47.5/20 kV

Monday, June 08, 2015, 14:35: BIAS/EL to 50/20 kV

Monday, June 08, 2015, 14:39: BIAS/EL to 50/25 kV

Monday, June 08, 2015, 16:54: BIAS/EL to 53/25 kV

Monday, June 08, 2015, 17:03: BIAS/EL/EE off


Tuesday, June 09, 2015, 08:02: BIAS/EL to 30/15 kV

Tuesday, June 09, 2015, 08:07: BIAS/EL to 40/20 kV.

Tuesday, June 09, 2015, 08:13: BIAS/EL to 50/25 kV

Tuesday, June 09, 2015, 08:27: BIAS/EL to 53/25 kV 

Tuesday, June 09, 2015, 08:57: BIAS/EL to 55/25 kV  

Tuesday, June 09, 2015, 09:31: Power supplies tripped on IG2 vacuum after a spark at ~57.5 kV

Tuesday, June 09, 2015, 09:40: BIAS/EL to 40/20 kV.

Tuesday, June 09, 2015, 10:00 : BIAS/EL to 55/25 kV  

Tuesday, June 09, 2015, 10:09: BIAS/EL to 57.5/25 kV

Tuesday, June 09, 2015, 10:22: Sparking activity at 58 kV. Tripped TP2 and BV2. Reduced to 50 kV. Leakage current increased.

Tuesday, June 09, 2015, 10:33: Sparking activity at 55 kV. Reduce to 45 kV. Increased BIAS current limit from 0.25 to 0.30 mA

Tuesday, June 09, 2015, 10:41: BIAS/EL to 50/25 kV. BIAS RDCUR 0.17 mA, was 0.08 mA at 8:13 this morning.

Tuesday, June 09, 2015, 11:28 : Restarted TP2. Tripped.

Tuesday, June 09, 2015, 11:50:  Increased BIAS current limit from 0.30 to 0.35 mA

Tuesday, June 09, 2015, 11:55 : BIAS/EL to 54.5/25 kV for 5 min, 0.12 mA . Reducing to 40 kV for lunch break.

Tuesday, June 09, 2015, 13:07: BIAS/EL to 50/25 kV 

Tuesday, June 09, 2015, 13:27: BIAS/EL to 55/25 kV 

Tuesday, June 09, 2015, 13:40: BIAS/EL to 57/25 kV 

Tuesday, June 09, 2015, 13:49: BIAS/EL to 57.5/25 kV. Increased BIAS current limit from 0.35 to 0.40 mA

Tuesday, June 09, 2015, 14:30: IG1 tripped after spark. Controller seems to be broken. Forced IG1. Fault report submitted June 10th.

Tuesday, June 09, 2015, 14:58: BIAS/EL to 45/25 kV

Tuesday, June 09, 2015, 15:46: BIAS/EL to 55/25 kV

Tuesday, June 09, 2015, 15:55: BIAS/EL to 56/25 kV

Tuesday, June 09, 2015, 17:30: BIAS/EL to 57/25 kV 

Tuesday, June 09, 2015, 17:46: BIAS/EL to 57.5/25 kV 

Tuesday, June 09, 2015, 18:00: BIAS/EL to 58/25 kV

Tuesday, June 09, 2015, 18:30: No sparks for 30 min

Tuesday, June 09, 2015, 18:55: One spark observed. BIAS/EL off.

Tuesday, June 09, 2015, 18:56: Turbos stopped. Stopped water circuit.


Thursday, June 11, 2015: IG1 seems to work again after a power cycle. Controller tested with another IG. Closing Fault report

Entry  Wednesday, June 03, 2015, 11:22, David Wang, Conditioning Station, Standard Operation, , , Target Hall Scheduled Activities April 07 - July 21 2015 Target_Hall_Scheduled_Activities__Apr_07_to_July_21__2015.pdfTarget_Hall_Scheduled_Activities__Apr_07_to_July_21_2015.mppTarget_Hall_Scheduled_Activities__Apr_07_to_July_21_2015.pdfTarget_Hall_Scheduled_Activities__Apr_07_to_July_21_2015.mpp

I revised the Target Hall schedule to July 21 2015. It is the time new TM2 with ZrC target started at ITW.

2015-06-04, Updated the schedule with   new PDF view. See attachments 3, 4

Entry  Tuesday, June 02, 2015, 14:39, David Wang, Conditioning Station, Standard Operation, TM4, SiC #31, TM4 and CS turbo- pumps are started . 

TM4 and CS turbo-pumps are started this afternoon. Everything is good so far.

Entry  Tuesday, June 02, 2015, 14:38, David Wang, Conditioning Station, Repair, TM4, , replace broken TM4 IG1 002.JPG006.JPG

 TM4 IG1 filament was broken during last run  at ITE.  The broken filament is replaced with a new one today when TM4 is located at CS.

2015-06-03 , Leak checked the new 25 conflat gasket today. No leak. See attachments

Entry  Tuesday, June 02, 2015, 14:32, David Wang, South Hot-Cell, Standard Operation, TM4, SiC #31, Leak check on TM4 HS water line with new SiC #31 target. at SHC 003.JPG005.JPG001.JPG

Chad and I leak checked TM4 HS water line with SiC #31 target installed. leak rate:0.0xE-9atm.cc/sec.  No leak.  The line will be helium pressurized at CS later.

2015-06-03, helium pressure test the line at CS. 70psi 3 minutes. leak rate 0.0xE-9 atm.cc/sec. No leak.   See attachments

Entry  Tuesday, June 02, 2015, 11:54, Travis Cave, Conditioning Station, Standard Operation, TM4, SiC#31, Module moved 

TM#4 with SiC#31 has been moved from the south hot cell to the conditioning station.

Entry  Tuesday, June 02, 2015, 10:39, Travis Cave, South Hot-Cell, Standard Operation, TM4, SiC#31, Electrical Check TM4_SiC31_elecchk_SHC.PDF

Electrical check on TM#4 with SiC#31. See attached PDF for details.

Entry  Tuesday, June 02, 2015, 09:43, chad fisher, South Hot-Cell, Standard Operation, TM4, SiC#31, SiC#31 installed 

Ta #45 has been removed from TM4 and SIC#31installed.

Entry  Tuesday, June 02, 2015, 06:51, David Wang, South Hot-Cell, Standard Operation, TM4, , Target Hall Scheduled Activities April 07 - June 26 2015 Target_Hall_Scheduled_Activities__Apr_07_to_June_26_2015.mppTarget_Hall_Scheduled_Activities__Apr_07_to_June_26_2015.pdf

Target Hall schedule weekly update. All jobs are finished on time so far.

Entry  Monday, June 01, 2015, 14:24, Travis Cave, South Hot-Cell, Standard Operation, TM4, Ta#45, Electrical Check TM4_Ta45_elecchk_postbeam.PDF

Post beam electrical check on the Ta#45 target installed on TM#4. See attached PDF.

Entry  Monday, June 01, 2015, 11:23, Travis Cave, ITE, Standard Operation, TM4, Ta#45, Module moved 

TM#4 with Ta#45 has been moved from the east target station to the south hot cell.

Entry  Friday, May 29, 2015, 09:16, Travis Cave, Conditioning Station, Standard Operation, TM2, no target, Module moved 

TM#2 with no source tray has been moved from the conditioning station to the north east silo.

Entry  Wednesday, May 27, 2015, 08:57, Travis Cave, Conditioning Station, Standard Operation, TM2, , Module moved 

TM#2 with no source tray has been moved from the south hot cell to the conditioning station.

Entry  Tuesday, May 26, 2015, 14:34, chad fisher, South Hot-Cell, Repair, TM2, , Shutter replacement Shutter.jpg

The shutter in TM2 was successfully replaced today.

New lock washer and nut were installed onto shutter and nut torqued to 120 ft lbs.

Shutter guide alignment tool was used to insure tapped shutter guide holes were concentric with thru holes in shutter side mounting panel, button head screws replaced and torqued to 110 ft-lbs.

The shutter was manually cycled open and closed by David and everything is to operate well.

Entry  Tuesday, May 26, 2015, 11:49, Grant Minor, Assembly/Bench Test, Repair, TM2, , TM2 New Source Tray - Braze & Solder Report - 22 May 2015 6x

Hello,

For reference, I have attached a list of all solder joints in the TM2 Source Tray, and the alloys used for the most recent build (as per ITA6144).   I have also provided data sheets for the alloys, and PDF copies of all the drawings calling out the joints.

Certanium 34 C (222 deg C melt point) was used for all low-temperature solder applications, except for the steel inserts in the water blocks.  Previous revisions of the Source Tray drawings called out a higher-temperature McMaster lead-based solder (304 deg C melt point).  The change to Certanium 34 C on the prints was made in Bevan's era, during the transitional update of the source tray drawings between the TM1 and TM3 source tray projects, just before I took over updating the drawing packages.  I believe Bevan made this change on general advice from Guy Stanford, who stated that Certanium 34 C is a much easier solder to work with and makes a more mechanically reliable joint.  However, the change really should have had more review and validation testing before being implemented.

This said, we now have a source tray that uses Certanium 34 C, and rework of every joint would set us back too far in the schedule to meet the deadline, so we will have to run with it as it is.

Of particular concern are the joints on the target oven and coil heating blocks, which are now using a lower temperature solder (222 deg C melt vs 304 deg C melt).  We have experienced a coil block failure on TM4 due to a failed solder joint, although the failure mode is not known for certain.  We also had two recent failures on the test stand of a coil joint soldered with Certanium 34 C, but this was due to an error in the connection of cooling water to the joints (i.e. the joints had no coolant flow and the solder melted... this is expected!).

Anders and I have performed independent thermal analysis on the joints due to the radiative and electric heating from the target, and have concluded that even with a lower temperature solder, there is a lot of margin, so the risk seems to be low.  This work will be published in a separate report to be circulated later.

Thank you and regards,

Grant

Entry  Friday, May 22, 2015, 15:44, David Wang, ITW, Standard Operation, TM1, UCx12, 5 Shielding blocks have been transferred from ITE to ITW. 

5 shielding blocks have been transferred from ITE to ITW. I  checked all ITW water signals, and they are good.  ITW is configured to take proton beam.

Entry  Wednesday, May 13, 2015, 13:55, chad fisher, South Hot-Cell, Repair, TM2, , Shutter removal TM2_20150513_131339.jpgTM2_20150513_134232.jpg

TM2 has been successfully de-shuttered.

All went pretty much according to plan except I had to remove one fastener out of the upper wiring harness (the one that has just been installed) to allow for enough clearance to rotated the shutter guide out of the way...I shutter to think what would have happened otherwise...anyways...

Close inspection of the shutter does show that the "thin" area isn't in very good shape; whether this is a result of removal or just the way it was is hard.Due to the ease of removal I would quess that it may have been a preexisting condition. That being said...I think we may want to consider replacing it.

 

Entry  Monday, May 11, 2015, 11:20, David Wang, South Hot-Cell, Standard Operation, TM2, , Target Hall Scheduled Activities April 07 - June 26 2015 6x

The schedule has some changes due to  new TM2 source tray coil cooling line leaking at test stand. Now,It is re-scheduled in such an estimation  that TM2 source tray could be ready at teat stand by this Friday(May-15th). see attachment 1,2.

2015-05-12,  Changed  and updated the TH activity schedule according to Dons new beam schedule which is re-arranged after the coil line leaking issue. See attachments 3,4. No major conflicts has been found on the new schedule.

2015-05 25, Updated the TH activity schedule according to present TM2 job processing. See attachment 5,6.

Entry  Monday, May 11, 2015, 10:45, Anders Mjos, Conditioning Station, Maintenance, , , RGA electronics box installed 2015-05_RGA_GND_connection.pdf

 The communications chip has been replaced. The electronics box has been grounded (see attached pdf).

Entry  Thursday, May 07, 2015, 11:02, Travis Cave, South Hot-Cell, Repair, TM2, No target, Wiring of TM#2 

Wires in TM#2 have been terminated at the top of the module.

Entry  Wednesday, May 06, 2015, 14:30, Travis Cave, South Hot-Cell, Repair, TM2, No target, Wiring of TM#2 Photo_2015-05-06_8_26_10_AM.JPGPhoto_2015-05-06_8_26_17_AM.JPG

Wires for TM#2 steering elements, and png gauge have been run down to the containment box level. Chad has placed them in the little cable trays. Slack has been pulled back. and termination of the wire will be done on the 7th of May. A modification was done to the signal line of the png gauge wire ultem block, as grounded screw was inserted to allow for strain relief so the end would hopefully quit breaking. See attached pictures for the details.

Entry  Tuesday, May 05, 2015, 10:57, chad fisher, South Hot-Cell, Repair, TM2, , TM2 Wiring TM2_New_Wiring_20150504_13.jpgTM2_Wiring_20150505_10.jpg

Old wiring was removed yesterday, new wiring run thru the vacuum chase. Old IMG gauge removed today, new cable trays installed and wires installed into cable trays.

Entry  Monday, May 04, 2015, 13:32, Anders Mjos, Conditioning Station, Maintenance, , , TK2 expansion tank topped up 

Caled cyclotron ops to open P23 and confirmed penthouse valve open.

Filled up TK2 to 21 in water leve.

Entry  Friday, May 01, 2015, 13:48, David Wang, South Hot-Cell, Standard Operation, TM2, , Target Hall Scheduled Activities April 07 - June 26 2015 update Target_Hall_Scheduled_Activities__Apr_07_to_June_26_2015.mppTarget_Hall_Scheduled_Activities__Apr_07_to_June_26_2015.pdf

Target Hall Scheduled Activities  April 07 - June 26  2015 update.      2015-05-01. All TH scheduled jobs are finished on time this week.

Entry  Friday, May 01, 2015, 08:27, chad fisher, South Hot-Cell, Repair, TM2, , Containment Box Removal 

Containment box has been removed in preparation for wire replacement.

Entry  Thursday, April 30, 2015, 08:50, Travis Cave, South Hot-Cell, Standard Operation, TM2, No target, Module move 

TM#2 with no source tray has been moved from the north east silo to the south hot cell.

Entry  Tuesday, April 28, 2015, 17:17, David Wang, ITW, Standard Operation, TM1, UCx12, TM1 has been connected in ITW. 

TM1 has been connected in ITW. Five turbo pumps have  been started. The TM1 containment box window line is capped on the service cap and the line is pump town to E-4 torr range.

Entry  Tuesday, April 28, 2015, 11:14, Travis Cave, ITW, Standard Operation, TM1, UC#12, Module move 

TM#1 with UC#12 has been moved from the conditioning station to the west target station.

Entry  Tuesday, April 28, 2015, 11:09, Anders Mjos, ITW, Maintenance, , , Resistance measured of TGHT and TBHT lines to ITW Resistance_from_Electrical_Room_to_Target_Station.xlsx

The new TBHT and TGHT power supplies were brough up to high current; 350 A and 420 A respectively. The TGHT power supply was limited by PLC to 420 A. The resistance calculated for both the TBHT and TGHT copper lines from the electrical services room to the ITW pit was 1.35 mOhm. See attached spreadsheet for details.

Dave Morris has been contacted to correct the current limit for the TGHT supply to 600 A.

Entry  Tuesday, April 28, 2015, 10:26, David Wang, ITW, Standard Operation, TM1, UCx12, ITW target pit o-ring seal replacement. 

Dan and I replaced ITW target pit o-ring seal(.275DIA X42"ID). It is an annual job before first beam to ITW. The old o-ring was moved and the groove was vacuum cleaned. The new o-ring has been installed properly.

Entry  Tuesday, April 28, 2015, 10:21, David Wang, Conditioning Station, Standard Operation, TM1, UCx12, CS and TM1 was vented with Argon gas  

Dan and I vented CS and TM1 with Argon gas before it is moved this morning.

Entry  Monday, April 27, 2015, 17:09, Grant Minor, ITE, Development, TM2, , TM2 - New Source Tray - Water Block Seal Groove Inspection Report IMG_1859.JPGTM2_New_Source_Tray_Water_Block_Inspection_Results_24_April_2015.pdfTM2_water_block_inspect_24Apr2015.pdfTM2_New_Source_Tray_Water_Block_Inspection_Results_April_2015.xlsx

The water blocks soldered to the TM2 cooling lines (see Ref. Assy. ITA6144) were inspected.

See attached inspection reports and drawings.

It was found that only 18% of the seal groove diameters and 55% of the depths were in spec.

The source tray must be tested on the test stand with c-seals to ensure that these blocks will seal properly on the module.

Entry  Monday, April 27, 2015, 16:12, Keith C Ng, South Hot-Cell, Development, TM2, , Ceramic Standoffs in TM2 source tray steerer assembly IMG_3106.JPG

On drawing ITA6008 for the Encole 0.5" ceramic standoffs there is a note to match pairs of ceramics to within +/-0.001". This step was missed on the current build of TM2 source tray (ceramics were not measured).

Measured the lengths of the rest of the ceramic standoffs in inventory and they range from 0.5035" to 0.4950" in length. The ceramics have been sorted by length and grouped into bags.

 IMG_3106.JPG

Entry  Monday, April 27, 2015, 10:28, David Wang, Conditioning Station, Standard Operation, TM1, UCx12, TM4 has been partially disconnected at CS. 

TM1 has been partially disconnected at CS for tomorrow move. The CS TP1S is still running and will be stopped and disconnected tomorrow morning.

Entry  Thursday, April 23, 2015, 12:56, Anders Mjos, Conditioning Station, Maintenance, TM1, , IG1 Good Vacuum limit changed IG1GoodVacuum.png

Changed by Dave Morris. 

New value is 1E-5 T (old value was 7.09E-5 T)

Entry  Thursday, April 23, 2015, 09:08, David Wang, Conditioning Station, Maintenance, TM1, UCx12, Huge Leak on TM1 contaiment box window. 006.JPG008.JPG011.JPG009.JPGTM1_leak_check_at_CS_2015-04-23.pdf

There is a huge leak on TM1 containment box window. I did a 70 psi helium pressure test on all TM1 water circuits this morning. The LD base leak rate was 0.0XE-9 atm.cc/sec. When applying the 70 psi helium to containment box window circuit, the leak rate on LD jumped to 1XE-4 atm.cc/sec in 5 seconds.I released the helium source right away,t but the conditioning station is full of helium  molecules already, and the leak rate on LD stays at 1xE-5 atm.cc /sec.  The leak on this circuit is huge.    Other water lines are good.        

Entry  Wednesday, April 22, 2015, 11:05, David Wang, Conditioning Station, Standard Operation, TM1, , electrical check on TM1 at CS under vacuum 

I did an electrical check on TM1 at CS. The resistance check:A-B 3.918m ohm, A-C 5.905m ohm,A-D 4.070m ohm,B-C5.462m ohm,B-D3.633m ohm. They are very close to the check we did in SHC. The only unusual thing I found during the check is the ohmmeter reading between A and 60 KV common (6.2K )and the Megga reading between them  at 250 V which is 0. I repeated 4 times and always got the same readings. However, after so many times check, the Megga reading between A and 60KV   suddenly went back to normal(300 M at 250V) at the final check.  And,it stays at 300M now.  All other measurements are same as we did at SHC before.         

Entry  Tuesday, April 21, 2015, 17:14, Isaac Earle, South Hot-Cell, Standard Operation, TM1, UC#12, UC#12 Installed in TM1 IMG_4836.JPGIMG_4833.JPG

On Friday April 17th, UC#12 target was installed in TM1.  One of the copper water lines was bent slightly as the target was lifted into the module which caused ~15 minute delay due to difficulty getting the VCR nut threads to engage.  Other than this the install went smoothly.

During replacement of the containment box panel two of the threaded holes were found to be stripped.  One on the top at the center, the other in the bottom right corner.  These two holes were left without fasteners (see attached photo).  It is unknown at this time whether these holes were already stripped, or if they were stripped during this installation.

Entry  Tuesday, April 21, 2015, 13:01, Grant Minor, ITW, Development, TM2, , TM2 MK4 Optics Tray - banana plug bore modification (on bench) ita6092_redlines_gminor_21apr2015.pdfTM2_Optics_Tray_Bore_Mod_21Apr2015_1.JPGTM2_Optics_Tray_Bore_Mod_21Apr2015_2.JPGTM2_Optics_Tray_Bore_Mod_21Apr2015_3.JPG

The MK4 optics tray prepared for TM2 (as per ITA6082) had an undersized bore for the banana plug, making insertion of the plug extremely difficult / impossible.

Reference stores parts were collected to check the fit:  male plug 3-4/01152 and female jack 1-6/1201.  The size of the female jack was checked with a #21 drill at .159".

The bore on the optics tray was drilled out dry using the #21 drill to the same depth as the original blind hole, by Maico and Dan McDonald.  Chips were carefully collected in a rag, and the hole was blown out with compressed air.

The fit was checked to be snug but possible, using the male plug and the Remote Handling ultem base (ref ITA6023).

Redlines and photos are attached.

 

Entry  Monday, April 20, 2015, 10:22, David Wang, Conditioning Station, Standard Operation, TM1, UCx12, TM1 with UCx12 has been connected to CS and ready for conditioing. 

The TH will be locked during the TM1 conditioning time due to  an interference issue between CS HV cover and a gas analysis valve on top of TM1. A work permit has been issued for the conditioning job because of it.

Entry  Monday, April 20, 2015, 10:12, Anders Mjos, Conditioning Station, Standard Operation, TM1, UC#12, Conditioning UC#12 

Monday, April 20, 2015, 09:35: Started cooling water circulation

HV cover did not fit due to interference with the air sampling valve. Target Hall will have to be locked out for conditioning to proceed. WP I2015-04-20-2

Monday, April 20, 2015, 10:09: Started chiller staging

Target hall and HV enclosure has been locked out.

Monday, April 20, 2015, 13:45: 22 kV, 0.04 mA BIAS 

Monday, April 20, 2015, 14:58: No sparks observed. BIAS off


Tuesday, April 21, 2015, 08:26:  Starting heater auto-ramp to 500 / 230 A at 2 A/min

Tuesday, April 21, 2015, 08:32: BIAS/EE to 20 / 1.5 kV

Tuesday, April 21, 2015, 12:59: TGHT / TBHT at 327 / 230 A. Pausing the auto-ramping. Bill will be monitoring TCS while I am off-site.

Tuesday, April 21, 2015, 15:56: Continue auto-ramping

Tuesday, April 21, 2015, 17:34: Auto-ramping finished. TGHT / TBHT at 500 / 230 A


Wednesday, April 22, 2015, 08:43: Vacuum tripped heaters and BIAS over night. Switching off to do a leak check on the service cap.

Wednesday, April 22, 2015, 09:03: Stopping turbo and roughing pump for David. David is preparing a leak check.

Wednesday, April 22, 2015, 09:06: Started roughing pump.

Wednesday, April 22, 2015, 09:22: Roughing pump trips off after a few minutes of pumping.

Wednesday, April 22, 2015, 13:11: Stopped water flow.

Wednesday, April 22, 2015, 16:07: Starting turbos 

Wednesday, April 22, 2015, 16:15: All turbos at speed.


David found a leak on the window line this morning.
https://elog.triumf.ca/TIS/RH-ISAC/896

Thursday, April 23, 2015, 11:12 : Starting cooling pack

Good vacuum limit on IG1 changed from 7E-5 T to 1E-5 T

Thursday, April 23, 2015, 12:53 : Starting heater auto-ramp to 500 / 230 A at 2 A/min. Bad vacuum limit reduced to 8E-6 T

Thursday, April 23, 2015, 13:03 : BIAS/EE to 15/ 1.5 kV

Thursday, April 23, 2015, 13:28 : BIAS/EE to 20/ 1.5 kV. No sparking observed

Thursday, April 23, 2015, 17:23: Auto-ramping finished. TGHT / TBHT at 500 / 230 A

Thursday, April 23, 2015, 17:51: Fault on cooling circuit (Fault 2).. Manually starting CP1

Thursday, April 23, 2015, 18:01: Cycled power of chiller unit. System recovered. Enabled staging.

Thursday, April 23, 2015, 18:42 : One minor spark observed. Starting cool down at 12 and 9 A/min

Thursday, April 23, 2015, 19:51 : Heaters and BIAS off


Friday, April 24, 2015, 08:21 : Water cooling off

Entry  Monday, April 20, 2015, 07:27, David Wang, ITE, Standard Operation, TM4, , Target Hall Scheduled Activities April 07 - June 26 2015 Target_Hall_Scheduled_Activities__Apr_07_to_June_26_2015.mppTarget_Hall_Scheduled_Activities__Apr_07_to_June_26_2015.pdfTarget_Hall_Scheduled_Activities__Apr_07_to_June_26_2015.pdfTarget_Hall_Scheduled_Activities__Apr_07_to_June_26_2015.mpp

Weekly target hall schedule update.2015-04-20

weekly target hall schedule update 2015-04-27 attachments 3,4.

Entry  Friday, April 17, 2015, 14:04, Travis Cave, South Hot-Cell, Standard Operation, TM1, UC#12, Module move 

TM#1 with UCx#12 has been moved from the south hot cell to the conditioning station.

Entry  Friday, April 17, 2015, 11:56, Travis Cave, South Hot-Cell, Standard Operation, TM1, UC#12, Electrical check TM1_UC#12_tgt_elec_chk_SHC.PDF

Electrical check of TM#1 with UCx#12 attached. See attached PDF for details.

Entry  Friday, April 17, 2015, 09:09, Travis Cave, South Hot-Cell, Standard Operation, TM1, No target, Module move 

TM#1 with no target has been moved from the south west silo to the south hot cell for the installation of the UCx target.

Entry  Wednesday, April 15, 2015, 09:01, Anders Mjos, Conditioning Station, Development, , , Archiver variables added by Controls 

 

 

 

 

 

 

 

 

 

 

The following variable have been added to the archiver (as per work request)

TCS:TS5:RDTEMP 
TCS:TCM1:EE:RDTEMP 
TCS:TCM1:COIL1:RDTEMP 
TCS:TCM1:TBHT:RDTEMP 
TCS:TCM1:TGHT:RDTEMP 
TCS:TCM1:MSP:RDTEMP 
TCS:TCM1:HVC1:RDTEMP 
TCS:TCM1:HS:RDTEMP 
TCS:FC:SCALECUR 
TCS:COL:SCALECUR 
TCS:TK2:RDLEVEL 
TCS:TK2:RDLEVEL 
TCS:DIF1:RDFLOW 
TCS:CHILL:RDHRS

The archiver was restarted.

 

 

Entry  Monday, April 13, 2015, 08:59, David Wang, ITE, Standard Operation, , , Target Hall Scheduled Activities April 07 - June 26 2015 Target_Hall_Scheduled_Activities__Apr_07_to_June_26_2015.pdfTarget_Hall_Scheduled_Activities__Apr_07_to_June_26_2015.mppTarget_Hall_Scheduled_Activities__Apr_07_to_June_26_2015.pdfTarget_Hall_Scheduled_Activities__Apr_07_to_June_26_2015.mpp

See attachments 1, 2 for target hall schedule from 07 April to 26 June 2015. The first TM1 move which is scheduled on 16 April 2015 could be delayed because of SHC operator availability. I will update the schedule once Don confirms the move date with Isaac.

Updated the schedule. The TM1 move has been re-scheduled to Friday, 17 April 2015.    See attachments 3,4.

Entry  Friday, April 10, 2015, 15:40, David Wang, ITE, Standard Operation, TM4, , 5 Shielding blocks have been transferred from ITW to ITE. 

5 shielding  blocks have been transferred to ITE. The ITE is configured to take proton beam.

Entry  Wednesday, April 01, 2015, 13:12, David Wang, ITE, Standard Operation, TM4, Ta#45, TM4 has been connected in ITE 

TM4 has been connected in ITE. ITE six turbo-pumps have been started. So far so good.

Entry  Wednesday, April 01, 2015, 13:08, David Wang, ITE, Standard Operation, TM4, , Replaced ITE tank to module 42X0.275 o-ring 001.JPG002.JPG004.JPG005.JPG006.JPG

I replaced ITE tank to module 42 ID X 0.275 o-ring. The o-ring is changed once a year before the first beam time. The flanges was cleaned and the new o-ring was installed. It works fine.

Entry  Wednesday, April 01, 2015, 10:52, Travis Cave, ITE, Standard Operation, TM4, Ta#45, Module move 

TM#4 with Ta#45 has been moved from the conditioning station to the east target station.

Entry  Wednesday, April 01, 2015, 06:56, David Wang, Conditioning Station, Standard Operation, TM4, Ta#45, TM4 has been disconnected at CS. 

TM4 has been disconnected at CS. The CS and TM4 is venting for move. Anders stopped vacuum and water system yesterday.

Entry  Tuesday, March 31, 2015, 11:36, chad fisher, South Hot-Cell, Development, TM2, , TM2 Optics Tray Complete 20150331_OPTICS_FRONT.jpg20150331_OPTICS_MIDDLE.jpg20150331_OPTICS_BACK.jpg

TM2 optics tray is complete.

Master alignment tray: 0 up/down, 0 left/right

Optics tray: Front 0 up/down, 0 left/right. Middle 0 up/down, 0 left/right. Back 0 up/down, 0 left right.

 

Entry  Monday, March 30, 2015, 09:03, Anders Mjos, Conditioning Station, Standard Operation, TM4, Ta#45, Ta#45 Conditionoing Ta#45_Conditioning.docx

Monday, March 30, 2015, 08:59: Reset chiller by switching on off power (fault 2)

Monday, March 30, 2015, 09:02: Switched on CHILL:CP2, TS5 at 34 C

Monday, March 30, 2015, 10:24 : Cage locked. EE to GND. BIAS and EL ON.

Troubleshooting BIAS current limiting. Turned out to be a EPICS initialization issue. Resolved by setting/changing the current limit again in EPICS.

Monday, March 30, 2015, 14:00: BIAS/EL 18 / 9 kV

Monday, March 30, 2015, 14:16: BIAS/EL 24 / 12 kV

Monday, March 30, 2015, 16:03: BIAS/EL 30 / 15 kV. Occasional sparking while stepping up since 26 kV

Monday, March 30, 2015, 16:13: BIAS/EL 30.8 / 15 kV. 110% of scheduled 28 kV. BIAS/EL 0.04 / 0.09 mA

Monday, March 30, 2015, 17:26 : Maintained BIAS over 1 hour. One spark after.

Monday, March 30, 2015, 17:27 : BIAS / EL off.


Tuesday, March 31, 2015, 08:12: Cage access. EE to EE PS. Cage locked.

Tuesday, March 31, 2015, 08:24: BIAS/EL/EE at 30.8 / 15 / 1 kV

Tuesday, March 31, 2015, 08:26 : EE to 2 kV, 1.96 mA

Tuesday, March 31, 2015, 08:46: No sparks for 20 min.

Tuesday, March 31, 2015, 08:48 : BIAS/EL/EE at 20 / 9.3 / 1.5 kV

Tuesday, March 31, 2015, 08:57: Started auto ramping of heaters to 580 / 230 A at 2 A/min.

Tuesday, March 31, 2015, 10:54: TBHT at 230 A

Tuesday, March 31, 2015, 14:05: TGHT at 580 A

Tuesday, March 31, 2015, 14:21: BIAS/EL/EE to 30.8 / 15 / 2 kV

Tuesday, March 31, 2015, 17:48: Source stable for 4h

Tuesday, March 31, 2015, 18:20: Lowered IAS/EL/EE to 20 / 9.3 / 1.5 kV. IG2 at 6.2E-6 T

Tuesday, March 31, 2015, 21:27: Starting ramp down at 15/12 A/min. IG2 at 6.8E-6 T

Tuesday, March 31, 2015, 21:51: BIAS/EL/EE to zero and off. IG2 at 6.6E-6 T

Tuesday, March 31, 2015, 22:17: TGHT and TBHT off

Tuesday, March 31, 2015, 22:41: Turbos off.

Tuesday, March 31, 2015, 22:42: Water off.

Entry  Monday, March 30, 2015, 07:38, David Wang, ITE, Standard Operation, TM4, , TH Shut Down Activities Schedule Feb 23th- Apr 15th update Target_Hall_shut_down_activities.pdfTarget_Hall_shut_down_activities.mppTarget_Hall_shut_down_activities.pdfTarget_Hall_shut_down_activities.mpp

Updated schedule this morning after last Fridays ISAC facility support group meeting.

Updated schedule on 2015-April -02. See attachments 3,4. The scheduled all shut down jobs are done on time.The TM2 move to SHC will be delayed to May.There will be a new beam running time TH activities schedule (start from April 15) replacing this shut down schedule on next time  weekly update.

Entry  Friday, March 27, 2015, 11:29, David Wang, Conditioning Station, Standard Operation, TM4, Ta#45, TM4 is connected at CS 010.JPG013.JPG012.JPG

TM4 has been connected at CS which includes high current cables, water lines, EE cable, and Enizel lens cable. The HV cover has been  installed onto the TM4 service cap.The CS water system is started. All water signals are good so far.   Anders will start  HV and heaters conditioning on next Monday.

Entry  Friday, March 27, 2015, 10:03, David Wang, Conditioning Station, Standard Operation, TM4, Ta#45, Helium pressure test on TM4 HS line at CS 001.JPG005.JPG006.JPG

The helium pressure test on TM4 HS line at conditioning station is done. No leak. I also leak checked all vacuum seals on TM4 service cap. They are all good.

Entry  Thursday, March 26, 2015, 09:20, Travis Cave, Conditioning Station, Standard Operation, TM4, Ta#45, Electrical check TM4_Ta#45_tgt_elec_chk_CS.PDF

Electrical check of TM#4 with Ta#45 at the conditioning station, see attached pdf for details.

Entry  Wednesday, March 25, 2015, 14:34, David Wang, Conditioning Station, Standard Operation, TM4, Ta#45, TM4 and CS turbo- pumps are started . 

I connected TM4 and CS vacuum system after TM4 move. CS roughing pump was started first this morning. Later, Anders, Bill and I started 3 turbo pumps on TM4 and CS. The pumping down is good so far. The CS vacuum system ion gauges are turned on also.

Entry  Wednesday, March 25, 2015, 14:25, David Wang, South Hot-Cell, Standard Operation, TM4, Ta#45, Leak check on TM4 HS water line with new Ta#45 target. at SHC 

Chad and I leak checked TM4 HS water line with new Ta#45 target installed at SHC. Leak detector base leak rate 0.0Xe-9 atm.cc/sec, base pressure 0.0Xe-4 torr. Chad sprayed helium twice on each of HS 2 VCR joints.No leak has been found. The joints are leak tight. The helium pressure test  will be done at CS later.

Entry  Wednesday, March 25, 2015, 10:37, chad fisher, South Hot-Cell, Development, , , TM2 optics tray build 20150325_101718.jpg20150325_101735.jpg20150325_102024.jpg

TM2 optics tray build is continuing. Going well. Hope to have assembly and alignment finished by Friday.

 

 

Entry  Tuesday, March 24, 2015, 13:57, Travis Cave, South Hot-Cell, Standard Operation, TM4, Ta#45, Electrical check TM4_no_tgt_elec_chk_CS.PDFTM4_Ta45_elec_chk_SHC.PDF

TM#4 electrical checks with and without the target installed, installed target is Ta#45.

Entry  Tuesday, March 24, 2015, 09:47, chad fisher, South Hot-Cell, Standard Operation, TM4, Ta#45, Ta#45 installed 

Ta#45 has been installed onto TM4 and is ready for leak and electrical check. High current fasteners torqued to 130 in.lbs.

 

 

Entry  Tuesday, March 24, 2015, 08:46, Travis Cave, Conditioning Station, Standard Operation, TM4, No target, Module move 

TM#4  with no target has been moved from conditioning station to the south hot cell.

Entry  Monday, March 23, 2015, 14:03, chad fisher, South Hot-Cell, Standard Operation, , Ta#45, Ta#45 inserted into hot cell 

Ta#45 has been inserted into the hot cell. Swipe taken of inner tool port area: 100000 counts/min.

Entry  Monday, March 23, 2015, 07:56, David Wang, ITE, Standard Operation, , , TH Shut Down Activities Schedule Feb 23th- Apr 15th update Target_Hall_shut_down_activities.pdfTarget_Hall_shut_down_activities.mppTarget_Hall_shut_down_activities.pdfTarget_Hall_shut_down_activities.mpp

This schedule is following Dons schedule on module moves. See attachments for updating.

2015-03-27: Weekly update the schedule. The shut down job is close to the end. See attachment 3, 4.

Entry  Friday, March 20, 2015, 13:37, chad fisher, South Hot-Cell, Development, , , TM2 Optics Tray 20150320_113132[2].jpg20150320_113018_1[1].jpg

Final assembly and alignment of TM2 optics tray continued today. Front section is "aligned".

Entry  Tuesday, March 17, 2015, 10:33, Travis Cave, Spent Target Vault, Standard Operation, , UC#11, Spent Target Move Vault_Storage_March_17_2015.pdf

The spent UC#11 has benn moved from the south hot cell to the spent target vault. See attached PDF for details.

Entry  Monday, March 16, 2015, 14:16, Travis Cave, Conditioning Station, Standard Operation, TM4, No target, Module move 

TM#4 from south hot cell to the conditioning station no target is attached to the module.

Entry  Monday, March 16, 2015, 09:41, Travis Cave, ITE, Standard Operation, TM4, UC#11, Module move 

TM#4 with UC#11 moved from the east target station to the south hot cell.

Entry  Friday, March 13, 2015, 13:36, Travis Cave, Spent Target Vault, Standard Operation, , ThO#1, Spent Target Move Storage_Vault_March_13_2015.pdf

The ThO#1 has been placed in the storage vault placed in pail #122 in spot 2B of the vault. It was 6.2mSv/hr upon removal from the south hot cell. see attached PDF for details.

Entry  Thursday, March 12, 2015, 13:33, Anders Mjos, South Hot-Cell, Standard Operation, TM1, ThO#1, Target inspection 

Chad, Anders and Alex inspected the target this morning. The target had no significant visible damage to the container. Some material was deposited on the Extraction Electrode.

Phots on DocuShare

Entry  Thursday, March 12, 2015, 13:04, David Wang, ITE, Standard Operation, TM4, , 5 Shielding blocks have been transferred from ITE to ITW. 

5 shielding blocks have been transferred from ITE to ITW for next week TM4 move.

Entry  Thursday, March 12, 2015, 09:48, Travis Cave, South Hot-Cell, Standard Operation, TM2, No target , Module move 

TM#2 with no target and no source tray has been moved from the conditioning station to the north east silo.

Entry  Tuesday, March 10, 2015, 09:01, Travis Cave, South Hot-Cell, Standard Operation, TM1, ThO#1, Module move TM1_THO_elec_chk_postbeamSHC.PDF

TM#1 has been moved from the west station to the south hot cell had the ThO#1 target removed and then the modules was moved from the south hot cell to the south west silo. Also an electrical check was done on the target before it was removed.

Entry  Monday, March 09, 2015, 14:01, chad fisher, South Hot-Cell, Standard Operation, TM1, ThO#1, ThO#1 removed 

ThO#1 has been removed from TM1 and placed into the plastic dissection box.

Containment box cover has been reinstalled as per usual.

Entry  Monday, March 09, 2015, 09:42, chad fisher, South Hot-Cell, Development, , , Hot Cell Table Swiping 

3 swipes of the south hot cell table were taken from the target hall through the roof hatch (2 standard, 1 alpha).

Initial results of the table swipes are pending however swipes of the pool tool and end effector are clean, 0 counts, booties, gloves clean.

Fall arrest equipment has a puzzling 6000 counts, and suit 500 counts.

 

 

Entry  Thursday, March 05, 2015, 14:30, chad fisher, South Hot-Cell, Development, , , Dissection Box 20150305_142144.jpg

Box for dissecting targets almost complete. Should be done tomorrow.

Entry  Thursday, March 05, 2015, 07:17, David Wang, ITW, Standard Operation, , , TH Shut Down Activities Schedule Feb 23th- Apr 15th update 6x

TH shut down jobs are processing as scheduled this week. Discussed with Don, and we think the jobs scheduled in next week should be processed as we planned. See attachments for updated schedule.

I updated the schedule today. See attachment 3, 4 for updating.  2015-Mar-10.

2013-Mar -13, I updated the schedule to show the jobs we finished this week. See attachment 5,6

Entry  Thursday, March 05, 2015, 06:44, David Wang, ITE, Maintenance, TM4, , 5 Shielding blocks have been moved to ITE. 

5 Shielding blocks have been moved to ITE for next week TM1 move and RPG Radon test.

Entry  Monday, March 02, 2015, 10:52, David Wang, ITE, Maintenance, TM4, UCx, ITE primary and secondary vacuum vessels leak check. 

Dan and I leak checked ITE primary and secondary vacuum vessels with TM4  in ITE. The leak detector was hooked to ITE TP2 BV2. Leak detector  base leak rate: 0.0xE-09 atm.cc/sec, base pressure: 0.0xE-4 torr. All secondary vacuum vessel seals has been checked(helium spray), and no leak has been found. On the ITE primary vacuum vessel, we  leak checked every thing except the TM4 service cap and water lines inside the TM4. NO leak has been found on ITE primary vessels. The primary vacuum seals on TM4 service cap and TM4 waterlines(helium pressure test) will be checked at CS later.

Entry  Friday, February 27, 2015, 09:34, chad fisher, South Hot-Cell, Maintenance, , , Hot cell Entry February 25 2015 ISAC_South_Hot_Cell_Entry.pdf

See attached report.

Summary:

Radio problems just before entry to cell. Inspection afterwards revealed batteries charge but battery in one radio shorts out after a couple loads/cycles.

Fields in hot cell range from 630 uSv/h @ 1 m to 1.5mSv/h @ 1m. Contributing to the fields is the febiad coil line removed from TM4 in the south west corner of the hot cell.

Contamination/particulate on table as mostly black colored and of a fairly substantial size, but seamingly easy to collect. Distinquishable pieces of target material present.

Hot cell window show no sign of leaking on the inside of cell.

Pre-filter changed.

Manipulators lubricated.

Hot cell entry procedures appear to still be fairly successful in minimizing contamination migration from the hot cell.

 

Entry  Thursday, February 26, 2015, 09:22, David Wang, ITW, Standard Operation, , , TH Shut Down Activities Schedule Feb 23th- Mar 25th Target_Hall_shut_down_activities.mppTarget_Hall_shut_down_activities.pdf

TH shut down activities schedule from Feb 23th-March 25th. The schedule will be updated each week. See attachment 1.

Feb-27-2015: Updated the schedule, and uploaded as PDF file. See attachment 2.

Entry  Wednesday, February 25, 2015, 10:44, David Wang, ITW, Maintenance, , , 2015 shut dwon ITW water sensor coils and pedal wheels replacement 2015_shut_down_ITW_water_sensors__replacements.pdf

Dan and I replaced pedal wheels and coils on ITW water flow sensors. It is a shut down job we did every two years. See attachment for detail.

Entry  Monday, February 23, 2015, 12:28, David Wang, ITE, Maintenance, , , 2015 shut down coils and pedal wheels replacement on ITE water flow sensors. 2015_shut_down_ITE_water_sensors__replacements.pdf

Dan and I replaced pedal wheels and coils on ITE water flow sensors. It is a shut down job we did every two years. See attachment for detail.

Entry  Tuesday, February 17, 2015, 13:07, Anders Mjos, ITW, Development, , , Resistance measured of TGHT and TBHT lines to ITW 

 See e-log entry for ITE for details. The copper bars have not been removed. They can be used for testing the new power supplies.

Local measurement was done by Ray with a voltmeter. The voltmeter was consistent with EPICS readback and local readback on the power supplies. A voltage drop of 0.137 V @ 580 A was measured across the bus bar from the TGHT power supply to the cooled transmission lines.

Entry  Tuesday, February 17, 2015, 13:06, Anders Mjos, ITE, Development, , , Resistance measured of TGHT and TBHT lines to ITE 002.JPGResistance_from_Electrical_Room_to_Target_Station.xlsx

The copper bars was installed by David and Anders. After the measurements were completed, the copper bars were removed.

See photo and attached spread sheet.

Entry  Monday, February 16, 2015, 11:57, David Wang, Crane, Repair, , , TH crane 

Dave.Morris installed a new battery on crane control PLC board and uploaded the program. Travis, Dan and I tested the crane in local, remote, and test mode. The crane works fine. Also, the TH lock up has been tested. Everything is good.

Entry  Thursday, February 12, 2015, 09:11, David Wang, Crane, Repair, TM4, , TH crane troubleshoot and annual inspection. 

Gordon crane technicians continued their troubleshooting on this Tuesday. They found the crane up-limit protection switch which is installed on the same bracket with the the crane down view camera is broken. The spring inside the limit switch  which is used for pushing the action plunge out in the switch lost its function. This up limit switch is the last protection for the crane so it is set as when it is in action the crane main contact coil  which controls crane  power supply will be in open position. The broken switch is replaced by a new one( same type) on this Wednesday. The crane annual inspection has been  finished after the switch replacement. The crane works fine now.

Entry  Wednesday, February 11, 2015, 13:13, chad fisher, South Hot-Cell, Maintenance, , , New gas bottle storage rack 20150211_115656.jpg

The new gas bottle storage rack has been installed by/for the south hot cell.

 

Entry  Friday, February 06, 2015, 12:27, David Wang, Crane, Repair, , , TH crane troubleshoot  

Gordon crane technician started TH crane trouble shooting this morning. The problem is found that there is no 115VAC power supply to energize  a main coil which is used to switch on 450V AC power supply to crane. He did a test and found  the crane could be operated  by big yellow pedant in control room when he manually gave the coil 115VAC power supply to energize it.. At that moment, the crane is set to big yellow pedant operating mode. But, he can not figure out why there is no 115VAC power to this coil.The wiring  tracking back is not an easy job for him. The troubleshooting is  stopped now. The job will be resumed on next week with more skilled technician involving in from Gordon crane.

Entry  Friday, February 06, 2015, 08:06, David Wang, Crane, Repair, , , TH crane lost movement controls since last Friday. 

Last Friday, During the crane per use check, I found the main power supply to to crane was shut off. I was told   Don and Travis shut off the main power before Triumf power outage. Travis restored crane main power and I  could turn on the main relay on radio pedant  in TH.  But, I didnt have all crane main bridge movement controls on TH raido pedant except rotation. I still have all movement controls on small trolley from the radio pedant. When I operated radio pedant, Travis could hear the relay works in crane control room, but in TH no crane movements. It looks like a crane control problem so Dave Morris was contacted. Dave found one of battery on PLC board is dead and need to be replaced.He did order the battery right way. On this Wednesday, Dave noticed us we could temporarily run the crane. I went to T.H  for checking. At the beginning, I found I cant not turn on the crane main relay from radio pedant in TH. Don was in crane control room. He switched the crane control from TH radio  mode to control room pedant( big yellow control box laid on the ground, the mode switch is located on the up left corner of first main panel)  and he turned on the main relay by doing this and got all movement controls from the big yellow pedant. After switching the mode back to TH radio mode I also got all the controls from TH radio pedant. Everything worked fine on crane so we moved the man lift into TH on Wednesday afternoon and arranged the TH crane inspection on Thursday. On Thursday morning, Gordon Crane guys came in TH and started their inspection. At the beginning, everything works fine. But after they did some operation and checks on crane, the crane main relay could not be switched on again (from TH  raid box). The crane inspection job are suspended. RH group tried to active the main relay by switching the mode back to yellow pedant in crane control room just like we did on Wedsday, but it did not work this time. David Morris was contacted to check from his side if anything wrong. He checked and told us the program is working and everything  is good from his side. A crane expert is needed to trouble shoot this problem. Neil Wong is going to bring Gordon crane guys and start to trouble shoot the problem this morning.

Entry  Monday, February 02, 2015, 14:06, chad fisher, South Hot-Cell, Repair, TM2, , TM2 Tray build TM2_Tray_20150202_134752.jpgTM2_Tray_20150202_134759.jpg

Master target jig installed to locate attachment bracket ITA3389 as well as conductor insulator block b (aluminum / for soldering version) and oven conductor blocks (ITD0353 and 03356). 

There were NO ITA6145 fasteners or TGN0076 either. Standard 1/4-20 x 1" fasteners have been used in there place for now. Keith is following up with getting the missing fasteners into the shop.

Oven conductor blocks will have to be lapped before lines are attached as they both have dents on the high current mating surfaces.

 

 

 

Entry  Monday, February 02, 2015, 09:59, chad fisher, South Hot-Cell, Repair, TM2, , TM2 Tray Build 

Missing heli coils installed this morning.

Threads had to be chased with tap for 1/4-20 heli coil and missing countersinks hand applied to allow for installation. Care was taken to ensure no "swarf" was spread and operation was super clean. Chased holes blown out with canned air and a vacuum placed on the other side.

Final assembly can and will now continue.

Entry  Thursday, January 29, 2015, 11:31, chad fisher, South Hot-Cell, Repair, TM2, , TM2 Tray Build TM2_Tray_20150126_112232.jpg

On Tuesday morning I attempted to complete assembly of the source tray for TM2 however discovered that 3 1/4-20 x 0.25 titanium helicoils had not been installed into the mounting plate as they should have been. Checked and asked around for them but to no avail. I have ordered some, they should have been here yesterday.

Also, I have noticed that the threaded portion of the target pins ITA0328A appear to be too long and as such may be (are indeed) touching the supports. I am going to remove 1/32" or appropriate to remedy this problem (drawing shows 0.035 clearance).

Entry  Wednesday, January 28, 2015, 10:42, Anders Mjos, Conditioning Station, Maintenance, TM2, , TCS shut down for site wide power outage 
 
Entry  Monday, January 26, 2015, 09:36, chad fisher, South Hot-Cell, Repair, TM2, , TM2 Tray Alignment TM2_Tray_20150126_090448.jpg

TM2 tray alignment was confirmed with the alignment tray this morning:

Front target 0.000 vertically, 0.000 horizontally.

Back target 0.003 low, 0.000 horizontally

Also, the master target jig was installed and measurements taken:

Front master target - 0.007 high, 0.000 left/right

Rear Master Target - 0.007 high, 0.000 left/right

Rear tray target - 0.003 low

 

Entry  Tuesday, January 20, 2015, 13:45, chad fisher, South Hot-Cell, Repair, TM2, , TM2 Tray Alignment TM2Alignment_Target_Front_Jan_20.jpgTM2_Alignment_Target_Rear_Jan_20.jpg

TM2 Tray Alignment is complete except for verification with alignment tray.

First attempt results were:

Front Target: Low 0.011, Left 0.011

Rear Target: Low 0.013, Left 0.002

Final iteration:

Front Target: Vertical 0, Horizontal 0

Rear target: Vertical - 0.003 low, Horizontal 0

Pictures were very hard to get but are below...camera is impossible to get square to lens so pictures are not entirely representative of looking through transit.

 

Entry  Monday, January 12, 2015, 14:29, chad fisher, South Hot-Cell, Repair, TM2, , TM2 Tray Build Status TM2_Tray_20150112_01.jpg

Countersink problem with supports has been remedied. Scratches, dings, and pitting has been buffed out and supports re-cleaned and re-assembled.

Friedhelm was consulted regarding the appearance of fine scratches on the main stand-off insulators...the best two matching ones were chosen and assembly continued.

Alignment will start tomorrow.

 

 

Entry  Thursday, January 08, 2015, 15:24, Anders Mjos, Conditioning Station, Development, TM2, , Fault 2 on chiller unit Capture.PNGVFD_Fault.jpg

 Found both VFDs with OF3 fault (over voltage during constant speed operation).

Thursday, January 08, 2015, 16:37: Cycled power on the chiller to clear faults.

Entry  Thursday, January 08, 2015, 10:34, chad fisher, South Hot-Cell, Standard Operation, , , TM2 Tray Build Status and Problems TM2_Tray_20150108_09.jpgTM2_Tray_20150108_10.jpgTM2_Tray_20150108_11.jpgTM2_Tray_20150108_12.jpg

Final assembly of the source tray for TM2 was started this morning.

Sliding tray was received from keensert installation and cleaned.

Mounting plate/ionizer tube location jig was rechecked against assembly ITA3136...Mounting plate was loosened, jigs for centering the ceramic shields installed and fasteners re-torqued to 57 in lbs.

Upon attempted assemble of ITA3536 and 3537 (support frames) it was noticed that the countersinks were not deep enough...the heads of the screws protrude and would interfere with/damage the support insulators. These items have been given to Dan to have the counterbores adjusted...drawing should be changed to insure a small gap.

Also, one of the support frames has marks on its side that may be a high voltage issue.

Upon inspection of the components in question (ITA3540 & 3538) it was found that they have been made to spec and model; however the spec& model does not allow for adequate theoretical clearance given tolerances. Countersinks will be adjusted and changes documented.

"Pitting" will attempt to be lapped.

 

Entry  Thursday, January 08, 2015, 08:04, David Wang, ITE, Standard Operation, TM4, , TM4 water lines have been disconnected in ITE and purged. 

TM4 waterlines have been disconnected and purged in ITE. The TM4 vacuum system is still in operation.

Entry  Wednesday, January 07, 2015, 09:31, Anders Mjos, Conditioning Station, Development, TM2, , High Voltage Conditioning 

No Source Tray installed. Loop on cooling circuit D. All other circuits blanked off.

Voltages stated below are set point voltages. These corresponds reasonably well with the local read backs on the power supplies. The read back voltages in EPICS are somewhat lower.

Wednesday, January 07, 2015, 09:16: 20 / 10 kV (BIAS / EL)

Wednesday, January 07, 2015, 09:20: Vacuum responses from BIAS 27 kV. Corresponds to each increase in bias voltage.

Wednesday, January 07, 2015, 09:40: 30 / 15 kV 

Wednesday, January 07, 2015, 10:28: Sparking and vacuum responses continues with every 100 V BIAS increase. If the voltage is lowered and brought back up, no sparks are observed; the module is conditioning.

Wednesday, January 07, 2015, 12:09: 34 / 17.5 kV

 Wednesday, January 07, 2015, 13:05: 35 / 17.5 kV

Wednesday, January 07, 2015, 14:50: 37.5 / 20 kV

Wednesday, January 07, 2015, 15:40: 38.5 / 20 kV

Wednesday, January 07, 2015, 16:02: BIAS and EL power supplies off.


Thursday, January 08, 2015, 10:00: HV condtioning continues

Thursday, January 08, 2015, 10:11: 35 / 20 kV

Thursday, January 08, 2015, 10:29: 38.5 / 20 kV

Thursday, January 08, 2015, 11:43: 40 / 20 kV

about 15 sparks per hour (5 / 20 min)

Thursday, January 08, 2015, 14:41: 42.5 / 22.5 kV

Thursday, January 08, 2015, 15:08: Communication lost with RGA. Could not be recovered.

Thursday, January 08, 2015, 15:58: 45 / 22.5 kV

Thursday, January 08, 2015, 16:27: BIAS and EL power supplies off.


Friday, January 09, 2015, 08:52: 45 / 22.5 kV

Tried to recover RGA by unplugging and plugging power cord, but no success.

Friday, January 09, 2015, 10:45: Increased sparking at 48 kV - reduced to 47.5 kV

Friday, January 09, 2015, 11:53 : 50 / 25 kV

Friday, January 09, 2015, 12:28: ~ 1 spark / minute for the last 10 min

 Friday, January 09, 2015, 15:27: ~25 sparks / hour for the last 20 min

Friday, January 09, 2015, 16:18: ~18 sparks / hour for the last 20 min


Monday, January 12, 2015, 09:31: 50 / 25 kV

Monday, January 12, 2015, 10:31: No sparks for 20 min after ~30 min of conditioning.

Monday, January 12, 2015, 12:24: BIAS / EL power supplies tripped on conductivity (spark)

Monday, January 12, 2015, 13:13: 55 / 27.5 kV

Monday, January 12, 2015, 14:32: 1 spark for the last 10 min

Monday, January 12, 2015, 15:38: 57 / 30 kV

Monday, January 12, 2015, 15:48: ~60 sparks / hour for the last 10 min

Monday, January 12, 2015, 16:00: BIAS and EL power supplies off.


Tuesday, January 13, 2015, 08:45: 55 / 27.5 kV

Tuesday, January 13, 2015, 09:18: ~60 sparks / hour for the last 10 min

Tuesday, January 13, 2015, 10:17: No sparks for the last 10 min

Tuesday, January 13, 2015, 10:30: 57.5 / 30 kV

Tuesday, January 13, 2015, 11:34: 59 / 30 kV

Tuesday, January 13, 2015, 13:23: No sparks for the last 25 min 

Tuesday, January 13, 2015, 14:11: 60 / 30 kV

Tuesday, January 13, 2015, 14:42: Spark tripped TP2 and TP1S and both power supplies

Tuesday, January 13, 2015, 15:02: 60 / 30 kV (local read back 60.5 / 30 kV, 0.1 / 0.15 mA)

Tuesday, January 13, 2015, 15:38: BIAS and EL power supplies off.


Wednesday, January 14, 2015, 08:34: 60 / 30 kV

Wednesday, January 14, 2015, 10:41: 3 sparks / hour for the last 60 min

Wednesday, January 14, 2015, 13:39: 61 / 30 kV

Wednesday, January 14, 2015, 14:29: 61.5 / 30 kV (local read back 62 / 30 kV, 0.1 / 0.15 mA)

Wednesday, January 14, 2015, 15:40: ~ 6 sparks / hour for the last 20 min

Wednesday, January 14, 2015, 16:07: TP2 found to be tripped off. Restarted.

Wednesday, January 14, 2015, 16:23: 60 sparks / hour for the last 20 min

Wednesday, January 14, 2015, 16:28: BIAS and EL power supplies off.


Thursday, January 15, 2015, 08:27: 60 / 30 kV

Thursday, January 15, 2015, 11:24: ~35 sparks / hour for the last 20 min

Thursday, January 15, 2015, 14:09: 12 sparks / hour for the last 60 min

Thursday, January 15, 2015, 15:33: 58 / 30 kV

Thursday, January 15, 2015, 15:49: 56 / 30 kV

Sparks observed both at 58 and 56 kV

Thursday, January 15, 2015, 15:57: BIAS and EL power supplies off.


Monday, January 19, 2015, 09:53: 55 / 30 kV

Monday, January 19, 2015, 11:44: ~20 sparks / hour for the last 20 min

Monday, January 19, 2015, 12:53: ~10 sparks / hour for the last 20 min 

Monday, January 19, 2015, 16:30: 50 / 30 kV

Monday, January 19, 2015, 17:31: BIAS and EL power supplies off.


Tuesday, January 20, 2015, 08:54: 40 / 20 kV

Tuesday, January 20, 2015, 09:05: 50 / 25 kV

Tuesday, January 20, 2015, 13:43: 8 sparks / hour for the last 60 min

Tuesday, January 20, 2015, 16:43: 3 sparks / hour for the last 60 min


Wednesday, January 21, 2015, 09:10: 40 / 20 kV

Wednesday, January 21, 2015, 09:20: No sparks

Wednesday, January 21, 2015, 09:23: 50 / 25 kV

Wednesday, January 21, 2015, 10:33: 3 sparks / hour for the last 60 min

Wednesday, January 21, 2015, 13:43: 6 sparks / hour for the last 60 min

Wednesday, January 21, 2015, 16:07: 5 sparks / hour for the last 60 min

Wednesday, January 21, 2015, 16:09: BIAS and EL power supplies off.


Thursday, January 22, 2015, 09:11: 40 / 20 kV

Thursday, January 22, 2015, 10:14: No sparks

Thursday, January 22, 2015, 10:16: 45 / 25 kV

Thursday, January 22, 2015, 11:26: No sparks

Thursday, January 22, 2015, 16:57: No sparks

Thursday, January 22, 2015, 16:57: BIAS and EL power supplies off.


Friday, January 23, 2015, 09:28: 40 / 20 kV

Friday, January 23, 2015, 09:39: No sparks

Friday, January 23, 2015, 09:40: 50 / 25 kV 

Friday, January 23, 2015, 16:16: No sparks.

Friday, January 23, 2015, 16:17: BIAS and EL power supplies off. 


Monday, January 26, 2015, 09:17: 40 / 20 kV

Monday, January 26, 2015, 09:29: No sparks

Monday, January 26, 2015, 09:30: 50 / 25 kV

Monday, January 26, 2015, 09:52: No sparks

Monday, January 26, 2015, 09:53: 55 / 27.5 kV

Monday, January 26, 2015, 16:55: No sparks for 7 hours. BIAS and EL power supplies off. 


Tuesday, January 27, 2015, 09:10: 40 / 20 kV

Tuesday, January 27, 2015, 09:16: 50 / 25 kV  

Tuesday, January 27, 2015, 09:31: 55 / 27.5 kV

Tuesday, January 27, 2015, 09:51: No Sparks

Tuesday, January 27, 2015, 09:53: 57.5 / 30 kV (one spark while increasing BIAS voltage)

Tuesday, January 27, 2015, 10:14: No sparks

Tuesday, January 27, 2015, 10:18: 58 / 30 kV. Some sparks

Tuesday, January 27, 2015, 10:46: 59 / 30 kV. Some sparks while increasing BIAS voltage

Tuesday, January 27, 2015, 11:43: 59.5 / 30 kV. Some sparks while increasing BIAS voltage

Tuesday, January 27, 2015, 13:24: Spark

Tuesday, January 27, 2015, 13:33: 11 sparks for the last 10 min

Tuesday, January 27, 2015, 13:33: 59 / 30 kV

Tuesday, January 27, 2015, 13:35: 57.5 / 30 kV 

Tuesday, January 27, 2015, 16:14: ~3 sparks / hour for the last 60 min

Tuesday, January 27, 2015, 16:53: ~3 sparks / hour for the last 60 min

Tuesday, January 27, 2015, 16:55: BIAS and EL power supplies off. 


Wednesday, January 28, 2015, 09:11: 40 / 20 kV

Wednesday, January 28, 2015, 09:17: 50 / 25 kV 

Wednesday, January 28, 2015, 09:27: 55 / 27.5 kV 

Wednesday, January 28, 2015, 10:35: 11 sparks observed. BIAS and EL off - preparing for power outage

Entry  Tuesday, January 06, 2015, 11:21, Anders Mjos, Conditioning Station, Development, TM2, , He leak check of cooling circuits. 2015-01-06_He_leak_check_water_circuits.pdf

No leak detected on either He-detector (connected directly to Service Cap) or on RGA. See attached screen shots.

A vacuum increase (air only on RGA) was seen when de-pressurizing circuit I.

Entry  Tuesday, January 06, 2015, 11:14, David Wang, ITE, Standard Operation, TM4, , 4 Shielding blocks have been moved out of ITE . 

4 shielding blocks have been moved out of  ITE to block storage area. Fiona did the survey and with me during the move.

Entry  Monday, January 05, 2015, 15:01, Anders Mjos, Conditioning Station, Development, TM2, , RGA switched on 
 
Entry  Monday, January 05, 2015, 12:47, Anders Mjos, Conditioning Station, Development, TM2, , Cooling package started 

 by "enable staging" button. MP3 has to be turned off-on to open WPV1

Entry  Tuesday, December 23, 2014, 14:10, Anders Mjos, Conditioning Station, Development, TM2, , He leak check of the Service Cap using RGA 

The RGA showed no response to He-spray on the Service Cap. He stable at 3.5E-9 T partial pressure, water at 1.3E-6 T. IG1 at 9.9E-8 T

Entry  Monday, December 15, 2014, 15:55, Grant Minor, Conditioning Station, Repair, , , Access to ISAC TCS TK2 Expansion Tank - Fall Arrest TK2_Expansion_Tank_Elevation_ISAC1_Exp_Hall_15Dec2014.JPGTK2_Expansion_Tank_-_Fall_Arrest_Config_1_-_15Dec2014.JPGTK2_Expansion_Tank_-_Fall_Arrest_Config_2_-_15Dec2014.JPGTK2_Expansion_Tank_-_Fall_Arrest_Config_3_-_15Dec2014.JPG

Hello all,

Access was required this morning to the TCS TK2 Expansion Tank to open a valve and re-fill the tank.

As the access path to this tank lacked any form of Fall Protection, Fall Arrest was employed.

Worksafe BC Part 11 Section 11.2 requires fall protection to be employed at elevations greater than 3 meters.  The expansion tank is located at an elevation far exceeding this regulation.
http://www2.worksafebc.com/publications/ohsregulation/part11.asp

The worker, Allon Messenberg, was fitted with a harness, personal self-retracting lifeline / lanyard with shock-pack, and carried two steel rope ring-ended slings with him to tie off to the structural beams overhead.  All products used were DBI-Sala safety products, which are kept in the Remote Handling machine shop Fall Protection Equipment lockers.  Several RH group members have keys to this locker, including me.

Three configurations were required to gain access to the tank (photo attached):
Configuration 1: Traversing the section between the 2nd floor offices and the ventilation duct.
Configuration 2: Traversing the section between the ventilation duct and the "cross point" of the structural beams.
Configuration 3: Tied-off to the "cross point" of the structural beams and working within the reach limits of the personal SRL and shock-pack.

Transitions between the three configurations required brief moments of un-clipping from the harnesses.  This will be solved in the future via the use of additional carabiners and lanyards.

Operations has advised me that they have observed either TRIUMF workers or contractors working in this area without wearing Fall Arrest equipment.  My request is for staff and operations to stay vigilant in observing access to this area. 

Any work performed in this area without the usage of fall arrest must be reported in an NCR.

I welcome any comments from those who have ideas for improving the safe method of access to this tank.

The cooling package is described in the TCS operating manual, Document-103881.  Page 8 states clearly that Fall Arrest is required to access this valve.

Regards,

Grant

Entry  Monday, December 15, 2014, 08:50, Anders Mjos, Conditioning Station, Maintenance, TM2, , TK2 level below 15 in (secondary loop) 

 The level dropped below 15 in over the weekend. MP2 stopped, but MP3 condtinued pumping.

    Reply  Monday, December 15, 2014, 09:41, Anders Mjos, Conditioning Station, Maintenance, TM2, , Water leak found at the isolation transforer 

Anders Mjos wrote:

 The level dropped below 15 in over the weekend. MP2 stopped, but MP3 condtinued pumping.

 e-fault submitted and Niel Wong has been contacted.

Niel Wong came and had a look at the system. We decided to close the circuit as the water is no longer used with the new power supplies. The circuit will be monitored, but not repaired unless it is needed again.

       Reply  Monday, December 15, 2014, 12:53, Anders Mjos, Conditioning Station, Maintenance, TM2, , TCSTK2 topped up 

Anders Mjos wrote:

Anders Mjos wrote:

 The level dropped below 15 in over the weekend. MP2 stopped, but MP3 condtinued pumping.

 e-fault submitted and Niel Wong has been contacted.

Niel Wong came and had a look at the system. We decided to close the circuit as the water is no longer used with the new power supplies. The circuit will be monitored, but not repaired unless it is needed again.

 Due to the water leak, the expansion tank needed topping up. It was filled from 14 in to 20 in. See work permit I2014-12-15-2.

       Reply  Monday, December 15, 2014, 13:25, Anders Mjos, Conditioning Station, Maintenance, TM2, , BIASSW1 temperature and flow removed from interlock chain 

Anders Mjos wrote:

Anders Mjos wrote:

 The level dropped below 15 in over the weekend. MP2 stopped, but MP3 condtinued pumping.

 e-fault submitted and Niel Wong has been contacted.

Niel Wong came and had a look at the system. We decided to close the circuit as the water is no longer used with the new power supplies. The circuit will be monitored, but not repaired unless it is needed again.

The valved off water circuit has been valved off and  TCS:WFB2:BIASSW1 and TCS:TCM2:BIASSW1 have been removed from the power supply interlock chain by Dave Morris.

Entry  Monday, December 08, 2014, 15:22, Anders Mjos, Conditioning Station, Development, TM2, , Circuit D water test TCS_Heater_Transmission_Power.xlsxCircuit_D_test_results_for_TM2_status_meeting_2014-12-11.pdfHeated_water_leak_test_plan.pdfHeated_water_leak_test_Circuit_D_RESULTS.docx

Monday, December 08, 2014, 14:00: Dan M and Anders connected the water supply to circuit D and installed the module cover.

Monday, December 08, 2014, 14:50: Circulating water on circuit D. IG1 vacuum stable at 3.1E-7 T. No response on mass 18 on RGA

Monday, December 08, 2014, 15:30: Test TGHT and TBHT PS. Can be switched on, but set points need to be corrected.

Monday, December 08, 2014, 16:11: Started CHILLCP2

Monday, December 08, 2014, 16:26: Stopped CHILLCP2


Tuesday, December 09, 2014, 09:02: Started CHILLCP1. TS5 at 31.5 C

Tuesday, December 09, 2014, 09:33: Stopped CHILLCP1. TS5 at 17. 1 C

Tuesday, December 09, 2014, 14:54: Tested TGHT to 600 A and 2.05 V (local read back). EPICS read back and set point is not correct. Circuit resistance ~ 3.4 mOhm.

Tuesday, December 09, 2014, 15:14: Tested TBHT to 272 A and 0.97 V (local read back). EPICS read back and set point is not correct. Circuit resistance ~ 3.6 mOhm.

Tuesday, December 09, 2014, 16:01: TGHT and TBHT switched off.


Wednesday, December 10, 2014, 08:30: TGHT and TBHT power supplies cannot be run with TS5 > 25. Bypasses/Forces not implemented. Waiting for controls.

Wednesday, December 10, 2014, 10:44: Water is stable on RGA, however N, O and Ar shows repeated short term spikes of ~4x magnitude. Spikes are also visible on IG1


Vacuum stable over night.

Thursday, December 11, 2014, 08:22: Starting CHILLCP3. TS5 at 33.1 C, TBHT at 30.2 C

Thursday, December 11, 2014, 08:58 : Staging enabled


Vacuum stable over night.

Dave M corrected scale of TGHT and TBHT.

TS5 forced


 

Lost water in expansion tank over the weekend. See other e-log entries regarding the water leak and fix. Vacuum stable over the weekend.

Monday, December 15, 2014, 13:49: TGHT and TBHT PS at 600 A and 270 A

Monday, December 15, 2014, 14:06: TGHT to 700 A

Monday, December 15, 2014, 18:03: Autoramping down at 5 A/15 s

Monday, December 15, 2014, 18:26: TGHT and TBHT at 0 A. TS5 is at 35 C


Vacuum stable over night

Tuesday, December 16, 2014, 08:07: TGHT and TBHT to 700 A and 270 A

Tuesday, December 16, 2014, 09:00: Stopped MP2. MP3 tripped. TGHT and TBHT tripped.

Tuesday, December 16, 2014, 09:05: started MP2, TGHT and TBHT

Tuesday, December 16, 2014, 16:21: TGHT to 600 A. Will leave both TGHT and TBHT on over night to keep the water warm.


Vacuum stable over night. TS5 at 37.5 C TBHT return at 34.5 C

Wednesday, December 17, 2014, 08:15: TGHT to 750 A

Wednesday, December 17, 2014, 08:35 : TGHT to 800 A

Wednesday, December 17, 2014, 16:09 : TGHT to 700 A. TS5 at 40 C TBHT return at 37 C


Vacuum stable over night. TS5 at 39.3 C and TBHT return at 36.2 C

Thursday, December 18, 2014, 07:54: Starting CHILLCP1

Thursday, December 18, 2014, 08:34: Stopped cHILLCP1 TS5 at 20 C

Thursday, December 18, 2014, 09:07: TGHT to 800 A

Thursday, December 18, 2014, 16:10: TGHT to 700 A


Vacuum stable over night. TS5 at 39.0 C and TBHT return at 35.9 C

Friday, December 19, 2014, 08:17: TGHT to 800 A

Friday, December 19, 2014, 11:54: TGHT to 650 A. TS5 at 39.9 C 


Vacuum stable over the weekend. TS5 at 38.4 C and TBHT return at 35.4 C

Monday, December 22, 2014, 08:31 : Started CHILLCP3

Monday, December 22, 2014, 09:30: Stopped CHILLCP3 

Monday, December 22, 2014, 10:08: TGHT to 800 A

Monday, December 22, 2014, 16:25: TGHT to 700 A


Vacuum stable over night. TS5 at 38.4 C and TBHT return at 35.3 C

Tuesday, December 23, 2014, 08:16: TGHT to 800 A

Tuesday, December 23, 2014, 13:10 : Starting CHILLCP3. TS5 at 39.5 C and TBHT return at 36.4 C

Tuesday, December 23, 2014, 13:14: TGHT and TBHt to 0 and off. 

Leak check found no leaks on Service Cap

Tuesday, December 23, 2014, 14:14 : Stopped CHILLCP3

Tuesday, December 23, 2014, 14:20: RGA filament off

Tuesday, December 23, 2014, 14:23: Stopped MP2 and MP3

Entry  Friday, December 05, 2014, 13:46, Anders Mjos, Conditioning Station, Development, TM2, , Not able to start water system 

 TCS:WPV1 does not open when staging is enabled. Multiple attempts have been made, but the valve remains closed.

    Reply  Monday, December 08, 2014, 13:52, Anders Mjos, Conditioning Station, Development, TM2, , Fixed - Not able to start water system 

Anders Mjos wrote:

 TCS:WPV1 does not open when staging is enabled. Multiple attempts have been made, but the valve remains closed.

 Dave Morris looked at the PLC controls and found that the code was not writing to the output after the PLC migration. He corrected it.

Entry  Friday, December 05, 2014, 15:41, Anders Mjos, Conditioning Station, Development, TM2, , RGA results 2014-12-05-14-25_TM2.png2014-12-05-14-25_TM2.txt

Measurement taken at 14:25. IG2 at ~7.7E-6 T

Entry  Friday, December 05, 2014, 11:58, David Wang, Conditioning Station, Development, TM2, , helium pressure test on TM2 tube heater +(D) water lines. 6x

At CS, The leak detector is hooked directly to the TM2 top service cap. The base LR 0.0xE-9 atm.cc/sec, base pressure 0.0xE-4torr. Applied 80 psi helium to TM2 tube heater +(D) line . During 3 minutes applying time , I did  not see any tiny change on LD readings. The line is perfectly vacuum sealed.  See attachment pictures.

Entry  Friday, December 05, 2014, 07:47, David Wang, Conditioning Station, Development, TM2, , TM2 at CS 

The pumping down on TM2 at CS was good overnight. However, the back up line pressure is still too high for LD to get to 0.0-E-9atm.cc/sec . It only could get to 1.2xE-7 atm.cc/sec. It is not enough for a good leak check . I dont want to have any ambiguous situation on this" D" line leak check. So,I am going to reconfigure the leak detector to the spare KF25 pot on the TM2 service cap. All pumps are stopped . The CS and TM2 will be vented soon. After that, a manual valve will be installed on that spare KF25 pot for future helium pressure check at CS. Then, The TM2 and CS will be pumped down again.

Entry  Thursday, December 04, 2014, 16:37, David Wang, Conditioning Station, Development, TM2, , connected TM2 and CS vacuum system . 

I connected TM2 and CS vacuum system. All vacuum pumps on TM2 and CS are started .The pumping down is good so .far

Entry  Thursday, December 04, 2014, 09:57, Travis Cave, Spent Target Vault, Standard Operation, , , Spent target placed in F-308. 

Spent targets in the mini storage were placed into the F-308s yesterday, all F-308 have been removed from the the target hall and they no reside for the time being in the hallway between the north and south hot cells.

Entry  Thursday, December 04, 2014, 09:54, Travis Cave, South Hot-Cell, Standard Operation, TM2, no target, Electrical check TM2_elec_check_no_source_traySHC.PDF

Results of electrical check of TM#2 with no source tray and no containment box attached. See PDF for results.

Entry  Thursday, December 04, 2014, 09:49, Travis Cave, Conditioning Station, Standard Operation, TM2, no target, module move 

TM#2 has been moved from the south hot cell to the conditioning station.

Entry  Tuesday, December 02, 2014, 13:33, David Wang, South Hot-Cell, Development, TM2, , Leak check on TM2 tube heater +(D) at SHC 2014-12-02_003.JPG2014-12-02_001.JPG2014-12-02_004.JPG

Chad and I leak checked TM2 tube heater+(D) circuit at SHC with water bypass loop and new seals installed on the water block. The LD base LR 0.0xE-9 atm.cc/sec,base pressure0.0xE-4 torr. Chad sprayed helium on the leak check area in SHC for 5 seconds. No any response has been found on LD during 1minutes waiting time. The test was repeated again and the result is same. NO LEAK at this stage!  After the TM2 is moved to CS , The D line will be pressured with 80 psi helium for helium pressure leak test before any hot water is circuited through it.  

Entry  Tuesday, December 02, 2014, 10:15, chad fisher, South Hot-Cell, Repair, TM2, , TM2 Reburb. Loop Install TM2_20141202_01.jpg20141203_142215.jpg20141203_143530.jpg

Final polish, clean with methanol and clean compressed air.

Loop installed and torqued to 90 in lbs.

Minimum of approximately 1"  between loop and containment box at closest point.

Entry  Monday, December 01, 2014, 14:48, Travis Cave, Spent Target Vault, Standard Operation, , , F-308s moved 

The F-308s have been moved into the target hall,  for filling on wednesday.

Entry  Monday, December 01, 2014, 14:06, chad fisher, South Hot-Cell, Repair, TM2, , TM2 REFURB. WATER LOOP TEST TM2_20141201_01.JPGTM2_20141201_02.JPGTM2_20141201_03.JPGTM2_20141201_04.JPGTM2_20141201_05AC.jpg

Some issues with the turntable and having to wait for a decision on whether to remove TM2 from the hot cell so that TM4 with dead UCx target could be put in this morning.

Progress on TM2:

  • Containment box has been removed from TM2.
  • Water block jig has been installed.
  • Existing blank off has been removed.
  • Sealing surfaces have been inspected.
  • First stage of sealing surface cleaning has been performed.

Tomorrow:

  • Polish of sealing surfaces.
  • Installation of loop.
  • Vacuum/helium leak check of loop.

TM2_20141201_03 - sealing surfaces before cleaning...kind of dirty

TM2_20141201_05AC - sealing surfaces after cleaning...looks good!

Entry  Monday, December 01, 2014, 12:05, maicodallavalle, Spent Target Vault, Maintenance, , , F-308 Maintenance 

F-308's have been serviced and are ready to be filled with spent targets. F-308's witch were serviced are #6,#13,#15,#16,and #19.

Entry  Friday, November 28, 2014, 13:06, Travis Cave, South Hot-Cell, Standard Operation, TM2, no target, module move 

TM#2 with no target or source tray has been moved from the north east silo to the south hot cell.

Entry  Wednesday, November 26, 2014, 11:11, Travis Cave, Spent Target Vault, Standard Operation, , Ta#38, Nb#7, TiC#3, NiO#2, and SiC#29, Spent targets moved to mini storage 

The following targets have been moved to the mini storage from the target storage vault:

  1. Ta#38
  2. Nb#7
  3. TiC#3
  4. SiC#29
  5. NiO#2

These target will be removed from the mini storage and placed into the F-308's on December 3rd.

Entry  Tuesday, November 25, 2014, 12:45, David Wang, ITE, Standard Operation, TM4, UCx11, 5 Shielding blocks have been transferred from ITW to ITE. 

5 Shielding blocks have been transferred from ITW to ITE. The ITE is configured to take proton beam.

Entry  Tuesday, November 25, 2014, 11:33, David Wang, South Hot-Cell, Development, , , Remove UCX 11 target transfer stand from SHC back to TH. 

The stand was used for transferring UCX11 targte from TH to SHC. The stand wit target was craned down from TH into SHC last week and stayed there over weekend. Chad and I removed the stand out of SHC yesterday. It was heavily contaminated. RPG and I spent more than 3 hours to clean this stand. See the emails I pasted below for  detail information.

Thanks, David, for letting me know about this. Here are survey results after my afternoon in Target Hall:

I spent 1.5 hours on additional decon of the stand, crane hook, and area around where David was doing the decon, finding up to 10k cpm (44-2) on some parts at first. Danka came to help after a bit (THANK YOU, DANKA) and we left the items covered in plastic and surveyed the area. Contamination survey results are as follows, numbers are units of cpm on the 44-2/RM14:

Tacky mats inside TMH door: 6000/2000

Tacky mats in hall before TMH door: 200/0

Tacky mats at boot box: 8000/4000

My booties: 50/0

Air sample at the decon area: 50/60 (also 100 cpm on alpha probe)

Floor swipes post-decon of floor: 0/0

Early results from a 10 min assay of the tacky mats shows predominantly Kr-85, Be-7, Sr-85, Rb-83, and Sr-82. A longer assay is underway.

The following measurements were made using the checking cave at the boot box (units of cpm):

David's respirator cartridges: 160

David's respirator: 0

Davids tank suit and booties: 1200

My suit: 100

My respirator: 0

The rags used for the decon work were contained in a bag and left behind the silos by the DST. This bag measured 240 uSv/h OC and 2 uSv/h at 0.5m

Thanks,

Andrew

 

On 11/24/2014 12:57 PM, David Wang wrote:

Hi all, The UCx#11 target transferring stand is moved back from SHC to TH. However, the stand was heavily contaminated. On the first Windex clean up towel, the counts directly shoot over the 500K counts which is the maximum scales on both RM14 and 44-2. After almost 2 hours, more than 20 times cleaning up with Windex spray and paper towel wipe , the counts dropped below 300 now. It is extremely difficult to clean up this stand.  I dont think we should move the target this way again unless we have a solution on the contamination clean up. The stand is still hanging  on the crane, and waiting for RPG checking.                        Thanks    David

Entry  Friday, November 21, 2014, 10:40, Travis Cave, Spent Target Vault, Standard Operation, , Ta#44, Spent target move Vault_Storage_November_21_2014.pdf

The spent Ta#44 target has been removed from the south hot cell, it was placed in pail #121 and placed in spot 4A of the storage vault. It was 276mSv/hr upon removal from the south hot cell.

Entry  Thursday, November 20, 2014, 14:13, David Wang, Conditioning Station, Standard Operation, TM4, UCx11, CS and TM4 was vented with Argon gas 

CS and TM4 was vented with Argon gas this morning before it was moved from CS to ITE.

Entry  Thursday, November 20, 2014, 14:12, David Wang, ITE, Standard Operation, TM4, UCx11, TM4 is connected in ITE. 

TM4 has been connected connect in ITE. Water is supplied to TM4 module only.

Entry  Thursday, November 20, 2014, 11:49, Travis Cave, ITE, Standard Operation, TM4, UC#11, module move 

TM#4 with UCx#11has been moved from the conditioning station to the east target station.

Entry  Wednesday, November 19, 2014, 11:12, David Wang, Conditioning Station, Standard Operation, TM4, , CS roughing pump is started.  

CS roughing pump is started for TM4 and UCX 11 target.

Entry  Wednesday, November 19, 2014, 09:18, Travis Cave, South Hot-Cell, Standard Operation, TM4, UC#11, Electrical check TM4_elec_check_UC11_SHC.PDF

TM#4 with UC#11 electrical check done. See attached PDF for the results.

Entry  Wednesday, November 19, 2014, 08:49, chad fisher, South Hot-Cell, Standard Operation, TM4, UCx#11, Ta#44 Removed Ucx#11 Installed 

Ta#44 has been removed from TM4 and UCx#11 has been installed and is ready for testing.

New fasteners were installed for all mounting and current connections.

High current fasteners were torqued to 130in lbs.

Entry  Tuesday, November 18, 2014, 11:15, David Wang, ITE, Standard Operation, TM4, Ta#44, TM4 has been disconnected in ITE. 

Dan and I disconnected TM4 in ITE.

Entry  Tuesday, November 18, 2014, 11:14, David Wang, South Hot-Cell, Standard Operation, , UCx11, crane down UCx 11 target into SHC from TH 

I craned down UCx11 target from TH into SHC. Chad was in SHC service area watching on it. The source tray moving jig was installed on the crane for this moving.

Entry  Tuesday, November 18, 2014, 10:28, Travis Cave, South Hot-Cell, Standard Operation, TM4, Ta#44, module move 

TM#4 with Ta#44 has been moved from the east target station to the south hot cell.

Entry  Monday, November 17, 2014, 13:45, chad fisher, South Hot-Cell, Repair, , , Jig for roof install of target Target_roof_install_20141117_01.jpgTarget_Roof_install_Jig_20141117_02.jpgTarget_roof_install_20141117_03.jpgTarget_roof_install_20141117_04.jpg

Jig for installation of target through hot cell roof has been assembled and placed in the target hall.

Entry  Monday, November 17, 2014, 11:38, Travis Cave, Conditioning Station, Standard Operation, TM3, no target, module move 

TM#3 with no target has been moved from the conditioning station to the north west silo.

Entry  Thursday, November 13, 2014, 14:05, David Wang, ITE, Repair, TM4, , Dan and I replaced flow wheel on ITE HVC2 water flow sensor. 

Dan and I replaced flow wheel on ITE HVC2 water flow sensor. The old wheel did rotate smoothly inside its SST case. The new wheel works fine.

Entry  Thursday, November 13, 2014, 14:01, David Wang, ITW, Repair, TM1, , I replaced flow wheel and coil on ITW MSP water flow sensor. 

I replaced flow wheel and coil on ITW MSP water flow sensor which is located in ITW pit. Before replacement, I checked the signal strength and frequency form e-board on this circuit. The signal was good in 10minutes watching. Still, I replaced them. The flow sensor works fine after replacement. I made a comment  on Isac e-fault system about this issue.

Entry  Thursday, November 13, 2014, 13:52, David Wang, ITW, Standard Operation, TM1, ThO#1, 5 Shielding blocks have been transferred from ITE to ITW. 

Dan and I transferred 5 shielding blocks from ITE to ITW. The ITW is configured to take proton beam.

Entry  Thursday, November 06, 2014, 13:43, David Wang, Conditioning Station, Development, TM3, , CS vacuum system has been connected to TM3. 

CS  vacuum system has been connected to TM3 for control system test(Dave.Morris).

Entry  Thursday, November 06, 2014, 08:55, David Wang, ITW, Repair, TM1, ThO#1, primary vacuum back up pressureITH CG1 ,CG2,CG4A were high. 

I found primary vacuum back up pressure ITH CG1, CG2, and CG4A were unusually high this morning. They should be about 10 -20 mtorr after one night pumping, but all of thier reading were 340-350-mtorr. Thease cause the current draw on primary turbo pumps were all over 2.0A(should be about 1.0A). I let Paul closed all BVs on primary side . The pressure dropped quickly to normal range after all BVs were closed. This shows the back up line are good. The problem are from   one of  the connections  on primary BVs. I let Paul opened the BVs one by one,but the problem did not show again. Now ,the current draw on the turbo pumps are back to normal also.

I will keep monitoring the system and take a look on all KF25 clamps on BVs once I have a chance to access to ITW.

Entry  Thursday, November 06, 2014, 08:07, David Wang, ITW, Standard Operation, TM1, ThO#1, TM1 has been connected in ITW. 

TM1 has been connected in ITW. All turbo pumps are started. The pumping down on ITW is good so far. The water is supplied to TM1 for HV conditioning.

Entry  Wednesday, November 05, 2014, 14:21, Anders Mjos, Conditioning Station, Development, , , Jumper installed on TGHT, TBHT and COIL Jumper1.jpgJumper2.jpg

 A copper bar jumper (ITD0488) was installed on the TGHT, TBHT and COIL conductors on the taregt hall side for TCS testing.

Entry  Wednesday, November 05, 2014, 10:20, Travis Cave, South Hot-Cell, Standard Operation, TM1, ThO#1, module move 

TM#1 with ThO#1 has been moved from the south hot cell to the west target station.

Entry  Tuesday, November 04, 2014, 13:17, chad fisher, South Hot-Cell, Standard Operation, TM1, ThO#1, TM1 w/ ThO#1 ready 

Tm1 with ThO#1 is buttoned up and ready for transport.

Entry  Tuesday, November 04, 2014, 11:05, David Wang, South Hot-Cell, Standard Operation, TM1, ThO#1, Leak check on TM1 HS water line withThO#1 installed. 

Chad and I leak checked HS line on TM1 with ThO#1 target installed. The LD pumped down to base leak rate 0.0xE-9 atm.cc/sec, base leak rate 0.0xE-4 torr. The pumping down process is normal. Chad sprayed helium on both VCR joints (each for 2 seconds) , and he did a flush spray around the target for 5 seconds. No any response had been found on LD during and after the spray( 40seconds waiting time). The target is leak tight.

Entry  Monday, November 03, 2014, 13:47, Travis Cave, South Hot-Cell, Standard Operation, TM1, ThO#1, Electrical check TM1_elec_check_ThO1_SHC.PDF

TM#1 with ThO#1 electrical check see attatched PDF for details.

Entry  Monday, November 03, 2014, 11:16, chad fisher, South Hot-Cell, Standard Operation, TM1, ThO#1, ThO#1 Installed 

ThO#1 has been installed onto TM1 and is ready for leak and electrical checking. High current fasteners torqued to 130 in lbs.

Entry  Monday, November 03, 2014, 10:27, Travis Cave, South Hot-Cell, Standard Operation, TM1, no target, module move 

TM#1 has been moved from the south west silo to the south hot cell.

Entry  Wednesday, October 22, 2014, 13:05, Anders Mjos, Conditioning Station, Maintenance, , , Controls upgrade on TCS 

 See work permit for details

Entry  Wednesday, October 22, 2014, 09:41, David Wang, Conditioning Station, Development, TM3, , TM3 has been disconnected at CS. 

TM3 has been disconnected at CS. It is vented and ready to move.

Entry  Tuesday, October 21, 2014, 14:53, Travis Cave, Spent Target Vault, Standard Operation, , ZrC#6, Spent target move Vault_Storage_October_21_2014.pdf

ZrC#6 has been moved from the south hot cell and into storage. It was placed in pail 120 in slot 5C of the vault. For more details see PDF.

Entry  Tuesday, October 21, 2014, 08:55, chad fisher, South Hot-Cell, Repair, , , Manipulator repair 

The east manipulator handle has been adjusted and is ready for use.

Entry  Monday, October 20, 2014, 14:18, chad fisher, South Hot-Cell, Repair, , , Manipulator Repair 

The broken cable on the east manipulator has been replaced.

The handle will need some adjustments which will take place first thing tomorrow.

Entry  Monday, October 20, 2014, 09:13, David Wang, Conditioning Station, Development, TM3, , TM3 TP2 failed 

TM3 TP2 stopped working this morning at 4:00 AM. I tried to start it but failed. On normal start mode , It could not pass 6K RPM. On soft start mode , the pump cant pass 17KRPM. Talked with Anders, We are not going to replace this pump since we are not going to run this module for a while. I will stopped all   vacumm pumps on CS and TM3 this morning.

Entry  Monday, October 20, 2014, 08:59, David Wang, Conditioning Station, Development, TM3, , Started TCS water system. 

I started TCS water system this morning to check if the chillers work properly.

Entry  Friday, October 17, 2014, 13:36, Anders Mjos, Conditioning Station, Maintenance, , , TCS:Chil staging not operational 

NOTE: If cooling is required, the compressors will have to be run manually. Make sure to switch it off again when the water has reached an acceptable temperature.

The staging did not work properly this morning. Dave Morris have been contacted and will look into it.

Entry  Thursday, October 16, 2014, 15:40, Anders Mjos, Conditioning Station, Maintenance, , , Chiller unit TCS_Cooling_System.pdf

NOTE: If there is a problem with the chiller unit (ie Fault 1 or Fault 2), a power cycle may reset the VFDs for the fans and clear the problem. To do so it is necessary to wait long enough for the VFDs to power off completely. The display will first start to flash before going dark. Wait another few seconds before powering the system back up. The chiller unit is located on the ISAC I Penthouse Roof.

A service tech from Daikine was on site today and has cleaned the chiller unit. In the process he also cycled the power which returned the operation back to normal. The tech provided us with manuals for the VFDs. These can be consulted on DocuSharefor looking up error codes.

Fault 1 refers to unit 1 and Fault 2 to unit 2.

Entry  Wednesday, October 15, 2014, 12:55, Travis Cave, South Hot-Cell, Standard Operation, TM1, no target, module move 

TM#1 with no target has been moved from the south hot cell to the south west silo.

Entry  Tuesday, October 14, 2014, 17:19, Anders Mjos, Conditioning Station, Standard Operation, TM3, No target, High Voltage Conditioning TCS_TM3.docx

Wednesday, October 14, 2014

 The BIAS voltage was brought up between 1:30pm and 5pm. Sparks tripped the BIAS power supply at voltages between 20 - 24 kV. Multiple attempts were made. The current was about 50-60 uA.


Wednesday, October 15, 2014

Temperature in the cooling circuit is too hight to do a HV test. The cooling circuit was started, but shuts off after ~10 m


Thursday, October 16, 2014

David and I found that the fans on the cooling unit on the roof did not run and that the compressors get hot and likely trip on over temperature protection (hot to the touch). We found the manual in the control panel of the unit.

10am: HV to 20kV before a spark tripped the PS. Current at 40 uA - resistivity at 11.9 Mohm

5pm: HV to 20kV before fluctuations in current, then a spark tripped the PS. Current around 40 uA. Resistivity 12.6 Mohm


Friday, October 17, 2014

8am: Staging did not start over night. TS5 temp is 31 deg C, which would have tripped power supplies. Reset and enabled staging.
The system increased staging until all 3 compressors were running.
9am: Cooling supply temperature reached ~3 deg C. Disabled staging and switched off all pumps
2pm: Switched off water circulation for the weekend.

 

Entry  Tuesday, October 14, 2014, 13:31, Travis Cave, South Hot-Cell, Standard Operation, TM1, no target, Electrical check TM1_elec_check_no_target.PDF

Electrical check of TM#1 with no target attached at the south hot cell see attached PDF for details.

Entry  Tuesday, October 14, 2014, 12:19, David Wang, ITW, Standard Operation, TM1, , TM1 was disconnected in ITW. 

TM1 was disconnected in ITW this morning. Heat shield circuit is purged.

Entry  Tuesday, October 14, 2014, 11:52, Travis Cave, South Hot-Cell, Standard Operation, TM1, ZrC#6, Electrical check TM1_ZrC6_postbeam.PDF

TM#1 with ZrC#6 post beam electrical check see attached pdf for results.

Entry  Tuesday, October 14, 2014, 11:51, Travis Cave, South Hot-Cell, Standard Operation, TM1, ZrC#6, module move 

TM#1 with ZrC#6 has been moved from ITW to the south hot cell.

Entry  Friday, October 10, 2014, 10:47, David Wang, Conditioning Station, Development, TM3, , TM3 has been connected in CS 

TM3 has been connected in CS. All water supplies are bypassed theTM3 on the top of the service cap. TM3 TP2 was difficult to start. It is started finally after couple of time try.The pump runs fine now. 

Entry  Wednesday, October 08, 2014, 09:39, Travis Cave, Conditioning Station, Standard Operation, TM3, no target, module move 

TM#3 has been moved from the North West Silo to the conditioning station.

Entry  Friday, September 26, 2014, 10:56, Travis Cave, Spent Target Vault, Standard Operation, , UC#10, Spent target move Vault_Storage_September_26_2014.pdf

UC#10 has been moved from the south hot cell to the spent target vault. It was placed in Pail #119 and in slot 8B. For further details see attached PDF.

Entry  Wednesday, September 24, 2014, 15:16, David Wang, ITE, Standard Operation, TM4, Ta#44, Reconnected TM4 in ITE. 

TM4 has been reconnected back to ITE. I started all turbo pumps on ITE and TM4. The ITE TP4s was extremely difficult to start. This pump is new, and was replaced before  the last ITE beam time on July. After several times try and starting mode switch, it is started. Its temperature and current draw showed on controller and very good after the start. The current draw on ITE TP1s is  s a little bit high and unstable. I will keep watching on ITE TP1s. I think the ITE TP1s is close to the end of the pump life. Other pumps are good so far.  

Entry  Wednesday, September 24, 2014, 15:03, David Wang, South Hot-Cell, Standard Operation, TM4, Ta#44, Leak check on TM4 HS water line with new Ta#44 target. at SHC 

This morning Chad and I leak checked TM4 HS line with new Ta#44 target installed. I calibrated LD before the check. Before check, the LD base LR 0.0xE-9 atm.cc/sec, base LP 0.0xE-4 torr. Chad sprayed helium on both VCR fittings and did a flush around the target. There is no any response had been found on LD,. The line is good on leak tight. with spray method.  No helium pressure test on the HS line at CS since TM4 was moved back to ITE directly.

Entry  Wednesday, September 24, 2014, 10:41, Travis Cave, ITE, Standard Operation, TM4, Ta#44, module move 

TM#4 with Ta#44 has been moved from the south hot cell to the east target station.

Entry  Tuesday, September 23, 2014, 13:31, Travis Cave, South Hot-Cell, Standard Operation, TM4, UC#10, Ta#44, Electrical check TM4_UC10_postbeam_shc.PDFTM4_Ta44_elecchk_shc.PDF

Electrical checks of TM#4 with UC#10 post beam and Ta#44 before beam see attached PDF for details.

Entry  Tuesday, September 23, 2014, 12:24, chad fisher, South Hot-Cell, Standard Operation, TM4, Ta#44, Ucx10 removed Ta#44 installed 

Ucx#10 has been removed from TM4 and placed in a pail with argon.

Ta#44 has been installed onto TM4 and target heater bolts torqed to 130 in.lbs.

Entry  Tuesday, September 23, 2014, 11:49, David Wang, ITE, Standard Operation, TM4, UCx #10, TM4 has been disconnected in ITE. 

TM4 has been disconnected and moved to SHC from ITE. ITE was vented with argon before move.

Entry  Tuesday, September 23, 2014, 10:50, Travis Cave, South Hot-Cell, Standard Operation, TM4, UC#10, module move 

TM#4 with UC#10 has been moved from the east target station to the south hot cell.

Entry  Tuesday, September 16, 2014, 10:41, David Wang, ITW, Standard Operation, TM1, ZrC #4, 5 Shielding blocks have been transferred from ITE to ITW. 

5 Shielding blocks have been transferred from ITE to ITW. The ITW is configured to take proton beam

Entry  Monday, September 15, 2014, 11:23, Travis Cave, Spent Target Vault, Standard Operation, , , Spent target field measurements Vault_Storage_September_15_2014.pdf

Field measurements on the spent target has finished see the attached PDF for details.

Entry  Friday, September 12, 2014, 14:21, Travis Cave, Spent Target Vault, Standard Operation, , , Spent target field measurements 

Five of the ten target we want to measure the fields on were done today. We will finish up on Monday, and the spent target storage spreadsheet will be updated then.

Entry  Wednesday, September 10, 2014, 11:47, David Wang, ITW, Standard Operation, TM1, , TM1 has been connected in ITW. 

TM1 has been connected in ITW.  ITW and TM1 turbo pumps have been started. Water is supplied to TM1 only. Everything is good so far.

Entry  Wednesday, September 10, 2014, 08:52, Travis Cave, ITW, Standard Operation, TM1, ZrC#6, module move 

TM#1 with ZrC#6 has been moved from the conditioning station to west target station.

Entry  Wednesday, September 10, 2014, 07:12, David Wang, ITW, Repair, TM1, , Removed ITW HS and COIL flow rate monitors. 

Removed ITW HS and COIL flow rate monitors installed at the beginning of this year. They were installed on these two circuits for testing.They are broken during last run in ITW due to radioactive field.

Entry  Monday, September 08, 2014, 13:44, David Wang, Conditioning Station, Standard Operation, TM1, ZrC#6, TM1 is disconnected at CS. 

Stopped TM1 and CS turbo pumps. Disconnected TM1 at CS. The CS and TM1 are under vacuum and naturally leak up. I will vent it on Wednesday morning.

Entry  Friday, September 05, 2014, 13:07, Travis Cave, Spent Target Vault, Standard Operation, , Ta#43, Spent target move Vault_Storage_September_5_2014.pdf

Ta#43 has been moved from the south hot cell to the spent target vault. See attached PDF for details.

Entry  Friday, September 05, 2014, 07:15, David Wang, Conditioning Station, Standard Operation, TM1, , helium pressure test on TM1 HS water line at CS. 

Helium pressure test on TM1 HS water line at CS is done. 80psi helium with LD 0.0xE-9 atm.cc/sec. 3 minutes test and no response on LD. The line is leak tight.

Entry  Thursday, September 04, 2014, 11:19, David Wang, Conditioning Station, Standard Operation, TM1, , TM1 is connected in CS. 

TM1 is connected in CS. All turbo pumps are started.

Entry  Thursday, September 04, 2014, 09:47, David Wang, South Hot-Cell, Standard Operation, TM1, , Leak check on TM1 HS water line with new target installed 

Chad and I  leak checked the TM1 HS line with new target installed. Base leak rate 0.0xe-9 atm.cc/sec. No any response has been found on LD. The line will be pressurized at CS with helium tomorrow.

Entry  Thursday, September 04, 2014, 09:45, Travis Cave, Conditioning Station, Standard Operation, TM1, ZrC#6, module move 

TM#1 with ZrC#6 has been moved from the south hot cell to the conditioning station.

Entry  Wednesday, September 03, 2014, 13:56, Travis Cave, South Hot-Cell, Standard Operation, TM1, ZrC#6, Electrical check TM1_ZrC6_elec_chk_shc.PDF

TM#1 with ZrC#6 electrical check at the south hot cell. The conductance of target on circuit A-D is a little lower then normal.

Entry  Wednesday, September 03, 2014, 13:55, Travis Cave, South Hot-Cell, Standard Operation, TM1, Ta#43, module move 

TM#1 with Ta#43 has been moved from the ITW to the south hot cell.

Entry  Wednesday, September 03, 2014, 10:50, David Wang, ITW, Standard Operation, TM1, , TM1 has been disconnected in ITW. 

  TM1 has been disconnected in ITW.

Entry  Wednesday, August 20, 2014, 10:25, David Wang, ITE, Standard Operation, TM4, , 5 Shielding blocks have been transferred from ITW to ITE. 

5 Shielding blocks have been transferred from ITW to ITE. ITE  is configured to take proton beam.
 

Entry  Wednesday, August 13, 2014, 12:21, David Wang, ITE, Repair, TM4, UCx10, ITE TP4S is replaced 

ITE TP4S was broken down last night . I stopped the ITE pumps and vented station with Argon this morning. Edi and I replaced the broken pump with a new pump. The ITE is under roughing now.

Entry  Monday, August 11, 2014, 14:30, David Wang, ITE, Standard Operation, TM4, UCx #10, TM4 is connected in ITE. 

TM4 is connected in ITE. All ITE  turbo pumps are started. I will check the pumping down process tomorrow morning. Everything is fine so far.

Entry  Monday, August 11, 2014, 14:27, David Wang, Conditioning Station, Standard Operation, TM4, , TM4 are vented with argon and disconnected at CS. 

TM4 are vented with argon and disconnected at CS this morning.

Entry  Monday, August 11, 2014, 10:38, Travis Cave, South Hot-Cell, Standard Operation, TM4, UC#10, Electrical check TM4_UC10_elec_chk_shc.PDF

Electrical check of TM#4 with UC#10 from thursday.

Entry  Monday, August 11, 2014, 10:34, Travis Cave, Conditioning Station, Standard Operation, TM4, UC#10, module move 

TM#4 with UC#10 has been moved from the conditioning station to the east target station.

Entry  Friday, August 08, 2014, 08:47, David Wang, Conditioning Station, Standard Operation, TM4, UCx #10, helium pressure test on TM4 HS water line at CS. 015.JPG012.JPG016.JPG014.JPG

Helium pressure test on TM4 HS water line at CS is finished. 80psi helium no leak. 

Entry  Thursday, August 07, 2014, 17:07, David Wang, Conditioning Station, Standard Operation, TM4, UCx #10, TM4 is connected in CS. 

TM4 is connected at CS. All turbo pumps are started. The pumping down is good so far.

Entry  Thursday, August 07, 2014, 13:58, David Wang, South Hot-Cell, Standard Operation, TM4, UCx #10, Leak check on TM4 HS water line with new UCX target. 

Isaac and I leak checked TM4 HS line with new UCX target. The leak detector base LR 0.0xE-9 atm.cc/sec, base pressure0.0xE-4torr. Isaac sprayed helium  on both VCR connections(5 seconds each) and flushed helium around the target for 6 seconds. No response on leak detector.

Entry  Thursday, August 07, 2014, 10:45, Travis Cave, South Hot-Cell, Standard Operation, TM4, no target, module move 

TM#4 has been moved from the south west silo to the south hot cell.

Entry  Wednesday, August 06, 2014, 11:12, Travis Cave, South Hot-Cell, Standard Operation, , SiC#30, Spent target move Vault_Storage_August_6_2014.pdf

SiC#30 in pail #117 has been move to the spent target vault and placed in spot 2C. See attached PDF for details.

Entry  Wednesday, August 06, 2014, 11:11, Travis Cave, South Hot-Cell, Standard Operation, TM3, no target, module move 

TM#3 with no target has been moved to the northwest silo for storage.

Entry  Tuesday, August 05, 2014, 11:53, David Wang, ITE, Repair, , , Reconnected ITE entrance module 

ITE entrance module is reconnected in ITE.

Entry  Tuesday, August 05, 2014, 10:40, Travis Cave, ITE, Standard Operation, , , module move 

ITE Entrance module has been moved back to the east station.

Entry  Thursday, July 31, 2014, 08:08, chad fisher, South Hot-Cell, Standard Operation, TM3, SiC#30, SiC#30 Removed and inpect TM320140731_01.jpgTM320140731_02.jpgTM320140731_03.jpgTM320140731_04.jpg

SiC#30 has been removed from TM3. A quick exam of TM3 source tray did not  yield any obvious signs of damage.

9 pin connector on the target showed the usual sparking/arcing marks.

Heat shield has been removed from the target. Inside of heat shield has some unusual marks on it and quite a lot of black deposits.

 

Entry  Wednesday, July 30, 2014, 11:51, Travis Cave, Conditioning Station, Maintenance, , , entrance module move 

ITE Entrance module has been moved from the east station to the conditioning station.

Entry  Monday, July 28, 2014, 17:26, Ron Kuramoto, ITW, Repair, , , ITW:IV5 Air leak repair DSCN0087.JPG20140728_142855_-_small.jpg20140728_143202_-_small.jpg

Air leak was found at the Solenoid control valve located in the Pre-Separator & DB0 room.  The gasket between the solenoid body and its manifold block was broken, see attached photos. The gasket and solenoid body were replaced. Air was turned back on to IV5 (B/L gate valve) with no apparent air leaks. The gate valve was actuated open & closed from the control room seeing both limits successfully.

Repair was done by Dimo Y. who received 0.01 mSv, and assisted by Anthony I. & Ron K. who both received zero dose.
Rad fields measured by RPG were; 1300 uSv/hr above B/L and 350 uSv/hr @ the Solenoid valves at knee height.
 
 

DSCN0087.JPG

 

20140728_142855_-_small.jpg

 

20140728_143202_-_small.jpg

Entry  Monday, July 28, 2014, 14:45, David Wang, Conditioning Station, Development, TM2, , turned off TM2 and CS turbo pumps. 

I turned off TM2 and CS turbo-pumps. TM2 will be moved from CS to silo tomorrow morning.

Entry  Monday, July 28, 2014, 14:37, David Wang, Conditioning Station, Development, TM2, , helium pressure test on TM2 tube heater +(D)and -(C)water lines. 7x
  • TM2 installed in Conditioning Station
  • Varian Leak detector connected directly to Target Module 2 Service cap.
  • Vacuum draw in Target Station with both module turbo pumps
  • Leak detector baseline normal (10^-4 Torr, 10^-9 Std cc/s He)
  • Since no Source tray is installed, and tube heater supply conductor is blanked off in target enclosure, it was necessary to test both supply and return points.
  • For each line tested, 80 psi He was connected, and waited ~2 min to for a response on the leak detector.
  • Lines tested:
    • conductor D (tube heater), Supply -> no He response
    • conductor D (tube heater), Return -> no He response
    • conductor C (tube heater), Supply -> no He response
    • conductor C (tube heater), Return -> no He response
  • Based on this leak testing, both supply and return lines of conductors C & D are leak tight under 95 psi He (80 psig He supply to vacuum)

 

Entry  Monday, July 28, 2014, 09:29, Travis Cave, Conditioning Station, Standard Operation, TM2, no target, module move 

TM#2 has been moved from the south hot cell to the conditioning station.

Entry  Thursday, July 24, 2014, 18:21, Grant Minor, South Hot-Cell, Repair, TM2, No target / no source tray, Leak check on TM2 ionizer tube cooling lines C and D - module side ITA6021_Rev_14_screencapture_cooling_lines_24July2014.jpgTM2_hot_cell_leak_check_tube_heater_C_D_24July2014_small2.jpgTM2_hot_cell_leak_check_no_source_tray_24july2014.JPG

Target Ionizer tube cooling lines "C" and "D" in Target Module 2 were both leak checked at the Hot Cell.  The lines were both blanked-off.

Bill Paley was present with David Wang in the Target Hall, operating the leak detector.  Grant Minor and Anders Mjos were present with Chad Fisher at the Hot Cell.

The "D" circuit was already blanked off with a copper blank containing silver brazed stainless steel inserts and indium plated inconel c-seals.

The "C" circuit was already blanked off with an aluminum blank and rubber o-rings.

The cooling lines are indicated in the attached screencapture from ITA6021 Rev .14, and are also labelled in the attached photo.

The "D" circuit was checked first, starting at around 12pm.

1.  The helium flow was tested by blowing dust on the work table.

2. The base leak rate on the Varian leak detector was confirmed in the "D" circuit to be stable at 10^-9 atm cc / sec and the pressure was 10^-4 Torr.

3. Each soldered joint on the "D" circuit was sprayed with a 2-second blast of helium - no response at the Varian.

4. The joint between the module-half of the water block and the copper blank-off was sprayed with a 2-second burst - no response.

5. A general area flood of helium sprayed for 10 seconds was applied all around both the "D" and "C" blocks - no response.

It was concluded that the "D" circuit had passed this leak check.  The "C" circuit was checked next.  The detector was changed to the "C" circuit and the circuit was pumped down.  At around 2pm the leak check resumed.

6. The base leak rate on the Varian leak detector was confirmed in the "C" circuit to be stable at 10^-9 atm cc / sec and the pressure was 10^-4 Torr.

7. The solder joint area on the "C" circuit was sprayed with an 8-second burst of helium - no response.

8. The joint between the two halves of the water blocks was sprayed with a 6-second helium burst - no response.

It was concluded that the "C" circuit had passed this leak check.

The electrical continuity of the "C" and "D" circuits were confirmed in the Target Hall at the service cap, and in the module at the Hot Cell, to double check that the correct lines has been pumped and leak checked - this was OK.

The ionizer tube heater lines appear to be leak tight at the Hot Cell.

 

 

 

 

Entry  Thursday, July 24, 2014, 09:10, Travis Cave, South Hot-Cell, Standard Operation, TM2, no target, module move 

TM#2 has been moved to the hot cell from the north east silo.

Entry  Wednesday, July 23, 2014, 13:36, David Wang, ITW, Standard Operation, TM1, , TM1 in ITW. 

  TM1 has been connected in ITW . The new roughing pump replaced on last Friday works good. I started all turbo pumps in ITW. The ITW TP1 controller was broken during the starting time. Dimo and I changed a new controller for ITW TP1 in electrical room. The pumping down is good so far. ITW water supplies to TM1 only.      

Entry  Tuesday, July 22, 2014, 07:32, David Wang, Conditioning Station, Standard Operation, TM1, , Stop TM1 and CS turbo pumps and ruff pump. 

Stop TM1 and CS turbo pumps and ruff pump. TM1 is disconnect at CS. It will be vented tomorrow morning and moved to ITW.

Entry  Monday, July 21, 2014, 13:11, David Wang, Conditioning Station, Standard Operation, TM1, , helium pressure test on TM1 HS water line at CS. 

The TM1 HS line is  pressure tested this morning with 70 psi helium  at CS. No response has been found on leak detector.

Entry  Thursday, July 17, 2014, 11:49, David Wang, Conditioning Station, Standard Operation, TM1, , TM1 and CS turbo pumps have been started 

I connected TM1 at CS. All turbo pumps have been started. The pumping down is  good so far.

Entry  Thursday, July 17, 2014, 10:13, David Wang, Conditioning Station, Standard Operation, TM1, , Leak check on TM1 HS water line with new target installed 

Chad and I leak checked TM1 HS waterline with new target installed at SHC. The LD base LR:0.0xE-9atm.cc/sec, base pressure: 0.0xE-4 torr. Chad sprayed helium on both VCR fittings and flushed helium around the target. No response has been found on leak detector. The target HS line is leak tight so far. I will do helium pressure test on this line at CS on next Monday.

Entry  Thursday, July 17, 2014, 09:29, Travis Cave, South Hot-Cell, Standard Operation, TM1, Ta#43, module move 

TM#1 with Ta#43 has been moved from the south hot cell to conditioning station.

Entry  Wednesday, July 16, 2014, 14:28, Travis Cave, South Hot-Cell, Standard Operation, TM1, Ta#43, Electrical check TM1_Ta43_elec_chk_shc.PDF

TM#1 with Ta#43 electrical check see attached PDF.

Entry  Wednesday, July 16, 2014, 13:59, chad fisher, South Hot-Cell, Standard Operation, TM3, SiC#30, Sic#30 install 

Just some notes on the install of SiC#30 on TM3 last month...It was installed with all new fasteners and torque values provided by Anders were used...of main interest is probably the main high current fasteners which were torqued to 150 in lbs.

Entry  Wednesday, July 16, 2014, 13:56, chad fisher, South Hot-Cell, Standard Operation, TM1, UCx#9, UCx#9 off Ta on 

The UCx#9 target has been revomed from the target module...leg A was broken as suspected.

Ta#42 has been installed. High current connection fasteners torqued to 150 in lbs.

Entry  Wednesday, July 16, 2014, 13:02, Travis Cave, South Hot-Cell, Standard Operation, TM1, UC#9, Electrical check TM1_UC9_Elecchk_postbeam.PDF

Electrical check of the TM#1 with UC#9 post beam at the south hot cell.

Entry  Wednesday, July 16, 2014, 11:28, David Wang, ITW, Standard Operation, TM1, , TM1 had been dsiconnected in ITW. 

The TM1 and ITW  were vented with argon gas last night. TM1 had been disconnected in ITW this morning.

Entry  Wednesday, July 16, 2014, 10:32, Travis Cave, South Hot-Cell, Standard Operation, TM1, UC#9, module move 

TM#1 with UC#9 has been moved from the west target station to the south hot cell.

Entry  Tuesday, July 08, 2014, 09:57, David Wang, ITE, Standard Operation, TM3, , 5 Shielding blocks have been transferred from ITW to ITE. 

5 Shielding blocks have been transferred from ITW to ITE. The ITE is configured to take proton beam.

Entry  Monday, July 07, 2014, 14:45, Grant Minor, ITE, Maintenance, TM3, SiC #30, FEBIAD gas line check ITE_Febiad_Gas_Line_Check_7July2014_arrows.jpg

There were some problems this morning with provision of FEBIAD gas to the the target at ITE.  It was suspected that the gas line was improperly connected to the module, or that the valves at the module were not opened.

Remote Handling was asked to open the HV cover on TM3 at ITE and check the connection of the FEBIAD gas line.  Grant Minor, Maico Dalla Valle, Dan McDonald, and Anders Mjos entered the Target Hall before lunch on Work Permit I2014-07-07-1.

Maico entered ITE with suit and respirator, disengaged / disconnected the interlocks and removed the HV cover.  He inspected the FEBIAD gas line and found that it was properly connected, and that the valves were both open.  The gas line is shown in the attached image, with both valves marked in red.

Grant and Anders went into the electrical room to examine the supply gas bottle and supply circuit, and found that the supply gas pressure to the regulating valve was low.  It was concluded that the problem was not at the Target Module / Target Station.

Grant returned to the Target Station and instructed Maico to replace the HV cover.  After this was done, Grant confirmed with Jon Aoki over the phone that the interlock switch signals were both reading "OK".

Friedhelm Ames made an entry in today's ISAC Ops e-log regarding the supply pressure to the regulating valve.

ISAC E-log

 

Entry  Wednesday, July 02, 2014, 14:29, David Wang, ITE, Standard Operation, , , Reconnected TM3 in ITE. 

I reconnected TM3 in ITE. All turbo pumps have been started. The water supply to TM3 only in ITE. The HV keys are back to electrical room.

Entry  Wednesday, July 02, 2014, 09:02, Travis Cave, ITE, Standard Operation, TM3, SiC#30, module move 

TM#3 with SiC#30 has been moved from the conditioning station to the east target station.

Entry  Tuesday, June 24, 2014, 15:45, Anders Mjos, South Hot-Cell, Standard Operation, TM3, TiC#4, Ground Electrode and Extraction Electrode dirty after last run TiC#4_Dirty_GND_and_EE_electrodes.pdf

See attached pdf and DocuShare for more photos. It may be possible to clean some of it from the Ground Electrode.

    Reply  Friday, June 27, 2014, 11:26, Anders Mjos, South Hot-Cell, Standard Operation, TM3, , Ground Electrode Cleaned TM3_GND_Electrode_Cleaning.pdf

Anders Mjos wrote:

See attached pdf and DocuShare for more photos. It may be possible to clean some of it from the Ground Electrode.

 Chad cleaned the GND electrode yesterday June 26th - see attached PDF. Photos on DocuShare.

Entry  Friday, June 27, 2014, 10:16, David Wang, Conditioning Station, Standard Operation, TM3, , TM3 HS water lines helium pressure test. at CS 

TM3 HS water line helium pressure test is done at CS. 70 psi helium , 3 minutes.Base LR 0.0xE-9 atm.cc/sec, base pressure 0.0xE-4 torr.  No response. The line is leak free.

Entry  Thursday, June 26, 2014, 14:18, Travis Cave, Conditioning Station, Standard Operation, TM3, SiC#30, module move 

TM#3 with SiC#30 has been moved from the south hot cell to the conditioning station.

Entry  Thursday, June 26, 2014, 11:15, Travis Cave, South Hot-Cell, Standard Operation, TM3, SiC#30, Electrical check TM3_SiC30_elecSHC.PDFTM3_elecchkaftclean.PDF

Electrical check of the TM#3 with SiC#30 attached. Also an electrical check of TM#3 after the cleaning of ground electrode with no target attached.

Entry  Thursday, June 26, 2014, 10:57, David Wang, South Hot-Cell, Standard Operation, TM3, , Leak check on TM3 HS water line with new target. installed. 

Chad and I leak checked the TM3 HS water line with new target installed.  No leak has been found during the check. Leak detector base LR 0.0xE-9 atm.cc/sec, base pressure 0.0xE-4 torr. The line will be helium pressurized at CS later.

Entry  Wednesday, June 25, 2014, 13:46, Travis Cave, South Hot-Cell, Repair, TM3, no target, Electrical check TM3electestsinsulrepair.PDF

Electrical check of TM#3 after the insulator repair. See attached PDF for details.

Entry  Wednesday, June 25, 2014, 12:55, Anders Mjos, South Hot-Cell, Standard Operation, TM3, TiC#4, Object - possibly cable tie found in Containment Box TiC#4_Cable_Tie.pdf

 See attached PDF. The object is not accessible with only the front panel removed. Photos on DocuShare.

Entry  Tuesday, June 24, 2014, 15:14, Anders Mjos, South Hot-Cell, Standard Operation, TM3, TiC#4, Conductor insulator broken close to right TGHT terminal TiC#4_Broken_Insulator.pdf

When the Containment Box was opened today by Chad for a target change, we found the conductor insulator block B (ITD0054) to be broken close to the right TGHT terminal. Chad was nevertheless able to remove the target. See DocuShare and attached file for photos.

An attempt to replace the insulator will be made tomorrow with a spare.

A small sticky piece, likely off plastic material, was found next to the left main source tray insulator. The piece was removed from the Containment Box. See link above and attachment for photos.

    Reply  Wednesday, June 25, 2014, 12:49, Anders Mjos, South Hot-Cell, Standard Operation, TM3, TiC#4, Conductor insulator broken close to right TGHT terminal ITD0052C_revB.pdf

Anders Mjos wrote:

When the Containment Box was opened today by Chad for a target change, we found the conductor insulator block B (ITD0054) to be broken close to the right TGHT terminal. Chad was nevertheless able to remove the target. See DocuShare and attached file for photos.

An attempt to replace the insulator will be made tomorrow with a spare.

A small sticky piece, likely off plastic material, was found next to the left main source tray insulator. The piece was removed from the Containment Box. See link above and attachment for photos.

 The two insulators ITD0053 and ITD0054 was replaced this morning by Chad. Photos on DocuShare. All bolts torqued with torque wrench see attached PDF for values.

Entry  Tuesday, June 24, 2014, 11:58, Travis Cave, South Hot-Cell, Standard Operation, TM3, TiC#4, Electrical check TM3_TiC4_elec_chk_SHC_postbeam.PDF

Electrical check of the TiC#4 on TM#3 post beam at the south hot cell, see attached PDF for details

Entry  Tuesday, June 24, 2014, 11:33, maicodallavalle, Spent Target Vault, Standard Operation, , , F-308 Maintenance 

Five F - 308 flasks containing five ISAC spent targets were moved from the anteroom into the south hot cell area. When the F - 308's were in the south hot cell area the rest of the bolts were installed on all the top covers. All the bolts were torqued and all the cable locks were also installed. All F - 308's  were then moved into the Active Services Area.

Entry  Tuesday, June 24, 2014, 11:12, Travis Cave, South Hot-Cell, Standard Operation, TM3, TiC#4, module move 

TM#4 with TiC#4 has been moved from the east target station to the south hot cell.

Entry  Tuesday, June 17, 2014, 10:46, David Wang, ITW, Standard Operation, TM1, UC#9, 5 Shielding blocks have been transferred from ITE to ITW. 

5 shielding blocks have been transferred from ITE to ITW. ITW is configured to take proton beam. Argon venting system for ITW is ready also.

Entry  Friday, June 13, 2014, 10:33, Anders Mjos, ITW, Development, TM1, UC#9, Flow meter data 

Coil not used on TM1. Data and plots on DocuShare

Friday, June 13, 2014, 10:30. ITE receving p+

  Temp [C] Flow [lpm]
HS 30.0 6.3
COIL  30.2 11.6

 Monday, June 16, 2014, 09:30: p+ off for maintenance day

  Temp [C] Flow [lpm]
HS 32.7 6.3
COIL  27.7 11.6

 Thursday, June 19, 2014, 16:14: 10 uA p+ on ITW

  Temp [C] Flow [lpm]
HS 31.9 7.2
COIL  27.6 13.1

Tuesday, July 08, 2014, 10:32:

Data uploaded to DocuShare

Entry  Thursday, June 12, 2014, 09:42, Travis Cave, Spent Target Vault, Standard Operation, , , Targets moved from mini storage to F-308s Vault_Storage_June_12_2014.pdfMini_Vault_Storage_June_12_2014.pdf

Five targets have been moved from the spent target storage to the mini storage. The targets that were moved are UCx #'s 6,7,8 , SiC #28, and Nb #6.

Entry  Tuesday, June 10, 2014, 14:02, David Wang, ITW, Standard Operation, TM1, UC9#, TM1 and ITW turbo pumps have been started. 

TM1 has been connected to ITW. It is pumping down in ITW with 6 turbo-pumps on.

Entry  Tuesday, June 10, 2014, 13:20, Travis Cave, ITW, Standard Operation, TM1, UC#9, module move 

TM#1 with UC#9 moved from the conditioning station to west station.

Entry  Tuesday, June 10, 2014, 07:57, David Wang, Conditioning Station, Standard Operation, TM1, UC#9, TM1 are vented with argon and disconnected at CS. 

TM1 will be moved to ITW this morning.

Entry  Monday, June 09, 2014, 10:33, David Wang, Conditioning Station, Standard Operation, TM1, UC9#, Stop TM1 and CS trubo pumps and ruff pump. 

The CS and TM1 is still under vacuum. They will be vented with argon tomorrow mornig

Entry  Tuesday, June 03, 2014, 09:12, David Wang, Conditioning Station, Standard Operation, TM1, UC9#, TM1 HS line helium pressure test and TM1 electrical check at CS 7x

TM1 HS line helium pressure test and TM1 electrical check at CS under vacuum are finished. Everything is good. See attachment

Entry  Monday, June 02, 2014, 15:40, David Wang, Conditioning Station, Standard Operation, TM1, , TM1 and CS turbo pumps have been started 

TM1 and CS turbo pumps have been started. The vacuum readings are fine on all gauges.

Entry  Monday, June 02, 2014, 13:53, Travis Cave, Conditioning Station, Standard Operation, TM1, UC#9, module move 

TM#1 with UC#9 has been moved from the south hot cell to the conditioning station.

Entry  Monday, June 02, 2014, 11:59, David Wang, South Hot-Cell, Standard Operation, TM1, , Leak check on TM1 HS water line with new UC9# target installed 

Chad and I leak checked TM1 HS and UC9# VCR fittings. No response had been found on leak detector during the test. I will do helium pressure  test on it at CS later.

Entry  Monday, June 02, 2014, 11:28, Travis Cave, South Hot-Cell, Standard Operation, TM1, UC#9, Electrical check TM1_UC9_elec_chk_SHC.PDF

TM#1 with UC#9 electrical check see attached pdf for details.

Entry  Monday, June 02, 2014, 11:25, chad fisher, South Hot-Cell, Standard Operation, TM1, UCx #9, UCx #9 Installed 
UCx #9 has been installed.
Entry  Monday, June 02, 2014, 10:52, Travis Cave, South Hot-Cell, Standard Operation, TM1, no target, module move 

TM#1 with no target has been moved from the north west silo to the south hot cell.

Entry  Friday, May 30, 2014, 09:41, Travis Cave, Spent Target Vault, Standard Operation, , Ta#42, Spent target move Vault_Storage_May_30_2014.pdf

Ta#42 in pail #114 has been moved from the south hot cell to the spent target storage vault and place in spot 7B. The target was 277mSv/hr upon removal from the south hot cell. See attached PDF of vault status.

Entry  Wednesday, May 28, 2014, 08:48, Travis Cave, South Hot-Cell, Standard Operation, TM4, no target, module move 

TM#4 with no target has been moved from the south hot cell to the south west silo.

Entry  Tuesday, May 27, 2014, 11:45, Travis Cave, South Hot-Cell, Standard Operation, TM4, Ta#42, Electrical check TM4_Ta42_elec_chk_SHC_postbeam.PDF

TM#4 electrical check with Ta#42 attached post beam at the south hot cell.

Entry  Tuesday, May 27, 2014, 10:42, Travis Cave, ITW, Standard Operation, TM4, Ta#42, module move 

TM#4 with Ta#42 has been moved from  the west target station to the south hot cell.

Entry  Tuesday, May 27, 2014, 09:42, maicodallavalle, Spent Target Vault, Maintenance, , , F-308 Maintenance 

All of the serviced F-308's have been moved to the South Hot cell area.

Entry  Tuesday, May 27, 2014, 09:38, maicodallavalle, Spent Target Vault, Maintenance, , F-308 Maintenance , F-308 Maintenance 

All the F-308's can back from being certified at Nordion.  All of the F-308's have been serviced and are ready to be filled with spent targets.

Entry  Wednesday, May 21, 2014, 13:56, Travis Cave, Spent Target Vault, Standard Operation, , , Spent target assay Vault_Storage_May_22_2014.pdf

All targets in the vault have been assayed and measured. Results will be posted soon.

Results of assay are now attached in a new layout.

Entry  Wednesday, May 21, 2014, 13:56, Travis Cave, Spent Target Vault, Standard Operation, , , Spent target assay 

All targets in the vault have been assayed and measured. Results will be posted soon.

Entry  Thursday, May 15, 2014, 14:38, David Wang, ITE, Repair, TM3, TM3, Bias short on ITE 

Anders and I opened the HV cover in ITE and did  a visual check inside ITE HV  cover and top of TM3.Bill was with us and took the pictures. There was nothing obviously wrong when we opened the HV cover in ITE. We disconnected TM3 high current cables from ITE. Then we did an electrical check on TM3.The TM3 was good and passed megga test (465Mohm at 500V). The module was good and was separated electrically from the ITE at that moment. Then, we went back to electrical room and measured the resistance between bias and ground with ground bar opened and power supply disconnect. It was still shorted at that moment .We thought the short is located inside HV chase between electrical room and ITE. Then, we went back to ITE again and reconnected TM3 back to ITE. We wiped two blue nylon insulators between bias and ground, and no obviously spark track or dirty on them. We put HV cover back in ITE locked area, and went back to electrical room again.We decided to do a final electrical check there. We thought the short should be still there and we just want to confirm it . But this time the short  is gone. Everything goes back to normal.   The short disappeared and We test bias to 5KV and the current looks normal now.  

Entry  Wednesday, May 14, 2014, 19:01, Grant Minor, ITE, Maintenance, TM3, , HV short inspection at ITE 

Friedhelm Ames commented to me that there appears to be a short between High Voltage and Ground at TM3 at ITE.

Friedhelm, Anders and I initiated a survey by Andrew from RPG, and entered the Target Hall at approximately 5pm to visually assess the HV cover at the MAA.  There was no clear indication of a problem.  We opted to wait for David to return as we weren't sure exactly what we were looking for.

Friedhelm and Anders confirmed in the Electrical Room that the short is in the Target Hall.

Entry  Wednesday, May 07, 2014, 10:15, David Wang, ITE, Repair, TM3, , ITE TM3, entrance module and BL2A3 window flange seals leak check.. 

ITE TM3, entrance module, and 2A3 window flange seals have been leak checked this morning after 2 new seals replacement.The LD base leak rate was 0.0xE-9 atm.cc/sec,  base pressure was 0.0 XE-4 Torr. I sprayed lots helium around the TM3, entrance module and 2A3 flange seals. No any response had been found on LD during the  spraying. All three flanges are sealed perfectly now.

Entry  Wednesday, May 07, 2014, 10:08, David Wang, ITE, Repair, TM3, , ITE entrance module flange seal had been replaced. 7x

ITE entrance module flange seal had been replaced yesterday.The flange and the seal groove were cleaned with Acetone before the new seal is installed. See pictures

Entry  Tuesday, May 06, 2014, 14:05, Travis Cave, ITE, Standard Operation, , , module move 

The entrance module was out a new seal went in and then the entrance module went back, and then TM#3 went back. So all modules are now back in place in the east target station.

Entry  Monday, May 05, 2014, 13:11, David Wang, ITE, Repair, TM3, , ITE Entrance module has been disconnected. 011.JPG025.JPG033.JPG035.JPG032.JPG

ITE entrance module has been disconnected and the lifting yoke is installed for module move. See attached pictures.

Entry  Monday, May 05, 2014, 13:05, David Wang, ITE, Repair, TM3, , ITE target module flange seal has been replaced. 004.JPG008.JPG008.JPG007.JPG

ITE target module flange seal has been replaced.The flan surface and the o-ring groove have been cleaned with Acetone before the new seal is installed. See attached picture.

Entry  Monday, May 05, 2014, 10:40, Travis Cave, ITE, Standard Operation, TM3, TiC#4, module move 

TM#3 with TiC#4 has been moved from the east station to the south west silo.

Entry  Wednesday, April 16, 2014, 17:08, Keith C Ng, ITE, Repair, , , 2a3 window - He leak check 

Helium leak checked 2a3 window after installing using remote line:

- There was a leak found between the target and entrance module at the target pit, rate of 9E-6 atm-cc/sec.

- One test performed with the remote helium line to the window. There was a response but the leak detector was located above the window access channel, drift cannot be ruled out.

- 3 more tests performed with vacuum group, with leak detector relocated farther away from ITE and isolated with plastic. 2 tests using remote line had no response. One test done with a wand through 2a3 wall penetration had a response of 3.2E-9 atm-cc/sec (not using remote line).

Vacuum group (D. Yosifov) comments that due to the much larger leak at the top of the tank he cannot say with confidence the response seen is a leak at the window (due to leak at top) but if there is, a tolerable leak rate.

Entry  Friday, April 04, 2014, 16:59, Anders Mjos, ITW, Development, , , Flow meters installed on Heat Shield and Coil water return 20140404_165829_1.jpg

David W. has installed two SST Proteus flow meters, model OV7006FTA32, on ITW Heat Shield and Coil. The flow meters are connected to a power supply and a data logger in the electrical room.

The Heat Shield flow meter has SN 00278112 and is on the Black wire pairs and connected to CH3 & CH4 on the logger.

The Coil flow meter has SN 00278113 and is on the Green wire pairs and connected to CH1 & CH2 on the logger.

The first channel (CH1, CH3) is temperature in degrees Celcius and the second channel (CH2, CH4) is flow rate in liters per minute.

A camera has been placed on the logger.

Flow rates today (2014-04-04):

HS        8.2 - 8.3 lpm
COIL    8.0 - 8.1 lpm

Calibration sheets


UPDATE 2014-04-11: Corrected HS to CH3 & CH4.

    Reply  Wednesday, April 16, 2014, 10:16, Anders Mjos, ITW, Development, TM3, Ta#42, Flow meters installed on Heat Shield and Coil water return 

 

Anders Mjos wrote:

David W. has installed two SST Proteus flow meters, model OV7006FTA32, on ITW Heat Shield and Coil. The flow meters are connected to a power supply and a data logger in the electrical room.

The Heat Shield flow meter has SN 00278112 and is on the Black wire pairs and connected to CH3 & CH4 on the logger.

The Coil flow meter has SN 00278113 and is on the Green wire pairs and connected to CH1 & CH2 on the logger.

The first channel (CH1, CH3) is temperature in degrees Celcius and the second channel (CH2, CH4) is flow rate in liters per minute.

A camera has been placed on the logger.

Flow rates today (2014-04-04):

HS        8.2 - 8.3 lpm
COIL    8.0 - 8.1 lpm

Calibration sheets


UPDATE 2014-04-11: Corrected HS to CH3 & CH4.

 

PDFs of temperature and flow traces are available on DocuShare

Monday, April 28, 2014, 09:27. p+ off since 8:20

  Temp [C] Flow [lpm]
HS 28.3 8.38
COIL 26.3 8.01

Tuesday, April 29, 2014, 09:28: p+ 30 uA

  Temp [C] Flow [lpm]
HS 31.7 8.40
COIL 27.6 8.13

Monday, May 05, 2014, 10:49: p+ off since 8:39
(Downloaded data and updated traces on DocuShare)

  Temp [C] Flow [lpm]
HS 27.1 8.47
COIL 26.6 8.11

 Wednesday, May 14, 2014
(Downloaded data and updated traces on DocuShare)

  Temp [C] Flow [lpm]
HS 33.5 7.7
COIL 29.0 7.5

 

Entry  Tuesday, April 15, 2014, 08:53, Travis Cave, ITE, Standard Operation, TM3, TiC#4, module move 

TM#3 with TiC#4 has been moved from the conditioning station to the east target station.

Entry  Monday, April 14, 2014, 13:58, David Wang, ITE, Repair, , , Reconnected ITE entrance module 

I reconnected the entrance module back to the ITE station. All diagnostic cables, turbo- pump, air lines, water lines on ITE entrance module and BL2A3 window are connected back.

Entry  Monday, April 14, 2014, 11:57, Travis Cave, ITE, Standard Operation, , , entrance module move 

The East Entrance module has been moved from the south west silo to the east target station. The move went well.

Entry  Friday, April 11, 2014, 18:17, Keith C Ng, ITE, Repair, , , 2a3 window - install 

Today:

1) Installed new cradle and shortened beam pipe section in wall penetration.

- Removed tank dust cover from flange and cleaned

- Held flange faces together from 2A tunnel side to check alignment, slightly biased to the East axially and a small gap present in the top when resting

 

2) Prepared new 2A window

- Connected preswaged  (1/2 turn) swagelok nuts to the existing copper lines in the target hall, 1/4 turn from finger tight, 3/4 turns total

- Leak checked cooling lines with pressurized air at 75psi and snoop, no leaks were found at the joint

- Grooves were cleaned and helicoflex delta seals were installed with vacuum grease used in the periphery to hold ring in window, applied at 6 points every 60deg

 

3) Window installation

- Lowered window into position by cooling lines

- Window located into tank flange first then slid beam pipe towards it, capturing the window with seals

- Lowered clamp into place in hole

 

4) Clamp installation

- Lowered clamp into access hole and started closing clamp with steel RH drive bar

- torqued to 50 ft-lbs collar gap was still ~8"

- Increased torque to 60 ft-lbs then 70 ft-lbs stopped closing of clamp when the displacement did not change between the stop ring and clamp yoke

- It was decided not to continue to close this clamp, more assessment may be necessary

 

6) We will attempt to pump on the seal in its current configuration, tools have been removed.

Entry  Friday, April 11, 2014, 11:35, David Wang, Conditioning Station, Standard Operation, TM3, , Helium pressure test on TM3 HS water line with new Ta target. at CS 6x

The helium pressure test on TM3 HS water line with new Ta target is finished at CS. The circuit is leak tight.. No any response on LD. See pictures.

Entry  Thursday, April 10, 2014, 14:03, Bevan Moss, Conditioning Station, Standard Operation, TM3, TiC#4, HV conditioning 10042014_Tm3_TiC#4_HV_conditioning.JPG10042014_TM3_TiC#4_HV_conditioning.txt

 The TiC#4 target that is on TM3 was conditioned to 25kV today with the EINZEL lens at 12.5kV. There was one spark shortly after reaching 25kV that reset the bias PS and another one  after the module sat at 25kV for ~30 minutes. Attached is the strip tool data and screen shot. Prior to starting the conditioning the power on the chiller needed to by cycled as the VFD on the fans had tripped due to a recurring inrush problem.

Entry  Wednesday, April 09, 2014, 11:10, David Wang, South Hot-Cell, Standard Operation, TM3, , TM3 heat shield circuit leack check at SHC 

This Monday morning, Chad and I leak checked heat shielding circuit on TM3 with new target installed. The base LR on LD :0.0xE-9 atm.cc/sec, base pressure 0.0xE-4 torr. Chad sprayed helium twice on the VCR joints. No leak has been found. The circuit will be pressured with helium at CS.

Entry  Tuesday, April 08, 2014, 09:05, Travis Cave, South Hot-Cell, Standard Operation, TM3, TiC#4, module move 

TM#3 with TiC#4 has been moved from the south hot cell to the conditioning station.

Entry  Monday, April 07, 2014, 14:13, chad fisher, South Hot-Cell, Standard Operation, TM3, TiC#4, TiC#4 installation 

TiC#4 has been installed onto TM3

Entry  Monday, April 07, 2014, 11:49, Travis Cave, South Hot-Cell, Standard Operation, TM3, TiC#4, Electrical check TM#3_elec_test_TiC#4_surf.PDF

Electrical test of TM#3 with TiC#4 attached. See PDF.

Entry  Monday, April 07, 2014, 10:48, Travis Cave, South Hot-Cell, Standard Operation, TM3, no target, Electrical check TM#3_elec_test_no_target.PDF

TM#3 electrical check at the south hot  cell with no target to give us a base line and show that things are ok with the module for the start of the running year.

Entry  Friday, April 04, 2014, 14:59, Keith C Ng, ITE, Maintenance, , , measurement of new beam tube section wall_to_flange_length.pdf

R. Kuramoto and A. Laxdal measured the distance from the 2A tunnel to the tank flange of ITE. The new fabricated beam pipe with bellows was used to gauge the distance to the tank flange; The flange face of the beam tube was butted up to the tank flange and the beam tube was marked at the plane of the wall. A metal rod was used to gauge the distance to the tank face using the same method.

From the inside of the tunnel wall:

- To tank flange: 45 5/16"

- To ITE vacuum tank face: 49"

See attached PDF.

Entry  Friday, April 04, 2014, 14:16, Travis Cave, South Hot-Cell, Standard Operation, TM3, no target, module move 

TM#3 with no target has been moved from the south west silo to the south hot cell.

Entry  Wednesday, April 02, 2014, 09:14, Travis Cave, ITW, Standard Operation, TM4, Ta#42, module move 

TM#4 with Ta#42 has been moved to the west target station.

Entry  Monday, March 31, 2014, 13:22, Bevan Moss, Conditioning Station, Standard Operation, TM4, Ta #42, HV conditioning 31032014_TM4_Ta#42_HV_Conditioning.txt31032014_Ta#42_HV_conditioning.JPG

 TM4 with Ta#42 was HV conditioned to 35kV with the optics tray at 17.5kV. There was some vacuum response while ramping but well within normal. Attached is a screen shot and the associated data.

Entry  Thursday, March 27, 2014, 10:47, Travis Cave, Conditioning Station, Standard Operation, TM4, Ta#42, Electrical check TM#4_Ta42surf_electest_CS.PDF

TM#4 with Ta#42 in the conditioning station under vacuum electrical check.

Entry  Wednesday, March 26, 2014, 08:36, Travis Cave, Conditioning Station, Standard Operation, TM4, Ta#42, module move 

TM#4 with Ta#42 has been moved from the south hot cell to the conditioning station.

Entry  Wednesday, March 26, 2014, 06:57, David Wang, South Hot-Cell, Standard Operation, TM4, Ta#42, Leak check on TM4 HS water line with new Ta #42 target. 

Chad and I leak checked TM4 HS line with Ta#42 target on the module. The leak detector base LR 0.0xE-9 atm.cc/sec, base pressure0.0xE-4 torr. Chad applied helium to the joints, and flushed the helium around the target. No leak has been found.I will do helium pressure test on this circuit at CS later.

Entry  Tuesday, March 25, 2014, 13:29, Travis Cave, South Hot-Cell, Standard Operation, TM4, Ta#42, Electrical check TM#4_notarget_electest_SHC.PDFTM#4_Ta42surf_electest_SHC.PDF

TM#4 was checked electrically with and without target on it, see attached PDFs for details.

Entry  Tuesday, March 25, 2014, 09:11, chad fisher, South Hot-Cell, Standard Operation, TM4, Ta#42, Ta#42 install and "new" 9 pin TM4_20140325_01.jpg

Ta#42 has been installed onto TM4. The "new" 9 pin connector was not an issue...attually went on better than any other previous one. Leaving the mounting screws loose on the target half allowed use of the manipulator to center the pins and insert them with ease.

Entry  Monday, March 24, 2014, 12:01, Travis Cave, ITW, Standard Operation, TM4, no target, module move 

TM#4 has been moved from the west target station to the south hot cell.

Entry  Friday, March 21, 2014, 16:49, Keith C Ng, ITE, Repair, , , 2a3 window - tank flange inspection 20140321_2a3window_RHB_6777.JPG20140321_2a3window_P1030055.JPG20140321_2a3window_P1030057.JPG20140321_2a3window_IMG_0846.JPG

Today:

1) Cleaned flange with methanol and cotton glove, appears to be clean.

20140321_2a3window_IMG_0846.JPG

 

2) Installed new beam tube and cradle into wall penetration, cradle was setup same as previous cradle (which is now removed). On advancing into position, the flange on the flexible bellows appears to get stuck on the spigot of the fixed tank flange. Removed and measured slot, is undersize (.373-.374), will re-machine slot for spigot.

20140321_2a3window_P1030055.JPG20140321_2a3window_P1030057.JPG

 

3) On visual inspection, ITE tank flange appears to be warped in a location consistent with the clamping area of the window clamp. Further investigation is required.

20140321_2a3window_RHB_6777.JPG

Entry  Thursday, March 20, 2014, 08:19, Travis Cave, Conditioning Station, Standard Operation, TM1, no target, module move 

TM#1 with no target moved from the conditioning station to north west silo.

Entry  Wednesday, March 19, 2014, 16:48, Keith C Ng, ITE, Repair, , , 2a3 window - beam tube removal 11x

Today:

1) Vaccumed top and around clamp. Disconnected clamp from flanges and removed from beam line. Currently bagged and stored in metal pail next to target pit area. Clamp is 500 µSv @ 1/2 m.

 20140319_2a3window_IMG_0813.JPG20140319_2a3window_IMG_0815.JPG20140319_2a3window_IMG_0814.JPG20140319_2a3window_IMG_0819.JPG

 

2) Removed 2A3 window from beam line. Pried apart joint from top of target station using pole tool. Window is 95 mSv o.c. 5000 µSv @ 1/2 m. Currently stored in a metal shield & covered with lead blanket infront of spent target vault.

20140319_2a3window_IMG_0823.JPG20140319_2a3window_IMG_0824.JPG20140319_2a3window_IMG_0828.JPG20140319_2a3window_IMG_0829.JPG

 

3) Did preliminary clean of tank side flange with cotton glove. See videos in RH group folder. A mark still remains on flange.

 

4) Installed dust cover over tank flange.

 

5) Removed old leaking beam tube + support from wall penetration. Currently stored in 2A tunnel, both pieces are bagged. 500 µSv @1/2m, 12000 µSv o.c. Took 2 vials/samples of the deposits inside the plastic piping surrounding the beam tube supports. Material appears to be crystalline and moist.

20140319_2a3window_RHB_6711.JPG20140319_2a3window_IMG_0834.JPG20140319_2a3window_IMG_0843.JPG

Entry  Wednesday, March 19, 2014, 15:46, David Wang, ITW, Standard Operation, TM4, , TM4 and ITE air to vacuum leak check and TM4 water lines helium test. 7x

With TM4 located in ITW, All air to vacuum seals  on ITW primary and secondary vacuum vessels have been leak  checked with leak detector hooked directly onto the TM4 service cap.The base LR :00xE-9atm.cc/sec. The ITW IG1 was 1.16xE-6 torr which was good. No leak has been found during the checking.Also, the TM4 water lines(except HS) had been  pressurized with 70 psi helium on each for 2 minutes. There was no response during the test. The ITW and TM4 are good on leak checking.See attachment pictures

Entry  Tuesday, March 18, 2014, 16:01, Keith C Ng, ITE, Repair, , , 2a3 window - prep and clean Fullscreen_capture_03182014_35409_PM.bmp.jpgFullscreen_capture_03182014_35316_PM.bmp.jpg

Continued with vacuuming inside wall penetration to remove debris. Changed filter bag in nilfisk vacuum, left old filter in place however vacuum continues to stall after >5min use. Vacuum gets quite warm before self shutting off. Debris seems to be falling back down on to joint if vacuum is turned off.

Took some screenshots of video showing removed debris and rust(?) on beam pipe. Video located on remote handling group folder.

Will attempt to remove clamp tomorrow.

 

Fullscreen_capture_03182014_35409_PM.bmp.jpgFullscreen_capture_03182014_35316_PM.bmp.jpg

Entry  Monday, March 17, 2014, 15:39, Keith C Ng, ITE, Repair, , , 2a3 window - prep and clean 

Cleaned top of the ITE vacuum flange and top of window clamp. Attempted to clean the bellows/beam pipe through the wall, mostly dust and small particles. When cleaning bottom of the wall penetration we picked up a stone/fragment and the vacuum stopped. Appears to be a rock of some kind. 800cpm.

Videos on \\trwindata\groups\remote handling\Videos\2014\2014_2A3window folder, videos 3 and 4.

Entry  Thursday, March 13, 2014, 16:23, Keith C Ng, ITE, Repair, , , 2a3 window - inspection Fullscreen_capture_03132014_41458_PM.bmp.jpgFullscreen_capture_03132014_41527_PM.bmp.jpg

Video inspected 2a3 window joint this morning.

Screenshots from video showing debris forming around aluminum cradle and brown/red dust on top of beam pipe.

Fullscreen_capture_03132014_41458_PM.bmp.jpgFullscreen_capture_03132014_41527_PM.bmp.jpg

Inspection video can be seen in its entirety at \\trwindata\groups\remote handling\Videos\2014\2014_2A3window

Entry  Thursday, March 13, 2014, 07:35, David Wang, ITW, Standard Operation, TM4, , TM4 and ITW turbo pumps have been started 

I connected ITW  vacuum system to TM4. TM4 and ITW turbo pumps have been started successfully. The pumping down is good so far.

Entry  Wednesday, March 12, 2014, 16:33, Keith C Ng, ITE, Repair, , , 2A3 window removal and replacement 20140312_2a3window_RHB_6676.JPG20140312_2a3window_RHB_6682.JPG2a_bp_sw1_white_powder_under_w11.PDF2a_bp_sw2_white_powder_under_w11.PDF2a_bp_sw3_rust_w11.PDF

prep'ed area for work:

- removed shield plug from window clamp area

- inspected clamp from tunnel side and from top of target station: video recorder was not working, will try again tomorrow.

- corrosion seen on beam pipe cradles, see photos. corrosion also seen on beampipe, clamp and vacuum tank. will try to vaccuum loose rust tomorrow.

note: gamma spec of rust, white powder from RPG located in \\trwindata\groups\remote handling\Documents\2014\2A3 Window folder (added pdfs as attachments 2014 mar 4)

 

20140312_2a3window_RHB_6676.JPG

20140312_2a3window_RHB_6682.JPG

 

Entry  Wednesday, March 12, 2014, 09:45, Travis Cave, ITW, Standard Operation, TM4, no target, module move 

TM#4 has been moved from the north west silo to the west target station.

Entry  Tuesday, March 11, 2014, 10:47, Travis Cave, ITE, Repair, , , entrance module move 

ITE entrance module has been moved from the east station to the south east silo.

Entry  Monday, March 10, 2014, 09:39, Travis Cave, ITE, Standard Operation, TM3, no target, module move 

TM#3 with no target has been moved from the east target station to the south west silo.

Entry  Friday, March 07, 2014, 12:45, David Wang, ITE, Standard Operation, TM3, , TM3 and ITE air to vacuum leak check and TM3 water lines helium test. 001.JPG002.JPG003.JPG010.JPG013.JPG

With TM3 located in ITE, All air to vacuum seals  on ITE primary and secondary vacuum vessel have been leak  checked with leak detector hooked directly on the TM3 service cap.The base LR :00xE-9atm.cc/sec. The ITE IG1 was 1.6xE-6 torr which was good. No leak has been found during the checking.Also, the TM3 water lines(except HS) had been  pressurized with 70 psi helium on each for 2 minutes. There was no response during the test. The ITE and TM3 are good on leak checking.See attachment pictures

Entry  Thursday, March 06, 2014, 14:12, David Wang, Conditioning Station, Standard Operation, TM1, , TM1 air to vacuum and water lines leak check at CS. 8x

TM1 air to vacuum and water lines leak check at CS are finished this afternoon. The leak detector  is hooked directly to TM1 service cap so the base LR at LD is 0.0xE-9 atm.cc/sec. I sprayed helium to all air to vacuum seal on the service cap, also applied 70 psi to all water lines(except HS) for 2 minutes each. There is no any tiny response had been found on LD. So All TM1 water lines(except HS) and air to vacuum seals are leak free. The HS circuit can not be tested at this time since the VCR caps are not installed. The turbo pumps at CS and TM1 will be turned off before I leave.  See attachment pictures.

Entry  Thursday, March 06, 2014, 12:59, David Wang, Conditioning Station, Maintenance, TM1, , Restart TM1 and CS TPs  

Restarted TM1 and CS turbo pumps after the power off. Everything is fine .

Entry  Thursday, March 06, 2014, 06:58, David Wang, ITE, Maintenance, TM3, , ITE vacuum and leak check on ITE BL2A window flange. 

ITE and TM3 Turbo pumps have been started successfully yesterday. The vacuum reading on all ITE high vacuum gauges are at low E-6 range after one night pumping down which are good so far. There is no any sign of leak on BL2A window and the flange seal on ITE side. Yesterday afternoon, Ron , Edi ,and I  did a leak check on the ITE BL2A window flange(2aTunnel side). The leak detector was hooked onto BL2A in tunnel. Ron and I supplied helium from TH  to the helium test line(located in  ITE pit) which  we have on ITE BL2A window flange.   The helium test line end nozzle is just located under  the bottom of the 2A window flange. Edi was in BL2A tunnel checking the leak detector. We supplies 10- 15 psi helium 3 times to the test line. Each time for 10 seconds. The helium flow was checked twice and they were good. The LD base LR was 2.2xE-5 atm.cc/sec, After 70 seconds , The leak rate on LD was increased to 5.3 xE-5 atm.cc/sec. The leak rate reading  recovered after 20seconds. There is no obviously conclusion where the leak is. At that moment, Ron said, he and Edi would like to do  some further leak check  in 2A tunnel,and I went back to my job.

Entry  Thursday, March 06, 2014, 06:28, David Wang, Conditioning Station, Maintenance, TM1, , TM1 had been moved from silo to CS 

TM1 has been successfully moved from silo to CS. The CS vacuum system is connected  to TM1. Turbo pumps on TM1 and CS have been started yesterday afternoon . The starting of TM1 turbos was easy. The pumping down over night is good so far.

Entry  Wednesday, March 05, 2014, 10:07, Travis Cave, Conditioning Station, Standard Operation, TM2, no target, module move 

TM#2 with no target or source tray has been moved from the conditioning station to the north east silo. TM#1 with no target has been moved into the conditioning station.

Entry  Tuesday, March 04, 2014, 10:19, Travis Cave, ITE, Standard Operation, TM3, no target, module move 

TM#3 has been moved from the silo to the east target station.

Entry  Tuesday, February 25, 2014, 10:00, David Wang, Conditioning Station, Repair, TM2, , helium pressure test on TM2 tube heater (+) water line with blank off(C-seal) installed on WB. 10x

I did the helium pressure  test  on TM2 tube heater (+) water line  with blank off(C-seal) installed on  water block at CS.The leak detector was hooked directly to the top of the module this time. So base leak rate and base pressure were at the bottom scale on LD. 30 -80 psi helium was applied to the D lines(both side)  with10 psi   increasing each time. There is no any tiny response hasbeen found during the test. The lines are perfectly sealed. Also i sprayed the helium on the top of the service cap .All  air to vacuum seals on the top are good either. See attachment pictures.

Entry  Tuesday, February 25, 2014, 06:53, David Wang, South Hot-Cell, Repair, TM2, , Leak check on TM2 tube heater (+) water line with blank off(C-seal) installed on WB. 

Chad and I did the leak check   on TM2 tube heater (+) water line  with blank off and C-seal  installed on  WB at South Hot Cell.The line was easy to pump down to 0.0xE-9atm.cc/sec and 0.0XE-4 torr on leak detector. Chad flushed lot helium around the water block (10 sec spray). No response had been found on leak detector.

Entry  Monday, February 24, 2014, 13:52, Travis Cave, South Hot-Cell, Standard Operation, TM2, no target, module move 

TM#2 moved from the south hot cell to the conditioning station.

Entry  Monday, February 24, 2014, 12:09, chad fisher, South Hot-Cell, Repair, TM2, , C-seal blank off test TM2_20140224_1.jpg

Circuit D has passed the vacuum leak check. Jig has been removed and containment box re-installed for move to conditioning station.

Entry  Monday, February 24, 2014, 11:05, chad fisher, South Hot-Cell, Repair, TM2, , Circuit D blank off 

The blank off with the o-ring has been removed, manipulator fixed, circuit D water block sealinhg surfaces cleaned and blank off with c-seals installed and torqued. Leak check will occur shortly.

Entry  Thursday, February 20, 2014, 11:04, chad fisher, South Hot-Cell, Repair, TM2, , Readying TM2 for C-Seal Leak Check TM2_20140220_01.jpg

Containment box has been removed and water block jig installed.

Entry  Thursday, February 20, 2014, 09:45, Travis Cave, Conditioning Station, Standard Operation, TM2, no target, module move 

TM#2 has been moved from the conditioning station to the south hot cell.

Entry  Tuesday, February 18, 2014, 11:26, David Wang, Conditioning Station, Repair, TM2, , I stopped turbo pumps and disconnected vacuum system on TM 2 and CS 

I stopped turbo pumps and disconnected vacuum system on TM2 and CS. The TM2 will be moved to SHC for C seal installation on "D" water block.

Entry  Monday, February 17, 2014, 09:32, David Wang, Conditioning Station, Repair, TM2, , helium pressure test on TM2 tube heater +(D) water line. 6x

I did the helium pressure test on Tube heater+ line this morning. The vacuum on CS and TM2 are very good. The base lake rate on leak detector was 1.7xE-7 atm.cc/sec. Base pressure was 0.0xE-4torr.  I applied helium to the "D"line .The test started from 30psi up to 80psi on both side "D" line.The base leak rate slightly changed to 1.9xE-7 atm.cc/sec during the test,but not base pressure. At this base leak rate level, No obvious leak had been found . See attachment pictures. The test will be repeated later when the base leak rate could be pumped into E -8 or E-9(the best) range.            

Entry  Thursday, February 13, 2014, 14:23, David Wang, South Hot-Cell, Repair, TM2, , Leak check on TM2 tube heater (+) water line with blank off(elastic seal) installed on WB. 005.JPG001.JPG

Chad and I did the leak check on TM2 tube heater (+) water line  with blank off( + elastic o ring seal) installed on "D"  water block in SHC. We got the same no leak result as we got with rubber insert this morning.

Entry  Thursday, February 13, 2014, 13:30, David Wang, South Hot-Cell, Repair, TM2, , pressure test on TM2 tube heater +(D) water line. 

Chad and I did the pressure test on TM2tube heater+(D) water  line at SHC with shop air.We tested from 30psi to 80psi on both side of D line. The bubbles were found at 50-55psi on blank off seal in SHC.

    Reply  Thursday, February 13, 2014, 14:15, David Wang, South Hot-Cell, Repair, TM2, , pressure test on TM2 tube heater +(D) water line. 007.JPG008.JPG013.JPG

David Wang wrote:

Chad and I did the pressure test on TM2tube heater+(D) water  line at SHC with shop air.We tested from 30psi to 80psi on both side of D line. The bubbles were found at 50-55psi on blank off seal in SHC.

 I would like to correct this E-LOG. There is no real  leaking bubble had been found during the whole test according to the information supplied by Chad  Fisher during  this afternoon meeting. I would like to attach some pictures took from TH during this test.

Entry  Thursday, February 13, 2014, 09:24, David Wang, South Hot-Cell, Repair, TM2, , Leak check TM2 tube heater (+) water line with rubber insert blocked WB in SHC 001.JPG002.JPG003.JPG004.JPG

Chad and I  did the Leak checked TM2 tube heater (+) water line  with rubber insert plugged water block on " D"  in SHC. The Leak detector was very easy to pump down to the bottom leak rate and pressure. Chad checked the helium flow in SHC, and sprayed 10 second helium on  the block. There is no response had been found during the test. The test was repeated again and no leak has been found. See attachment pictures.

Entry  Tuesday, February 11, 2014, 13:56, chad fisher, South Hot-Cell, Repair, TM2, , waterblock cleaning TM2_20140207_2.jpgTM2_20140211_2.jpg

New cleaning and polishing pads have been inserted onto the hot cell as well as rubber bungs and a new blank off.

The inital waterblock cleaning with the "scotch bright" pads has been completed. See attached pictures...the first picture being before and the second after.

Tommorow the water block will have bungs put in and a leak check to check the block will take place. After that, the new blank off will be installed and tested.

 

Entry  Friday, February 07, 2014, 10:29, chad fisher, South Hot-Cell, Repair, TM2, , TM2 C.B. and circuit D TM2_20140207_1.jpgTM2_20140207_2.jpg

Containment box has been removed and the blank off from circuit D has been removed for inspection of both the blank off and water block sealing surface.

Entry  Wednesday, February 05, 2014, 14:12, Travis Cave, Spent Target Vault, Standard Operation, , , Targets moved from mini storage to F-308s 

All targets in the mini storage (4) have been moved from there and placed into the F-308s and those have been moved to the mech services room.

Entry  Wednesday, February 05, 2014, 14:05, David Wang, South Hot-Cell, Repair, TM2, , Leak check TM2 tube heater (+) water line from inside service cap in TH. 005.JPG008.JPG005.JPG

Bevan and I did a leak check on TM2 tube heater+ from inside service cap in TH. The leak detector base leak rate 0.0xE-9 atm.cc/sec, base  pressure 0.0xE-4totrr. One of side panel on service cap was opened. Bevan sprayed the helium to the "D" line inside the blue insulator.The helium flow was checked , and he sprayed twice. No response has been found on leak detector.  See attachment pictures

Entry  Tuesday, February 04, 2014, 09:42, David Wang, South Hot-Cell, Repair, TM2, , pressure test on TM2 tube heater +(D) water line. 10x

Chad and I did a pressure test on TM2 tube Heater+(D) water line.I pressurized the D line with shop air from quick connectors(both ends) on service cap.chad applied bubble soap onto the D water block in SHC. The test started from 5psi,and increased 5psi each time to 40 psi. From 5 to 35 psi, no bubble has been found on water block. At 40 psi , bubble appeared from blind blank off seal , but not from soldering joints. Since the o-ring seal for the blank off is  vacuum seal , but not for pressurizing, It is understandable the seal could not hold 40 psi pressure air. No bubble had been found on the D water block soldering joints .See attachment pictures.

Entry  Tuesday, February 04, 2014, 08:04, David Wang, South Hot-Cell, Repair, TM2, , Leak check TM2 tube heater (+) water line. IMG_0012.JPGIMG_0013.JPG

Chad and I leak checked TM2 tube heater(+) water line yesterday afternoon. The water line was difficult to pump down on base leak rate, but LD  base pressure was fine . The base pressure on leak detector was pumped to 0.0XE-4 torr quickly. The base leak rate only could be pumped  to  4.5 xE-8 atm.cc/sec after 1 hour waiting time. All vacuum connections to leak detector  in the target hall were leak checked and they were good. Chad checked helium flow in SHC. He sprayed helium twice on tube heater(+) water block soldering joints. I did not see any response on leak detector in TH.The base Leak rate and base pressure did not move up during the test.  See attachment pictures.

Entry  Monday, February 03, 2014, 14:45, Travis Cave, Spent Target Vault, Standard Operation, , , Spent targets to mini storage and the F-308s to the Target Hall Vault_Storage_February_3_2014.pdfMini_Vault_Storage_February_3_2014.pdf

Targets NiO#1(101), Nb#5(85), TaC#1(92), and ZrC#5(81) have been moved from the storage vault and placed in the mini storage. The F-308 flasks have also been moved in to the target hall as well. The attached are the current statuses of both vaults.

Entry  Thursday, January 30, 2014, 13:46, Travis Cave, Conditioning Station, Standard Operation, TM2, no target, module move 

TM#2 has been moved from the conditioning station to the south hot cell.

Entry  Wednesday, January 22, 2014, 15:20, Anders Mjos, South Hot-Cell, Standard Operation, , UC#8, Target Inspection - post beam 

The Target Assembly was inspected with Chad, Jens Henning and Anders today.

  • The Target Container was broken.
  • Material was deposited on the Heat Shield around the Target Center Block
  • Material was deposited on the IG-LIS source.
  • Electrical checks to ground (HS)
    • The Extraction Electrode passed the electrical check at 1000V
    • The Exit Electrode (c) held only 40V at 22 kOhm
    • The IG Electrode 1 (f) held 250V at 390 MOhm
    • The IG Electrode 2 (g) held only 40V at 22 kOhm
  • IG 1 and IG 2 both held 250V at 450 MOhm to Exit Electorde (c)
  • No spark marks were observed on the 9-pin connector

See photos of the inspection on DocuShare

Entry  Wednesday, January 22, 2014, 15:00, Travis Cave, Spent Target Vault, Standard Operation, , UC#8, Spent target move Vault_Storage_January_22_2014.pdf

UC#8 has been moved from the south hot cell to the vault storage. It was placed in pail 113 and placed in slot 8A of the vault. The field was 9.2mSv/hr upon removal from the south hot cell.

Entry  Wednesday, January 22, 2014, 10:51, David Wang, ITE, Repair, , , Removed 4 shielding blocks located on top of preseperator in TH 

Travis and I removed 4 shielding blocks located on top of pre-seperator  in TH. This is a job for ITE harp 9 re-installation after it  is repaired . The blocks move are successful.

Entry  Tuesday, January 21, 2014, 14:32, Travis Cave, South Hot-Cell, Standard Operation, TM4, no target, module move 

TM#4 has been moved from the south hot cell to the north west silo.

Entry  Monday, January 20, 2014, 14:37, Travis Cave, ITE, Standard Operation, TM4, UC#8, module move 

TM#4 with UC#8 has been moved from the east target station to the south hot cell.

Entry  Monday, January 20, 2014, 13:40, maicodallavalle, Spent Target Vault, Maintenance, , F-308, Empty F-308s 

Four empty F-308s just arrived back at Triumf. I moved them  from shipping to the Remote Handling Shop for service and inspection. I will work on them when not busy with my other shutdown work. ( Cyclotron work)

Entry  Monday, January 20, 2014, 13:38, David Wang, ITE, Standard Operation, TM4, , DISCONNECTED TM4 IN ITE. 

I DISCONNECTED TM4 IN ITE. ALL WATER LINES HAD BEEN PURGED OUT WITH PRESSURE AIR.

Entry  Monday, January 20, 2014, 13:35, David Wang, ITE, Standard Operation, TM4, , 5 shielding blocks had been moved out of ITE 

5 SHIELDING BLOCKS HAD BEEN MOVED OUT OF ITE.AIR SAMPLE AND SWIPED FIRST BLOCK AND ITE PIT.NOTHING HAD BEEN FOUND ON ALPHA MONITOR AND OTHER TWO MONITORS.

Entry  Thursday, January 16, 2014, 10:36, chad fisher, South Hot-Cell, Repair, , , East Manipulator Repair Manip_repair_20140114.jpgManip_repair_20140115.jpg

The repair/cable replacement on the east manipulator is now complete.

Yesterday's initail cable replacement went very well however, due to a minor glich, we were unable to test the tong movement until I was out of the hot cell. Tong did not fully close and felt like there was a "hard stop" at a repeatable spot in the  closing of the tong. Upon further investagation, I determined that the problem was definelty on the slave side.

I conducted a troublshooting exercise this morning to narrow down the problem. I quickly found that the new tong came from the manufacture with two incorrect fasteners (socket head cap screws) instead of set screws. As a result the tong was being kept from closing as the head of the socket head cap screws was interfering.

I replaced the SHCS was the set screws from the old tong. The tong now functions with full range of motion.

Jan. 15, 37 minutes in cell .26 mSv

Jan. 16, 16 minutes in cell (as I did some clean up of compressable waste) .05 mSv

Also, the inital repair utilized a prototype tool I designed (and with assistance from Maico, built). This tool made the repair much easier. I will be making small improvements to the design and issuing drawings to the vault and shop.

 

 

Entry  Thursday, January 09, 2014, 11:07, chad fisher, South Hot-Cell, Maintenance, , , Field Level 

I have managed to reduce the field at the broken manipulator from 12 mSv/h to 400 uSv/h.

Entry  Thursday, December 12, 2013, 11:14, Bevan Moss, Conditioning Station, Standard Operation, TM2, , HV Chase Electrical Test 

While under vacuum Travis and I completed diagnostics of the HV chase. Majority of the lines showed OL at 1kV but there were the following "failures"

A to P @ 250V 716kOhm
A to Q @ 1kV 25.18MOhm
B to C with ohm meter 8Mohm @250V 830kOhm
B to D @ 1kV 15.57MOhm
C to D @1kV 16.18 MOhm
P to Q @1kV 1.069 GOhm
G to J with ohm meter dead short.

Ideally all of these values would be OL and they may improve or get worse when the source tray is installed depending on where the electrical contact is. I need to discuss with Friedhelm but I believe that as these values the module can still operate. Without changing the HV chase there is very little chance of improving these values.

Entry  Monday, December 09, 2013, 14:47, David Wang, ITE, Standard Operation, TM4, , I moved 5 shielding blocks from block storage area to ITE. 

I moved 5 shielding blocks to ITE. The ITE is configured to take proton beam.

Entry  Monday, December 09, 2013, 13:15, Travis Cave, Spent Target Vault, Standard Operation, , Ta#41, Spent target move Vault_Storage_December_9_2013.pdf

The spent Ta#41 target has been moved from the south hot cell to the spent target storage vault. It is an unnumbered pail (should be pail 112) and placed in spot 7A of the vault it had a reading of 536mSv/hr upon removal from the south hot cell. See attached PDF for vault details.

Entry  Friday, December 06, 2013, 15:09, Bevan Moss, Conditioning Station, Standard Operation, TM2, , TM2 no source tray 55kV 1 hour 06122013_TM2_No_source_Tray_55kV_1_hour.JPG06122013_TM2_No_Source_Tray_55kV_1_Hour.txt

Today 55kV was applied to TM2 and held for over 1 hour with the EINZEL at 27.5kV. There were 2 sparks and the current was unstable at this voltage but this test should be considered a success. Once again while bringing the voltage up the canbus continued to be a problem. After successfully passing the test I continued to raise the BIAS and EINZEL. A spark at 57kV tripped a controller for the vacuum and the canbus. As stated before I believe the module will reach 60kV and that there is an interaction between the EINZEL and the BIAS. I am not certain if that interaction is internal or external to the module. Attached is a screen shot and the dumped data.

Entry  Thursday, December 05, 2013, 14:57, David Wang, ITE, Standard Operation, TM4, , Connected TM4 in ITW 

I connected TM4 in ITE. All turbo pumps have been started and wok fine including new TP3. Everything is good so far.

Entry  Thursday, December 05, 2013, 14:55, David Wang, South Hot-Cell, Standard Operation, TM4, , Leak check on TM4 target heat shield 

Chad and I leak checked TM4 heat shied water circuit at SHC. The pumping down was very good.Base leak rate 0.0xe-9 atm.cc/sec. BP 0.0xe-4torr. Sprayed helum twice on both VCR fittings.There is no response on leak detector.  The circuit is leak tight.

Entry  Thursday, December 05, 2013, 12:51, Travis Cave, South Hot-Cell, Standard Operation, TM4, UC#8 and no target, Electrical check TM#4_UC8_electest_SHC.PDFTM#4_notarget_electest_SHC.PDF

Electrical check was done on TM#4 without a target and with the UC#8 target on see attached PDF for results.

Entry  Thursday, December 05, 2013, 12:04, Travis Cave, ITE, Standard Operation, TM4, UC#8, module move 

TM#4 with UC#8 has been moved from the south hot cell to the east target station.

Entry  Wednesday, December 04, 2013, 14:09, Travis Cave, South Hot-Cell, Standard Operation, TM4, Ta#41, Electrical check TM#4_Ta41_electest_SHC_PostBeam.PDF

Electrical check of TM#4 with Ta#41 post beam at the south hot cell. See PDF for details

Entry  Wednesday, December 04, 2013, 13:57, chad fisher, South Hot-Cell, Standard Operation, TM4, Ta #47, Ta #47 Removed - broken bolt 

Ta #47 has been removed from TM4.

One containment box cover bolt would not come out. Upon attempted removal with the stud remover the bolt sheared...which is not uncommon...just hasn't happened in many years...CBB being stuck or shearing.

Nine pin connector shows the typical "arcing" mark.

Entry  Wednesday, December 04, 2013, 11:15, David Wang, ITE, Repair, TM4, , New bolts are installed on ITE TP3. 

I installed 8 new bolts(3/8-16 UNC x1.25  STL) on the ITE TP3. The ITE TP3 replacement job is done. Everything is connected back to the pump. and it is ready for starting.

Entry  Wednesday, December 04, 2013, 11:05, David Wang, ITW, Standard Operation, TM4, Ta41#, I disconnected TM4 in ITW 

I disconnected TM4 in ITW .The job took about 20minutes and I got 0.11 msv dose.

Entry  Wednesday, December 04, 2013, 10:44, Travis Cave, South Hot-Cell, Standard Operation, TM4, Ta#41, module move 

TM#4 with Ta#41 has moved to the south hot cell, the move it self was uneventful but, the fields on the module are extremely high when lowering it down into the south hot cell the module had a maximum field of about 392mSv/hr. The shield plug was also installed remotely as well due to the 12mSv/hr field at the top of the west target station due to shine from the dump.

Entry  Tuesday, December 03, 2013, 14:14, Bevan Moss, Conditioning Station, Standard Operation, TM2, , HV conditioning  TM2_conditioning_03122013.JPG

 It was attempted to HV condition TM2 to 55kV and leave it operating there for an hour to demonstrate stability. Unfortunately at 52.65kV a spark destroyed the canbus controller. This controller had shown issues in the past but seemed to magically fixed itself. I will contact Hubert for another card. Attached  is is a screen shot of the stip tools. 

Entry  Tuesday, December 03, 2013, 10:35, Travis Cave, ITW, Standard Operation, , , fields above and in the target station with blocks off 

The blocks have been removed from the west target station. The fields at the top of the target pit at the railing at waist level is about 80uSv/hr, Turbo pumps are about 805uSv/hr, backing lines for the turbos about a 1mSv/hr and the average field in the area of work down in the pit is about 600 to 750uSv/hr. The proton beam went off at 10:45 on December 2nd, these measurements were done at 09:00 on December 3rd.

 

Another set of field measurement was done at the west target station. At the top of the west target station at the railing the field ranged from 50 to 70 uSv/hr. The turbo pumps had field of about 650uSv/hr, the area over the dump was about 750uSv/hr, the area over the HV cover and the south side was about 450uSv/hr. These measurements were done at 13:15 on December 3rd.

Entry  Tuesday, December 03, 2013, 09:58, David Wang, ITW, Standard Operation, TM4, , I moved 5 shielding blocks from ITW to block storage area. 

I moved 5 shielding blocks from ITW to block storage area.

Entry  Monday, December 02, 2013, 11:29, Travis Cave, South Hot-Cell, Standard Operation, TM3, no target, module move 

TM#3 with no target has been moved from the south hot cell to the northeast silo.

Entry  Friday, November 29, 2013, 11:54, chad fisher, South Hot-Cell, Repair, TM3, , Steerer short investegation TM3_20131129_Steerer_1.jpgTM3_20131129_Steerer_2.jpgTM3_20131129_Steerer_3.jpg

Using in cell camera and transit the suspect line on the steerers was inspected as best as possible. An existing photo of the complete steerers before installation was used for comparison. The wiring and beading inspected today showed no obvious problems, breaks or spots where there may be a short. In comparison to the photo from construction, what we could see of the steerers looked identical to the original installation.

    Reply  Friday, November 29, 2013, 11:57, Bevan Moss, South Hot-Cell, Repair, TM3, , Steerer short investegation 

chad fisher wrote:

Using in cell camera and transit the suspect line on the steerers was inspected as best as possible. An existing photo of the complete steerers before installation was used for comparison. The wiring and beading inspected today showed no obvious problems, breaks or spots where there may be a short. In comparison to the photo from construction, what we could see of the steerers looked identical to the original installation.

 The test was repeated to confirm that there was a short.

Entry  Wednesday, November 27, 2013, 15:24, Bevan Moss, South Hot-Cell, Maintenance, TM3, , Wiring Harness Electrical Test IMG_1269.JPG

 Maico removed the containment box today allow Travis and I to further test the wiring harness. I disconnected the junction block and Travis and I repeated the test from yesterday. The all lines except the PNG tested OL. The module was then lowered and the twisted pair connected to the pin that corresponds to the steerer labeled BTM (it is likely this is not labeled correctly). This testing showed showed that the source of the short found yesterday is in the wiring harness or the source tray. The PNG gauge was then tested again. When beeping out the harness to find the location of the pin it was found that the short had gone away. This circuit was then tested with the megger at 500V and showed OL. Don Jackson has suggested looking at the SHV feed through. It is difficult to determine where the source of the problem is as it is intermittent. The source tray side wiring harness for the steerers was then disconnected from the steerers and tested to OL. Finally the connections on the source tray were tested. It was determined that the third socket down (see attached picture) has a short somewhere to ground. When Chad returns on Friday I will have him complete a visual inspection and if the source can be found we may be able to deflect the line. Failing that to repair this connection a new steerer cone assembly will need to be installed.

Entry  Wednesday, November 27, 2013, 12:50, Bevan Moss, South Hot-Cell, Standard Operation, TM3, , Ground devices wiring check 

 Travis and I completed an electrical check on the wiring harness for the devices on the ground plane. All lines passed 500V with the megger except for PNG and the BTM steerer. Those devices had a short to ground. of ~1.4ohm.

Entry  Tuesday, November 26, 2013, 14:10, Travis Cave, Crane, Maintenance, , , Thermal relay replaced 

The bad thermal motor protection relay for the crane has been replaced with a new unit. Crane was tested in pendant(local) operation and all drives worked.

Entry  Monday, November 25, 2013, 11:48, Travis Cave, South Hot-Cell, Standard Operation, TM3, no target, module move 

TM#3 with no target has been moved from the north east silo to the south hot cell.

Entry  Friday, November 22, 2013, 10:29, Travis Cave, Spent Target Vault, Standard Operation, , NiO#2, Spent target move Vault_Storage_November_22_2013.pdf

NiO#2 has been moved from the south hot cell into spent target storage. It was placed in pail 111 in slot 3C of the storage vault. It was 76.4mSv/hr upon removal from the south hot cell.

Entry  Thursday, November 21, 2013, 12:12, Anders Mjos, South Hot-Cell, Standard Operation, TM3, NiO#2, End of beam target inspection - ANODE does not hold 250V 

The target was inspected by Chad and Anders in the Hot Cell. Electrical megger tests were done during the assembly. It was found that Insulators No 3 (ITD0311) and No 2 (ITD0310) failed to hold voltage after the run.

  [V] [kOhm]
ANODE - HS 40 21
ANODE - TGT 100 55
HS - TGT 100 55
Lid removed    
ANODE - HS 40 21
ANODE - TGT 90 41
HS - TGT 100 55
Target removed    
ANODE - HS 245 139
No 3 Ins - TBHT 0 0
No 2 Ins 110 64
No 2 Ins removed    
ANODE - HS 540 OL

EE to HS was measured OL at 1000  V.

Photos can be found on DocuShare

 

 

Entry  Wednesday, November 20, 2013, 13:52, Bevan Moss, Conditioning Station, Standard Operation, TM2, , HV testing of TM2 20112013_HV_conditioning_TM2.JPG20112013_TM2_No_source_tray_HV_Test_no_cover.txt

 HV testing without the cover continued today. With the EINZEL lens at 30kV the target module was able to achieve 58.7kV. At this voltage any spark was reeking havoc on the electronics of the TCS. Vacuum gauges signals were occasionally lost, the thermocouple reading would occasionally be lost, turbo pump would turn off. All of these events caused the interlocks to trip resulting in the power supplies to be turned off. As a result I bypassed majority of the interlocks to prevent this from happening. Ultimately as spark took out the CANBUS controller first for the EINZEL lens and then for the BIAS. David Morris has been contacted to have them replaced. The damage of the CANBUS controller for these power supplies is becoming a common problem and should be investigated for if there is a better solution. During testing I experimented with raising the BIAS to near its limit followed by the EINZEL lens and vise versa. From this it was determined that the EINZEL must be raised to high voltage before the BIAS otherwise sparking occurs. Even a step from 0 to 500 volts on the ENIZEL lens with the BIAS at 55kV caused sparking. There are a few combinations of testing along this line I would like to continue with but initially my though is that the BIAS and ENIZEL do not have sufficient clearance for the BIAS to operate above 55kV. Attached is a screen shot of the strip tool and the data. I have not heard from David yet but I do not expect the TCS to be operational today. 

Entry  Wednesday, November 20, 2013, 09:52, Travis Cave, South Hot-Cell, Standard Operation, TM3, no target, module move 

TM#3 with no target has been moved from the south hot cell to the north east silo.

Entry  Wednesday, November 20, 2013, 08:50, chad fisher, South Hot-Cell, Standard Operation, TM3, NiO#2, NiO#2 removed TM3_20131120.jpgTM3_20131120_2.jpg

NiO#2 has been removed from TM3

Entry  Tuesday, November 19, 2013, 16:55, Bevan Moss, Conditioning Station, Standard Operation, TM2, , HV conditioning external_sparking.JPG19112013_HV_conditioning_TM2.JPG19112013_TM2_No_source_tray_HV_Test_no_cover.txt19112013_TM2_No_source_tray_HV_Test.txt

 HV conditioning of TM2 continued today. At ~53.5kV the module started to spark externally to the HV cover. This is the first time the cover has been tested to this high of a voltage due to the limitations of the modules. As such for the conditioning station to achieve 60kV while keeping the target hall open of personnel the cover and cage will need to be modified. To continue with HV testing of TM2 the cover was removed and the target hall locked out as per the procedure covered in Document 70039 "ISAC Conditioning Station: First Lock-Out and High-Voltage "ON". With the cover off the module was able to achieve ~56.7kV without the Einzel lens on. Eliminate the Einzel lens as a potential source of sparking it was brought to 25kV while the module continued conditioning. Maximum voltage achieve under this configuration was 57.1kV. Increments are now 50V steps. The Canbus continues to be very sensitive to any sparking and is slowing the process down considerably. It does however appear that the module is continuing to condition. I will continue tomorrow after the module moves to attempt to reach 60kV and hold it for 1 hour.

Entry  Tuesday, November 19, 2013, 14:24, David Wang, ITE, Repair, , , ITE TP3 
Hi all, The old  ITE TP3 pump is moved out and the new pump is  in postion .Since this time I used a new holding ring(1 piece) insead of old 2 pieces holding ring which are thicker than new ring, the old holding  bolts are a little bit too long for the thread holes on the  ITE exit 1. I have to find the right length bolts for this new holding ring. The pump is in position,and all connection are done except the holding bolts. I will put the new bolts on and tight them when I connect the TM4 in ITE next time. So, If I am not here at that time and you need to connect TM4 and start the pumps in ITE, please check all the bolts are tighted before you do anything.
Entry  Tuesday, November 19, 2013, 10:52, Travis Cave, South Hot-Cell, Standard Operation, TM3, NiO#2, module move 

TM#3 with NiO#2 moved from ITE to the south hot cell.

Entry  Monday, November 18, 2013, 16:44, Bevan Moss, Conditioning Station, Standard Operation, , , Testing of cooling package 

 I have tested all of the compressors for TCS. All are operational and cycled as they should. 

Entry  Monday, November 18, 2013, 16:42, Bevan Moss, Conditioning Station, Standard Operation, TM2, , HV Testing the_glory_of_TM2.JPG18112013_TM2_No_source_tray_HV_Test.txt

 The Glory of TM2 continues 100V at a time. Today I brought the module to 46kV and left it there for 1 hour. During this time there was only 1 spark. I then continues at up to 53kV. At this voltage the canbus continues to be temperamental when the module sparks. The module is still conditioning and I will continue more tomorrow. Attached is the dumped data and a screen shot of the conditioning from 46kV to 53kV.

Entry  Monday, November 18, 2013, 11:54, Bevan Moss, Conditioning Station, Repair, TM2, , Fault on TCS Chill 

 This morning when I went to start HV conditioning CP2 and CP3 both had faults and the temperature of the water was ~27C. I reset the compressors by flipping the system reset switch. This cleared the fault and allowed the compressors to come one. To the best of my knowledge these faults happen as a result of compressor fluid pressure too low or high and temperature too low or high and lack of flow. The system cannot determine which one it was that caused the trip. The system restarted and faulted again. As I was watching this time it can be determined that the fault was the result of an over temperature event. This was the caused by the cooling fans not coming on. Which was traced to the fan VFD controllers which both read OP3 which is an Over voltage during constant speed operation. The operating manual lists these as the possible causes

The input voltage is fluctuating abnormally.

• Power network is greater than 200 kVA

• Power factor capacitor switching

• SCR switching on power network

• The drive controller is regenerating— the load causes the motor to run at a frequency higher than drive controller output frequency.

• Intermittent output phase fault

The proposed solutions are

• Install a line reactor.

• Check the input and output circuits for phase failure and rectify. 

I will continue to monitor over the next few days to see if this continues to happen. If it does I will contact ESC.

Entry  Friday, November 15, 2013, 16:48, Bevan Moss, Conditioning Station, Standard Operation, TM2, , HV Testing TM2_conditioning_15112013.JPG15112013_TM2_No_source_tray_HV_test.txt

 High voltage testing was started on TM2 with no source tray today. The maximum stable for 1 minute voltage reached was 47.5kV but the module is still conditioning. With every step up in voltage the current goes up a large amount and slowly bleeds down. Large sparks disrupts the connection of the CANBUS to the PS which is irritating but the module can be brought up to the equivalent voltage in less than 30 seconds. Attached is a screen shot of most of the strip tool. I have also attached all of the dumped data. The module will be left under vacuum with the water running over the weekend and HV testing will continue on Monday. 

Entry  Thursday, November 14, 2013, 08:08, chad fisher, South Hot-Cell, Repair, TM2, , TM2 Blank off and jig removal TM2_20131108.jpgTM2_20131112.jpg

Firday, November 8 all water blocks (excluding I and K) were blanked off and vacuum leak checked. No responses were found. (First Picture)

I and K could not be blanked off without removal of the water block jig. Also, I dropped one of the blank offs onto the table, so one line could not be blanked off until a new clean blank off was inserted into the cell. In addition, there was still reminace of a bolt in block Ias it aslo could not be removed until the water block jig was removed.

Tuesday, November 12 a new blank off was put into the cell. The water block jig was removed, which was very easy, confirming documentation from installation (in 2008?) that it fit very well / the blocks were bent and soldered to the jig very carefully.

Screw was removed from I and both I and K were blanked off and vacuum leak checked. No response. (Second Piccture)

Containment box was re-installed and module ready to move to the conditioning station by noon.

 

 

 

Entry  Wednesday, November 13, 2013, 10:01, David Wang, Conditioning Station, Repair, TM2, , TM2 leak check at conditioning station TM2_leak_check_at_CS_2013-11-13.pdf

I leak checked TM2 at conditioning station this morning. All air to vacuum seals on the top of the module are good. All water lines are pressured with 60 psi helium for minutes each. One of the tube heater + water line( 2lines for tube heater + for supply and return) has a huge response on 60 psi helium pressurizing. The leak rate went from 6.0xE-9atm.cc/sec to maximum leak rate in 5 seconds and I saw a pressure increasing either. when I pressurize the other side tube heater + line ,the leak detector also had a response,but it is slower than first side .Since the top of the water adaptor isn't sealed , so I think the leak should be in one line only. All other water lines are leak tight since I didnt see any obvious response on leak detector at 5 to 6x E-9 atm.cc/sec which is very low on leak rate. 

Entry  Tuesday, November 12, 2013, 14:33, Bevan Moss, Conditioning Station, Repair, , , Cooling manifold returned 

 The cooling manifold for the conditioning station high power water cooled lines has been returned. The cooling package can once again be operated

Entry  Tuesday, November 12, 2013, 14:31, Bevan Moss, Conditioning Station, Standard Operation, TM2, , Turbo pumps started 

 The turbo pumps have been started on TM2 and the conditioning station.

Entry  Tuesday, November 12, 2013, 12:43, Bevan Moss, Conditioning Station, Standard Operation, TM2, , TM2 moved from SHC to TCS 

 TM2 was moved by myself and David from the SHC to the TCS. Move went well. Curiously the fields on the module were measured higher than the previous measurement (now ~5.8mSv/hour) .

Entry  Tuesday, November 12, 2013, 10:59, Bevan Moss, South Hot-Cell, Standard Operation, TM2, , Electrical Test tm2_elec_test.pdf

 Don Jackson and Myself completed started an electrical test on TM2. All lines passed the with OL to ground. When testing in between the lines individually there were several lines that read other than OL. It was decided to abandon the testing as there were too many "failures". The results are attached. The testing will be repeated in the conditioning station with vacuum. It is not expected that this will change anything as during a quick visual inspection it appears the lines are touching. Of note the water block jig was removed this morning by Chad.

Entry  Tuesday, November 12, 2013, 09:51, David Wang, ITE, Standard Operation, TM3, , TM3 disconnection 

TM3 has been disconnected this morning and  purged all HV water lines. I found the power plug for all turbo pump fans wasnt connected  during the last run. That maybe the one of the reason on that ITE TP3 failure.

Entry  Wednesday, November 06, 2013, 10:41, David Wang, South Hot-Cell, Repair, TM2, , Installed 2 turbopumps on TM2 

Bevan and I installed 2 turbo pumps on TM2. The o- ring flanges on TM2 had been cleaned before the installation.

Entry  Tuesday, November 05, 2013, 10:37, chad fisher, South Hot-Cell, Repair, TM2, , Thermocouple wire removal 

The old thermocouple wire has been sucessfully removed from the module.

Thanks Bevan, Travis and David.

Entry  Monday, November 04, 2013, 10:46, chad fisher, South Hot-Cell, Repair, TM2, , TM2 Exploration TM2_20131104.jpg

TM2 is now in the hot cell with the containment box off for inspection and eventual blank off off the water blocks.

Upon initail inspection the status (fron a hot cell point of view) is:

-Water block jig is equipped/on

-There is a thermocouple line that will need to be removed

-TM2 requires a new front containment box cover - already manufactured and waiting for installation

 

Entry  Friday, November 01, 2013, 09:08, Travis Cave, South Hot-Cell, Standard Operation, TM2, no target, module move 

TM#2 has been moved from the north west silo to the south hot cell. The module has a field of about 3.1mSv/hr when it was lowered into the hot cell.

Entry  Thursday, October 31, 2013, 11:38, Anders Mjos, ITE, Standard Operation, TM3, NiO#2, Padlle wheel frequency measurements ITE-TM3-NiO#2-HP-FEBIAD_Water_Flow_EOB.pdf

with TM4 in ITW as measured today in the electrical room by David and Anders.

Entry  Thursday, October 31, 2013, 10:36, David Wang, ITW, Standard Operation, TM4, , I moved 5 shielding blocks from ITE to ITW. 

I moved 5 shielding blocks from ITW to ITE. The ITW  is configured to take proton beam.

Entry  Thursday, October 24, 2013, 15:43, Anders Mjos, South Hot-Cell, Standard Operation, TM4, Ta#41, Target conductance Ta#41_electrical_measurement_TGHT_in_SHC.pdf

The conductance check on the electrical check was found to be outside of accepted values for the TBHT at 7.0 mOhm. A successful attempt to reduce the conductance was made by re-tightening the bolts on the TGHT legs in the SHC. Grant operated the manipulator and torqued the bolts to about 1/8 of a turn with the air ratchet. The conductance across the TGHT (A-B) could be improved from 7.0 mOhm to 6.2 mOhm by re-tightening the bolts. The value is still somewhat higher than usual, but was deemed to be acceptable. Measurements attached.

    Reply  Thursday, October 24, 2013, 15:54, Grant Minor, South Hot-Cell, Standard Operation, TM4, Ta#41, Target conductance 

Anders Mjos wrote:

The conductance check on the electrical check was found to be outside of accepted values for the TBHT at 7.0 mOhm. A successful attempt to reduce the conductance was made by re-tightening the bolts on the TGHT legs in the SHC. Grant operated the manipulator and torqued the bolts to about 1/8 of a turn with the air ratchet. The conductance across the TGHT (A-B) could be improved from 7.0 mOhm to 6.2 mOhm by re-tightening the bolts. The value is still somewhat higher than usual, but was deemed to be acceptable. Measurements attached.

1. TGHT leg bolts were loosened, and resistance was measured very high, as expected.

2. TGHT leg bolts were then tightened, loosened, and tightened again, and the resistance improvement was then measured (from 7.0 mOhm to 6.2 mOhm).

3. Another attempt was then made to loosen and tighten to see if there would be further improvement.  The right bolt was loosened, but the left bolt was found to be quite stiff and was left as-is (not fully loosened) for fear of breaking the supporting insulator.  Both bolts were then re-tightened, and resistance was checked to be about the same as achieved during the previous loosening / tightening attempt (step 2 above).

To tighten the bolts in all cases: the air ratchet was used first to turn the bolts "air tight" (air pedal only, no manual force) and then with the air pedal held down, manual torque was applied to turn no more than 1/8th of a turn.

    Reply  Friday, October 25, 2013, 14:09, Travis Cave, South Hot-Cell, Standard Operation, TM4, Ta#41, Target conductance TM#4_Ta#41_elec_test_SHC.PDF

Anders Mjos wrote:

The conductance check on the electrical check was found to be outside of accepted values for the TBHT at 7.0 mOhm. A successful attempt to reduce the conductance was made by re-tightening the bolts on the TGHT legs in the SHC. Grant operated the manipulator and torqued the bolts to about 1/8 of a turn with the air ratchet. The conductance across the TGHT (A-B) could be improved from 7.0 mOhm to 6.2 mOhm by re-tightening the bolts. The value is still somewhat higher than usual, but was deemed to be acceptable. Measurements attached.

 The full electrical check was done on October 25th 2013. The results are in the attached PDF. The higher value of the conductance was dealt with see Anders Mjos elog entry for those details.

Entry  Friday, October 25, 2013, 13:39, Anders Mjos, ITE, Standard Operation, TM3, NiO#2, Padlle wheel frequency measurements ITE-TM3-NiO#2-HP-FEBIAD_Water_Flow_wITW-TM4.pdf

with TM4 in ITW as measured today in the electrical room by David and Anders.

 

Entry  Friday, October 25, 2013, 10:26, Travis Cave, ITW, Standard Operation, TM4, Ta#41, module move 

TM#4 with Ta#41 has been moved from the south hot cell to the west target station.

Entry  Friday, October 25, 2013, 06:58, David Wang, South Hot-Cell, Standard Operation, TM4, , Leak check on TM4 target heat shield 

Maico and I leak checked HS circuit after Chad installed the target. The circuit was a little bit difficult o pump down because of residue water moister inside. But once the moisture was pumped out, the pumping down was smooth and fast. The base leak rate 0.0xE-9 atm.cc/sec, base pressure 0.0xE-4 torr. Maico checked helium flow before the leak test. Then,He sprayed helium to all 3 VCR fiitings on target with 2 seconds on each one, He also flushed 10 seconds helium around the target. There were no any response during all these test time on leak detector.He checked the helium flow again after the test  and confirmed the helium flow.  The HS circuit is leak tight.

Entry  Thursday, October 24, 2013, 11:32, Travis Cave, South Hot-Cell, Standard Operation, TM4, no target, module move 

TM#4 with no target has been moved from the conditioning station to the south hot cell.

Entry  Thursday, October 24, 2013, 11:31, Travis Cave, Spent Target Vault, Standard Operation, , UC#7, Spent target move Vault_Storage_October_24_2013.pdf

UC #7 has been moved from the south hot cell to the spent target vault, it was placed in pail #110 and put in slot 8B of the vault, it was 22.6mSv/hr upon removal from the hot cell. See attached PDF for vault details.

Entry  Wednesday, October 23, 2013, 12:07, Travis Cave, South Hot-Cell, Standard Operation, TM1, no target, module move 

TM#1 with no target has been moved back to the south west silo from the south hot cell.

Entry  Wednesday, October 23, 2013, 09:28, Travis Cave, South Hot-Cell, Standard Operation, TM1, UC#7, module move 

TM#1 with UC #7 has been moved from the south west silo to the south hot cell.

Entry  Tuesday, October 22, 2013, 17:07, Bevan Moss, Conditioning Station, Standard Operation, , , services shut down 

 The turbo pump, roughing pump, have been turned off and the valves for venting opened. The cooling package has also been turned off.

Entry  Tuesday, October 22, 2013, 17:04, Bevan Moss, Conditioning Station, Standard Operation, TM4, , HV testing 22102013_TM4_Coil_removed_EL_testing_(1).txt

 This afternoon TM4 with the coil removed was tested with HV. The EINZEL LENS was first tested independently while the bias canbus was being repaired. The current on the EL looked stable at 25kV for 5 minutes. At 27.5kV the current becomes unstable and occasionally sparks. This voltage was held for 30 minutes but the current did not appear to be becoming more stable. Further extended testing would be required to determine if this can be conditioned out. At this point I would suggest the EL has a HV limit near 25kV.

The BIAS and EL were then brought up to 35kV and 17.5kV respectively. This voltage was held for 35 minutes with the BAIS only sparking twice. The module can most likely hold a higher voltage but for the next 2 runs does not require more than 35kV. Further testing was not completed due to time constraints. It is recommended during the shut down that TM4 is tested to its limits. The data from the testing has been attached.

Entry  Tuesday, October 22, 2013, 16:52, Bevan Moss, Conditioning Station, Repair, , , Canbus base card for BIAS  

 The base card in the canbus BIAS module was determined to be faulty. Dave Morris removed a card VECC to repair the conditioning station. 

Entry  Tuesday, October 22, 2013, 14:23, Anders Mjos, ITE, Standard Operation, TM3, NiO#2, Padlle wheel frequency measurements ITE-TM3-NiO#2-HP-FEBIAD_Water_Flow.pdf

as measured today in the electrical room by David and Anders

Entry  Tuesday, October 22, 2013, 11:18, Travis Cave, ITW, Standard Operation, TM1, UC#7, module move 

TM#1 with UC#7 has been moved from the ITW to the south west silo.

Entry  Monday, October 21, 2013, 12:29, Bevan Moss, Conditioning Station, Repair, TM4, , BIAS Canbus 

 There is something wrong with the BIAS canbus controller. It says that it is not alive and has timed out. I have tried unplugging it and plugging it back in but that has not resolved the problem as it normally does. I have contacted Dave Morris and am waiting to hear from him. I cannot HV test without this controller.

Entry  Monday, October 21, 2013, 10:52, Bevan Moss, Conditioning Station, Standard Operation, TM4, , Cooling On and Electrical Connections Made 

 The electrical connection have been made and cooling package was started at ~10:50am today

Entry  Friday, October 18, 2013, 15:55, Bevan Moss, Conditioning Station, Standard Operation, TM4, , Turbo Pumps are on 

 The Turbo pumps are now running on TCS

Entry  Friday, October 18, 2013, 14:56, Travis Cave, South Hot-Cell, Standard Operation, TM4, no target, Electrical check TM#4_no_target_post_coilelectest.PDF

With the coil line removed an electrical check was done on TM#4 at the South Hot Cell see attached pdf.

Entry  Friday, October 18, 2013, 14:37, Bevan Moss, Conditioning Station, Standard Operation, TM4, , Roughing Started 

 The roughing pump has been started.

Entry  Friday, October 18, 2013, 14:33, Bevan Moss, South Hot-Cell, Standard Operation, TM4, , Module move 

 TM4 without a source tray was moved from the SHC to the TCS.  All went well.

Entry  Friday, October 18, 2013, 13:43, chad fisher, South Hot-Cell, Repair, TM4, , C2 Circuit Removal IMG_1224[1].JPGIMG_1227[1].JPGIMG_1230[1].JPG

The C2 circuit (coil 2) water lines and blocks have been revoed from TM4.

Water block jig could not be used as the window water block connection was nowhere near fitting into the jig (IMG_1224 image below) and therefore caused an interference causing the rest of the blocks to not mate with the jig. A different tool that has never been used was implimented and sucessful (IMG_1227 below).

 Sorry about the picture numbering format...new format will be implimented next time.

Entry  Friday, October 18, 2013, 10:17, Bevan Moss, ITW, Repair, , , Paddle Wheel 

 Yesterday I visually inspected the paddle wheel and noticed that it was spinning freely and constant. As the signal was intermittent replaced the coil at the back of the wheel only. This does not require access to the high active water. With the coil replaced the signal looked strong. I asked operations to keep and eye on it and advise if the problem has been resolved. I also discussed with David this morning and he informed me that this is the same procedure he would have followed.

Entry  Thursday, October 17, 2013, 17:16, Grant Minor, ITE, Repair, , , Pre-Separator-area (ITE Harp 9) Blocks Replaced 8x

The pre-separator-area blocks were replaced today by Bevan and Travis, with Grant present for photos and observation.

Photos are attached of each block replacement.

Some difficulty was encountered in replacing the "Layer #3" blocks (photo 9 attached).  An interference occurred between the outside of the west "Layer #3" block and an aluminum channel directly beside the rubber pad that supports the block.  The block was initially resting on this channel but slipped off, breaking off some concrete at the edge.   See photo 12 attached and notice crumbled concrete inside this channel around the area where the interference occurred. Photo 14 shows the damaged block edge.

It should be noted that when these two blocks are resting flat, there should be a gap between them (i.e. they should NOT be touching as shown in photo 9).

 

Entry  Thursday, October 17, 2013, 10:24, chad fisher, South Hot-Cell, Repair, TM4, , Coil Line Removal TM4_C2_circuit.pdf

The containment box was removed from TM4 earlier this morning in preparation for removal of the C2 circuit water lines, their respective water blocks and conductor block.

Entry  Wednesday, October 16, 2013, 18:53, Grant Minor, ITE, Repair, , , ITE Harp 9 Removed & Blanked-Off - blocks NOT YET replaced 11x

The blocks above the pre-separator section of the ISAC beam lines were removed today in the Target Hall by Bevan Moss and Chad Fisher with Lynne LeMessurier present from RPG.

The two blocks in the layer below the top layer above the pre-separator were damaged on removal (see attached photos).  This was due to an attempt to lift them in the incorrect sequence caused by misinterpretation of the labeling / numbering system drawn on the top of the blocks.  The blocks are labelled for the replacement sequence, but not for the removal sequence.  An attempt was made to lift a block that had an overlap with an adjacent block that was not visible, causing damage to two blocks.  A note was added in black marker to the critical block to indicate that it should be removed last (shown in attached photo).  The block replacement sequence will be photographed and a procedure document will be written by Bevan, with a bound copy of the procedure provided in the Target Hall, in order to prevent such an incident from occurring again.  Broken pieces of the blocks were collected and placed in a 5-gallon pail.

The removal of all of the blocks caused the depression in the target station to fluctuate around the trip point (17 inches of water column), which caused the ventilation alarm to trip on and off constantly.  Operations contacted me to ask if this could be remedied.  Bevan closed the damper to ITW, which brought the depression to a low enough value so that the alarm could be defeated properly.  This was around 2pm.

Preliminary co-ordination of the ITE Harp 9 removal job was discussed by Scott Kellogg and Ron Kuramoto around lunch time.  Keith Ng (RH) and Scott searched for the blank-off that was used during the last Harp 9 repair (removed from B/L in March 2013) but they could not locate it.  I was later able to find the blank-off bagged in a grey rubbermaid bin at the bottom of the stairs in the target storage vault pit (under the SHC / NHC ventilation and filters).  The blank-off was found bagged and tagged as surveyed at 100 counts @ 0.5m on March 27, 2013.  I gathered Scott, Ron Kuramoto, and Danka Krsmanovic to co-ordinate the Harp 9 removal and blank-off installation, starting at around 2:30 pm.

For the Target Hall Harp work, Ron Kuramoto and Scott prepared the required tools and plastic coverings / bags.  I acted as crane operator.  Danka was the surveyor present.  Anders Mjos joined the group for photos and moral support.

Scott disconnected services from the Harp device, and prepared it for lift.  I called operations to confirm that the section of B/L had been vented.  Ron and Scott used the RH tools to disconnect the 2 vacuum flange bullet bolts.  Ron directed the crane with signals and I lowered the chain rigging to the Harp, it was connected and removed from the BL with the main hoist.  (I made the mistake of directing the rigging of the harp to the main 20T hoist, when in fact the 3T Aux hoist should have been used, as the main hoist can't reach to the vacuum / storage pit on the west side of the hall.)

Danka performed several swipes and measurements of the Harp after removal.  Alpha contamination was discovered on the bottom of the Harp flange.

Ron and Scott installed the blank-off flange, then I called operations to indicate that pumping should start.

Ron and Scott retrieved the vacuum test flask jig / support structure from the West storage pit and brought it down to the pre-separator pit.  I lowered the Harp into this flask jig, and Scott used the side-wall location bolts from the top of the harp assembly to fasten the flanges of the Harp and the jig.

I had trouble at first activating the Aux hoist but soon realized that it's necessary to press the Aux pendant "ON" button down for several seconds before the power actually turns on to this hoist.

We then removed the main hoist hook and attached the Aux hoist to the Harp / flask.  The assembly was transported to the West storage pit.

Some of the handrails had to be removed to facilitate initial movements of the Harp assembly.  These handrails should be replaced tomorrow morning.

Scott also submitted a Work Order for a back-up blank-off today, job number 40303.

The pre-separator blocks have NOT been replaced yet, we will do this tomorrow morning.

It was a busy day, thanks to all for their efforts and for staying a bit late to get the blank-off installed.

Best regards,

Grant

Entry  Wednesday, October 16, 2013, 10:12, Travis Cave, South Hot-Cell, Standard Operation, TM4, no target, module move 

TM#4 with no target has been moved from the south west silo to the south hot cell.

Entry  Tuesday, October 15, 2013, 16:44, Grant Minor, Crane, Repair, , , Target Hall Crane - operational with temporary thermal sensor bypass ISAC_THall_Crane_elec_E5_1slash1_15Oct2013.pdf

E-mail correspondence on the Target Hall crane fault diagnosis between October 11th and 15th:

On 15/10/2013 3:34 PM, Grant Minor wrote:

Hello all,

Mike Smith from Norelco arrived this morning and spent some time with Travis from RH and Mike Rowe from Controls group examining the crane controls and electrical schematics.  A common understanding of the wiring and control signal scheme for the thermal sensor circuits was reached.  A scanned copy of Norelco / Seattle Crane drawing E5 - 1/1 with markups by Dave Morris (Oct 11th) and Mike Smith (Oct 15th) is attached.

The group then worked on top of the crane bridge to systematically isolate the thermistor circuits in each drive motor.  The thermistor readings were all normal / as-expected (about 180 Ohms for 3 in series), i.e. there was no indication of failure in any of the motor thermistors.  Fall arrest equipment was used to access the motors where required.

Next, the shunt circuit in each temperature sensor module was measured (terminals T1 and T2 on each module, on drawing E5 - 1/1).  The shunt in the operational module was measured at 500 kOhms.  The shunt in the suspected faulty module was measured at 79 kOhms.

It was concluded that there is most likely a fault in the module with the low shunt resistance.  The suspect module was left wired in bypass (shorted from terminals 14 to 11).  Mike Smith advised at that point that it would be safe to operate the crane in this mode temporarily until a replacement module can be installed.  I discussed this with him and Don Dale, and we agreed the risk is low, as we have not ever experienced a motor overheat scenario in the operating lifetime of the crane.

Mike Smith called me around 1pm to advise that he has located a replacement unit from their supplier in the US and I asked him to order 2 units on expedited overnight.  Mike expects the components to arrive Friday this week or Monday next week latest, factoring in delays at customs and local delivery times.  The units will be sent to Norelco first, then to TRIUMF locally.

Remote Handling is now continuing with Target Hall operations, using the crane as normal with the thermal module bypassed until the replacement module arrives.

Thanks to Dave Morris / Mike Lowe for their assistance in diagnosing this fault.

Here is a short summary of the Fault:

Cause of fault
- Most likely a failed thermal sensor module for one of the two pairs of bridge drive motors

Diagnosis
- Crane company (Norelco) consulted, with on-site inspections by tech Mike Smith on October 9th and October 15th
- Controls group / Mike Smith measured resistances in motor thermistors and sensors to systematically isolate fault to thermal sensor

Remedy actions taken

- Thermal sensor bypassed to temporarily restore crane function
- Risk of operating without sensor determined to be low through discussions with Norelco / Don Dale / Grant Minor
- Replacement thermal sensor + 1 spare (~ $300 ea + shipping) ordered from parts supplier through Norelco - expected delivery Monday October 21st

How could this fault have been prevented?
- Cause of failure within thermal sensor module unknown at this time
- Annual crane inspection performed by Norelco in March 2013 did not indicate any problems with this sensor (crane drive system functioned as normal)
- Suggested for future: routine inspection of sensor module shunt resistance to determine if there are any long-term signs of slow degradation

What can be done to prevent the fault in the future?
- The ISAC crane controls were designed in the late 1990's by Norelco sub-contractor Seattle Crane (now defunct)
- The crane is supposed to have two pairs of independent motors with separate thermal sensors, each capable of driving the crane if the other fails due to thermal trip
- My understanding is that the controls logic design should have been designed so that failure of one pair of motors does not prevent crane operation... it does not seem to be the case with the current design
- The design of the control logic related to these sensors could be re-evaluated and modified so that a trip from one thermal module does not prevent operation of the bridge if the other module is OK
- This is a project that will require some time and some controls and engineering resources
- In the interim, if the same failure occurs again, it may be possible to jumper the thermal sensor from the crane control room and continue operating normally - I will confirm with controls group / Norelco
- However, this is not advisable as it would be difficult in some cases to determine if the trip was due to a faulty thermal module, or an actual motor overheat scenario
- I will discuss further actions with Don Dale

Thanks and best regards,

Grant


On 11/10/2013 4:29 PM, Grant Minor wrote:

Hello all,

I spoke with the Norelco tech Mike Smith this afternoon regarding the failed thermal sensor component / circuit.  He will call Kone on holiday Monday (their office is not closed for Canadian Thanksgiving) and determine if they have a replacement module.

I explained (to the best of my understanding) the diagnosis performed by Dave Morris / controls group and the test that was done to isolate the thermal sensor unit.  Unfortunately, Mike Smith's drawings from Seattle crane contain notes and revisions that don't match the drawing that Dave Morris provided me (Seattle Crane dwg E5 - 1/1 revision 1 02-10-99), and he was unable to confirm in his opinion whether the bypass performed by Dave Morris has correctly isolated the problem components.  In addition, he believes that the bypass he performed on Wednesday isolated portions of circuitry that are inconsistent with this thermal sensor circuit.

Mike Smith will return Tuesday morning to review the bypass and schematics.  He recommended not operating the crane until he has a chance to confirm this thermal sensor issue.

From the drawings I have in hand and from discussions with Dave Morris, the failed component might be the thermistor sets inside the motor housing which are in series with the suspect module, or the module itself.  My understanding is that the crane is designed with two pairs of motors for the bridge drive, and each pair is protected by one of these thermal modules (thus there are two modules total).  Both modules would be the same age and both might be susceptible to the same failure mode.

As it is unclear to me the exact nature of the drive system failure, and I have a recommendation from Norelco to hold on operation of the crane, I must unfortunately state that the crane should not be used and we will have to wait until Tuesday to gather more information.

I am not so concerned about temporary loss of the thermal protection circuitry, as we have not had an overheating scenario in those motors in the lifetime of the crane (to my knowledge).  I am more concerned about getting 100% confirmation that we have addressed the problem.  If we attempt to use the crane and experience another failure during a lift that prevents us from placing the load down safely with the crane stuck in position over a target station, then we would be in much deeper trouble.

My apologies for this situation.

Best regards and have a good weekend,

Grant


On 11/10/2013 1:28 PM, Grant Minor wrote:
Thanks Dave,

I've contacted Norelco, Mike Smith and I are planning a path forward for further diagnosis and repair.

The crane MUST NOT be used to carry a load until it is identified whether the module or the sensors have failed, the reason for the failure, and the functionality of the thermal sensors has been restored.

Without the thermal sensor circuit we lose protection from motor overheat, an event which could have much more serious failure implications to the crane.

Cheers,

Grant

On 11/10/2013 1:04 PM, David Morris wrote:
The fault has been identified in the Target Hall Crane as a failed motor temperature module, or motor temperature sensor, on the East-West motion. The status contact in the module was bypassed allowing crane motion. There was no fault with the controls.

Dave

Entry  Tuesday, October 15, 2013, 15:34, Bevan Moss, ITE, Standard Operation, TM3, , Blocks moved from ITW to ITE 

 Blocks 1-4 have been moved from ITW to ITE. Block 5 was moved to a storage area as it will be in the way of the harp repair. Danka took air samples and found 200 counts of alpha on the air samples but nothing on the swipes. It is recommended that resporators be worn while blocks are being lifted and lowered. She will check the monitor tomorrow to confirm it is behaving as it should.

Entry  Tuesday, October 08, 2013, 18:12, Grant Minor, Crane, Repair, TM4, , Target Hall Crane Stuck in East-West Direction - Update THall_Crane_Bridge_Wheel_at_South_Rail_Splice_8Oct2013.JPGNORELCO_inv13045_joMS-064_31March2013.pdf

Grant Minor wrote this e-mail today:

***

Hello all,

During our planned operation of transporting TM4 from a storage silo to the Hot Cell, we had a problem with the East-West bridge drive on the Target Hall crane.  The crane bridge is currently stuck in position over the silo area.  We were unable to complete the transport operation.  TM4 has been placed back down into the silo and the crane hook block has been disconnected from the module lifting yoke.

We have been on the phone with Norelco this afternoon and have determined the likely cause of the problem.  There is a splice joint in the crane rails at this position, where a small gap exists between the rail sections.  If the crane bridge is stopped during operation such that the wheel comes to rests in this gap, the crane motors have insufficient torque for the wheel to overcome the gap and ride back onto the rail.  The Norelco tech Mike Smith remembers encountering this problem several years ago (before my time) but cannot remember how it was overcome.  The fix likely involved moving the wheel out of the gap with pry bars.

Target Hall Survey Needed at or before 7:00 am, Wednesday Oct 9th (Lynne, Fiona, Danka, Max or Dano?)

Mike Smith and possibly a few others from Norelco will come tomorrow morning at 7:00am, and require access to the Target Hall.  Since we have opened the Hot Cell in preparation for the module move, we will need a survey as early as possible to allow Mike and his crew to enter the hall without a suit and respirator.

Most of the Remote Handling group will be off-site for a Division meeting, but Travis and Maico will stay for the day to accompany the Norelco guys and help with the problem assessment.

Travis: Please take Mike to the control room when he arrives, one of the cameras is currently zoomed in on the wheel and problem rail section.

Maico: Scaffolding may be required to get access to the crane rail.  Unfortunately we don't have an operational crane to transport a man-lift into the hall ;)  Please see what you can do to get this ready in case we need it.  Max's leak check might have to go on hold until we get this resolved.  Please take responsibility for ensuring correct Fall Protection procedures are followed.  This means that nobody should be walking up on the crane rail unless they are tied in with harnesses, or there is scaffolding directly under them.

I can be reached on my cell phone at 778-319-4612.  The Division meeting is on UBC campus so I can return to TRIUMF fairly quickly if needed.

Thank you all for your assistance,

Grant

***

A photo of the THall camera view of the bridge wheel at the rail splice is attached, as well as Mike Smith's crane inspection report from March 2013.

    Reply  Wednesday, October 09, 2013, 19:33, Grant Minor, Crane, Repair, TM4, , Target Hall Crane not operational - likely controls / PLC hardware failure (not stuck wheel) 

Grant Minor wrote:

Grant Minor wrote this e-mail today:

***

Hello all,

During our planned operation of transporting TM4 from a storage silo to the Hot Cell, we had a problem with the East-West bridge drive on the Target Hall crane.  The crane bridge is currently stuck in position over the silo area.  We were unable to complete the transport operation.  TM4 has been placed back down into the silo and the crane hook block has been disconnected from the module lifting yoke.

We have been on the phone with Norelco this afternoon and have determined the likely cause of the problem.  There is a splice joint in the crane rails at this position, where a small gap exists between the rail sections.  If the crane bridge is stopped during operation such that the wheel comes to rests in this gap, the crane motors have insufficient torque for the wheel to overcome the gap and ride back onto the rail.  The Norelco tech Mike Smith remembers encountering this problem several years ago (before my time) but cannot remember how it was overcome.  The fix likely involved moving the wheel out of the gap with pry bars.

Target Hall Survey Needed at or before 7:00 am, Wednesday Oct 9th (Lynne, Fiona, Danka, Max or Dano?)

Mike Smith and possibly a few others from Norelco will come tomorrow morning at 7:00am, and require access to the Target Hall.  Since we have opened the Hot Cell in preparation for the module move, we will need a survey as early as possible to allow Mike and his crew to enter the hall without a suit and respirator.

Most of the Remote Handling group will be off-site for a Division meeting, but Travis and Maico will stay for the day to accompany the Norelco guys and help with the problem assessment.

Travis: Please take Mike to the control room when he arrives, one of the cameras is currently zoomed in on the wheel and problem rail section.

Maico: Scaffolding may be required to get access to the crane rail.  Unfortunately we don't have an operational crane to transport a man-lift into the hall ;)  Please see what you can do to get this ready in case we need it.  Max's leak check might have to go on hold until we get this resolved.  Please take responsibility for ensuring correct Fall Protection procedures are followed.  This means that nobody should be walking up on the crane rail unless they are tied in with harnesses, or there is scaffolding directly under them.

I can be reached on my cell phone at 778-319-4612.  The Division meeting is on UBC campus so I can return to TRIUMF fairly quickly if needed.

Thank you all for your assistance,

Grant

***

A photo of the THall camera view of the bridge wheel at the rail splice is attached, as well as Mike Smith's crane inspection report from March 2013.

E-mail from today:

Hello Dave, Jane, Franco, Michael, Don (controls + Franco), Remy,

We have lost the East-West bridge drive control functionality of the ISAC Target Hall crane, and unfortunately this very much prevents us from operating the ISAC facility.

The problem was originally thought to be a stuck bridge wheel but this was not actually the case.

Mike Smith from Norelco was on-site for most of today working with Michael Rowe in an attempt to diagnose the problem.

Mike believes the problem to be one of the following three items:
- input PLC board on the crane bridge
- output PLC board in the interface panel in B1 level Room 5 (ISAC remote crane control room)
- communication between the two boards (festooning hardware)

We are in a pretty dire situation without the ISAC target hall crane, and we lack the expertise within the Remote Handling group in PLC hardware to diagnose this on our own.  I need to ask for somebody's help from the controls group in diagnosing and repairing this problem.

I have notes from my telephone conversation with Mike Smith which I can discuss with a controls representative in the morning.  There is a pretty muddled history of the design and implementation of these controls but essentially Norelco outsourced the PLCs and festooning to a third party contractor, Seattle Crane in the US, which no longer exists anymore.  Neither Kone, Seattle Crane, or Norelco made appropriate as-built drawings of the wiring of the PLCs.  Mike Smith at Norelco had a stack of hand-written notes about the as-built configuration he made at the time of installation in the late 1990's but these notes have not been located yet.

The PLCs appear to be Allan Bradley but the modules are from approximately 1997 and we're not sure if spare units are available.

Mike Smith says the easiest thing to do at this point is install replacement PLC modules on the crane bridge and in the control room that have confirmed functionality.  If control is not restored then the problem is likely in the festooning.

Control of the crane bridge was temporarily attained by bypassing the controls (speed control / end limits, etc.) and sending drive signal directly to the drive motor controller in order to return the bridge to its home position at the access ladder.  This mode of operation is not safe as the crane has no speed reduction / limits to prevent driving the bridge into the walls at max speed.

Jane / Remy / Franco: please let me know who I should correspond with on the controls side and I will talk with them tomorrow morning.

Thanks,

Grant

Entry  Tuesday, October 08, 2013, 14:58, Anders Mjos, South Hot-Cell, Standard Operation, , SiC#29, Target to Heat Shield electrical short 

The SiC#29 CTL target has been taken apart with the help of Isaac and Chad. Electrical measurements were done between Target and Heat Shield as the target was disassembled. Work was done on October 2nd, 4th, 7th and 8th.

The megger showed about 30kOhm at 50V with the following changes

  • Bolts for CTL block loosened
  • Above bolts removed
  • CTL block pulled away from Heat Shield
  • CTL block removed
  • Heat Shield lid removed
  • Bolts for target removed
  • Shims between target and insulators

The megger showed about 50kOhm at 100V with the following changes

  • Target removed. Measured between cathode restraint and HS.

The megger showed OL at 540V with No 3 insulator removed. A measurement on No 3 insulator while it was sitting on the HS showed 70kOhm at 120V confirming that the insulator can no longer hold voltage.

While taking off the coil retainer plate, Chad noticed that all bolts were not tight.

Photos are available on DocuShare.

Entry  Tuesday, October 08, 2013, 14:55, Travis Cave, South Hot-Cell, Standard Operation, TM4, no target, module move 

TM#4 with no target was to be moved today but the move was aborted when the crane failed to move in the East - West direction. The crane does not preform this function in either remote or pendant operation.

Entry  Tuesday, October 08, 2013, 13:11, Travis Cave, Spent Target Vault, Standard Operation, , SiC#29, Spent target move Vault_Storage_October_8_2013.pdf

SiC#29 has been moved to the spent target vault. The target was placed in Pail #109 and placed into slot 2B it was 24.7mS/hr upon removal from the south hot cell. See attached PDF of the vault details.

Entry  Monday, October 07, 2013, 12:06, Travis Cave, ITE, Standard Operation, TM3, NiO#2, module move 

TM#3 has been moved from the conditioning station to the east target station, move went well.

Entry  Sunday, October 06, 2013, 20:28, Friedhelm Ames, Conditioning Station, Standard Operation, TM3, NiO#2, turbo pumps stopped 

vacuum readings before stopping

IG1: 7.4e-7 T

IG2 3.8 e-6 T

IG1S 1.95 e-6 T

Entry  Sunday, October 06, 2013, 17:08, Friedhelm Ames, Conditioning Station, Development, TM3, NiO#2, trip of all power supplies 

All power supplies tripped on high conductivity of the cooling water < 5 MOhm, It is not clear if this was caused by a spark or vice versa. According to the strip tool for this signal the resistance of the water went up. There might be a fault in this signal. I do not have permission to force this signal so I keep the heaters off. We should revisit the interlock conditions, this signal should not be included in the interlocks for the heaters. Both target and tube seem to be still o.k. As I do not want to destroy the target I keep the heaters off and restart the high voltage only.

Entry  Sunday, October 06, 2013, 15:39, Friedhelm Ames, Conditioning Station, Standard Operation, TM3, NiO#2, HEATERS STARTED 

The high voltage was sparking several times during the night. It may be correlated with the cycling of the cooling water temperature and conductance.

vacuum levels at 11:00

IG1 7.5e-7 T

IG2 3.9e-6 T

IG1s 2.0 e-6 T

heaters have been ramped up to TGH 580 A, TBHT 250 A,

anode 100 V 5.3 mA, coil 50 A Faraday cup 50 nA bias 20 kV EL 6 kV

vacuum

IG1 7.9e-7

IG2 4.5e-6

IG1s 2.2e-6

Entry  Sunday, October 06, 2013, 00:17, Friedhelm Ames, Conditioning Station, Standard Operation, TM3, NiO#2, high voltage conditioning 

high voltage conditioning was carried out over the day up to 24 kV. i will leave it at 20 kV over night. Current is at 22 micro Amps, heaters off.

vacuum: IG1 7.7e-7

IG2 4.07 e-6

IG1sS 2.2 e-6

 

Entry  Saturday, October 05, 2013, 14:45, Friedhelm Ames, Conditioning Station, Standard Operation, TM3, NiO#2, vacuum readings 

IG1 8.0 e-7 T

IG1S 2.5 e-6 T

IG2 4.3 e-6 T

I will start the high voltage now

 

Entry  Friday, October 04, 2013, 19:39, Grant Minor, Conditioning Station, Standard Operation, TM3, NiO#2, TCS vacuum improvement w/ heaters off - 2:20 pm to 7:17pm 

Here is the change in the TCS vacuum after heaters were turned off earlier today:

2:20 pm readings

TCS:IG1 (service cap) 9.3 x 10^-7 Torr

TCS:IG2 (diagnostics box) 5.71 x 10^-6 Torr

TCS:IG1S (secondary vacuum) 4.0 x 10^-6 Torr

7:17 pm readings

TCS:IG1 (service cap) 8.69 x 10^-7 Torr

TCS:IG2 (diagnostics box) 5.0 x 10^-6 Torr

TCS:IG1S (secondary vacuum) 3.38 x 10^-6 Torr

Entry  Friday, October 04, 2013, 19:05, Grant Minor, Conditioning Station, Standard Operation, TM3, NiO#2, HP Conditioning - e-mail notes from Oct 2nd to Oct 4th 

I have compiled the e-mail comments from people involved in High-Power Conditioning of TM3 w/ the new Rev 3 source tray and NiO#2 since Bevan Moss' last log on October 2nd below:

On October 2nd at 6:35pm Friedhelm Ames wrote:
TM3 heaters have been tested already yesterday in the conditioning station. Current and voltage readings were in the normal operating range.
The heaters were kept on over the night and no changes except a slow improvement in the vacuum has been seen. Today the high voltage was started. A high bias current of up to 150 micro Amps at 10 kV and an oscillation of the current with a frequency of about 3/minutes has been seen. Going higher in voltage resulted in an erratic behavior. After a visual inspection in the target hall some water leakage on top of the module was detected. it could be traced to 2 of the water connectors. They have been replaced. After this the high voltage current was down to normal values and the oscillation disappeared. With the heaters off the voltage could be raised to 22 kV, after which sparking occurred.
Earlier with the heaters on the functioning of the source has been tested. Extracted beam could be seen on the Faraday cup and the dependance on both the anode voltage and the coils could be verified.
One of the steerer plates (bottom) appears to have a short. As there is some redundancy in the steering elements in the target station optics, I don't believe this will effect the beam delivery very much.
A full test of all the source systems is planned for tomorrow including a careful attempt to rise the high voltage to a higher value. For the acceleration of 10C we will need 20.4 kV.

On October 3rd at 9:32am Bevan Moss wrote:

FYI Module is holding 24kV with zero sparks as of yet  I will continue with updates as I go

On October 3rd at 10:18am Bevan Moss wrote:

Sparking started at ~28kV I have had to dial it back to 22kV to hold stable voltage. I will continue with updates.

On October 3rd at 11:17am Bevan Moss wrote:

Sparking has forced the voltage down to 20kV. Friedhelm has asked me to turn everything on and start ramping the heaters.

On October 3rd at 4:15pm Bevan Moss wrote:

The heaters have been brought online and the Bias raised to 25kV. It has been sitting there for the last 10 minutes with 1 spark during this time. All other PS are on and beam is being extracted.

On October 3rd at 4:37pm Bevan Moss wrote:

Sparking has just occurred and the Vacuum is now getting worse significantly faster. Voltage was lowered to 21KV where it has been stable for the last 5 minutes. I am going to turn off the HV leave the module overnight with the heaters on. Hopefully we will have good Vacuum again in the morning.

On October 4th at 2:20pm Bevan Moss wrote:

I have finished completing another complete leak test on the module and it is leak tight. Once the heaters were turned off the vacuum did improve it is currently sitting at 9.3 x 10^-7 Torr in the service cap, 5.71 x 10^-6 Torr in the diagnostics box and 4.0 x 10^-6 in in the secondary.  I have raise the bias voltage and it can hold 20kV for 5 minutes but did have 1 spark. At 22.5kV it appears to be doing some conditioning as the current is unstable. I would not recommend moving TM3 to ITE on Monday until we can establish that the module can hold 25kV for at least 1 hour preferably with the heaters on. I have left the turbo pumps running in case there is more testing you would like to do. If you choose to move to ITE on Monday please have someone stop the turbo pumps otherwise I must wait an hour before venting on Monday. The TCS laptop on my desk should not have the screen saver come on so TCS can be operated through it.

Entry  Thursday, October 03, 2013, 10:18, Travis Cave, South Hot-Cell, Standard Operation, TM4, no target, module move 

TM#4 with no target has been moved from the south hot cell to the south west silo.

Entry  Wednesday, October 02, 2013, 14:47, Travis Cave, South Hot-Cell, Standard Operation, TM4, no target, Electrical check TM#4_elec_chk_No_Tgt_SHC.PDF

Electrical check done on TM#4 with no target, see PDF.

Entry  Wednesday, October 02, 2013, 13:44, Bevan Moss, South Hot-Cell, Standard Operation, TM4, , Right Coil is leaking tm4leak.jpg

 Today Maico and Travis completed and electrical test to determine the right and left coil on TM4. The left coil is the negative side. From there Maico pumped on both lines for a leak test. The leak cart pumped down to its lower limits on the left line and there was no response when sprayed with helium. The right line would not pump below 2.5 x 10^-2 Torr and had a base leak rate of 3.3 x 10^-7 atm*cc/sec (this indicates a massive leak). Without spraying helium the leak cart responded and peaked at 1.9 x 10^-6 atm*cc/sec. Attached is a picture of the module indicating the line.

 

Entry  Wednesday, October 02, 2013, 09:40, Bevan Moss, Conditioning Station, Standard Operation, TM3, NiO#2, HP conditioning 01102013_TM3_NiO2_TGHT_and_TBHT_ramp_up_eod.txt02102013_TM3_NiO#2_HP_testing_overnight_run.JPG02102013_TM3_NiO#2_HP_testing_overnight_run_archiver.JPG

Yesterday the TBHT was ramped to 250 amp and the TGHT was ramped to 440 amps. Attached is the data from that run the strip tool that had this screen shot crashed but it can be recreated with the data. The TBHT ps was not reading back accurate results as such there are large steps in current or voltage or some instability for no apparent reason. In addition to this the ramping program is still not working so the ramping was a very manual process. The strip tool was left running over night, I have attached a screen shot of the the run. You will notice there are changes in vacuum that corresponds to changes in the TGHT and the TBHT voltage. Anders and myself used the archiver to plot the data with TS6 (TS3 would be better and I will have it added to the achiver), the changes in voltage and vacuum match perfectly with the compressor coming on and off. This should be investigated and possibly the temperature range of the cycling of the compressor reduced.

Entry  Tuesday, October 01, 2013, 11:00, Travis Cave, Conditioning Station, Standard Operation, TM3, NiO#2, Electrical check TM#3_elec_chk_NiO#2_CS2.PDF

TM#3 with NiO#2 electrical check at conditioning station under vacuum, see pdf for details.

Entry  Tuesday, October 01, 2013, 10:59, Travis Cave, South Hot-Cell, Standard Operation, TM4, SiC#29, Electrical check TM#4_elec_chk_SiC#29_SHC_post2.PDF

TM#4 with SiC#29 electrical check post beam see pdf for details.

Entry  Monday, September 30, 2013, 16:04, Bevan Moss, Conditioning Station, Repair, TM3, NiO#2, Ion gauge filament replacement  

 The filament on IG1 for TM3 was replaced by myself and Edi. The old filament did not appear to be damaged but the controller claimed it was. The current gauge on TM3 is a single filament, ideally it would be upgraded to a double.

Entry  Monday, September 30, 2013, 16:02, Bevan Moss, Conditioning Station, Standard Operation, TM3, NiO#2, Vacuum 

 The roughing pump for TCS was started at ~3:00 and the turbo's turned on at ~4:00. This is the minimum time for the module to pump down.

Entry  Monday, September 30, 2013, 12:23, Travis Cave, South Hot-Cell, Standard Operation, TM3, NiO#2, Electrical check TM#3_elec_chk_NiO#2_SHC2.PDF

Results of the various electrical checks done on TM#3 while at the hot cell since the 27th of September. View PDF for the details.

    Reply  Monday, September 30, 2013, 16:00, Bevan Moss, South Hot-Cell, Standard Operation, TM3, NiO#2, Electrical check 

Travis Cave wrote:

Results of the various electrical checks done on TM#3 while at the hot cell since the 27th of September. View PDF for the details.

 There was also a leak check. There was some water remaining in the HS line but once removed the leak cart pumped down to 0.0 x 10-4 Torr and the leak tester was at the bottom limit. There was no response when sprayed with helium

Entry  Monday, September 30, 2013, 15:59, Bevan Moss, South Hot-Cell, Standard Operation, TM4, SiC#29, Module move from SW Silo to SHC 

 TM4 was move by myself and Grant. Move went smoothly, no hang ups.

Entry  Monday, September 30, 2013, 14:00, Travis Cave, Conditioning Station, Standard Operation, TM3, NiO#2, module move 

TM#3 with NiO#2 has been move from south hot cell to the conditioning station.

Entry  Friday, September 27, 2013, 12:53, Bevan Moss, Conditioning Station, Standard Operation, TM3, NiO#2, HP TGHT and TBHT conditioning 26092013_TM3_NiO#2_HP_testing.JPG26092013_TM3_NiO2_HP_testing.txt

 Yesterday TM3 had the TGHT current raised to 160 amps and the TBHT raised to 200 amps. At this power the TGHT showed typical results in that vacuum was affected and the increased voltage as the target increased in temperature. The tube heater on the other hand did not change voltage or show a change in vacuum. As a result it is believe there is a short somewhere in the module. I have attached a screen shot of the strip tool and the raw data.

Entry  Friday, September 27, 2013, 10:54, Travis Cave, Conditioning Station, Standard Operation, TM3, NiO#2, module move 

TM#3 with NiO#2 has been moved to the south hot cell from the conditioning station.

Entry  Thursday, September 26, 2013, 14:55, Bevan Moss, Conditioning Station, Standard Operation, TM3, NiO#2, HV conditioning 26092013_TM3_NiO2_HV_conditioning_first_attempt.txt

 The first attempt at HV conditioning of TM3 with the new source tray and NiO#2 target installed. Conditioning so far has been very slow, with the current increasing quickly to a maximum of 400uA. Voltage in these cases was lowered until the current was below 200uA. Attached is the raw data. It appears the source tray and target are conditioning just there is either something burning off or there is localized poor vacuum.

    Reply  Thursday, September 26, 2013, 15:25, Bevan Moss, Conditioning Station, Standard Operation, TM3, NiO#2, HV conditioning TM3_NiO#2_Frist_Attempt_HV_conditioning_Bias_and_El_V_and_I.JPG

Bevan Moss wrote:

 The first attempt at HV conditioning of TM3 with the new source tray and NiO#2 target installed. Conditioning so far has been very slow, with the current increasing quickly to a maximum of 400uA. Voltage in these cases was lowered until the current was below 200uA. Attached is the raw data. It appears the source tray and target are conditioning just there is either something burning off or there is localized poor vacuum.

 Attached screen shot. Vacuum was around 8.3 X 10^-6 on IG2 (which is in the diagnostics box)

Entry  Thursday, September 26, 2013, 15:00, Bevan Moss, Conditioning Station, Standard Operation, TM3, NiO#2, RGA not connecting 

 Following the helium pressure test Don attempted to connect to the RGA via the network. He was unable to do so. This scan was desired so a pre and post water scan could be compared to indicate if there was any leaking. It has been decided to carry on as the HV and HP tests are of greater importance. Don will continue to investigate the RGA. Travis inspected from the conditioning station roof and determined that the RGA is getting power.

Entry  Thursday, September 26, 2013, 14:47, Bevan Moss, Conditioning Station, Maintenance, TM3, NiO#2, Water pumps turned on 

 The water pumps for the conditioning station were turned on at ~11:45. It took longer to start the conditioning station as the air from the leak test had to be bled off and the make up water tank refilled. The valves on the water supply line were closed slightly to make up for the fact the water cooled power supply has been removed. DIF2 was installed by Maico so we can measure the flow in the primary side.

Entry  Thursday, September 26, 2013, 14:31, Bevan Moss, South Hot-Cell, Repair, TM3, NiO#2, Activities September 24 - 25 elec_check.pdf

September 24

 After the manipulator repair Maico installed the NiO#2 onto the target module. Once connected I completed a leak test on the HS line with Isaac. The leak testing cart would not pump down originally (something wrong with the cart) but eventually it did start to work. The cart pumped to its lower limits and did not respond even with the module was flooded with helium. A electrical test was then conducted by myself and and Don Jackson (see attached). During the standard test the Target to Anode and to 60kV common read lower than expected at ~47Momh @ 1kV. Also of note during the conductance check the measurement from c-d was low at 1.82 mohm.

3  additional tests were completed 2 of which were coil to common (both sides). The resisance was measure at 47 ohm with the megger and 1.32 Kohm with the uohmmeter. The coil lines lines were also measured to get and indication of the resistance of a copper line. These lines were measured while they were not jumpered both the coil + and coil - measured 5.73 mohm.

A meeting with Lia and Friedhelm was held and and the decision was to move the module and test it in the conditioning station. Fingers crossed that the module will still work.

Sept 25th

Maico finished installing the cover today for the module to be moved. Other elogs cover the other activities for today.

    Reply  Thursday, September 26, 2013, 14:42, Bevan Moss, South Hot-Cell, Repair, TM3, NiO#2, Activities September 24 - 25 

Bevan Moss wrote:

September 24

 After the manipulator repair Maico installed the NiO#2 onto the target module. Once connected I completed a leak test on the HS line with Isaac. The leak testing cart would not pump down originally (something wrong with the cart) but eventually it did start to work. The cart pumped to its lower limits and did not respond even with the module was flooded with helium. A electrical test was then conducted by myself and and Don Jackson (see attached). During the standard test the Target to Anode and to 60kV common read lower than expected at ~47Momh @ 1kV. Also of note during the conductance check the measurement from c-d was low at 1.82 mohm.

3  additional tests were completed 2 of which were coil to common (both sides). The resisance was measure at 47 ohm with the megger and 1.32 Kohm with the uohmmeter. The coil lines lines were also measured to get and indication of the resistance of a copper line. These lines were measured while they were not jumpered both the coil + and coil - measured 5.73 mohm.

A meeting with Lia and Friedhelm was held and and the decision was to move the module and test it in the conditioning station. Fingers crossed that the module will still work.

Sept 25th

Maico finished installing the cover today for the module to be moved. Other elogs cover the other activities for today.

 Also of note the turbo pumps were started on the conditioning station around 1:30. Don and Travis completed and electrical test, see other elogs. When attempting to start IG1 the controller indicated there was no filament, this gauge only has 1 to start. It will have to be replaced when the module is next vented. In addition to this it appear the PNG1 controller has failed again. I have emailed Dimo to see if we can get one to test. The img100 is new and different cables have been used. All 4 options for connections were also tested in case of a wiring mistake.

Entry  Thursday, September 26, 2013, 09:46, maicodallavalle, Conditioning Station, Repair, TM3, , Leak check / Pressure Test 

TM3 has had all of the water lines pressurized with Helium and the Helium Leak detector was connected to the turbo pumps. There were no leaks detected.

    Reply  Thursday, September 26, 2013, 14:37, Bevan Moss, Conditioning Station, Standard Operation, TM3, NiO#2, Leak check / Pressure Test 

maicodallavalle wrote:

TM3 has had all of the water lines pressurized with Helium and the Helium Leak detector was connected to the turbo pumps. There were no leaks detected.

 While pressurizing the lines it was found some of the lines had water in them. It is unknown where this water came from. Perhaps David connected the conditioning station last time it was in? Lines that were free of water were A, B, C, and window The leak detector pumped down to 4.0 x 10^-3 Torr and the leak rate was 1.4 x 10^-9 atm-cc/sec, there was no response during the leak test and the leak rate continued to decrease during the test.

Entry  Wednesday, September 25, 2013, 13:48, Travis Cave, Conditioning Station, Standard Operation, TM3, NiO#2, Electrical check TM#3_elec_chk_NiO#2_CS.PDF

Electrical check of TM#3 in the conditioning station under vacuum see attached PDF for details.

Entry  Wednesday, September 25, 2013, 11:08, Travis Cave, South Hot-Cell, Standard Operation, TM3, NiO#2, Electrical check TM#3_elec_chk_NiO#2_SHC.PDF

The module was checked electrically this morning before the module move. See the attached PDF for details.

Entry  Wednesday, September 25, 2013, 10:00, Travis Cave, South Hot-Cell, Standard Operation, TM3, NiO#2, module move 

TM#3 with NiO#2 has been moved from the south hot cell to the conditioning station.

Entry  Wednesday, September 25, 2013, 06:59, maicodallavalle, South Hot-Cell, Standard Operation, TM3, , Containment box cover 

The containment box cover has had all  the bolts installed and all bolts were checked with a mirror. TM3 has been raised and is ready for the last electrical  test before  it goes to the conditioning station.

Entry  Tuesday, September 24, 2013, 14:46, Bevan Moss, South Hot-Cell, Repair, , , Right manipulator repair 

 The right manipulator A-9885 Handle Cable Assembly has been repaired by Maico and myself. We repaired the manipulator following some verbal instructions from Chad on the modified repair strategy. This allows the repair to be completed without going into the hot cell. The instructions in the repair manual are very vague and can actually cause problems. For example it is best to pin the manipulator before completing any work. Other than that the work went smoothly with the exception that the counter weight hangs up on the manipulator occasionally and can cause the cable to come off of the pulley. Also it appears that the left manipulator has had the cable installed incorrectly as it rides on the housing of the wrist.

Entry  Tuesday, September 24, 2013, 08:15, Travis Cave, South Hot-Cell, Standard Operation, TM3, no target, Electrical check TM#3_elec_chk_no_target.PDF

Electrical check was done on TM#3 yesterday and again the coil lines to the 60kV common and the coil line to each other failed, as in they had a resistance. Everything else passed as showing an infinite value, all meggering was done at 1000V unless noted other wise. See attached PDF for details.

Entry  Monday, September 23, 2013, 16:10, Bevan Moss, South Hot-Cell, Repair, TM3, , Activities Sept 20 - 23 2013 

 September 20th

Today was a trying day. When attempting to make the water line connections for the window the VCR seal fell off several times. Each time this happens the seal becomes stuck at the bottom of the containment box. While trying to replace the seal the nut slipped down the line to the bottom of the containment box. When trying to recover said nut with the pick tool it too fell to the bottom of the containment box. Due to the design of the containment box the only way to recover the pick is to remove the containment box (several other attempts were made with no luck). Before anyone asks no the pick cannot be left in the containment box. When attempting to remove the containment box one of the bolts for the shutter panel stripped. I then found the stud removing tool and have successfully removed the bolt. Isaac is now going to finish removing the containment box and that will be as far as we can get today. 

September 22nd 

- containment box removed
- dropped tool and seals removed from box
- containment box reinstalled
- window water lines done up
- target installed (with difficulties detailed below)

The threads for the middle tube heater connection (circuit D) appear to be damaged and the bolt in that location cannot be fully screwed in.  The bolt was removed and showed damage to the threads.

September 23rd

A leak check of the window line was completed (https://elog.triumf.ca/TIS/RH-ISAC/459) and several electrical checks of the coil with and without the target in place. The values for the electrical checks continued to fail the open circuit criteria, an elog on the testing will be reported tomorrow. Isaac and Maico removed the target so that the helicoil could be repaired. The helicoil was repaired by chasing the threads with a modified tap but it was noted during the repair that the bolt holding the line in place and come loose and was no longer clamping the tube heater and ceramic tight. The target was also checked electrically to confirm that the coil was not shorted to common. It showed a open circuit resistance with a ohmmeter.

It was then attempted to re-install the target but as the target was being lifted a cable for the tong motion schematic broke (A-11682). 

Currently the target is sitting in the hot cell with the manipulator still broken. We are attempting to find parts and instructions as to how to replace the cable.

 

Entry  Monday, September 23, 2013, 13:55, David Wang, South Hot-Cell, Standard Operation, TM3, , window circuit leak check 

This morning, Bevan and I leak checked window circuit on TM3 at SHC after containment box was installed. It took about 20minutes to pump down the circuit to  0.0xE-9atm.cc/sec. Bevan sprayed helium on both VCR joints and a final splash. No response had been found on leak detector.

Entry  Thursday, September 19, 2013, 15:56, Bevan Moss, South Hot-Cell, Repair, TM3, , Activities for September 18th and 19th IMG_1127.JPGIMG_1134.JPGIMG_1137.JPGIMG_1139.JPGIMG_1143.JPG

September 18th

The wiring harness was completed by Maico and Travis today (see pics) and was installed into the target module. During installation the bracket went on with ease. The junction box appeared to be hung up on something but did engage eventually. The plug for the collimator is not quite long enough for the manipulators to install completely. I was only able to get it to just engage by sneaking the manipulator in from the shutter side and then pushing on it with a long rod. The wiring for the collimator is several inches too long but does not interfere with anything. The remote installation of the wiring to the IMG gauge was easy but there at least 1 foot of extra wire and with the thicker gauge it has a mind of its own. I was eventually able to wrap the wire under the table before so it will not interfere with anything. The module side junction box bracket was not clamped to the table I was able to do up one bolt but other one was blocked by the new steerer strain relief. There is no requirement for both to be done up.

 

September 19th

Travis completed and electrical test this morning and it was found that coil 1 touches coil 2 touch each other very slightly. By inserting a piece of cardboard between the closest water block and the lines we no longer in contact and passed the test. Once the cardboard was removed the lines remained separated but if touched slightly they would spring back into place and make contact. There was some debate as to if we should make a custom part to separate the line or if we should attempt to tweak the lines. I decided that it is known that a very small change in the position of the module will cause separation between the lines, that we should attempt to tweak the lines. I braced the lines with one manipulator to prevent loading the ceramic while Maico "tweaked" the line. The line was successfully moved to cause separation. Maico and I then completed a visual inspection of the remaining water blocks and noticed that the ground electrode cooling lines are estimated 1/8" away from one of the module side coil lines. All other places that can easily be inspected appear to have enough clearance.

Travis and Don then completed an electrical check again (https://elog.triumf.ca/TIS/RH-ISAC/457). This module still failed the test but as noted not due to continuity rather lower than infinite resistance from the coil to coil and positive coil to 60kV common. This indicates that there is dirty or failing insulation that is either from the fiber glass wrap or something within the service tray. From inspection from outside the hot cell the best guess as to where this is happening is just before to after the exit of the water lines from the service tray but there is no way to confirm this.

Although the module may be able to run for a period of time with these resistances the insulation may continue to break down and there is the risk that during a module move the lines may shift and touch again. This combined with the known HV issues of TM3 paints a dark picture of the service tray.

Friedhelm and Lia have been advised of these recent results and have decided to continue with the installation of the target and conditioning of the target. Should the module be able to operate and extract beam it will be installed in ITE. Friedhelm also came for a visual inspection of the module and agreed that the issue is on the module side and that the lines are too close to tell exactly where the issue may lie. The possibility of separating the the blocks with further insulation was discussed but there is limited area that this can be completed remotely. In addition to this there is no indication that further insulation/bracing will improve the problem and there is considerable risk that it could make the issue worse.

Installation of the containment box started this afternoon and is completed other than the tightening of the window VCR joints. 

Entry  Thursday, September 19, 2013, 11:09, Travis Cave, South Hot-Cell, Maintenance, TM3, no target, Electrical check 

Electrical check of TM#3 with no target was performed and it failed. There is a 135M Ohm short between the coils and a 165M Ohm short between the coil and 60kV common.  All other circuits passed they were infinite in value.

Entry  Thursday, September 19, 2013, 09:08, Travis Cave, South Hot-Cell, Standard Operation, TM3, no target, wiring harness 

The wiring harness for TM#3 was made and a continuity and megger test was done on it and it passed, it has since been installed into the hot cell and placed on the module.

Entry  Tuesday, September 17, 2013, 14:36, Bevan Moss, South Hot-Cell, Standard Operation, TM3, , Containment Box has been removed 

 The containment box has been removed. Tomorrow the wiring harness will be installed.

Entry  Friday, September 13, 2013, 08:05, David Wang, South Hot-Cell, Repair, TM4, , TM4 coil 1 leak check in SHC TM4_coil_1_leak_check.pdf

Leak checked TM4 coil1 in SHC with Isaac . The leak detector only can pump down to 1.5xE-7 atm.cc/sec. The leak detector got the response once the helium valve is open, not even close to the leak area. The leak detector got a very big response when the helium probe was put close to the coil terminal block on target front side and spray helium for 2 clicks. The leak detector got a small  response when the probe was put close to water block area and spray helium for 2 clicks. The leak is located on the front target side coil line but not from water blocks. The leak is too big to be further pin pointed by this method. See attachment

Entry  Friday, September 13, 2013, 07:49, David Wang, Conditioning Station, Development, TM3, , TM3 water lines leak check at CS TM3_water_lines_leak_check_at_CS.pdf

I leak checked TM3 water lines at CS with 60 psi and 80psi helium. The base leak rate is 5.0xe-9 atm.cc/sec. Each circuit 3 minutes helium pressurizing for each time test. No any respose had been found on leak detector during the test. See attachment

Entry  Thursday, September 12, 2013, 10:35, Travis Cave, South Hot-Cell, Standard Operation, TM4, SiC#29, Electrical check TM#4SiC#29FEBIADelechkpostbeam.PDF

TM#4 with SiC#29 post beam electrical check in the south hot cell see PDF for details.

Entry  Thursday, September 12, 2013, 09:29, Travis Cave, ITW, Standard Operation, TM4, SiC#29, module move 

TM#4 with SiC#29 has been moved to the south hot cell move went well.

Entry  Wednesday, September 11, 2013, 15:37, Bevan Moss, South Hot-Cell, Repair, TM3, , C-Seal leak checking and repair 

 This e-log is to cover the work completed from September 9th until the 11th. 

September 9th

Today Maico completed the leak checking blank off and leak checking tool (to replace the one that was contaminated). This tool was then leak checked with C-seals and no springs at the machine shop, both halves were determined to be leak tight. 2 sets of small c-seals without divots were selected and used for leak checking the module side and the source tray side. The heat shield line was tested in the ante-room and was determined to leak. Upon further investigation it was determined that the bore of the seal gland was determined to be over sized (0.450"). Isaac then installed the blank off onto the module and pump down was started, the testing car would not stabilize so Isaac tried turning the screw more allowing for further pump down. The leak check was then completed and there was no response. The flow of helium for the target module was checked but was much lower than typical as the second valve was not fully opened. 

September 10th

With the belief that the larger bore in combination with the small c-seals was the cause of the leak Maico found and polished another block that also had a larger bore. Once polished, small c-seals without dimples were selected and tested with the machine shop leak testing cart. These seals were leak tight but upon investigation the crush zone in one section of the seals was significantly reduced. The smallest width of the crush zone was measured to be ~0.007". This result is concerning as it means that larger bore water blocks can be sealed with small c-seals but once installed there is no way to tell one block from the other. There is no data on the lifetime of this combination of seal and bore. 

Following this test a small c-seal with dimples was selected and checked in the large bore. This combination resulted in a significant leak. Following that test the large c-seals were crushed in the larger bore water block. The torque required to crush the seal and to have the faces touch was more than that of a small c-seal regardless of what size bore it was crushed in. However with the larger bore the large c-seals could be completely crushed allowing for the copper faces to touch (the total force on the faces is unknown). The crushed seal was then inspected, it had a nice uniform crush zone that was relatively large when compared to a properly crushed small c-seal. Another testing with the large seal and a 0.025" wire diameter spring was completed. It was found that the wire interferes with the the seal when it exits from the groove. This interference causes a localized increased crushed zone but does not reduce the crush elsewhere or prevent the copper faces from touching. At this point it was decided to repair the heat shield using large seals. Large seals with springs were tested on the actual HS line in the anteroom and yielded that same results. The line was then installed by Maico inside the HC. It pumped down to the lower limit of the leak testing cart and sprayed with helium, no leak was detected. The containment box was then put back on by Isaac and Grant in preparation for a module move.

September 11th

Today the containment box installation was completed and the module moved. Following that Maico and myself entered into the ante-room and retrieved the blank off block from the HC via the tool port. The large c-seal used in the test and the small ones used in the blank off were then collected and bagged. The large c-seal had typical measurements. The small c-seals used in the blank off did not have typical measurements. They had not been compressed as much and the crush zone was near impossible to see (if visible at all). From the measurements it is believed that the block was not sufficiently tightened. It also calls into question the validity of the leak check due to the combination of less helium and reduced crush. 

After these measurements the tools that were contaminated but were to be recovered were bagged and checked by safety. They have been moved to the jacks area where Maico will decontaminate them. The old wiring harness from TM3 was bagged and given to safety for storage in the cyclotron tunnel. The plastic and all of the garbage was then lifted, bagged, and removed from the ante room. Safety surveyed the anteroom following this no alpha contamination was found but there was 5000 counts on the floor of the ante room. The contamination may have existed prior to this work.

 

Many pictures of the cseals have been taken and have been put into \\trwindata\remote handling\Photos\2013\2013_tm3_source_tray_refurb. A report detailing all of the testing and results would be invaluable.  

 

Entry  Wednesday, September 11, 2013, 13:43, David Wang, Conditioning Station, Development, TM3, , Started 3 turbo pumps on CS for TM3 

TM3 has been connected in CS.Three turbo- pumps have been started. The pumping down is fine so far.

Entry  Wednesday, September 11, 2013, 11:31, Travis Cave, Conditioning Station, Standard Operation, TM3, no target, module move 

TM#3 with no target has been moved to the conditioning station from the south hot cell.

Entry  Wednesday, September 11, 2013, 09:35, David Wang, ITW, Standard Operation, TM1, UCx, 5 shielding blocks have been moved to ITW 

I moved 5 shielding blocks to ITW this morning .I checked the water signals in electrical room before the moving, and everything is fine. The argon venting systemin ITW and electrical room is ready also.

Entry  Tuesday, September 10, 2013, 12:11, Isaac Earle, South Hot-Cell, Repair, TM3, , Module side heat shield water block polishing and blank-off installation 

 The sealing surfaces of the module side heat shield water block were polished on September 9th in the morning using Chad's polishing tool with the following attachments:

- Scotchbrite pads  (30 seconds)  (after this step indium material from the previous seal was no longer visible on the sealing surface)

- 2000 grit sandpaper (30 seconds)

- Felt material with isopropanol (30 seconds)

- Lint free pad (30 seconds)

 

After the final step the surface was rinsed with isopropanol and air dried using canned air.  The water block blank-off was then installed with the manipulators, tightened until snug using the air ratchet, then tightened an additional 1/4 turn while the water block was gripped firmly using one manipulator.  The seal was leak checked and passed successfully.

Entry  Friday, September 06, 2013, 16:41, Bevan Moss, South Hot-Cell, Development, TM3, , C-Seal crush investigation  6x

 Today Maico completed the new leak testing tool and blank off. He tested them with C-seals without springs and all was leak tight. He then inspected the crushed seals and noticed that there was an area that was crushed less on both seals (more prominent in one,  20130906_tm3sourtrayefurb_P1020975) and that this reduced crushed zone only appears on one side of the seal. This is similar to the failure seen on both sets of the heat shield lines. On the seal with the greatest change in crush zone the average crush zone was ~0.025 and the reduced crush zone was ~0.012". He inspected the leak tester and the blank off and determined they were within tolerance and that they had a total seal goove height of 0.074" which is nominal. New seals were selected and one had a visible dimple prior to crushing (20130906_tm3sourtrayefurb_P1020978)  and the other had some defects on the inside (20130906_tm3sourtrayefurb_P1020962). These defects were marked and crushed using the same leak testing tool and blank off. The seal with the dimple showed a reduced crush zone in the same area (20130906_tm3sourtrayefurb_P1030021) and the seal with the defects on the inside showed less or undetectable change in crush zone. Maico then inspected (20130906_tm3sourtrayefurb_P1020991) and crushed the "thicker seals" (more indium coating). When inserting the seals he noticed that they fit tight on the counter bore of the blank off. He then attempted to crush the seal to the point where the copper faces would touch (as design intent) but the seal locked. The gap between the 2 copper faces was measured to be ~0.001". This setup was leak tested and found to be leak tight. When inspecting the crushed thicker seals it was found that the material had actually been pushed sideways causing a lip to form around the crush zone (20130906_tm3sourtrayefurb_P1030003). Maico then fitted the wires for the testing of the module and the heat shield line. 

    Reply  Friday, September 06, 2013, 17:50, Grant Minor, South Hot-Cell, Development, TM3, , C-Seal crush investigation  

Bevan Moss wrote:

 Today Maico completed the new leak testing tool and blank off. He tested them with C-seals without springs and all was leak tight. He then inspected the crushed seals and noticed that there was an area that was crushed less on both seals (more prominent in one,  20130906_tm3sourtrayefurb_P1020975) and that this reduced crushed zone only appears on one side of the seal. This is similar to the failure seen on both sets of the heat shield lines. On the seal with the greatest change in crush zone the average crush zone was ~0.025 and the reduced crush zone was ~0.012". He inspected the leak tester and the blank off and determined they were within tolerance and that they had a total seal goove height of 0.074" which is nominal. New seals were selected and one had a visible dimple prior to crushing (20130906_tm3sourtrayefurb_P1020978)  and the other had some defects on the inside (20130906_tm3sourtrayefurb_P1020962). These defects were marked and crushed using the same leak testing tool and blank off. The seal with the dimple showed a reduced crush zone in the same area (20130906_tm3sourtrayefurb_P1030021) and the seal with the defects on the inside showed less or undetectable change in crush zone. Maico then inspected (20130906_tm3sourtrayefurb_P1020991) and crushed the "thicker seals" (more indium coating). When inserting the seals he noticed that they fit tight on the counter bore of the blank off. He then attempted to crush the seal to the point where the copper faces would touch (as design intent) but the seal locked. The gap between the 2 copper faces was measured to be ~0.001". This setup was leak tested and found to be leak tight. When inspecting the crushed thicker seals it was found that the material had actually been pushed sideways causing a lip to form around the crush zone (20130906_tm3sourtrayefurb_P1030003). Maico then fitted the wires for the testing of the module and the heat shield line. 

 Hello all,

As an addendum to Bevan's e-Log:

Maico also prepared eight (8) new retainer spring windings out of the .025" diameter stainless welding wire for the next seals that we will attempt in the Hot Cell and Ante Room

Maico, Bevan, Keith and I had a discussion about the bolt torque related to the c-seal and water block compression:
- It was found that not much torque is required to compress the "standard" design "thin" c-seals (Ultra-Seal P/N 50606 .001 - .0015 thou indium plating) - basically hand tight only with an allen wrench
- By hand-tightening the bolts with an allen key until the faces of the blocks came together, and then measuring the torque with a torque wrench, Maico discovered that about 8 foot-lbs = 96 inch-lbs (or 5/8ths of a turn past finger tight) was required
- The c-seals are fully compressed when the faces of the blocks are contacting... any additional torque applied is only to pre-load the bolts to ensure that they do not come loose due to temperature cycling and mechanical vibration
- Chad's Hot Cell torque tool is nominally set to about 168 - 180 inch-lbs (or about 14 to 15 foot lbs) based on an e-mail update from him 3-June-2013 - this torque is normal chart torque for a 1/4"-28 UNF SAE Grade 8 bolt pre-load of 3,250 lbs
- see http://www.imperialsupplies.com/pdf/A_FastenerTorqueCharts.pdf
- This amount of bolt pre-load torque may not be required if the bolts are SAE Grade 5.  I recommend at this point that the minimum possible pre-load torque be applied to achieve the chart recommended pre-load for the grade of the bolt, which should be investigated
- This is to ensure that we do not over-stress the thread inserts on the water blocks... if these inserts are damaged, we will basically render the service chase unusable and ruin the module

Cheers,

Grant

Entry  Wednesday, September 04, 2013, 19:01, Grant Minor, South Hot-Cell, Repair, TM3, , Inspection / Ante Room Leak Check Results on TM3 Heat Shield lines (3 Sept 2013) TM3_Heat_Shield_Water_Block_-_c-seal_vs_delta_seal_DRAFT_3Sept2013.pdf

Yesterday, Grant entered the Ante Room with David Wang to visually inspect the two sets of failed c-seals from the Heat Shield circuit, to remove the second set from the Heat Shield water blocks, and to leak check the heat shield circuit with o-rings and a water-block-to-leak-detector fitting.

Some photos of the inspected seals are in the attached design review presentation.  Some unusual marks were observed on both sets of failed seals.

The heat shield lines and water block assembly leak checked successfully to the bottom of the leak rate range ("UNDER" ~1x10-9 atm cc / sec on the Varian 979) with a great flood of helium on all joints with no response anywhere.

Entry  Wednesday, September 04, 2013, 18:53, Grant Minor, South Hot-Cell, Repair, TM3, , Maico's measurements of new c-seals and bench-tested c-seals c-seals_GStanford_file_chronological_4Sept2013.pdfGuyStanford_cseal_file_scanned_30Aug2013.pdf

Today Maico measured the thickness of three indium-plated inconel c-seals, presumably Ultra-Seal P/N 50606.  These seals had NOT been in the Hot Cell.

 

Uncompressed (new) "thin" c-seal

OD .435"

ID .300"

Thickness .094"

Uncompressed (new) "thick" c-seal

OD .438"

ID .280"

Thickness .096"

Compressed (used) "thin" c-seal (Beginning of Life bench test compression only, not long term compression)

OD .438"

ID .294"

Thickness .079"

 

Maico commented that he measured the thickness of a few other compressed "thin" c-seals and they all had .079" thicknesses.

The seal space when the blocks are bolted together (shown on ITA2342 Rev F) should be .070" (steel insert CB) + .002" (recess on module side)  + .002" (recess on source-tray side) = .074"

Thus the compressed seals seem to have .079" - .074" = .005" spring-back.

 

C-seal drawings from Ultra-Seal and Garlock in chronological order from Guy Stanford's design file are attached.  Guy's whole design file is also attached for reference.

Entry  Wednesday, September 04, 2013, 12:21, Bevan Moss, South Hot-Cell, Repair, TM3, , Ante-room work IMG_0983.JPG

 September 3rd

David Wang and myself lowered the leak testing cart into the Ante room and prepared the ante-room for the leak testing of TM3s line. David and Grant then entered the anteroom and inspected the old c-seal and leak tested the the heat shield line. The line pumped down to the lower limits of the leak detector and there was no response from the cart. A presentation with the results of the C-seal inspection results was completed by Grant Minor and email for a design review held on the 4th.

September 4th

David Wang and myself removed the leak detector and surveyed the anteroom and cart. The following results were found with the high spec gamma detector.

Leak Detector body and cart 0 

Leak Detector wheels 200 cpm

Floor off of plastic 300 cpm (there was contamination before)

Plastic in front of HC opening 2000 cpm

Working table after plastic was removed < 50 cpm

Tool box < 50 cpm

First tacky mat 2500 cpm

Second tacky mat 200 cpm

outside of door tacky mats 0 cpm

David then laid fresh plastic on the floor around the HC opening and covered the exposed floor as well.

Following this Travis and David measured the lengths of the wiring and attempted to separate the wiring harness from the Ultem block. It was found that the block was pinned and could not be separated, a new block will need to be made. The measured the following lengths:

Steerering - 26" to 27"

Collimator - 32" - 33"

PNG - 60"

 

Entry  Thursday, August 29, 2013, 17:16, Bevan Moss, South Hot-Cell, Repair, TM3, N/A, Heat Shield Repair 

 Today Chad entered the south hot cell on work permit 2013-08-29-3 to repair the leaking heat shield line. The heat shield line was removed from the module and the surfaces cleaned. New C seals and spring were inserted and the line re-attached. During this time Chad also installed the new vacuum gauge. Grant took video of this work and Keith some pictures. The video and pictures can be found on the M: drive (groups) in the RH folder. The total time taken was ~ 25 minutes. The line was then pumped on and the block was sprayed with helium. The pressure and leak rate started at 0.0 x 10^-4 Torr and 4.0 x 10^-8 atm*cc/Sec. When the helium tank was opened there was an immediate response with the leak rate climbing to 2.7 x 10^-7 atm*cc/Sec. It then stabilized at 2.0 x 10^-7 atm*cc/Sec and was sprayed with helium. Response time was ~2 seconds the leak rate climbed to ~2.3 x 10^-5 atm*cc/Sec the pressure also increased to ~3.0 x 10^-3. The leak detector cart was left attached for another 1.5 hours but still was not able to stabilize in the 10^-9atm*cc/Sec range. 

    Reply  Friday, August 30, 2013, 10:27, Bevan Moss, South Hot-Cell, Repair, TM3, N/A, Heat Shield Repair 

Bevan Moss wrote:

 Today Chad entered the south hot cell on work permit 2013-08-29-3 to repair the leaking heat shield line. The heat shield line was removed from the module and the surfaces cleaned. New C seals and spring were inserted and the line re-attached. During this time Chad also installed the new vacuum gauge. Grant took video of this work and Keith some pictures. The video and pictures can be found on the M: drive (groups) in the RH folder. The total time taken was ~ 25 minutes. The line was then pumped on and the block was sprayed with helium. The pressure and leak rate started at 0.0 x 10^-4 Torr and 4.0 x 10^-8 atm*cc/Sec. When the helium tank was opened there was an immediate response with the leak rate climbing to 2.7 x 10^-7 atm*cc/Sec. It then stabilized at 2.0 x 10^-7 atm*cc/Sec and was sprayed with helium. Response time was ~2 seconds the leak rate climbed to ~2.3 x 10^-5 atm*cc/Sec the pressure also increased to ~3.0 x 10^-3. The leak detector cart was left attached for another 1.5 hours but still was not able to stabilize in the 10^-9atm*cc/Sec range. 

 Also of note is that Chad received a full days dose and that when the plastic was surveyed there were ~150 counts found on it.

 

       Reply  Friday, August 30, 2013, 14:55, Bevan Moss, South Hot-Cell, Repair, TM3, N/A, Heat Shield Repair 

Bevan Moss wrote:

Bevan Moss wrote:

 Today Chad entered the south hot cell on work permit 2013-08-29-3 to repair the leaking heat shield line. The heat shield line was removed from the module and the surfaces cleaned. New C seals and spring were inserted and the line re-attached. During this time Chad also installed the new vacuum gauge. Grant took video of this work and Keith some pictures. The video and pictures can be found on the M: drive (groups) in the RH folder. The total time taken was ~ 25 minutes. The line was then pumped on and the block was sprayed with helium. The pressure and leak rate started at 0.0 x 10^-4 Torr and 4.0 x 10^-8 atm*cc/Sec. When the helium tank was opened there was an immediate response with the leak rate climbing to 2.7 x 10^-7 atm*cc/Sec. It then stabilized at 2.0 x 10^-7 atm*cc/Sec and was sprayed with helium. Response time was ~2 seconds the leak rate climbed to ~2.3 x 10^-5 atm*cc/Sec the pressure also increased to ~3.0 x 10^-3. The leak detector cart was left attached for another 1.5 hours but still was not able to stabilize in the 10^-9atm*cc/Sec range. 

 Also of note is that Chad received a full days dose and that when the plastic was surveyed there were ~150 counts found on it.

 

Today Chad entered hot cell again and removed the HS module side and Junction Block Wiring Harness (module side). In addition to this he blanked off the module side HS line. It took Chad 16 minutes to perform these tasks and he received a dose of 0.20 mSv bringing his total to 0.84 over the last 2 days. After exiting the hot cell Chad completed a leak check on the module side. The line pumped down to the limits of the leak testing cart 0.0x10^-4 Torr and 0.0x10^-9 atm*cc/sec and there was no response. A video of Chad in the hot cell can be found in:

M:\remote handling\Photos\2013\2013_tm3_source_tray_refurb

This afternoon was spent surveying the anteroom and receiving teaching from Chad as to how to be a hot cell operator. There was little in the way of contamination ~150 counts near the HC door and ~50 counts on the surrounding floor. The wiring harness has a field of 900 uSv/hr but is suspected most of that is coming from the aluminum steerer bracket. 

Entry  Thursday, August 29, 2013, 09:08, chad fisher, South Hot-Cell, Repair, TM3, , Heat Shield Circuit Leak 20130829_084751.jpg20130829_084754.jpg20130829_084949.jpg20130829_084957.jpg

The heat shield circuit was pressurized with air (15-20 psi) and snoop applied to the water block joint and brazes. Bubbles formed at the joint between the two water blocks indicating that the leak is a c seal problem. Pictures attached but also on docushare Collection-11285.

    Reply  Thursday, August 29, 2013, 10:09, Bevan Moss, South Hot-Cell, Repair, TM3, , Heat Shield Circuit Leak 

chad fisher wrote:

The heat shield circuit was pressurized with air (15-20 psi) and snoop applied to the water block joint and brazes. Bubbles formed at the joint between the two water blocks indicating that the leak is a c seal problem. Pictures attached but also on docushare Collection-11285.

 Last night prior to this leak check the Heat Shield was pumped on and helium sprayed on the circuit. The pressure was 0.0 x 10^-4 Torr. The leak was traced to water block. response time was 2 seconds and went from 5.5 x 10^-8 to 1.6 x 10^-6 atm*cc/sec. There was also a response without spraying helium (drift from the nozzle). The results of this testing prompted the testing completed in Chads elog.

       Reply  Thursday, August 29, 2013, 12:03, Grant Minor, South Hot-Cell, Repair, TM3, no target, Heat Shield Circuit Leak TM3_Rev_3_Heat_Shield_Water_Lines_leak_check_29Aug2013_1.jpgTM3_Rev_3_Heat_Shield_Water_Lines_leak_check_29Aug2013_2.jpgTM3_heatshield_snoop_test2_29Aug2013.pdf

Bevan Moss wrote:

chad fisher wrote:

The heat shield circuit was pressurized with air (15-20 psi) and snoop applied to the water block joint and brazes. Bubbles formed at the joint between the two water blocks indicating that the leak is a c seal problem. Pictures attached but also on docushare Collection-11285.

 Last night prior to this leak check the Heat Shield was pumped on and helium sprayed on the circuit. The pressure was 0.0 x 10^-4 Torr. The leak was traced to water block. response time was 2 seconds and went from 5.5 x 10^-8 to 1.6 x 10^-6 atm*cc/sec. There was also a response without spraying helium (drift from the nozzle). The results of this testing prompted the testing completed in Chads elog.

 Please find attached some schematics which help illustrate the setup for this heat-shield circuit leak check.

Entry  Thursday, August 29, 2013, 06:48, David Wang, Conditioning Station, Development, TM3, , TM3 leak check in CS with new source tray. TM3_leak_check_at_CS_2013__AUG_27th.pdf

A huge leak had been found on HS circuit during 60 psi helium pressurize test. Other circuits are free of obvious major leak at present .We will test them again once the TM3 is back to CS. See attachment for details

Entry  Wednesday, August 28, 2013, 14:25, Travis Cave, Conditioning Station, Standard Operation, TM3, no target, module move 

TM#3 with no target has been moved from the conditioning station to the south hot cell. The fields observed around the containment box of the module ranged from 0.80 mSv/hr to 1.8mSv/hr..

Entry  Wednesday, August 28, 2013, 14:17, Travis Cave, South Hot-Cell, Standard Operation, , UC#6, Spent target move Vault_Storage_August_28_2013.pdf

Spent target move, UC#6 has been moved from the south hot cell to the target storage. The target is in pail 108 and in slot 8C of the vault. See attached PDF for details.

Entry  Tuesday, August 27, 2013, 17:18, Grant Minor, Conditioning Station, Repair, TM3, no target, TM3 Rev 3 source tray - prelminary leak check results at CS TM3_leak_check_at_CS_27Aug2013.JPGsketch_TM3_water_feedthru_27Aug2013-1.pdf

David Wang started a helium leak check on TM3 at the CS this morning.

David will create an e-log once his check is complete, but here are the preliminary results:

- target oven +/- OK

- mounting support plate OK

- ionizer tube heater +/- OK

- extraction electrode OK

A large leak was found in the heat shield circuit:

- The module pumped down with the leak rate stabilizing at 4.8xE-9 atm.cc/sec
- 60 psi helium was applied to the heat shield fitting on the right side of the Y-shaped connector (see attached sketch, each side of the "Y" is separated by a face to face metal contact only, i.e. no o-ring seal separates supply and return water)
- The maximum leak response was detected in 10 seconds, with base pressure rising from 2.0E-2 torr to 2.8xE-2 torr
- The helium was vented from the line by using an allen wrench to open the valve on the water quick-connect (see attached photo)
- The module continued pumping down, and after some time, the allen wrench was used again to open the valve, but air rushed inside, indicating vacuum was being drawn inside the water line through the leaking interface
- As the module continued to pump, this vacuum vent air rush inside the water line could not be reproduced by opening the valve again with the allen key

The module is currently pumping down at the Conditioning Station. We will leak check the remaining lines tomorrow with whatever base leak-rate we have achieved, and then move TM3 to the Hot Cell for further diagnosis.

Entry  Tuesday, August 27, 2013, 14:14, Travis Cave, ITW, Standard Operation, TM1, UC#7, module move 

TM#1 with UCx#7 has been moved from the south hot cell to the west target station.

Entry  Tuesday, August 27, 2013, 11:56, Travis Cave, South Hot-Cell, Standard Operation, TM1, UC#7, Electrical check TM#1_UC#7__TgtElecChk_SHC_.PDF

TM#1 with UCx#7 electrical check, numbers look good, see PDF for details.

Entry  Tuesday, August 27, 2013, 11:54, Travis Cave, South Hot-Cell, Standard Operation, TM1, UC#6, module move 

TM#1 with UCx #6 has been moved to the south hot cell.

Entry  Monday, August 26, 2013, 18:26, Grant Minor, Conditioning Station, Standard Operation, TM3, , TM3 moved from Hot Cell to Conditioning Station 

Target Module 3 with no target, and a partially-installed Rev-3 source tray (no steerers connected, no IMG connected, entrance window lines blanked off on module side and not connected to containment box) was transported successfully to the Conditioning Station by Travis Cave and David Wang at around 4pm today.  David attached the vacuum system for start of pump-down to prepare for leak checking.

Entry  Monday, August 26, 2013, 18:22, Grant Minor, South Hot-Cell, Repair, TM3, , TM3 Rev 3 - all connetions made except steerers, IMG, and entrance window 8x

Today Chad finished making all connections to the new source tray, except for:

- steerers - broken wire, must be repaired at a later date

- IMG gauge - bracket required, old bracket thrown out with previous tray by accident, see ITA3301, must be installed at a later date

- entrance window - the window lines on module side were left blanked-off for leak checking, containment box must be removed in the next few days to complete steerer repairs so these lines were not connected to save work from having to be repeated

The containment box was replaced, and TM3 was moved to the CS for pump-down and leak checking (see other e-log).  David reported at 6:15 pm that the turbos were turned on at the CS and the vacuum looked normal (so far).

As stated above, Chad realized today that he had thrown out the old IMG gauge bracket with the previous source tray, and a new one must be manufactured.  The assembly is described by ITA3301.  Three components must be manufactured (ITA3302, ITA3303, and ITA2673).  A stock split-ring clamp for ITA2673 (MDC #716001) was graciously donated by Dimo Yosifov.  Grant Minor submitted a work order to the machine shop today for 2 each of ITA3302 and ITA3303.

Entry  Friday, August 23, 2013, 18:32, Grant Minor, South Hot-Cell, Repair, TM3, , TM3 Rev 3 - steerer wire broken from connector on module side TM3_Broken_Steerer_Wire_Module_Side_23Aug2013.JPGTM3_Broken_Steerer_Wire_Module_Side_23Aug2013-001.JPGTM3_Broken_Steerer_Wire_Module_Side_23Aug2013-002.JPGITA2826D_RevD02_23Aug2013.pdfThermocouple-style_connector_23Aug2013.JPG

While continuing on the TM3 Rev 3 source tray installation, Chad noticed today that one of the steerer wires is broken and has come out of the thermocouple-style connecter block (see attached photos).

From drawing ITA2826 (Rev D02 attached) it is likely that this is for either the "upper" or "right side" steerer plate.

Entry  Thursday, August 22, 2013, 19:38, Grant Minor, South Hot-Cell, Repair, TM3, , TM3 Rev 3 source tray - water blocks connected and torqued 6x

After a great struggle with the water block jigs, the TM3 source tray was finally advanced fully into the service tray and all water blocks were connected and torqued to spec in the hot cell by Chad Fisher.

Notes and description of problems encountered during the installation:

- The water lines for the optics tray interfered with the module-side water block jig, and had to be bent out of the way to clear while advancing the tray (see attached photos)

- The water block jig on the source tray side was too low relative to the module side, and had to be eventually unbolted completely from it's mounting bracket in order to raise it up into alignment

- A piece of aluminum plate was placed under the jig, and the pneumatic table was raised in order to move the jig upwards

- After many repeated attempts to engage the blocks by pressing the jigs together, it was discovered that some of the blocks had rotational misalignment with their respective counterparts on the module side, preventing the pins from engaging properly

- By looking through the bolt holes on several of the blocks, it was possible to determine which direction they had to be rotated

- Chads polishing tool was used to apply some torque to rotate the source-tray-side water blocks slightly so proper alignment of the pins could be achieved

- See the attached photo which indicates which blocks had to be rotated (blocks 5, 6, 9, 10, and 11)

- The blocks had the bolts installed and were also torqued in the numbered order shown in the attached photo

Next steps are to remove the water block jigs, re-connect the loosened brackets for the remaining water lines (entrance window, optics tray), re-install the containment box and associated VCR connectors, video inspect, and leak check.

Entry  Wednesday, August 21, 2013, 20:36, Grant Minor, South Hot-Cell, Repair, TM3, , TM3 module-side water block sealing surface inspection (post polishing) TM3_final_water_block_polishing_16-048.JPGTM3_final_water_block_polishing_16-031.JPG

The water block sealing surfaces on the module-side of TM3 were polished this week by Chad Fisher, using his air-ratchet controlled rotating head tools (single and double-surface polishing tools).

Photos of the polishing tools in-use are attached (from August 16 - 21, 2013)

Scotch-brite pads were used, followed by 2000 grit sandpaper, then white felt with isopropanol, then lint-free dry polishing pads, each on detachable heads that are used with the polishing tool.

The module-side water block surfaces were inspected by Grant Minor on 21 Aug 2013 using a level telescope and camera looking through the hot cell window.  Results can be viewed here, with photos indicating which block is being viewed in sequence.

https://documents.triumf.ca/docushare/dsweb/View/Collection-11251

Entry  Monday, August 19, 2013, 10:08, Anders Mjos, ITE, Repair, TM4, SiC#29, Leak Check ITE_Leak_Test_2013-08-19.pdf

All water circuits except Coil 1 were leak checked by David and Anders. No obvious signals were detected except some small possible responses. See attached notes for details.

Entry  Thursday, August 15, 2013, 16:35, Anders Mjos, ITE, Repair, TM4, SiC#29, Leak found on Coil 1 ITE_Leak_Test_2013-08-14.pdf

By pressurizing the water lines with 70 psi helium David and I detected a major leak on the Coil 1 circuit. The response maxed out on the leak rate on the leak detector and we could also see a pressure increase on the leak detector. ISAC controls reported a change in vacuum at the same time (link).

 

The Heat Shield and Coil 2 circuit was checked before we moved to Coil 1. No response was detected on these two circuits. We would like to check the remaining circuits as well, but this cannot be done today due to the large amount of helium still present. The remaining circuits will have to be checked tomorrow morning.

 

Entry  Thursday, August 15, 2013, 09:32, chad fisher, South Hot-Cell, Repair, TM3, , TM3 source tray installation status 

 

The installation of the module side water block jig has been successful.
 
During initial attempts yesterday afternoon, installation of the jig proved, as expected to be extremely difficult. This was primarily due a poorly position water block from a previous repair were the soldering jig had not been used to position the block; specifically coil 1. This is the same block that contributed with the difficulties in removing the old source tray.
 
I was able to utilize the water block polishing tools as handles to reposition this water block ( as well as another slightly difficult one) into its location in the water block jig.
 
Please be aware, as the jig was very difficult to install, it will be very difficult to remove later (as it was when removing the old source tray).
 
Chad
Entry  Thursday, August 15, 2013, 07:37, David Wang, ITE, Repair, TM4, , I moved 5 shielding blocks from ITE to block storage area. 

I moved5shielding blocks from ITE to block storage area, This is a job for preparing ITE vacuum surge investigation and leak check.

Entry  Wednesday, August 14, 2013, 11:50, Travis Cave, South Hot-Cell, Maintenance, TM3, , module move 

TM#3 and its new source tray have been both moved into the south hot cell.

Entry  Wednesday, August 07, 2013, 06:47, maicodallavalle, Spent Target Vault, Maintenance, , , F-308 

All the F-308's have been torqued up  and the locks installed. Ready to be moved.

Entry  Wednesday, July 31, 2013, 11:13, Travis Cave, Spent Target Vault, Standard Operation, , , Spent target move Vault_Storage_July_31_2013.pdfMini_Vault_Storage_July_31_2013.pdf

Five spent targets have been removed from the storage vault and placed into the mini storage. The target placed into the mini storage are UO#3, UC#'s  3,4,5 and SIC#23. See attached PDFs for vault details.

Entry  Tuesday, July 30, 2013, 14:42, David Wang, ITE, Standard Operation, TM4, , TM4 has been connected in ITE. 

TM4 has been connected in ITE. All turbo pumps have been started now. The pumping down on TM4 and ITE is good so far. The water interlock check on TM4 is done,and everything is fine. The ITE  IG1 still couldnt be turned on even if we replaced a new TM4  IG1 at CS. The problem is on the connecting cable from ITE to electrical room or gauge controller. I talked with Friedhelm  and vacuum group will be noticed on this problem.

Entry  Tuesday, July 30, 2013, 10:44, Travis Cave, ITE, Standard Operation, TM4, SiC#29, module move 

TM#4 with SiC #29 has been moved from the conditioning station to the east target station, move went well.

Entry  Monday, July 29, 2013, 14:32, Travis Cave, Spent Target Vault, Standard Operation, , Ta#40, Spent target move Vault_Storage_July_29_2013.pdf

Spent target Ta#40 has been placed into storage. The target was placed in pail #107 and was put into slot 5A of the vault. It had a field of 224mSv/hr upon removal from the south hot cell. See attached PDF for more details.

Entry  Friday, July 26, 2013, 11:06, David Wang, South Hot-Cell, Standard Operation, , , The steel shielding plug has been put on theSHC top in target hall 

to reduce the radioactive shining from  SHC Ta# 40 target.

Entry  Thursday, July 25, 2013, 10:08, David Wang, Conditioning Station, Standard Operation, TM4, SiC #29, TM4 HS helium pressure test andTM4 connection at CS 

Bevan and I did a helium pressure test on TM4 HS water circuit at CS. The leak detector is pumped to the bottom scale(E-9 atm.cc/sec and E-4torr). We applied 70 psi helium to the HS circuit for 3 minutes .  No response had been found. I also leak checked IG1 flange which was replaced yesterday. It is  good. We connected the TM4 to CS and put the HV cover on. The water cooling system will be started soon.

Entry  Thursday, July 25, 2013, 09:37, Travis Cave, Conditioning Station, Standard Operation, TM4, SiC#29, Electrical check TM#4_SiC#29_FEBIAD_TgtElecChkCS_.PDF

Electrical check of TM#4 with SiC#29 attached. Results are pretty much the same as yesterday for the coil to 60kV common, and anode to 60kV common. See attached pdf for details.

Entry  Wednesday, July 24, 2013, 17:46, David Wang, Conditioning Station, Standard Operation, TM4, Sic 29#, Started 3 turbo pumps on CS for TM4 

3 turbo pumps on TM4 and CS have been started. The pumping down is good so far, The TM4 PNG1 reading is more than 10 times higher than IG1 which is at the same chamber. It could be a controller problem.  Other 3 high vacuum gauges behavior normal.  The TM4 IG1 is replaced today and it works fine now.

Entry  Wednesday, July 24, 2013, 14:40, Travis Cave, Conditioning Station, Standard Operation, TM4, SiC#29, module move 

TM#4 with SiC#29 has been moved from the south hot cell to the conditioning station move went well.

Entry  Wednesday, July 24, 2013, 08:40, Travis Cave, South Hot-Cell, Standard Operation, TM4, SiC#29, Electrical check TM#4_SiC#29_FEBIAD_Tgt_Elec_Chk.PDF

Electrical check on TM#4 with SiC#29 has been done. The reading of the magnet coil and 60kV common is low at 750 ohms, normally this infinite. Awaiting further instruction on if this is a pass or fail. See attached PDF for the rest of the details.

Entry  Tuesday, July 23, 2013, 13:33, Travis Cave, South Hot-Cell, Standard Operation, TM4, Ta#40, Electrical check TM#4_Ta#40_SIS_Tgt_Elec_Chk_post.PDF

Results of electrical check on Ta#40 target on TM#4 post beam at the south hot cell

Entry  Tuesday, July 23, 2013, 10:55, Travis Cave, ITE, Standard Operation, TM4, Ta#40, module move 

TM#4 with Ta#40 has been moved from the east target station to the south hot cell move went well.

Entry  Monday, July 22, 2013, 15:52, Bevan Moss, Conditioning Station, Standard Operation, TM3, No Source Tray, HV testing update 

   I have fallen behind on the HV testing that has been completed on TM3. Data can be found on docushare in the TM3 Rev 3 folder files are too large to attach. From the last elog entry the following tests have been completed

July 8 2013 - Long HV conditioning 50kV achieved before sparking caused PS to trip. Was unable to recover to the same voltage

July 9 2013 - Attempted to repeat previous test lost PS at 45kV. Voltage continued to degrade during the day.

July 10 2013 - Max voltage achieve 42.5kV discussed with Friedhelm and decided to run the EINZEL lens at 50% of the BIAS in case this is the source of the sparking

July 10 2013 - Max voltage 40.5kV with EINZEL lens. Communicated with Friedhelm and Lia. It was decided 40kV was good enough. Started developing standard test (see below for testing procedure) for Module so a with and without source tray 

July 12 2013 - Only one spark on route to 40kV. PS tripped after ~10 minutes at 40kV. Near the end of the day there wasn't enough time to repeat test.

July 15 2013 - Test repeated, could not hold 40kV. 39kV held for 1 hour with EINZEL lens off. Sparking was making it difficult to keep on.

July 15 2013 - TM3 was electrically disconnected from the conditioning station. The station ran at 60kV for 1 hour with zero sparks.

July 16 2013 - Test repeated with goal of 39kV intense sparking after 20 minutes caused the PS to trip. Once again the EINZEL lens PS was tripping and eliminated from use to make the test easier. With the failure of this test once again Friedhelm was once again consulted. He advised to stop testing as it appears to be causing damage. There is concern that the module is degrading. Lia has stated this does not affect the source tray and that a source tray will be inserted into TM3 and she accepts responsibility if the module does not hold voltage. 

Standard testing procedure for the bias was as follows. Please note that the EINZEL lens was supposed to follow the BIAS steps at 50%. This procedure was approved by Friedhelm prior to operating. This test was never successfully completed and we will not be able to complete a "apples to apples" test once the source tray is installed.

> Step to 5000 kV If no sparking after 1 minute
> Step to 10000 kV If no sparking after 1 minute
> Step to 15000 kV If no sparking after 1 minute
> Step to 17500 kV If no sparking after 1 minute
> Step to 20000 kV If no sparking for at least 1 minute after 5 minutes
> Step to 22500 kV If no sparking for at least 1 minute after 5 minutes
> Step to 25000 kV If no sparking for at least 1 minute after 5 minutes
> Step to 27500 kV If no sparking for at least 1 minute after 5 minutes
> Step to 30000 kV If no sparking for at least 1 minute after 5 minutes
> Step to 31000 kV If no sparking for at least 1 minute after 5 minutes
> Step to 32000 kV If no sparking for at least 1 minute after 5 minutes
> Step to 33000 kV If no sparking for at least 1 minute after 5 minutes
> Step to 34000 kV If no sparking for at least 1 minute after 5 minutes
> Step to 35000 kV If no sparking for at least 2 minute after 10 minutes
> Step to 35500 kV If no sparking for at least 2 minute after 10 minutes
> Step to 36000 kV If no sparking for at least 2 minute after 10 minutes
> Step to 36500 kV If no sparking for at least 2 minute after 10 minutes
> Step to 37000 kV If no sparking for at least 2 minute after 10 minutes
> Step to 37500 kV If no sparking for at least 5 minute after 10 minutes
> Step to 38000 kV If no sparking for at least 5 minute after 10 minutes
> Step to 38500 kV If no sparking for at least 5 minute after 10 minutes
> Step to 39000 kV If no sparking for at least 5 minute after 10 minutes
> Step to 39500 kV If no sparking for at least 5 minute after 10 minutes
> Step to 40000 kV Maximum 3 sparks per hour maximum test time 3 hours.

 

 

Entry  Thursday, July 18, 2013, 10:08, Travis Cave, Conditioning Station, Standard Operation, TM3, no target, module move 

TM#3 with no target and no source tray has been moved from the conditioning station to the north east silo, move went well.

Entry  Wednesday, July 17, 2013, 10:10, David Wang, Conditioning Station, Development, TM3, , CS cooling and vacuum system have been turned off  

CS water cooling and vacuum system have been turned off at 10:00 AM this morning.The TM3 will be disconnected and moved to silo tomorrow morning.

Entry  Wednesday, July 17, 2013, 08:29, David Wang, Conditioning Station, Development, TM3, , TM3 leak check in CS without source tray. 

Leak checked TM3 without source tray in CS this morning. The CS and TM3 vacuum: IG1(top of the TM3 service cap)4.9x E-7Torr, IG2(diagnostic box  primary)1.9XE-6 Torr. IG1S (secondary vessel)7.9X E-7Torr. The leak detector was at 0.0XE-4 torr and 0.0XE-9 atm.cc/sec level during the leak checked. All water lines quick connector fittings, NPT thread fittings, water cap seals, blue insulator seals, bellow, gauges seals, turbo-pumps, all blanket panels,and TM3 to CS vessel seal have been sprayed with helium and leak checked. No leak has been found. The TM3 is leak tight in CS.

Entry  Tuesday, July 16, 2013, 13:09, David Wang, ITE, Standard Operation, TM4, , TM4 has been disconnected in ITE. 

TM4 has been disconnected in ITE. All water lines on TM4 have been purged. ITE is venting now.

Entry  Tuesday, July 09, 2013, 14:26, David Wang, ITW, Standard Operation, TM1, UCx, 5 shielding blocks had been transferred from ITE to ITW 

5 shielding blocks had been  transferred from ITE to ITW.  The  ITW is configured to take proton beam.

Entry  Friday, July 05, 2013, 10:02, Bevan Moss, Conditioning Station, Standard Operation, TM3, No source tray, TM3 module move to TCS 

TM3 has been moved from the south hot cell to the conditioning station. David and I completed the move. All went well.

Entry  Friday, July 05, 2013, 09:22, chad fisher, South Hot-Cell, Repair, TM3, , Service Tray Water Block Inspection 

I have inspected the service tray water block and suggest that they SHOULD be cleaned/polished before we install the new source tray.

The water blocks have slight water scalling to the inside of the ID of where the c seals locate.

I have taken two close up  pictures of each water block for reference and to document their current state. They can be found at http://documents.triumf.ca/docushare/dsweb/View/Collection-10841
 

Entry  Thursday, July 04, 2013, 11:37, David Wang, ITW, Standard Operation, TM1, UCx, I reconnected TM1 to ITW. 

 I  reconnected TM1 to ITW on 02 July.The pumping down is good so far. TM1 water interlock check is good also.

Entry  Wednesday, July 03, 2013, 10:43, Travis Cave, South Hot-Cell, Standard Operation, TM3, no target, module move 

TM#3 with no target and no source tray was moved from the north east silo to the south hot cell the move went well.

Entry  Wednesday, July 03, 2013, 08:44, chad fisher, Travis Cave, South Hot-Cell, Standard Operation, , , Ta#39 Transfered to spent target storage vault Vault_Storage_July_3_2013.pdf

Ta#39 has been transferred to spent target storage vault. Ta#39 was placed into pail #106 and placed into spot of 4C of the spent target vault. The pail measured 95.8mSv/hr upon removal from the hot cell. See attached PDF for details.

Entry  Wednesday, July 03, 2013, 08:43, chad fisher, South Hot-Cell, Standard Operation, , , Ta#39 Transfered to spent target storage vault 
 
Entry  Tuesday, July 02, 2013, 10:58, Travis Cave, Conditioning Station, Standard Operation, TM1, UC#6, module move 

TM#1 with UC#6 has been moved from the conditioning station to the west target station, move went well.

Entry  Tuesday, July 02, 2013, 09:37, chad fisher, South Hot-Cell, Development, TM3, , TM3 Rev.2 Source Tray Disposal 

Tm3 Rev.2 source tary has been transfered to the vault tunnel storage.

Entry  Thursday, June 27, 2013, 14:27, chad fisher, South Hot-Cell, Development, , , Polishing Cleaning tool - Water blocks 20130626_144941.jpg

The polishing/cleaning tool prototype is now finished and appers to work great.

Thanks to Dan and Maico for the great job making my design a reality.

Entry  Thursday, June 27, 2013, 14:23, chad fisher, South Hot-Cell, Standard Operation, TM1, Ta#39, Ta#39 Autopsy performed 

An autopsy of Ta#39 was performed yesterday and today. Ta#39 will be sent to the spent target storage vault on Tuesday.

 

 

Entry  Thursday, June 27, 2013, 14:21, chad fisher, South Hot-Cell, Standard Operation, TM1, Ucx#6, Ucx#6 installed Ta#39? rewmoved 

Ucx#6 was installed on TM1 on Wednesday.

Ta#39 was removed.

Entry  Wednesday, June 26, 2013, 11:03, David Wang, South Hot-Cell, Standard Operation, TM1, , Leak check on TM1 UCx target heat shield 

Chad and I leak checked the TM1 UCx target heat shield at SHC. No leak has been found so far.

Entry  Tuesday, June 25, 2013, 14:56, Bevan Moss, Conditioning Station, Standard Operation, TM1, UCx#6, Roughing Pumps Started 

 The roughing pumps have been started on the conditioning station. As it is late in the day for David he will make the turbo pump connections tomorrow.

Entry  Tuesday, June 25, 2013, 14:24, Travis Cave, Conditioning Station, Standard Operation, TM1, UC#6, module move 

Module moves of TM#1 with Ta#39 from ITW to SHC then TM#1 with UCx#6 from SHC to the conditioning station moves went well.

Entry  Tuesday, June 25, 2013, 13:20, Travis Cave, South Hot-Cell, Standard Operation, TM1, UC#6, Electrical check TM#1_UC#6_SIS_Target_Elec_Chk.PDF

Results from the electrical check of TM#1 with the UC#6 target. See attached PDF.

Entry  Friday, June 21, 2013, 09:26, chad fisher, South Hot-Cell, Development, TM3, , Mock-up Leak Check Results 

The Mock-up has been leak tested after the remote connection of the water blocks and is leak tight!

Thanks everybody who contributed to its success.

Entry  Thursday, June 20, 2013, 13:47, Travis Cave, Spent Target Vault, Standard Operation, , , Spent Target Assay Vault_Storage_June_20_2013.pdf

Ten targets have been assayed or had field measurements(they were too hot to ship but were assayed the last time an assay was done) done on them  over the past two days. Of those that have been assayed we have total of ten shippable targets. See the attached PDF for the latest details of the storage vault.

Entry  Wednesday, June 19, 2013, 08:15, chad fisher, South Hot-Cell, Development, TM3, , Mock up water block connections 20130619_080806[1].jpg20130619_080808[1].jpg

All water block connections on the mock-up have bben achieved. It is now ready for leak checking.

The front half of the water block jig proved extremely difficult to remove.

Entry  Tuesday, June 18, 2013, 14:00, chad fisher, South Hot-Cell, Development, TM3, , Mock-up testing / water block connections 

The testing of the mock-up and tooling has commenced.

Source tray mock-up has been driven into the mock-up and the first two water block connections have been made; the first with the torque limiting 
T-handle tool and the second with the torque limiting air rachet attachment. Both seem to work well, although achieving the required torque with the manipulators proved to be near the limit of the manipulator.

 

 

Entry  Thursday, June 13, 2013, 09:21, chad fisher, South Hot-Cell, Development, , , Warm Cell Mock-up 20130613_084421[1].jpg20130613_084426[1].jpg

the warm cell mock-up has been inserted into the warm cell and final preparation for the remote test are being made.

Entry  Thursday, June 13, 2013, 09:18, chad fisher, South Hot-Cell, Repair, TM3, , Source Tray/Extraction Column Removal 

TM3 Rev 2 source tray/extraction column insertion into its storage was completed yesterday and it was then removed from the hot cell and put into the anteroom until June 25th when it will be moved into the vault tunnel.

 

The Box did have 10000 counts of contamination "all over" it. It has recieved inital decontamination and is down to 1000 counts.

 

 

 

 

Entry  Wednesday, June 12, 2013, 10:39, Travis Cave, South Hot-Cell, Standard Operation, , , spent source tray removal 

The spent source tray for TM#3 has been removed from the south hot cell and well be placed in the the hot cell ante room. To sit till maintenance day to be moved over to the vault storage tunnels.

Entry  Tuesday, June 11, 2013, 10:05, David Wang, ITW, Standard Operation, TM1, , Disconnected TM1 in ITW. 

Dan and I  disconnected TM1 in ITW.

Entry  Tuesday, June 04, 2013, 15:34, Bevan Moss, Conditioning Station, Repair, , , Relay replaced 

ESC was called out again to inspect the chiller as it was showing the same problem as before. This time when started one fan came on (this is not what happened last time) but the fan controlled by the VFD did not. It was eventually traced to a relay that has been replaced. The system was tested as best it could without a load and appears to be working. It will be difficult to tell until a heat load is in place if the fix has solved everything. 

Entry  Tuesday, June 04, 2013, 12:36, David Wang, ITE, Standard Operation, TM4, , 5 shielding blocks are transferred from ITW to ITE 

Dan an I  transferred 5 shielding blocks from ITW to ITE. The ITE is configured to take proton beam.

Entry  Friday, May 31, 2013, 11:19, Travis Cave, Spent Target Vault, Standard Operation, , SiC#28 (RFQ Target), Spent target move Vault_Storage_May_31_2013.pdf

Spent target SiC#28 (RFQ Target) has been moved from the south hot to the storage vault. The target was placed in pail #105 in spot 2C of  the spent target vault. The target had a field of 24.8mSv/hr at about a meter upon removal from the south hot cell. See attached PDF for the status of the vault. It currently only has six free spots left.

Entry  Wednesday, May 29, 2013, 12:07, chad fisher, South Hot-Cell, Development, , SiC#28 RFQ, RFQ Autopsy 

Major portions of the RFQ target have now been sucessfully dismantled. More minor dismantling with conclude this afternoon.

Entry  Wednesday, May 29, 2013, 06:32, David Wang, ITE, Standard Operation, TM4, Ta#40, TM4 has been connected in ITE. 

TM4 has been connected in ITE. The pumping down is fine so far.TM4 water interlock check was done yesterday.

Entry  Tuesday, May 28, 2013, 10:42, Travis Cave, South Hot-Cell, Standard Operation, TM4, Ta#40, Electrical check TM#4_Ta#40_SIS_Target_Elec_Chk.PDF

Results of the electrical check on  TM#4 with Ta#40, it passed. See attached PDF for results.

Entry  Tuesday, May 28, 2013, 10:37, Travis Cave, ITE, Standard Operation, TM4, Ta#40, module move 

TM#4 with Ta #40 moved from the conditioning station to the east target station, move went well.

Entry  Monday, May 27, 2013, 16:36, Bevan Moss, Conditioning Station, Standard Operation, TM4, Ta#40, Argon Venting Started 

 Argon venting has started. It will be left to vent over night. 

Entry  Monday, May 27, 2013, 16:07, Bevan Moss, Conditioning Station, Standard Operation, TM4, Ta #40, HV conditioning 

 The HV conditioning reached a maximum of 44kV today before a spark took out the canbus card. I will attach the data once I have had a chance to format it. 

Entry  Monday, May 27, 2013, 16:01, Bevan Moss, Conditioning Station, Repair, , , CanBUS card 

 During HV conditioning of TM4 with Ta#40 there was a spark at ~43 kV that caused the Bias card to "fry". Dave Morris has been contacted and has said he will replace it tomorrow.

Entry  Monday, May 27, 2013, 15:59, Bevan Moss, Conditioning Station, Repair, , , Compressor fault 

 Once again the 7.5 compressors are tripping due to faults. I believe it is due to over pressure as a result of the chiller fans not coming on. I have contacted ESC.

Entry  Monday, May 27, 2013, 11:55, chad fisher, South Hot-Cell, Standard Operation, , , Special Tooling for RFQ target 

The special tool made for the RFQ target autopsy has been inserted into the hot cell.

 

4-40 button head screws have been successfully lossened.

Entry  Monday, May 27, 2013, 10:37, Bevan Moss, Conditioning Station, Maintenance, TM4, , Cooling Systems topped off 

Rob walker has flushed and refilled the primary side of the system (note the water still looks nasty). This morning the primary side of system needed to be bled as there were air pockets. Also TK2 had reached its low point and needed to be topped up.

Entry  Monday, May 27, 2013, 10:35, Bevan Moss, Conditioning Station, Standard Operation, TM4, Ta #40, Pumps Started HV testing to follow 

The pumps have been turned on at ~9:30 this morning. Current values are 6.61 Mohm TCS:DIC1 @19.4 C. HV testing will start momentarily.

Entry  Thursday, May 23, 2013, 14:12, Bevan Moss, Conditioning Station, Maintenance, , , Primary Circuit Drained and Flushed 

 Rob Walker has drained the primary side of the conditioning station. It will be flushed, filled  and chemically treated. It was desired to chemically treat the primary side before before but it took so long that sediment was found (things started to grow).

Entry  Thursday, May 23, 2013, 14:08, Bevan Moss, Conditioning Station, Standard Operation, TM4, Ta #40, Turbo Pumps on 

 The turbo pumps have been turned on and are running

Entry  Thursday, May 23, 2013, 14:07, Bevan Moss, Conditioning Station, Repair, , , Chiller Unit Repaired 

 ESC came today and "repaired" the chiller. There was something wrong with the VFD controller. The were able to get it to start and run correctly again but were not able to recreate the problem. At this point it appears that it has magically disappeared. 

Entry  Thursday, May 23, 2013, 11:14, David Wang, South Hot-Cell, Standard Operation, TM4, TA#40 , TM4 TA# 40 HS leak check at SHC 

TM4 Ta#40 HS leak check is done at SHC . No leak has been found so far. There will be  a helium pressure test on it at CS.

Entry  Thursday, May 23, 2013, 09:51, Travis Cave, Conditioning Station, Standard Operation, TM4, Ta#40, module move 

TM#4 with Ta#40 has been moved from the south hot cell to the conditioning station.

Entry  Wednesday, May 22, 2013, 14:11, chad fisher, South Hot-Cell, Standard Operation, TM4, Ta#40, Ta#40 installed 

Ta#40 has been installed.

Leak checking and high voltage tomorrow before the move.

Entry  Wednesday, May 22, 2013, 10:41, Travis Cave, South Hot-Cell, Standard Operation, TM4, SiC#28 (RFQ Target), module move 

TM#4 with SiC#28 has been moved from the south west silo to the south hot cell.

Entry  Tuesday, May 21, 2013, 11:52, Bevan Moss, Conditioning Station, Standard Operation, TM3, No Source Tray, May 16th Long HV conditioning 16052013_TM3_long_HV_conditioning.xlsx

On May 16th 2013 the module was HV conditioned all day. As a result the maximum stable voltage has been increased to about 47kV (~4kV more than last test). A maximum voltage of 49kV was achieved but the module was very unstable. Attached is the data from the testing. Note that occasionally the sparking caused the PS to reset, it was turned back on and the voltage increased back to what it was (or lower) quickly.

Entry  Tuesday, May 21, 2013, 11:38, Travis Cave, ITE, Standard Operation, TM4, SiC#28 (RFQ Target), module move 

TM#3 with SiC#28 (RFQ Target) has been moved from the east target station to the south west silo.

Entry  Friday, May 17, 2013, 12:02, Travis Cave, Conditioning Station, Standard Operation, TM3, , module move 

TM#3 with no target or source trays has been moved from the conditioning station to the NE silo.

Entry  Friday, May 17, 2013, 10:04, chad fisher, South Hot-Cell, Repair, , , Manipulator Repair 

Manipulator has been sucessfully repaired. Recieved 0.19 mSv. Took Approx. 10-20 minutes

Entry  Wednesday, May 15, 2013, 18:12, Bevan Moss, Conditioning Station, Standard Operation, TM3, No source tray, HV test repeat 15052013_TM3_HV_test_repeat.xlsx

 After discussion with Friedhelm it was decided to continue trying to condition the module today before moving it tomorrow. The voltage was quickly raised until 40 kV where it was left for ~30 minutes. Sparking was minimal. It was then slowly raised to 44.3 kV it held this voltage for ~8 minutes when the current started to climb (remained below 200uA as set as a limit in previous tesing). There was also sparking at this point. This continued for ~2.5 minutes until once again the water resistivity sensor tripped again. It appears that there is a~ 44kV limit on TM3. Attached is the data. I will present all of the data to the group tomorrow showing the results of multiple testing.

 

 

Entry  Wednesday, May 15, 2013, 17:32, Bevan Moss, Conditioning Station, Standard Operation, TM3, , TM3 in place but not connected 15052013_TM3_in_place_but_not_connected.xlsx

 To confirm that the sparking was coming from the module rather than the conditioning station TM3 was grounded and the conditioning station biased. Attached are the results. Highlights include that there was no sparking and the station was able to achieve 60kV (limited by controls from going higher). The current from the raw file has been corrected by the required factor of 5.

Entry  Wednesday, May 15, 2013, 16:51, Bevan Moss, Conditioning Station, Standard Operation, TM3, No Source Tray, Repeat of HV Test 150502013_TM3_No_Source_Tray.xlsx

 The HV test completed on Monday was repeated today over a much longer time period. By taking longer there was slightly less sparking but once again a maximum voltage of ~44kV was achieved. The  resistivity of the water was much higher during this run so the leakage current was less but still in the >100 uA range. The spark that occurred during the ramp up to the maximum voltage caused the "water resistivity" limit to trip. This was a feed back through the control not the actual water changing as it recovered instantaneously. 

Entry  Wednesday, May 15, 2013, 16:21, Bevan Moss, Conditioning Station, Repair, , , BIAS Current readings off by a factor of 5 

 A special thanks to Kazuya, Jane and Ray who jumped on this issue right away! The limit of the BIAS PS was set as 20000uA when in reality it is 4000uA. The issue has now been corrected. Please remember to divide the current by 5 for any elogs older than this one.

Entry  Wednesday, May 15, 2013, 10:25, Bevan Moss, Conditioning Station, Repair, , , ONICON flow meter 

 Scott Adair from Riada sales came to site to complete diagnostics on the ONICON flow meter. He could not determine the problem and believes that there was a short in the head. He has taken the flow meter for what should be warranty repair. The flow meter is for diagnostics only, the conditioning station can still operate without it.

 

 

Entry  Wednesday, May 15, 2013, 10:20, Bevan Moss, Conditioning Station, Repair, , , Roof top chiller failed 

I have been getting a fault on the roof top chiller for the 2 tandem 7.5 ton chillers. I have checked and we have water flow and the temperatures are nowhere near freezing. I believe they are over heating as the fans on that side are not coming on. The blades are free to turn by hand but the VFD controller keeps saying off. I have tried turning it on and off and that also did nothing. I have contacted ESC for further advice.

Entry  Wednesday, May 15, 2013, 10:17, Bevan Moss, Conditioning Station, Standard Operation, TM3, No Source Tray, Preliminary Results from HV testing module_hv_test_0KV.rgaMODULE_hv_test_42kv.rgaTM3_13052013_no_source_tray.xlsx

 Testing on TM3 without a source tray was completed on 13/05.2013. All items were tied to common and the water blocks were left open at the bottom of the module. They were left with the quick connections at the top. The vacuum was in the low 10^-6T range so this was deemed acceptable. The cooling lines withing the cage in the target hall were shorted so flow could continue. As you will see from the results a maximum of 44kV was achieved before a major spark turned the power supply off. I will be compiling all the the data so it can be compared. Also attached is the archiver data, strip tool data, and RGA data.

Entry  Wednesday, May 15, 2013, 10:00, David Wang, ITE, Standard Operation, TM4, , Disconnected TM4 in ITE. 

HS had been purged. The ITE is under venting. The TM4 will be moved to SH on next Tuesday which is May 21th.

Entry  Tuesday, April 23, 2013, 11:19, Bevan Moss, Conditioning Station, Standard Operation, TM3, N/A, HV Test All common TM3_40kV_22042013.txt22042013_TM3_40kV_Archiver.csvRGA_files.zip

 A HV test was conducted yesterday on TM3. There was no target and all items were tied to common or ground. The conductivity of the water ranged from 7.1 to 7.5 Mohm. 40kV @ ~600uA without continuous sparking was achieved. The Strip tool was run but something went wrong with the export and the vacuum gauge data is missing. I have attached the file for reference and the pulled data from the achiver (only logs every 300 seconds). RGA scans were taken periodically during the test nothing unexpected was measured but we also do not know what normal looks like. The RGA application is available at http://www.thinksrs.com/downloads/soft.htm. Other items of note include significant sparks disrupts the communication between the computer and the RGA, the PNG1 gauge and its controller, and TP2 local readout screen. 

    Reply  Monday, May 13, 2013, 15:10, Bevan Moss, Conditioning Station, Standard Operation, TM3, N/A, HV Test All common TM3_40kV_22042013.xlsx

Bevan Moss wrote:

 A HV test was conducted yesterday on TM3. There was no target and all items were tied to common or ground. The conductivity of the water ranged from 7.1 to 7.5 Mohm. 40kV @ ~600uA without continuous sparking was achieved. The Strip tool was run but something went wrong with the export and the vacuum gauge data is missing. I have attached the file for reference and the pulled data from the achiver (only logs every 300 seconds). RGA scans were taken periodically during the test nothing unexpected was measured but we also do not know what normal looks like. The RGA application is available at http://www.thinksrs.com/downloads/soft.htm. Other items of note include significant sparks disrupts the communication between the computer and the RGA, the PNG1 gauge and its controller, and TP2 local readout screen. 

 Data has been put into and excel spread sheet

Entry  Tuesday, April 23, 2013, 13:48, Bevan Moss, Conditioning Station, Standard Operation, TM3, N/A, EL testing 23042013_TM3_EL_RGA.zip23042013_TM3_EL_39.csv

This morning the Einzel Lens was tested on TM3 as the intention is to reuse this piece of equipment. The EL was able to achieve 39.9kV at ~1.35mA before a major spark happened and the power supply turned off. Also during testing the penning gauge suddenly shot up after a spark, it did not recover and had been acting strange in previous test, it was decided to ignore its value and continue testing but it should be replaced in the future. When I went to save the strip tool data I tried to save it as SDDS binary data out of curiosity and the tool crashed, it turns out this is on old feature and doesn't work anymore. A file was created but I cannot recover any of the data. If I do manage to do so I will will attach it later. Attached is the RGA and Archiver data. 

Other items of note:

Voltage was increased in 1000V increments until ~32kV when it started to have sparks. Increases were then reduced to 500V until 38kV when it sparked and further reduced to 100V increments where it worked until 39.9kV

There is a inline and ballast resistor on the EL circuit values of each respectively are 145Kohm and 200 Mohm

The rga application is available at
http://www.thinksrs.com/downloads/soft.htm

    Reply  Monday, May 13, 2013, 14:59, Bevan Moss, Conditioning Station, Standard Operation, TM3, N/A, EL testing TM3_EL_39.9kV_23042013.txt

Bevan Moss wrote:

This morning the Einzel Lens was tested on TM3 as the intention is to reuse this piece of equipment. The EL was able to achieve 39.9kV at ~1.35mA before a major spark happened and the power supply turned off. Also during testing the penning gauge suddenly shot up after a spark, it did not recover and had been acting strange in previous test, it was decided to ignore its value and continue testing but it should be replaced in the future. When I went to save the strip tool data I tried to save it as SDDS binary data out of curiosity and the tool crashed, it turns out this is on old feature and doesn't work anymore. A file was created but I cannot recover any of the data. If I do manage to do so I will will attach it later. Attached is the RGA and Archiver data. 

Other items of note:

Voltage was increased in 1000V increments until ~32kV when it started to have sparks. Increases were then reduced to 500V until 38kV when it sparked and further reduced to 100V increments where it worked until 39.9kV

There is a inline and ballast resistor on the EL circuit values of each respectively are 145Kohm and 200 Mohm

 

The rga application is available at
http://www.thinksrs.com/downloads/soft.htm

 

 The lost Binary file. Binary files are no longer used and cause the the tool to crash. The option has not been removed from the strip tool users are just supposed to know not to use it.

Entry  Friday, May 10, 2013, 14:05, Bevan Moss, Conditioning Station, Standard Operation, TM3, No Source Tray, Turbo Pumps On 

The turbo pumps are on. TP1 and TP2 once again timed out and had to be restarted before they would stay on.

Entry  Friday, May 10, 2013, 11:28, Bevan Moss, Conditioning Station, Standard Operation, TM3, No Source Tray, Roughing Started 

 Roughing on TM3 was started at 11:26am today

Entry  Friday, May 10, 2013, 11:11, Travis Cave, South Hot-Cell, Standard Operation, TM3, no target, Electrical check TM#3_elec_chk_no_tgt_no_tray.PDF

TM#3 electrical check with no target and no source tray, see pdf.

Entry  Friday, May 10, 2013, 11:02, Travis Cave, South Hot-Cell, Standard Operation, TM3, no target, module move 

TM#3 with no target and no source tray has been moved from the south hot cell to the conditioning station.

Entry  Friday, May 10, 2013, 09:26, chad fisher, South Hot-Cell, Repair, TM3, , Containment box reinstalled IMG_1062[1].JPGIMG_1063[1].JPG

the containment box has been reinstalled onto TM3. After electrical checks it is ready to move to the conditioning station...for electrical tests.

Entry  Thursday, May 09, 2013, 14:23, chad fisher, South Hot-Cell, Repair, TM3, , Water Block Jig Removal IMG_1059[1].JPG

The source tray side of the water block jig has been removed in preparation for moving the module to the  conditioning station for electrical tests.

Entry  Thursday, May 09, 2013, 10:13, chad fisher, South Hot-Cell, Development, , , Mock-up Progress IMG_1056[1].JPGIMG_1057[1].JPGIMG_1058[1].JPG

The source tray for the mock-up has been setup for waterline bending and soldering/brazing.

Thanks to Travis for finding the photos for the TM3 rebuild that took place in the anteroom in 09' and Maico and Dan for the support in ironing the issues with the source tray side soldering issues.

 

Entry  Wednesday, May 08, 2013, 13:48, chad fisher, South Hot-Cell, Repair, TM3, , IMG wiring check 

Checks of the wiring for the IMG are complete and have passed.

Entry  Wednesday, May 08, 2013, 10:12, chad fisher, South Hot-Cell, Repair, TM3, , TM3 9 pin wiring removal IMG_1055[1].JPG

The 9 pin wiring has successfully been removed from TM3.

Entry  Tuesday, May 07, 2013, 12:07, David Wang, ITW, Standard Operation, TM1, , I moved 5 shielding blocks from ITE to ITW. 

Water interlock check  on ITW is done. All water signals are strong on EL panel.  ITW is configured to take proton beam.

Entry  Monday, May 06, 2013, 15:45, Bevan Moss, Conditioning Station, Repair, TM3, , 55 pin connector removed 20130506_55_pin_conector_removal_IMG_3530.JPG20130506_55_pin_conector_removal_IMG_3525.JPG20130506_55_pin_conector_removal_IMG_3532.JPG20130506_55_pin_conector_removal_IMG_3535.JPG

Travis and I removed the 55 pin connector from the service cap today. The feed through was left in place as a new design for the replacement has yet to be designed. It was not possible to test if the cables could be pulled easily as I believe there is still 1 cable tie in the containment box. The wires were cut flush with the top of the copper tube in case Chad cannot remove them via the hot cell. Other items removed include several cable ties and a clamp used to hold a cable tie. The side panels on the service cap we difficult to remove so copper never sieze was added when they were re-installed.  I have attached some pictures from before and after a complete record can be found in the TM3 docushare folder.

Entry  Friday, May 03, 2013, 09:53, chad fisher, South Hot-Cell, Repair, TM3, , 9 pin connector wiring IMG_1047[1].JPGIMG_1048[1].JPGIMG_1050[1].JPG

With the aid of nic new manipulator snap fingers made by Maico the peek cable ties restraining the 9 pin connector wiring to the gas lines have been cut.

Entry  Thursday, May 02, 2013, 10:09, chad fisher, South Hot-Cell, Repair, TM3, , Service tray water block leak check 

David and I preformed a helium leak check on the service tray waterblocks and verify that no damage had been done during jig installation. All 14 circuits were checked and verified to be ok except circuit E and circuit I which were unstable when helium was applied. The resonse time on E and I would suggest that it is an issue with the bungs that were used and not the braze joint however.

Entry  Tuesday, April 30, 2013, 07:51, chad fisher, South Hot-Cell, Repair, TM3, , Coil line flow check 

David and I checked circuits p and q (the water cooled coil ciruit) for flow this morning as, with the source tray still in the module, there was both a leak and a leak tight blockage. Both p and q allowed air flow through them confirming that the blockage was in the surce tray side of the system.

The heat shield circuit was also tested for flow and it passed.

Entry  Tuesday, April 30, 2013, 07:47, chad fisher, South Hot-Cell, Repair, TM3, , TM3 Source Tray Removal IMG_1043[1].JPG

The source tray has sucessfully been removed from TM3.

I will put a report in the TM3 rev 3 docushare directory as there were some items of note during this procedure.

Entry  Monday, April 29, 2013, 15:58, Bevan Moss, South Hot-Cell, Repair, TM3, , Source Tray Removal 20130429_TM3_SOURCE_TRAY_REMOVAL_IMG_0620.JPG

Chad removed the source tray from TM3  today, see attached picture (video was also taken). There was some interference between the window cooling lines and the frame work as well as the clamps for the ground electrode and the water block alignment jig. There was also interference between the optics alignment post (specifically the mushroom top) and the water block alignment jig. Investigation into these inferences needs to be completed as they could cause trouble for the insertion of the new source tray and alignment of the copper lines. During removal it was easy to bend copper tubes out of the way but this clearly would not work during installation.

Entry  Friday, April 26, 2013, 14:31, chad fisher, South Hot-Cell, Repair, TM3, , TM3 refurb E.O.D. IMG_1039.JPG

Service tray side of the waterblock jig is installed and all locking tabs enagaed save the heat shield circuit. Locking tab for heat shield circuit with be worked on Monday morning and installation of the source tray side of the waterblock jig should commence on monday as well.

Entry  Friday, April 26, 2013, 11:20, chad fisher, South Hot-Cell, Repair, TM3, , Water Block Jig (back half) 

The back half of the water block jig (services tray side) has been sucessfully located onto the module.

About 50% of the waterblocks have centered themselfs it their respective cups and the rest look good for concentricity but will require some gentle wiggling to get them to seat.

Entry  Wednesday, April 24, 2013, 14:09, chad fisher, South Hot-Cell, Repair, TM3, , TM3 Refurbishment E.O.D.  

Optics tray has been removed from module.

Waterblock jig installation has commenced. Of note, jig installation on TM3 has proven more dificult than the previous installation on TM2. Many of the waterblock assemblies are skewed (not perpendicular to plane that they should be...perpendicular to).

As I am away tomorrow, jig installation willl continue on Friday. With the source tray hopefully being removed on Monday.

Entry  Wednesday, April 24, 2013, 11:48, chad fisher, South Hot-Cell, Repair, TM3, , TM3 Source Tray Removal 

Work on TM3 source tray removal started at 10:40 am today.

The containment box has been removed, and disconnection of the optics tray is 90 complete.

 

Pictures can be found in the April Refurb Work Folder in the tm3 rev3 refurb pictures folder.

Entry  Wednesday, April 24, 2013, 10:36, maicodallavalle, Spent Target Vault, Maintenance, , , F-308 

The F-308's have been serviced and are ready to be filled. All inspection records are stored  in docushare.

https://documents.triumf.ca/docushare/dsweb/View/Collection-1085
Entry  Wednesday, April 24, 2013, 10:14, Travis Cave, South Hot-Cell, Standard Operation, TM3, no target, module move 

TM#3 has been moved from the conditioning station to the south hot cell, move went well.

Entry  Wednesday, April 24, 2013, 09:00, Bevan Moss, Conditioning Station, Development, , , New user testing 

 Controls has created a new user group that can operate the conditioning station but cannot use any of the bypasses or forces. The cooling package will be used to test this new profile. The main loop bypass has been opened to allow this testing to happen without the risk of over pressure.

Entry  Tuesday, April 23, 2013, 16:11, Bevan Moss, Conditioning Station, Maintenance, TM3, N/A, Chiller Fault 2 

 During Testing it was noticed that Fault 2 was indicated and one of the compressors would not run. Fault 2 does not indicate what the issue was and during inspection nothing could be detected. It had something to do with TCS:CHILCP3 and possibly CP2. CP1 could still be operated and was controlled manually to keep the temperature in the correct range. This was not required but it does affect the conductivity. The main power switch on the chiller unit was turned on and off and the fault was cleared. As far as I know this indicated either a freeze protect, flow, or refrigerant pressure fault. I will ask for TCS:TS6 and TCS:DIF2 to be added to the archiver so this can be further investigated in the future.

Entry  Tuesday, April 23, 2013, 15:59, Bevan Moss, Conditioning Station, Standard Operation, TM3, N/A, Systems off 

 Both the Cooling Package and Vacuum have been turned off in preparation for the module move tomorrow

Entry  Tuesday, April 23, 2013, 15:52, Bevan Moss, Conditioning Station, Standard Operation, TM3, N/A, Further HV Testing TM3_BIAS_EE_CB_23042013.xlsxTM3_BIA_EE_CD_23042013_RGA_files.zip

 Further HV testing was completed today from ~2:00 until 3:00. The resistivity of the water was 11.7 - 12.7 Mohm. The EE was turned on to 1500 V and had a leakage current of 1.465 mA with a inline and ballast resister of 20 kohm and 1 Mohm respectively. In addition to this all of the CB were turned on to 500V. The voltage on the source tray with all bias items tied together and the voltage was then raised to 30kV in 5kV steps. It was then raised until 37kV in 1kV step at which point the first spark was detected. Steps were then reduced to 500V until 39.5kV was achieved. Sparking was noticed when stepping up from one voltage to the next and steps were reduced to 100V. At 39.7 kV there were several sparks and the voltage was held for 8 minutes until there had been at least 4 minutes since the last spark. Voltage was increased to 41.2 kV at 292.97 uA when a spark caused the HVCLTBHT paddle wheel flow sensor to trip. Flow was affected but the interlock was tripped due to noise and as a result the BIAS and EE voltage dropped to zero. At this point the required data had been collected and it was decided to shut the station down. RGA scans were taken during the test and are attached. The edited data with graphs is attached in the excel folder. PNG1 was not monitored as it has failed.

 

The rga application is available at
http://www.thinksrs.com/downloads/soft.htm

 

 

 

Entry  Monday, April 22, 2013, 11:35, Bevan Moss, Conditioning Station, Repair, TM3, N/A, TCS:DIF2 broken 

 The flow meter on the primary side (TCS:DIF2) of the conditioning station is broken. I investigated and there is flow, the gauge is not fouled, and the PLC does read back when current supplied. The gauge is also reciving 24V but the output is 0V and 0mA. I will contact ESC and the supplier.

Entry  Monday, April 22, 2013, 11:31, Bevan Moss, Conditioning Station, Standard Operation, TM3, N/A, Cooling Package Started 

 Cooling Package was started at 9:25 this morning inlet conductivity is 0.08 Mohm at 22.9C. Resistance reached 5.33 Mohm by 11:30

Entry  Monday, April 22, 2013, 09:33, David Wang, Conditioning Station, Repair, TM3, , Leak check TM3 at conditioning station 

TM3 leak check at conditioning station without target: TM3 all air to vacuum seals have been leak checked . They are all good. Water lines TAR(+-), TUBE(+-), GAS, MSP , COIL2(+-), EE, HS(1,2) , GE,and WINDOW have been helium pressurized to 70 psi for 2 minutes each . No response had been found on leak detector. They are leak tight.. Leak detector BR 0.0xE-9atm.cc/sec, BP 0.0xE-4 torr. TM3 and CS vacuum: PNG15.2xE-6 torr, IG1 8.8xE-7 torr,IG2 2.8xE-6torr, IG1S 1.3xE-6 torr.      

Entry  Friday, April 19, 2013, 13:32, Bevan Moss, Conditioning Station, Standard Operation, TM3, N/A, Turbo Pumps Started 

 Both Turbo Pumps are now operational.

    Reply  Friday, April 19, 2013, 15:25, Bevan Moss, Conditioning Station, Standard Operation, TM3, N/A, Turbo Pumps Started 

Bevan Moss wrote:

 Both Turbo Pumps are now operational.

 Turbo pumps 1 and 2 both found randomly off, have been restarted

Entry  Friday, April 19, 2013, 10:51, Bevan Moss, Conditioning Station, Standard Operation, TM3, N/A, Roughing Started 10:48 

With the Turbo pump replaced I have started roughing at 10:48

Entry  Friday, April 19, 2013, 10:48, Bevan Moss, Conditioning Station, Maintenance, TM3, N/A, Turbo Pump 2 replaced 

 Turbo Pump 2 has been replaced on TM3. I got a count of 350 on the sleeve of my tank suit.

Entry  Friday, April 19, 2013, 10:48, Bevan Moss, Conditioning Station, Maintenance, TM3, N/A, Turbo Pump 2 replaced 

 Turbo Pump 2 has been replaced on TM3. I got a count of 350 on the sleeve of my tank suit.

Entry  Wednesday, April 17, 2013, 15:17, Bevan Moss, Conditioning Station, Standard Operation, TM3, N/A, Turbo Pumps Failed 

 Both Turbo pumps on TM3 have failed. They were both attempted to start in soft mode. TP2 could only achieve ~19kpm and TP1 ~10kpm. I have turned off the scroll pump and vented through the turbo pumps.

Entry  Wednesday, April 17, 2013, 10:59, Travis Cave, Conditioning Station, Standard Operation, TM3, no target, module move 

TM#3 with no target has been moved from the south hot cell to the conditioning station. Move went well. The fields around the module was 1.6mSv/hr.

Entry  Wednesday, April 17, 2013, 10:35, David Wang, ITE, Standard Operation, TM4, , I moved 5 shielding blocks back to ITE. 

5 shielding block had been moved  back to ITE. The ITE is configured to take proton beam.

Entry  Wednesday, April 17, 2013, 09:26, Travis Cave, South Hot-Cell, Standard Operation, TM3, no target, Electrical check TM3_DLB_9_PIN_CONN_ID_and_CHK.PDFTM3_Elec_CHK_no_target.PDF

Electrical check was performed on TM#3 with no target nothing was wrong was found, but our megger does not go above 1000 volts so any problems above this value would not be seen, see attached pdf for details.

Also the 55 pin(top) double 9 pin (bottom) connector was tested as well. When it was meggered to 60kV common more then 50% of the lines failed, when those line were identified with a resistance package two were unable to be indentified. The wiring for this double 9 pin connector should be removed to prevent HV problems. New wiring is not physically possible to re-install in its place, see the PDF for the wiring details.

Entry  Wednesday, April 17, 2013, 09:02, chad fisher, South Hot-Cell, Repair, TM3, , TM3 ready for conditioning station 

The heat shield circuit blank offs have been re-installed and front cover replaced. TM3 is ready to move to the conditioning station for testing.

Entry  Tuesday, April 16, 2013, 11:20, chad fisher, South Hot-Cell, Repair, TM3, , TM3 Referb. start IMG_3523.JPGIMG_3524.JPG

Front containment box cover has been removed and heat shield circuit blank offs removed in preparation for installation of dummy target.

 image #1 - initail view after front panel removal.

image #2 - Heat shield circuit blank offs removed.

Ready for baseline electrical tests and 9 pin cinnector tests.

Entry  Tuesday, April 16, 2013, 11:10, Travis Cave, South Hot-Cell, Standard Operation, TM3, no target, module move 

TM#3 has been moved from the NE Silo to the south hot cell, move went well.

Entry  Monday, April 15, 2013, 11:00, chad fisher, South Hot-Cell, Standard Operation, TM3, , Items for TM3 dummy target installation 

New gaskets and fasteners have been inserted into the south hot cell in preparation for installing the dummy target onto TM3 tomorrow.

Entry  Friday, April 12, 2013, 10:32, David Wang, ITW, Repair, TM1, , ITW EXIT1 tank to module o-ring leak check. 

I leak checked new installed ITW EXIT1 tank to module o-ring.No leak had been found . Also ,TM1 primary vessel air to vacuum seals had been checked at the same time. There was no response had been found on leak detector.

Entry  Friday, April 12, 2013, 10:27, David Wang, ITW, Standard Operation, TM1, , I reconnected TM1 to ITW. 

TM1 has been reconnected in ITW. Water interlock check for TM1 is done.

Entry  Thursday, April 11, 2013, 07:18, David Wang, Conditioning Station, Maintenance, TM1, Ta#29, helium pressure tested all water lines in TM1 at CS 

On April 08th, all water lines in TM1 had been helium pressure tested(70psi) at conditioning station. No leak had been found.

Entry  Tuesday, April 09, 2013, 09:06, Travis Cave, Conditioning Station, Standard Operation, TM1, Ta#39, Electrical check TM1_Ta39_CS_ELEC_CHK3.PDFTM1_Ta39_CS_ELEC_CHK4.PDFTM1_Ta39_CS_ELEC_CHK5.PDF

TM#1 with Ta#39 has not passed it electrical check again, while sitting at the conditioning station at air. The readings have not been consistant. See the current PDF for details.

 

TM#1 with Ta#39 electrical check at the target station see attached PDF (CHK 4).(April 9th 2013) PASSED

TM#1 with Ta#39 electrical check at the target station see attached PDF (CHK 5).(April 10th 2013) PASSED

Entry  Monday, April 08, 2013, 16:16, Bevan Moss, Conditioning Station, Standard Operation, TM1, Ta #39, Venting with Argon 

 TM1 started venting at 4:15 pm with Argon. I will leave the valve open over night.

Entry  Monday, April 08, 2013, 12:10, Travis Cave, Conditioning Station, Standard Operation, TM1, Ta#39, Electrical check TM1_Ta39_CS_ELEC_CHK2.PDF

TM#1 with Ta#39 had the electrical check done on it again it passed, changes this time were the water lines were purged and it was under a better then roughing vacuum. See the attached pdf for details.

Entry  Monday, April 08, 2013, 09:01, Travis Cave, Conditioning Station, Standard Operation, TM1, Ta#39, Electrical check TM1_Ta39_CS_ELEC_CHK.PDF

TM#1 with Ta#39 at the conditioning station, has failed its electrical test see attached pdf for details. Also while setting up for the electrical test one of the high powered flexible connectors popped out its crimp and another is working it out its crimp.

Entry  Thursday, April 04, 2013, 12:07, Bevan Moss, Conditioning Station, Standard Operation, TM1, Ta #39, Roughing started 

 Roughing started at 12:06. It was believed there was a problem with the compressed air but there was none, TM1 doesn't leak and so you cannot hear that the connection is made.

    Reply  Thursday, April 04, 2013, 14:31, Bevan Moss, Conditioning Station, Standard Operation, TM1, Ta #39, Roughing started 

Bevan Moss wrote:

 Roughing started at 12:06. It was believed there was a problem with the compressed air but there was none, TM1 doesn't leak and so you cannot hear that the connection is made.

 Roughing stopped as the module and cover requires modifications that require the vacuum to be opened.

Entry  Thursday, April 04, 2013, 11:06, Travis Cave, South Hot-Cell, Standard Operation, TM1, Ta#39, module move 

TM#1 with Ta#39 has been moved from the south hot cell to the conditioning station move went well.

Entry  Wednesday, April 03, 2013, 14:39, Travis Cave, South Hot-Cell, Standard Operation, TM1, Ta#39, Electrical check TM1_Ta39_SHC_ELEC_CHK.PDF

Electrical check on TM#1 with Ta#39 installed at the south hot cell. Target passed the electrical checks, see attached pdf for details.

Entry  Wednesday, April 03, 2013, 13:28, chad fisher, South Hot-Cell, Standard Operation, TM1, Ta#39, Ta#39 installed 

Ta#39 has been installed onto TM1.

Entry  Wednesday, April 03, 2013, 12:26, David Wang, ITE, Maintenance, TM4, Sic LIS/RFQ, Leak check on ITE TM4. 

TM 4 had been leak check in ITE due to   relatively high PNG1 and IG1 readings.All TM4 primary and secondary  vessel air to vacuum seals had been leak checked. All water lines in TM4 had been helium pressured . There is no leak had been found so far.

Entry  Wednesday, April 03, 2013, 10:59, Travis Cave, South Hot-Cell, Standard Operation, TM1, no target, module move 

TM#1 has been moved from the south west silo to the south hot cell, move went well.

Entry  Tuesday, April 02, 2013, 10:07, chad fisher, South Hot-Cell, Standard Operation, TM1, Ta#39, Ta#39 inserted into hot cell 

Ta#39 has been inserted into the hot cell in preparation for TM1 target change.

Entry  Wednesday, March 27, 2013, 12:08, David Wang, South Hot-Cell, Standard Operation, TM4, Sic LIS-RFQ, TM4 heat shield circuit leak check with SiC LIS-RFQ target 

Chad and I did the TM4 heat shield leak check yesterday at SHC. The leak detector was pumped to 4.6 xE-9atm.cc/sec, and 0.0xE-4 torr after 1.5 hours pumping. Chad sprayed helium twice on both VCR fittings. There is no response had been found during each 45 seconds waiting time. Since the module moved to ITE directly,we didnt have helium pressure test this time. I  would say thee heat shield circuit is leak tight. so far.

Entry  Wednesday, March 27, 2013, 11:49, David Wang, ITE, Standard Operation, TM4, Sic LIS-RFQ , Connected TM4 in ITE 

TM4 has been reconnected to ITE after the module moving. The roughing is started . The water will be supplied to ITE after  testing  the water  pumps . The water interlock check will be done on next week also.

Entry  Wednesday, March 27, 2013, 10:44, Travis Cave, ITE, Standard Operation, TM4, SiC#28 (RFQ Target), module move 

TM#4 with SiC#28 has been moved from the south hot cell to the east target station move went well.

Entry  Tuesday, March 26, 2013, 14:17, Travis Cave, South Hot-Cell, Standard Operation, TM4, SiC#28 (RFQ Target), Electrical check TM4_SiC28_RFQ_SHC_ELEC_CHK.PDF

Electrical check of TM#4 SiC#28 (RFQ Target) has been completed. It passed the standard electrical checks for the target part, but the electrical check for the RFQ part is suspect, see the attached PDF for the details.

Entry  Monday, March 25, 2013, 14:19, Travis Cave, Conditioning Station, Standard Operation, TM4, CS Test Target #1, module move 

TM#4 with the CS Test target has been moved from the conditioning station to the south hot cell. Move went well.

Entry  Saturday, March 23, 2013, 18:14, Aurelia Laxdal, Conditioning Station, Development, TM4, FEBIAD HP with Dummy Target, Commissioning TCS - Part 2 Completed 

After few hickups the TCS was successfuly commissioned.

In the morning, in the middle of the heaters conditioning: 360A/250A for the TGHT/TBHT, the target heater PS tripped and it didn't recover immediately.  I cannot tell if the card is still OK. Before this even, there were few bias current sparks created when the ionized tube was raised above 250A; this also tripped the Einzel lens. Re-started the Heaters, and did the conditioning with the rest (HV, Optics) Off. After the heaters were at nominal values, raised the rest: HV to 30kV and the Optics. And everything held fine. The current on the FC was 3micro-Amperes. The water temperature levels stayed below 25 deg Celsius.

The problems that need to be fixed:

1. The biggest problem was created by the target power supply: the new card is not calibrated, the voltage is not regulating, but the main problem is the grounding of the output of power supply. Friedhelm measured 0.2V across the return and the cage (200mili-ohms resistance) .  This was probably overlooked.

2. The Auto-ramping routine didn't work. Controls would need to fix this.

3. The RGA didn't want to connect from the account Don created for me. So, we have only a RGA scan taken on Friday by Don, when the target was cold.

 

    Reply  Monday, March 25, 2013, 10:59, Bevan Moss, Conditioning Station, Development, TM4, FEBIAD HP with Dummy Target, Commissioning TCS - Part 2 Completed IRH1511.pdfISK4574D-rev7.pdf

Aurelia Laxdal wrote:

After few hickups the TCS was successfuly commissioned.

In the morning, in the middle of the heaters conditioning: 360A/250A for the TGHT/TBHT, the target heater PS tripped and it didn't recover immediately.  I cannot tell if the card is still OK. Before this even, there were few bias current sparks created when the ionized tube was raised above 250A; this also tripped the Einzel lens. Re-started the Heaters, and did the conditioning with the rest (HV, Optics) Off. After the heaters were at nominal values, raised the rest: HV to 30kV and the Optics. And everything held fine. The current on the FC was 3micro-Amperes. The water temperature levels stayed below 25 deg Celsius.

The problems that need to be fixed:

1. The biggest problem was created by the target power supply: the new card is not calibrated, the voltage is not regulating, but the main problem is the grounding of the output of power supply. Friedhelm measured 0.2V across the return and the cage (200mili-ohms resistance) .  This was probably overlooked.

2. The Auto-ramping routine didn't work. Controls would need to fix this.

3. The RGA didn't want to connect from the account Don created for me. So, we have only a RGA scan taken on Friday by Don, when the target was cold.

 

 Response to item 1. 

This morning I investigated the output of the TGHT power supply. The negative output of the power supply is tied to common as per ISK4574D Rev 7 (attached) and the released drawing IRH1511 Rev A (PDF attached but officially located in the SW vault). If this is not the intent of the IRH1511 should be released to Rev C reflecting the desired configuration. 

 In regards to the calibration of the card I will inform the PS group. 

Entry  Monday, March 25, 2013, 09:35, Bevan Moss, Conditioning Station, Standard Operation, TM4, CS Test Target #1, Cooling Package and Vacuum Stopped 

 The cooling package and vacuum was stopped today at 9:26 so the module can be move.

Entry  Friday, March 22, 2013, 18:49, Aurelia Laxdal, Conditioning Station, Development, TM4, FEBIAD HP with Dummy Target, Commissioning TCS - Part 1 

Today, the commissioning of the TCS went well. The water/vacuum interlocks were checked OK. Then, the TCS was HV conditioned up to 33kV.

Tomorrow, the heaters will be ramped up.

Entry  Wednesday, March 20, 2013, 08:19, David Wang, Conditioning Station, Repair, TM4, , Leak check new installed TM4 TP1 at conditioning station. 

I leak checked new installed TM4 TP1 at conditioning station. The CS vacuum gauges reading were at 1.0-1.5xE-6 torr . Leak detector base leak rate 0.0xe-9atm.cc/sec, base pressure 0.0xe-4torr. I sprayed helium around the pump  inlet flange and KF 25 pump outlet flange to pump joint. There is no response on leak detector. The new installed TP1 is leak tight.

Entry  Tuesday, March 19, 2013, 13:49, Bevan Moss, Conditioning Station, Standard Operation, TM4, CS Test Target #1, Tubros Started 

 Turbo Pumps have been started and are in normal operation. TP1 which has recently been replaced was started in soft start and had no issues. TP2 was started normally and tripped prior to reaching speed. It was left for a while and restarted. When restarted it was still at 17KRPM, it reached normal operation.

Entry  Tuesday, March 19, 2013, 09:55, Bevan Moss, Conditioning Station, Standard Operation, TM4, CS Test Target #1, Turbo pump 1 replaced roughing started 

 David replaced the broken turbo pump this morning and I have started roughing at 9:54.

Entry  Monday, March 18, 2013, 15:28, Bevan Moss, Conditioning Station, Standard Operation, TM4, CS Test Target #1, Vented With Argon Vented_with_Argon.JPG

 The conditioning station has been vented with argon. Time taken is not known but it is less than 3 hours. See attached picture for convectron gauge readings. CG1A is in air.

Entry  Monday, March 18, 2013, 12:39, Bevan Moss, Conditioning Station, Repair, TM4, CS Test Target #1, TGHT PS Failure IMG_0529.JPG

The Model of the Power Supply (PS) is TSQLG 480-20/1500 and serial number is 2755.02.01.01.09.

We went to test the PS and supplied the required 480V and turned the local switch to on. At this point nothing happened, the controls screen didn’t light up nothing. We tried to run the PS in remote mode as that is what it had previously been set at and again there was no response. At this point I called the electrician the check that we were in fact supplying 480V. He checked all the way to the contactor inside of the PS (see attached picture). He also checked the 3 larger fuses and 6 smaller ones, they have not failed.

I have inquired with Jens Lassen who is more familiar with these PS and he has not had this issue before. He is going to have another look at the PS with the electrician specifically checking the 24VDC for the control board. Any further information or checks you could provide would be very helpful.

 This PS is needed for commissioning of a system and unfortunately this failure has come at a very in opportune time.  Although the PS is show to be several years old we have not actually used it aside from some minor tests ie does it turn on (it has previously).  I have phoned the manufacture to determine what else can be check and what the next steps are. Werner requested that I send an email (completed) so he could give it to their engineers.

Entry  Monday, March 18, 2013, 12:03, Bevan Moss, Conditioning Station, Repair, TM4, CS Test Target #1, Turbo Pump 1 Failure and Venting 

 Over the weekend Turbo pump one failed. It was attempted to restart the turbo in soft start but that also failed. Although the Vacuum was good enough to operate both Turbos are required to pass commissioning. As such the pumps were turned off at ~10:00 today. Venting started at 12:00.

Entry  Thursday, March 14, 2013, 10:04, Bevan Moss, Conditioning Station, Standard Operation, TM4, CS Test Target 1, Cooling Package Started Cooling_system_start.JPGCooling_System_start_3_min.JPG

 The cooling package was started at 10:00 today. See attached picture. There is another snap shot at 10:03.

    Reply  Thursday, March 14, 2013, 11:56, Bevan Moss, Conditioning Station, Standard Operation, TM4, CS Test Target 1, Cooling Package Started Cooling_package_1155.JPG

Bevan Moss wrote:

 The cooling package was started at 10:00 today. See attached picture. There is another snap shot at 10:03.

 The conductivity of the cooling package is above 5Mohm which is the minimum limit for the PS. This was achieved at 11:55. See attached picture.

Entry  Thursday, March 14, 2013, 11:25, Bevan Moss, Conditioning Station, Standard Operation, TM4, CS Test Target #1, Turbos Started turbo_started_1115.JPGvacuum_running_1124.JPG

 Turbos started at 11:14. TP1S achieved full speed in less than 2 minutes. TP1 and 2 tripped at 9 minutes. Restarted and reached at speed after another 1 minute 20 seconds.

Entry  Thursday, March 14, 2013, 07:18, David Wang, South Hot-Cell, Standard Operation, TM4, , TM4 window cooling line leak check 

It took a long time(more than 1 hour)   to pump down the TM4 window  cooling line during leak check time. The base leak rate could only be pumped to 5.8xE-9 atm.cc/sec.Base pressure is 0.0xE-4 torr which is bottom reading. Chad and i did the leak check at this base leak rate .No leak had been found. The window cooling line is leak tight at this stage. A pressure helium test will be fulfilled in conditioning station on this cooling line later.

Entry  Thursday, March 14, 2013, 07:09, David Wang, South Hot-Cell, Standard Operation, TM4, , TM4 electrical test at SHC after windown and containment box back. 

TM4 electrical test at SHC after windown and containment box back is done. Everything is fine.

Entry  Wednesday, March 13, 2013, 15:26, Bevan Moss, Conditioning Station, Development, TM4, CS Test Target #1, Roughing Started 

 Roughing pumps were turned on at 15:23 13/03/2013.

Entry  Wednesday, March 13, 2013, 14:31, Bevan Moss, Conditioning Station, Standard Operation, TM4, CS Test Target #1, Module Move 

 TM4 with CS Test Target #1 was moved from the SHC to the Conditioning Station. All went well. The welding cables came a little close to the cage, David will bend them in more in the future.

Entry  Wednesday, March 13, 2013, 14:30, Bevan Moss, Conditioning Station, Development, , , Faraday Cup 

 Dave Morris and I investigated the Faraday Cup today. It was found to be plumed in the wrong direction (fails in). This is not an issue for the conditioning station as there is nothing down stream from the cup. Dave will change the controls to reflect this.

Entry  Wednesday, March 13, 2013, 11:23, chad fisher, South Hot-Cell, Repair, TM4, , Ground Electrode Leak 

The containment box has been re-installed and the window waterlines reconnected and leak checked.

The window lines did pass the leak check, however the leak dectoctor did not pump down past 5.8 x 10-9.

The front cover has also been reinstalled.

I have requested that the module have an electrical check before it moves as the containment box has been off as well as the water blocks being leak checked. Either one of these procedures could causes the water liunes and blocks to alter there position sightly which could cause as short...this is why I have requested an electrical check.

 

Entry  Wednesday, March 13, 2013, 07:22, chad fisher, South Hot-Cell, Repair, TM4, , Ground Electrode Leak / Inspection Results IMG_3449.JPGIMG_3450.JPGIMG_3451.JPGIMG_3452.JPGIMG_3454.JPG

Further attempts to localize the leak were unsucessful. The circuit was pressurized with 60 psi air and snoop solution was applied to both the braze joints and the mating surface between the two halfs of the water blocks. Unfortunately, no visible bubbles could be dectected.

This was reported to Grant and Pierre and it was decided to continue with removing one of the vcr gaskets from the optics cooling lines (on the same circuit) and replacing it with a gasket with a sector cut out to allow this circuit to be pumped out and eliminate any virtual leak type response. The feedthru at the service cap will be capped.

Areas that had snoop solution on them were rinsed with methonal.

A cursory inspection of the extraction column was preformed and some pictures of the back side of the mounting plate and surrounding area were taken as there was some interesting discoloration found in the area below the back of the 9 pin connectors.

Picutres of the snoop procedure can be found at https://documents.triumf.ca/docushare/dsweb/View/Collection-9994

 

Entry  Tuesday, March 12, 2013, 09:18, chad fisher, South Hot-Cell, Repair, TM4, , Ground Electrode Leak 

On Monday, March 11 the containment box was removed from TM4 and a vacuum leak check preformed in an attempt to locate the leak in the ground electrode circuit.

Following Pierre's work plain helium was sprayed was the highest joint accessible towards the lowest.

A two second spray of helium was applied to the first joint (the reducer from the service tray to the line that goes to the service tray side of the water block connection), no response from the leak detector after 1 minute.

 two second spray of helium was applied to the braze joint of the servive tray side of the waterblock connection; almost immediate response from the leak detector (see David Wand for actual values for leak rate).

The inital joint at the reducer was rechecked to insure the response was not just a risidual slow response from the reducer joint and confirmed by no response after 2 miniutes that it was not.

The braze joint at the service tray block was then tested again with a two second spray and again almost an imediated response.

A meeting was conveined and decided to pressurize this circuit with air and apply snoop solution to the suspect area to try to identify wether the leak is in the braze joint or possibly c-seal...This will take place on Tuesday, March 12th.

 

 

Entry  Friday, March 08, 2013, 15:50, Bevan Moss, ITE, Standard Operation, TM4, CS Test Target #1, Module Move from ITE to SHC 

 Today David and I moved the module from ITE to the SHC. Move went very smoothly, David operated the cameras and has had basic training in how to manually lock out the controls.

Entry  Wednesday, March 06, 2013, 14:12, David Wang, ITW, Repair, , , ITW EXIT1 tank to module o-ring replacement 
 ITW EXIT1 o-ring replacement is fininshed today. The ITW EXIT 1 is back to ITW. The old o-ring lost most its elastic property and changed to stiff sqaure shape inside the slot.The flange surface around the o-ring slot was dirty. I cleaned the o-ring surface completely before putting the new o-ring . Everything should be fine now. There will be a leak check late on this new installed o-ring.
Entry  Wednesday, March 06, 2013, 12:50, Travis Cave, South Hot-Cell, Maintenance, , , module move 

ITW EX1 have been moved back to the west target station from the south hot cell.

Entry  Wednesday, March 06, 2013, 10:09, Travis Cave, ITW, Maintenance, , , module move 

ITW EX1 has been moved from the west target station to the south hot cell for the seal replacement on the west station.

Entry  Friday, March 01, 2013, 11:35, David Wang, ITE, Maintenance, TM4, , Leak check on ITE and TM4. 
 The leak check on TM4 and ITE is done. All primary vacuum vessel , secondary vacuum vessel  on TM4 and ITE are leak tight. There is no any response had been found on leak detector(leak detector base LR 0.0xE-9 arm.cc/sec). All water lines had been pressurized to 70 psi helium for 3 minutes. They are all perfect leak tight( I cant find even a tiny response on leak detector) except GE water cooling line. On the GE water line, the leak detector got a instantaneous response once I applied the helium to the circuit.The leak rate climbed directly from 0.0xe-9 atm.cc/sec to 1.5 xe-5 atmcc/sec even if I stopped the helium pressurizing immediately. Once I purged the helium out of the line, the leak rate return to 0.0XE-9 atm.cc/sec quickly. I repeated the test on GE water line again and got exactly same result as the before. I would say the leak on the ITE GE water circuit isn't a small leak. The same test could be fulfilled once the TM4 is in CS later. 
Entry  Tuesday, February 26, 2013, 13:53, David Wang, Conditioning Station, Repair, TM4, , Replaced TM4 TP1 

Bevan and I replaced TM4 TP1 today at conditioning station .The pump will be started this week when I do ITE and TM4 leak check .

Entry  Tuesday, February 26, 2013, 13:24, Travis Cave, Conditioning Station, Standard Operation, TM4, CS Test Target #1, module move 

TM#4 with CS Test Target #1 (dummy target) moved from the conditioning station to the east target station. Move went well.

Entry  Tuesday, February 26, 2013, 10:26, Travis Cave, ITW, Standard Operation, TM1, , module move 

TM1 moved from the west station to the southwest silo. Move went well.

Entry  Friday, February 22, 2013, 13:13, Bevan Moss, Conditioning Station, Development, TM4, CS Test Target #1, Broken Turbo Pump IMG_0528.JPG

 Today while putting the cover on the cord that goes to the controller was bumped. This bent the connector down and caused a vacuum leak. I tried to tighten the bolts in the hope the leak would go away but it did not and I sheared one of the bolts off. David is inquiring with Edi if the pump can be repaired or if it needs to be replaced. The good news is that the interlocks work exactly as planned. Upon detecting a leak they shut the turbos down and closed all of the valves they even beat the turbo controllers for overload.

David believes we can rotate the pump slightly to avoid this problem in the future. Hopefully repairs can start on Monday. 

The conditioning station will be shut down for the weekend.

Entry  Friday, February 22, 2013, 13:02, Bevan Moss, Conditioning Station, Development, TM4, CS Test Target #1, HV test with Water vacuum_for_40k.JPG

 Hello Ray and Yi

Completed a HV test with the water flowing today.

8.96 Mohm

56.4 PSI across the load

16.5 GPM through the loads

some sparking occurred see attached file.

module was biased with all items tied to common to 40kV. Leakage current was less than 100uA.

This was a very successful test.

Entry  Thursday, February 21, 2013, 14:05, David Wang, ITW, Repair, TM1, , Disconnected EXIT1 in ITW. 

Disconnected EXIT1 in ITW. All cables , wires and air lines are label marked.

Entry  Thursday, February 14, 2013, 09:31, David Wang, ITW, Repair, , , ITH MP1 is replaced. 

Edi and I replaced the broken ITH MP1 in target hall with a new pump. The old pump was leak on oil. There were no oil had been left in the old pump by checking the sight glass.Thats the reason of  the pump  failure.The tray which the old pump sat on was full of leaking oil ( highly contaminated ). The old pump was bagged in 3 thick plastic bags ,and the tray was cleaned before the new pump was installed. The working area had been cleaned up and surveyed couple of times after the job. Everything is good. The new pump had been tested after the installation. It works fine.

Entry  Friday, February 08, 2013, 11:42, Grant Minor, ITE, Maintenance, , , TAPC 477 resolved - ISAC elec. room gas cylinder TAPC-477_resolved_8Feb2013.pdf

See attached TAPC 477 documentation.

Entry  Wednesday, February 06, 2013, 14:34, Bevan Moss, Conditioning Station, Development, TM4, CS Test Target #1, 40kV All Common w/o Water Test 40kV_no_water_HV_test.JPG

 Today the module was biased to 40kV in the conditioning station. The current draw was 0uA. Sparking started at 27 kV. I have attached the recording from the strip tool of the vacuum while we were testing. After consulting Pierre if we should take the module to a higher voltage it was decided not to. The purpose of this test we to check the interaction between the module, cover, new cooling line, EE and EINZEL cables. This test was considered a success and although there are no anticipated problems care should be taken when taking the module past 40kV for the first time.

Entry  Monday, January 28, 2013, 12:26, Travis Cave, Conditioning Station, Development, , , Switches connected 

the switches and the solenoid are all wire up to 24VDC, when you open either of the little doors the solenoid switches this is also true if there is a power loss. currently the solenoid is powered.

Entry  Thursday, January 24, 2013, 13:30, David Wang, ITW, Standard Operation, TM1, , ITW-TM1 2013 winter shut down leak check. 

2013 winter shut down ITW-TM1 primary vacuum vessel, secondary vacuum vessel, and water lines leak check: connected leak detector to TP2(primary and water lines) and TP4S (secondary). base leak rate 0.0xE-9atm.cc/sec,base pressure 0.0XE-4torr. Sprayed helium to all primary vacuum seal and there is no response on leak detector. Helium pressurized all water lines(except HS) at 70psi ,3mins.Tube heat(+) no response, tube heater(-)1.6xe-9atm.cc/sec, target oven(-)5.8xe-9atm.cc/sec, target oven (+) 6.9xe-9atm.cc/sec, EE 5.7xe-9atm.cc/sec, MSP no response, window 7.5 xe-9atm.cc/sec.All water lines are water leak free.  Two leaks had been found on secondary vacuum vessel. One is on exit 1 to tank o-ring (east side, E-N corner). The leak detector got   responses from 1.4 to1.7 xe-7 atm.cc/sec scale . The test  hadbeen repeated 4-5 times and   confirmed the location   . The second one is a small leak which  is on exit 2 to tank o-ring(east side, close to E-N corner). The leak detector got  responses from 1.4 to 1.8xe-8atm.cc/sec scale. The test had been repeated 3 times and confirmed the location. As the present plan. we will replace the exit1 to tank o-ring during this year shut down time.

Entry  Friday, January 18, 2013, 17:01, Grant Minor, Conditioning Station, Development, TM4, , Photos of the CS with TM4 (after the no-module HV test, only vacuum connected) CS_post_HV_test_w_TM4_18Jan2013_001.jpgCS_post_HV_test_w_TM4_18Jan2013_003.jpgCS_post_HV_test_w_TM4_18Jan2013_004.jpgCS_post_HV_test_w_TM4_18Jan2013_005.jpg

Attached are some photos of TM4 in the Conditioning Station after the no-module HV test completion.  Only vacuum services are connected.

Entry  Friday, January 18, 2013, 16:56, Grant Minor, Conditioning Station, Standard Operation, TM4, , VAT valve btwn roughing and nuc. vent. closed 

Bevan attempted to start pumping down on TM4 today remotely but there was an issue.  He will report on Monday.

I went into the Target Hall this afternoon while on the phone with Bevan and performed the following:

- Checked the knurled vent valves on the side of each turbo, both were found to be in the tightened position (all the way clockwise)

- Closed the VAT valve between the scroll pump and the nuclear ventilation

Entry  Friday, January 18, 2013, 11:17, David Wang, South Hot-Cell, Standard Operation, TM4, dummy target, TM4 heat shield circuit leak check with dummy target on. 

Chad and i did a leak check on TM4 heat shield circuit with installed dummy target at SHC today. The leak detector is pumped to 0.0xE-9atm.cc/sec.Chad sprayed helium twice on each  VCR joints .There is no any response had been found on the leak detector during each 45 seconds waiting time. The TM4 heat shield circuit with dummy  target is leak tight so far.  

Entry  Friday, January 18, 2013, 11:15, Travis Cave, Conditioning Station, Standard Operation, TM4, CS Test Target #1, module move 

TM#4 with the test target #1 is now in the conditioning station, move went well.

Entry  Friday, January 18, 2013, 09:10, Travis Cave, South Hot-Cell, Standard Operation, TM4, CS Test Target #1, Electrical check CS_Test_Target_#1_Elec_check.PDF

Electrical check performed on the CS Test Target #1 at the south hot cell. See PDF for details.

Entry  Thursday, January 17, 2013, 11:18, Travis Cave, South Hot-Cell, Standard Operation, TM4, , module move 

TM#4 has been moved from the SW silo to the south hot cell, move went well.

Entry  Thursday, January 17, 2013, 10:06, chad fisher, South Hot-Cell, Standard Operation, , , SiC Test Target for TM4/CS 16x

I have inserted the test target for TM4 and the CS into the hot cell.

I had some concerns about the condition of the target which I have discussed with Pierre and he has cleared. Pictures are attached.

Entry  Tuesday, January 15, 2013, 14:37, Travis Cave, Spent Target Vault, Standard Operation, , TiC#3, Spent target move Vault_Storage_January_15_2013.pdf

TiC #3 was moved from the south hot cell in to the vault storage today, it was placed in slot 4B and was in pail #104, it had a reading of 98.7mSv/hr upon removal from the south hot cell. See attached PDF for vault details.

Entry  Tuesday, January 15, 2013, 10:49, David Wang, ITW, Standard Operation, TM1, no target, TM1 vacuum system connection in ITW 

I connected TM 1 vacuum system in ITW. The TM1 and ITW will be pumped out for shut down routine leak check.

Entry  Monday, January 14, 2013, 14:09, Travis Cave, ITW, Standard Operation, TM1, no target, module move 

TM#1 has been moved from the south hot hell to the west target station, move went well.

Entry  Thursday, January 10, 2013, 10:40, David Wang, ITW, Maintenance, , , Replaced all high active water system magnetic pedal wheels in ITW and ITE. 

I replaced all high active water system magnetic pedal wheels in ITW and ITE. This is a preventive maintenance job we planned for this winter shut down.

Entry  Tuesday, January 08, 2013, 14:18, Travis Cave, South Hot-Cell, Standard Operation, TM1, no target, Electrical check TM#1_no_tgt_Jan_8_2013.PDF

TM#1 was electrically check with out a target see attached PDF for results.

Entry  Tuesday, January 08, 2013, 08:48, Travis Cave, South Hot-Cell, Standard Operation, TM1, TiC#3, Electrical check TiC#3_Elec_Check_Post_beam.PDF

TM#1 with TiC #3 post beam. See attached PDF for results.

Entry  Thursday, January 03, 2013, 10:05, David Wang, ITW, Standard Operation, TM1, , Disconnected TM1 in ITW. 

TM1 has been disconnected in ITW. All  water lines had been purged. Travis was with me during the job.

Entry  Wednesday, January 02, 2013, 12:11, David Wang, ITW, Standard Operation, TM1, , I moved 5 shielding blocks from ITW to block storage area 

I moved 5 shielding blocks from ITW  to block storage area for preparing the TM1 disconnection. Air sampled and swiped blocks and ITW and everything is fine.Fiona was with me all the time during the moving.

Entry  Thursday, December 06, 2012, 08:57, Travis Cave, Spent Target Vault, Standard Operation, , UCx#5, Spent target move Vault_Storage_December_6_2012.pdf

UCx #5 has been moved from the south hot cell to the storage vault. It is in Pail 102, in spot 2A of the vault and had a field of 32.6mSv/hr upon extraction from the south hot cell. See attached PDF for vault details.

Entry  Wednesday, December 05, 2012, 15:53, Anders Mjos, South Hot-Cell, Standard Operation, , UCx#5, Target inspection - target tube broken 

The target was inspected today.

It was found that the target tube had broken on both sides of the centre block in the region that contain target material. The Ta-foil heat shield was removed from the let side tube to allow inspection.

Photos can be found on DocuShare:
https://documents.triumf.ca/docushare/dsweb/View/Collection-9357

Entry  Wednesday, December 05, 2012, 13:26, Grant Minor, South Hot-Cell, Standard Operation, TM4, N/A, TM4 moved from SHC to South West Silo 

TM4 was successfully moved from the South Hot Cell to the South-West Silo remotely by Grant Minor, with help from David Wang and Don Jackson.  The move was without problems.  See ISAC Work Permit 2012-12-04-1.

Entry  Tuesday, December 04, 2012, 14:20, chad fisher, South Hot-Cell, Standard Operation, TM4, UCx#5, UCx#5 Removal 

UCx #5 has been removed from TM4. The left oven leg is indeed broken.

Target has been placed in a pail with an argon feed.

Entry  Tuesday, December 04, 2012, 13:33, David Wang, ITE, Standard Operation, TM4, UCX#5, Disconnected TM4 in ITE. 

I disconnected TM4 in ITE. All water lines had been purged.Travis was with me .

Entry  Tuesday, December 04, 2012, 13:27, Travis Cave, ITE, Standard Operation, TM4, UCx#5, module move & electrical check UC#5_SIS_Post_beam.PDF

TM#4 with UC#5 has been moved from east target station to the south hot cell move went well.  Also the electrical check post beam was done on the module see attached pdf for the results.

Entry  Monday, December 03, 2012, 19:34, Grant Minor, ITE, Standard Operation, TM4, LpUCx, Argon supply opened for ITE vent Argon_Vent_ITE_Cylinder_Pressure_3Dec2012.jpgArgon_Vent_ITE_Secondary_Regulator_Pressure_Relief_3Dec2012.jpgArgon_Vent_ITE_Needle_Valve_3Dec2012.jpg

Around 7pm tonight I opened the main valve approximately 1.5 turns on the Argon bottle used for venting ITE, located in the ISAC electrical room. The cylinder pressure gauge increased to about 1500 psi. I adjusted the secondary regulator (pressure relief valve) until it read 2psi. I opened the needle valve in the vent line completely. The pressure on the pressure relief valve dropped slightly and I adjusted it again until it read 2psi. The Argon supply should be ready for venting ITE w/ TM4. The station should be vented around midnight to prepare for TM4 disconnect tomorrow morning. If there are problems with the venting process, an operator should check the pressure on the secondary regulator / pressure relief valve to ensure it is reading 2psi. - Grant Minor

Entry  Wednesday, November 21, 2012, 09:36, Travis Cave, Spent Target Vault, Standard Operation, , , Spent target move 

On Nov 20th the 5 targets in mini storage have been moved to the F-308s, those F-308s have since been moved to the hot cell ante room. They will sit there until Monday.

Entry  Wednesday, November 14, 2012, 11:51, Travis Cave, Spent Target Vault, Standard Operation, , , Moving the spent targets to mini storage. Vault_Storage_November_14_2012.pdfMini_Vault_Storage_November_14_2012.pdf

Five spent targets have been moved from the storage vault to the mini storage vault. The five targets are as follows: SiC #25, Ta #34, Ta #32, Ta #31, Nb #4. See the attached PDFs for full details.

Entry  Wednesday, November 14, 2012, 11:04, David Wang, ITE, Repair, TM4, , Change ITE dump water circiut flow wheel 

I changed ITE dump water circuit flow wheel due to its poor performance. The new flow wheel works fine. The signal on electrical board is strong and constant. One shielding block on ITE was moved out for the job, and it has been moved back after the job.The ITE is ready to take proton beam. Travis was with me when i did the job.

Entry  Wednesday, November 14, 2012, 10:57, David Wang, ITW, Standard Operation, TM1, , TM1connected in ITW 

I connected TM1 in ITW yesterday. Everything is good so far. Travis was with me when i did the job.

Entry  Tuesday, November 13, 2012, 10:55, Travis Cave, ITW, Standard Operation, TM1, TiC#3, module move 

TM#1 with TiC #3 moved from the conditioning station to the west target station,  move went well.

Entry  Friday, November 09, 2012, 14:35, Travis Cave, Spent Target Vault, Standard Operation, , Nb#7, Spent target move Vault_Storage_November_9_2012.pdf

Nb#7 was moved from the south hot cell to the target storage vault. The target was placed in pail #103 in slot 6A of the vault and had a reading of 178 mSv/hr upon removal from the south hot cell. See attached PDF for full vault details.

Entry  Friday, November 09, 2012, 09:20, Travis Cave, Conditioning Station, Standard Operation, TM1, TiC#3, Electrical check TM_1_TiC_3_Elec_check_CS_Vac.PDF

Electrical check performed on TM#1 with TiC#3 at the conditioning station under vacuum. See PDF for details.

Entry  Thursday, November 08, 2012, 09:37, chad fisher, South Hot-Cell, Standard Operation, TM1, Nb#7, Nb#7 Autopsy 

Nb#7 was dismantled and ready for inspection.

Entry  Thursday, November 08, 2012, 08:42, David Wang, Conditioning Station, Standard Operation, TM1, TiC #3, TM1 TiC #3 target heat shield helium pressure check is done. 

TM1 TiC #3 target  heat shield  helium pressure check  is done at conditioning station. Applied 80 psi helium to HS circuit for 5 minutes . There is no response had been found on leak detector. The leak detector base LR 0.0x E-9 atm.cc/sec, and BP 0.0xE-4 torr. CS and TM1 vacuum are at low E-6 torr range. The HS circuit is leak tight.

Entry  Wednesday, November 07, 2012, 11:09, David Wang, South Hot-Cell, Standard Operation, TM1, TiC , TM1 heat shield circuit leak check with TiC target at hot cell 

Chad and i did a leak check on TM1(Lp-TiC) heat shield water circuit at south hot cell. There is no leak had been found on it. The circuit  is leak tight at present. I will do  helium pressure check on this circuit at  conditioning station once the vacuum is good enough.

Entry  Wednesday, November 07, 2012, 10:25, Travis Cave, Conditioning Station, Standard Operation, TM1, TiC#3, module move 

TM#1 with TiC#3 has been moved from the south hot cell to the conditioning station, move went well.

Entry  Wednesday, November 07, 2012, 09:25, Travis Cave, South Hot-Cell, Standard Operation, TM1, TiC#3, Electrical check TM_1_TiC_3_Elec_check_SHC.PDF

TM#1 with TiC#3 target has had the electrical performed on it. See attached PDF for details.

Entry  Tuesday, November 06, 2012, 14:00, chad fisher, South Hot-Cell, Standard Operation, TM1, TiC#3, TiC#3 Installed 

TiC#3 sucessfully installed and ready for leak and electrical check.

Entry  Tuesday, November 06, 2012, 12:08, David Wang, ITW, Standard Operation, TM1, Nb#7, TM1 disconnected in ITW 

Bevan and I disconnected TM1 in ITW this morning. The TM1 was moved to south hot cell later.   

Entry  Tuesday, November 06, 2012, 11:34, chad fisher, South Hot-Cell, Standard Operation, TM1, , Nb#7 Removal IMG_0797[1].JPGIMG_0798[1].JPGIMG_0799[1].JPG

Attached are pre-removal pictures of NB#7 and the inside face of the containment box cover before cleaning.

Entry  Tuesday, November 06, 2012, 11:06, Travis Cave, ITW, Standard Operation, TM1, Nb#7, module move 

TM#1 with Nb#7 has been moved from the west target station to the south hot cell move went well.

Entry  Friday, November 02, 2012, 13:18, Travis Cave, Spent Target Vault, Standard Operation, , , spent target assay Vault_Storage_November_2_2012.pdf

This week six targets and the two source trays were assayed and surveyed from the storage vault. see attached PDF for details.

Entry  Friday, November 02, 2012, 08:45, maicodallavalle, Spent Target Vault, Maintenance, , , F-308 

The F-308 have been cleaned and serviced. There were three F-308's that came back with some contamination.#13, #15 and #19 were found to have contamination. They were decontaminated. All of the loose contamination was removed. There is still some fixed contamination. The levels of contamination are low enough to still be used for shipping spent targets. They have been moved to the north hot cell area and are ready for to be filled with spent targets. 

Entry  Wednesday, October 31, 2012, 11:24, David Wang, ITE, Standard Operation, TM4, , Transfer five shielding blocks from ITW to ITE. 

Bevan and I transferred five shielding blocks from ITW to ITE. ITE is ready for taking proton beam.

Entry  Wednesday, October 24, 2012, 11:53, Travis Cave, Spent Target Vault, Standard Operation, , NiO#1, Spent target move Vault_Storage_October_24_2012.pdf

The NiO #1 spent target was placed into storage today. It is in pail number 01 (101 on Vault Status page) and located in slot 4A of the vault. It was 35.5 mSv/hr upon removal from the south hot cell. See attached PDF for vault details.

Entry  Wednesday, October 24, 2012, 11:51, Travis Cave, ITE, Standard Operation, TM4, UCx#5, module moved 

Yesterday TM#4 with UCx#5 was moved to the east target station from the conditioning station,  move went well.

Entry  Tuesday, October 16, 2012, 07:14, David Wang, Conditioning Station, Standard Operation, TM4, UCX#5, TM4 heat shield helium pressure test and electrical check at CS 

TM4 heat shield helium pressure test and electrical check were done  at CS  last week. The results are good. NO leak had been found on heat shield circuit.The electrical check is also good.

Entry  Tuesday, October 09, 2012, 14:53, Bevan Moss, Conditioning Station, Development, TM4, UCx#5, Module Move 

TM4 was remote moved from the SCH to the TCS today. This was the first time the module was moved with the framework for the cage in place. The ion gauge on the service cap is closer to the cage than anticipated and as a result the pins for the gauge were sheared off. Discussion as to how to repair the gauge (both short term and long term needs to be had). We will try and rough down the TM tonight, it is not believed the vacuum will be affected.

Entry  Tuesday, October 09, 2012, 13:44, chad fisher, South Hot-Cell, Standard Operation, TM4, UCx#5, NiO#1 removal UCx#5 installation IMG_0780[1].JPG

NiO#1 was removed this morning.

UCx#5 was inserted into the hot cell around 1 pm, installed and leak checked and ready to go to the conditioning station 1:40pm

did have a little trouble with the 9 pin connector. It had to be lossened to get it to mate properly. It was le-tightened once the proper fit was achieved.

Entry  Tuesday, October 09, 2012, 11:17, Bevan Moss, ITE, Standard Operation, TM4, NiO#1, Module Move 

 TM4 with NiO#1 was moved from ITE to the SHC today. The move went well with no issues.

Entry  Tuesday, October 09, 2012, 10:35, David Wang, ITE, Standard Operation, TM4, NiO #1, Disconnected TM4 in ITE. 

I disconnected TM4 in ITE this morning. The heat shield circuit has been purged with air.

Entry  Thursday, October 04, 2012, 11:06, David Wang, Conditioning Station, Repair, , , Replace conditioning station scroll pump in target hall 

Grant and I replaced the conditioning station broken  srcoll pump with a refurbished scroll pump which is supplied by vacuum group. The replaced pump is bagged and waiting for RPG further survey in target hall . The target hall is survey after the job, and everything is fine.

Entry  Tuesday, October 02, 2012, 11:47, David Wang, ITW, Standard Operation, TM1, Nb#7, I moved 5 shielding blocks from ITE to ITW. 

5 shielding blocks have been moved from ITE to ITW. ITW is configured to take proton beam now.

Entry  Thursday, September 27, 2012, 09:13, David Wang, ITE, Repair, TM4, , ITE MSP water circuit flow wheel had been replaced  

ITE MSP water circuit flow wheel was replaced yesterday due to poor performance.

Entry  Tuesday, September 25, 2012, 14:33, David Wang, ITW, Standard Operation, TM1, Nb#7, TM1connected in ITW 

TM 1 is in ITW now. All connections are done. The turbo pumps had been started this afternoon. The vacuum looks good so far. The water interlock check which related to TM1 are done. They are good. All TM1 water signals are visually checked and they are strong.  The rest interlock check ( MCR XT page) will be finished before shielding blocks moving. The MAA is locked and ITE is ready for proton beam.        

Entry  Tuesday, September 25, 2012, 10:34, Travis Cave, ITW, Standard Operation, TM1, Nb#7, module move 

TM#1 with Nb#7 moved from the conditioning station to the west target station. Move went well.

Entry  Thursday, September 20, 2012, 09:16, David Wang, Conditioning Station, Standard Operation, TM1, Nb#7, TM1 Nb#7 target heat shield helium pressure check is done. 

Leak detector pumped down to base LR1.3xE-9 atm.cc/sec, and BP 8xE-3 torr. All high vacuum gauge readings at CS and TM1 are at low -6 range from 1.2xE-6torr to 4.6x E-6 torr. Applied 80 psi helium  to heat shield circuit for 5minutes and there is no any response on leak detector. The heat shield circuit is leak tight.

Entry  Thursday, September 20, 2012, 08:45, Travis Cave, Conditioning Station, Standard Operation, TM1, Nb#7, Electrical check TM1_Nb7_Elec_chk_CS.PDF

Electrical check was done at the conditioning station this morning results are on the attached PDF.

Entry  Wednesday, September 19, 2012, 11:24, Travis Cave, Conditioning Station, Standard Operation, TM1, Nb#7, module move 

TM#1 with Nb#7 was moved from the south hot cell to the conditioning station. Move went well.

Entry  Wednesday, September 19, 2012, 11:23, Travis Cave, South Hot-Cell, Standard Operation, TM1, Nb#7, Electrical check TM1_Nb7_Elec_chk_SHC.PDF

TM#1 with Nb#7 attached was electrically checked at the south hot cell yesterday, see attached pdf for details. Some notes about this test the oven to the 60kV common is 2Mohm this was noticed on the target prior to installation on the module, and the 60kV common to chassis is low at 874Mohm (low as in a non infinite value).

Entry  Tuesday, September 18, 2012, 13:47, chad fisher, South Hot-Cell, Standard Operation, TM1, Nb#7, Nb #7 install Cover Baseline IMG_3191.JPGIMG_3192.JPG

Nb #7 was installed and tested today.

Inside face of the containment box cover was cleaned with methanol and a baseline picture taken in an effort to track deposits and marking as requested bty Anders.

Entry  Tuesday, September 18, 2012, 13:41, David Wang, South Hot-Cell, Standard Operation, TM1, Nb#7, leak check heat shield circuit 

Chad and i did a leak check on TM1 heat shield circuit with new Nb#7 target installed. It took about 5 mins pump down the circuit to leak rate 0.0x E-9atm.cc/sec and 0.0x E-4 torr on leak detector.

All vacuum lines and joints which connected to the leak detector had been helium sprayed and they are leak  tight. Chad sprayed helium on each VCR joints for 2 seconds every time. During 45sec waiting time, there is no any response on leak detector. Chad repeated same test again for double checking and we got same result. Chad finally flushed the helium around the target heat shield for 10 seconds.we waited for 45minute and found no response on the leak detector. The heat shield circuit is leak tight at this stage. I will do a helium pressure test on this circuit when TM1 is in CS and under vacuum.

Entry  Tuesday, September 18, 2012, 09:13, Travis Cave, South Hot-Cell, Standard Operation, TM1, no target, module move 

TM#1 moved from the south west silo to the south hot cell, move went well.

Entry  Friday, September 14, 2012, 10:45, Travis Cave, Spent Target Vault, Standard Operation, , UCx#4, Spent target move Vault_Storage_September_14_2012.pdf

UCx#4 has been moved from the south hot cell to the spent target vault. The target was placed in pail #99 and now resides in spot 3C of the vault. It measured 55.3mSv/hr at ~1m from the hot cell. See attached PDF for further spent target vault details.

Entry  Thursday, September 13, 2012, 13:27, Travis Cave, South Hot-Cell, Standard Operation, TM1, no target, module move 

TM#1 has been moved from the south hot cell to the south west silo. Move went well.

Entry  Thursday, September 13, 2012, 11:03, Travis Cave, South Hot-Cell, Standard Operation, TM1, UCx#4, module move 

TM#1 with UCx#4 has been moved from the west target station to the south hot cell. Move went well.

Entry  Wednesday, September 12, 2012, 11:59, David Wang, ITW, Standard Operation, TM1, UCx, TM1 disconnected in ITW 

I removed 5 shielding blocks from ITW to block storage area, and disconnected TM1 in ITW. After UCx run,  the radioactive level around the turbo pumps and primary vacuum lines are pretty high. This affect the general field inside the ITW pit around working area.i took 15 minuts to finish the job and i got 0.1msvr dose. the general field around my working area is about 350 usv/h.

Entry  Wednesday, September 12, 2012, 07:00, David Wang, ITE, Standard Operation, TM4, NiO #1, ITM4 in ITE connected and pumping down 

TM4 had been connected in ITE. Six turbo pump had been started . thepumpming diwn is very good so far. The water interlock check on ITE and TM4 had been finished and everything is good.All water signals are strong and constant by visually checking.

Entry  Friday, September 07, 2012, 10:37, Travis Cave, Conditioning Station, Standard Operation, TM4, NiO#1, Electrical check TM#4_NiO#1a.PDF

Electrical check of the TM#4 with NiO#1 was done again today. see attached file for results.

Entry  Friday, September 07, 2012, 09:47, Travis Cave, Spent Target Vault, Standard Operation, , UO#3, Spent target move Vault_Storage_September_6_2012.pdf

The spent UO#3 was moved from the south hot cell to the storage vault. It was in pail 98 and placed in spot 1A of the vault, the field measured upon removal from the hot cell were 42mSv/hr. See attached PDF for vault details.

Entry  Friday, September 07, 2012, 08:54, David Wang, Conditioning Station, Standard Operation, TM4, NiO #1, TM4 NiO #1 target heat shield helium pressure check is done. 

leak detector pumped down to 0.0xE-9 atm.cc/sec, and 0.0xE-4 torr. All high vacuum gauge readings at CS and TM4 are at low -6 range from 2.2xE-6torr to 4.2x E-6 torr. Applied 80 psi helium  to heat shield circuit for 5minutes and there is no any response on leak detector. The heat shield circuit is leak tight.

Entry  Wednesday, September 05, 2012, 14:40, Travis Cave, Conditioning Station, Standard Operation, TM4, NiO#1, Electrical check TM#4_NiO#1.PDF

See attached PDF for details. 60kV Common to the target is low at 343k but I've been told will work. Test will be done again on Friday after it has sat a few days under vacuum.

Entry  Wednesday, September 05, 2012, 14:36, chad fisher, South Hot-Cell, Standard Operation, TM4, NiO #1, UOx removal NiO installation 

UOx was removed from TM4 yesterday and NiO#1 installed.

Video was taken.

Main stand-off insulators continue to deteriorate.

Entry  Wednesday, September 05, 2012, 11:55, Travis Cave, Conditioning Station, Standard Operation, TM4, NiO#1, module move 

TM#4 with NiO#1 has been moved from the south hot cell to the conditioning station. Move went well.

Entry  Tuesday, September 04, 2012, 14:34, David Wang, South Hot-Cell, Standard Operation, TM4, NiO #1, TM4 heat shield circuit leak check with NiO#1 target 

Chad and i did a leak check on TM4 heat shield circuit with new NiO#1 target installed. It took about 40 mins(much longer than usual) to pump down the circuit to leak rate 0.6x E-9atm.cc/sec and 0.0x E-4 torr o leak detector.

All vacuum lines and joints which connected to the leak detector had been helium sprayed and they are leak  tight.Chad sprayed helium on each VCR joints for 2 seconds every time. During 1min waiting time, there is no any response on leak detector. Chad repeated same test again for double checking and we got same result. Chad finally flushed the helium around the target heat shield for 10 seconds.we waited for 1minute and found no response on the leak detector. The heat shield circuit is leak tight at this stage. I will do a helium pressure test on this circuit when TM4 is in CS and under vacuum.

Entry  Tuesday, September 04, 2012, 11:11, Travis Cave, South Hot-Cell, Standard Operation, TM4, UO#3, module move 

TM#4 with UO#3 has been moved from the east target station to the south hot cell for a target exchange. The move went well.

Entry  Friday, August 31, 2012, 12:10, chad fisher, South Hot-Cell, Maintenance, , , Hot Cell Maitenance 

Entered south hot cell Wednesday and replaced the pre-filter air filter as well as the front two light bulbs. Also removed two bags of compressible garbage, one bag of metal, and of course the bagged air filter (as Joe M. expressed as interest in havung it).

Inital checks found approximately 4000 cpm on the cell side of the temporary Al. panel used during the cell entry, 2000 cpm on the tacky mats layed out beside the work area but nothing on the floor under the plastic that had been layed down for the job.

 

Chad

Entry  Thursday, August 30, 2012, 13:57, David Wang, ITE, Standard Operation, TM4, , Disconnected TM4 in ITE. 

I disconnected TM 4 in ITE on AUG 29th morning.The vacuum lines stay untouched and they will be disconnected on SEP 04th.

Entry  Thursday, August 23, 2012, 07:34, David Wang, ITW, Repair, , , Replaced broken air lines on ITW HARP5B cylinder. 

Prob guys replaced broken air lines on ITW HARP 5B Cylinder.Several shielding blocks had been moved out to make the cylinder accessible. After the replacement,the HARP5B works fine.All shield blocks had been moved back to original position. The job is done.

Entry  Monday, August 20, 2012, 12:28, David Wang, ITW, Standard Operation, TM1, , I moved 5 shielding blocks from ITE to ITW, 

I moved 5 shielding blocks from ITE  to ITW.ITW is configured to take proton beam now.

Entry  Tuesday, August 14, 2012, 14:27, David Wang, ITW, Standard Operation, TM1, UCx, TM1connection in ITW 

Connected TM1 in ITW,started 6 turbo pumps, and finished TM1 water interlock check . Every thing is good so far.

Entry  Tuesday, August 14, 2012, 11:16, Travis Cave, ITW, Standard Operation, TM1, UCx#4, module move 

TM#1 with UCx#4 moved from the conditioning to the west target station move went well.

Entry  Tuesday, August 14, 2012, 11:16, Travis Cave, ITW, Standard Operation, TM1, UCx#4, module move 

TM#1 with UCx#4 has been moved from the conditioning station to the west target station move went well.

Entry  Tuesday, August 07, 2012, 14:06, David Wang, ITW, Repair, , , ITW TP4S has been replaced 

 I replaced ITW TP4S today as we scheduled. The working area is swiped and air sampled .Everything is fine.

The Series # of the old pump is 200927, and the new one is 600080. The E-fault 6081 which is related to the job will be closed.

Entry  Thursday, August 02, 2012, 11:48, Travis Cave, Spent Target Vault, Standard Operation, , Ta#38, Spent target move Vault_Storage_August_2_2012.pdf

Ta#38 was moved from the south Hot Cell to the Spent Target Vault. Target is in pail #97, and was placed into tray 6 slot B of the vault. Field around the pail upon removal from the Hot Cell were 226mSv/hr at about 1/2 metre. See attached PDF for vault details.

Entry  Thursday, August 02, 2012, 07:48, David Wang, Conditioning Station, Standard Operation, TM1, UCx, TM1 UCx target heat shield helium pressure check is done. 

Connected leak detector to TM1 and CS vacuum system. The vacuum readings on TM1 and CS:PNG4 3.6 xE-6 Torr, IG1 1.1xE-6torr, IG4(diagnostic box) 3.4xE-6 Torr. Leak detector base pressure:0.0xE-4 torr, base leak rate: 0.0xE-9 atm.cc/sec. Applied 80 psi helium to heat shield circuit for 4 mins . There is no response on leak detector. The heat shield circuit is leak tight.

Entry  Wednesday, August 01, 2012, 09:14, Travis Cave, Conditioning Station, Standard Operation, TM1, UCx#4, Electrical check TM#1_UC#4_under_vac.PDF

TM#1 with UCx#4 electrical check done at the conditioning station under vacuum, see attached sheet for results.

Entry  Tuesday, July 31, 2012, 14:04, Travis Cave, Conditioning Station, Standard Operation, TM1, UCx#4, module move 

TM#1 with UCx#4 has been moved from the south  hot hell to the conditioning station. No problems with the move.

Entry  Tuesday, July 31, 2012, 12:50, David Wang, South Hot-Cell, Standard Operation, TM1, UC x, TM1 heat shield circuit leak check with UC x target 

Chad and i did a leak check on TM1heat shield with UCx target on.The circuit are pumped  down to the bottom leak rate and base pressure is 3xE-3 torr on the leak detector. There are two VCR caps on heat shield circuit. Chad sprayed helium on both of them   ( tested individually,2 seconds every time ) . The test repeated 1 time.There is no response on leak detector during 45 seconds waiting time on both time.Chad flushed helium around the target for 15 second. During 1 minutes waiting time , there is no response on leak detector.The heat shield circuit is leak tight at this stage. It will be helium pressure  in CS later.

Entry  Tuesday, July 31, 2012, 12:24, chad fisher, South Hot-Cell, Standard Operation, TM1, UCx#4, UCx#4 Installed 

Starting at 11:00 am and finishing at 12:10 Ucx#4 previous target was removed and UCx#4 installed and leak checked on TM1.

During module move to the hot cell UCx#4 was housed in a bag under argon.

Entry  Tuesday, July 31, 2012, 10:50, Travis Cave, South Hot-Cell, Standard Operation, TM1, Ta#38, module move 

TM#1 with Ta#38 has been moved from the west target station to the south hot cell, no problems with the move.

Entry  Tuesday, July 31, 2012, 09:52, David Wang, ITW, Standard Operation, TM1, Ta38, TM1 disconnected in ITW 

I disconnected TM1 in ITW.  Heat shield line has been purged .

Entry  Thursday, July 26, 2012, 08:33, David Wang, ITE, Standard Operation, TM4, , I moved 5 shielding blocks from ITW to ITE thisTuesday morning . 

  All water interlock checks for ITE had been done. The ITE water signals strength and frequency(Espcially on MSP circuit) had been checked from electrical room, and everything is good.

Entry  Wednesday, July 18, 2012, 16:49, Grant Minor, South Hot-Cell, Development, , , South Hot Cell Ventilation Alarm Trip 

Today (Wednesday July 18th) at around 4:15 pm I was taking a small tour group from VECC into the Target Hall. In the process of discussing the mechanical design of the Target Modules and South Hot Cell turntable I inadvertently lifted the Aluminum Hatch Cover of the Hot Cell about 2 inches in an effort to explain something. This tripped the ventilation alarm before I realized what I was doing. I evacuated the visitors from the Target Hall, checked booties and gloves at the check station before having the visitors step over the boot box. I called operations and let them know what I had done. The Target Hall was locked out and is awaiting a survey for the morning of July 19th before work can proceed.

Entry  Wednesday, July 18, 2012, 16:49, Grant Minor, South Hot-Cell, Development, , , South Hot Cell Ventilation Alarm Trip 

Today (Wednesday July 18th) at around 4:15 pm I was taking a small tour group from VECC into the Target Hall. In the process of discussing the mechanical design of the Target Modules and South Hot Cell turntable I inadvertently lifted the Aluminum Hatch Cover of the Hot Cell about 2 inches in an effort to explain something. This tripped the ventilation alarm before I realized what I was doing. I evacuated the visitors from the Target Hall, checked booties and gloves at the check station before having the visitors step over the boot box. I called operations and let them know what I had done. The Target Hall was locked out and is awaiting a survey for the morning of July 19th before work can proceed.

Entry  Friday, July 13, 2012, 16:33, Bevan Moss, Crane, Repair, , , Crane has stopped working 

In the AM today David and I used the crane to raise the ground plate sheet metal into place. This afternoon when I attempted to return the crane to its usual place I discovered that the crane no longer worked. Upon further inspection it appears that the PLC has lost power. I will follow up on this Monday morning. The crane is not supporting any load at this point.

    Reply  Monday, July 16, 2012, 11:55, Bevan Moss, Crane, Repair, , , Crane has stopped working 

Bevan Moss wrote:

In the AM today David and I used the crane to raise the ground plate sheet metal into place. This afternoon when I attempted to return the crane to its usual place I discovered that the crane no longer worked. Upon further inspection it appears that the PLC has lost power. I will follow up on this Monday morning. The crane is not supporting any load at this point.

 Turns out I am just not very observant. David had turned the main break to the crane off as a result when he turned it back on this morning the crane magically started working again.

Entry  Monday, July 09, 2012, 16:08, David Wang, ITE, Standard Operation, TM4, UO#3, ITM4 in ITE connected and pumping down 

 TM4 has been moved to ITE and connected there today. I started six turbo pumps this afternoon. One of TP4 back valve (one in pairs) didn’t open .It caused the TP4 difficult to start. I disconnected that control cable that plug to solenoid valve and reconnected it. Then it works fine. After this, TP4 started to normal speed easily. The vacuum readings are OK so far. Tomorrow morning they all should be around 6-7 X E-6 torr range. Water interlock checks related to TM4 have been finished. NO water supply to ITE dump and entrance to keep the system pressure over 90psi. All TM4 water signals are good and strong by watching them from electrical panel. Gas line connected and valves opened. Control page set to fibiad .

Entry  Monday, July 09, 2012, 10:51, Travis Cave, ITE, Standard Operation, TM4, UO#3, module move 

TM#4 with UO#3 from the conditioning station to the east target station. Move went well.

Entry  Friday, July 06, 2012, 14:38, David Wang, Conditioning Station, Standard Operation, TM4, UO#3, TM4 UO#3 target heat shield helium pressure check is done. 

Connected leak detector to TM4 and CS vacuum system. The vacuum readings on TM4 and CS:PNG4 3.6 xE-6 Torr, IG1 2.3xE-6torr, IG4(diagnostic box) 3.9xE-6 Torr. Leak detector base pressure:6.0xE-3 torr, base leak rate: 1.0xE-9 atm.cc/sec. Applied 80 psi helium to heat shield circuit for 5 mins . There is no response on leak detector. The heat shield circuit is leak tight.

Entry  Friday, July 06, 2012, 11:34, Travis Cave, Spent Target Vault, Standard Operation, , SiC#27, Spent target move Vault_Storage_July_6_2012.pdf

SiC#27 has been moved from the south hot cell to the spent target vault. Target was placed in pail #96, placed in slot 3A, the fields at the hot cell were 178mSv/hr. For the latest on the vault see attached document.

Entry  Friday, July 06, 2012, 09:24, Travis Cave, Conditioning Station, Standard Operation, TM4, UO#3, Electrical check TM#4_UO#3_elec_check_under_vac.PDF

Electrical check of the target was done at the conditioning station under vacuum, see attached file for details.

Entry  Wednesday, July 04, 2012, 14:16, Travis Cave, Conditioning Station, Standard Operation, TM4, UO#3, module move 

TM#4 with UO#3 moved from the south hot cell to the conditioning station. The fields of the module at the hot cell was 74.4 mSv/hr.

Entry  Wednesday, July 04, 2012, 13:18, David Wang, Conditioning Station, Standard Operation, TM4, uo#3, leak check on heat shield circuit 

Chad and I leak checked the heat shield circuit after uc#3target installed. It took 5minutes to pump down the circuit to the leak detector bottom scales.   All the vacuum lines and connections are leak checked by spraying helium. Chad sprayed helium to each vcr fittings for 2 seconds. There is no any response on leak detector . The test repeated one time and the result is same. The heat shield circuit is leak tight at this stage . We will move TM4 to conditioning station and pressure helium test the circuit.

Entry  Wednesday, July 04, 2012, 11:33, Travis Cave, South Hot-Cell, Standard Operation, TM4, UO#3, Electrical check TM#4_UO#3_elec_check.PDF

Electrical check of TM#4 with  UO#3 attached at the south hot cell see attached PDF for full results. It has been noted that the Anode to 60kV common is of a low value after consulting with Friedhelm Ames it was determined will will run with what we have.

Entry  Tuesday, July 03, 2012, 12:26, Travis Cave, South Hot-Cell, Standard Operation, TM4, SiC#27, module move 

TM#4 with SiC#27 moved from the east station to the south hot cell. Fields at East MAA were 127mSv/hr and the fields at the south hot cell was 77.5 mSv/hr.

Entry  Tuesday, July 03, 2012, 10:50, David Wang, ITE, Standard Operation, TM4, , Disconnected TM4 in ITE. 

I disconnected TM4 in ITE this morning. The window circuit and heat shield circuit had been purged. The general field inside ITE is about 200usv/h.

Entry  Tuesday, June 26, 2012, 14:10, David Wang, South Hot-Cell, Repair, TM3, , TM3 heat shield and window circuits leak check is done. 

Chad and i did a leak check on TM3 heat shield and window circuits.Both circuits are pumped easily down to the bottom leak rate and base pressure on the leak detector. There are two VCR caps on heat shield circuit. Chad sprayed helium on both of them   ( tested individually,2 seconds every time ) . There is no response on leakdetecor during 45 seconds waiting time. On window circuit there are 2 VCR joints. Chad sprayed helim on these joints(2seconds for each), and no response on leak detector. All joints  are double checked(sprayed twice on each of them). The result is they are leak tight.

Entry  Monday, June 25, 2012, 14:39, David Wang, ITW, Standard Operation, , , I moved 5 shielding blocks from ITE to ITW, 

and set up ventilation for ITW. ITW is ready for taking proton beam now. All water interlock checks for ITW are done. The ITW water signals strength and frequency had been checked from electrical room, and everything is good.

Entry  Monday, June 25, 2012, 07:53, chad fisher, South Hot-Cell, Repair, TM3, N/A, TM3 Refurb. Work 

On Friday, June 22 the following work was carried out.

  • Further inspection of the source tray.
  • Testing of existing tray removal and installation tool...it works fine, there was just a specific method for proper coupling to the target module. There was no documentation for this tool, so it took a little bit of insight with the drawings and a little trial and error. A document should be written for this tool so its proper use is documented...I will do this.
  • Blank-offs installed on heat shield water lines.
  • New gaskets installed on window water lines.
  • Containment box re-installed.

Pictures can be found at: http://documents.triumf.ca/docushare/dsweb/View/Collection-8639


 

Entry  Thursday, June 21, 2012, 14:33, chad fisher, South Hot-Cell, Repair, TM3, N/A, Pictures TM3 June 21st 8x

Here are the pictures from today...there is video too but it is not uploaded yet.

Entry  Thursday, June 21, 2012, 14:30, chad fisher, South Hot-Cell, Repair, TM3, N/A, TM3 Refurbishment Start 

Started refurb of TM3.

Planned activities:

Inspection

Water line blank off

Started 1:00pm

  • Video inspection before containment box removed - noticed discoloration on top right (if looking from h/c window) 4" insulator
  • Containment box cover removed
  • Containment box removed

As I am much older, wiser and handsomer then last time I removed this style of box, I realised there was a better, safer procedure for the removal...I will be updating the doc. accordingly.

End 2:25 pm

 

Entry  Thursday, June 21, 2012, 14:00, Travis Cave, South Hot-Cell, Repair, TM3, no target, module move 

TM#3 has been moved from the south west silo to the south hot cell for the start of its second refurb/repair. The fields of the module when it was lowed in was 2msv/hr.

Entry  Wednesday, June 20, 2012, 11:39, Grant Minor, South Hot-Cell, Development, TM3, N/A, TM3 Planned Activites at South Hot Cell Jun 20 to 29 2012 

(Copy of e-mail correspondence sent June 20th 2012)

After some discussions this morning I’ve decided on the following best path forward for TM3 at the Hot Cell leading up to the Canada Day long weekend.

 

General Goals:

-          Blank-off TM3 water line terminations (coil, heat shield, water-cooled window)

-          Test sliding tray removal tool to determine fit on TM3 chassis

 

We will skip the Conditioning Station leak tests and return TM3 directly to a silo for the following reasons:

-          We will have a visitor next week and this will impact Chad’s time available to do Hot Cell work

-          Helium pressure leak checks on the blanked-off circuits are only one small portion of a large set of diagnostic tests (leak, electrical, HV, etc.) that must ultimately be performed on TM3 to determine its fitness. This full set of tests must be carefully documented in a procedure and executed systematically when there is adequate time at the CS to do all of them, with results recorded.  There is currently not adequate time for this work between now and Canada Day.

-          If we were to detect a leak from one of these tests, it would not tell us anything about where the leak is in that given circuit (there are multiple possible points).  The service cap would have to be opened regardless, which we don’t have time for.

-          The aforementioned bullets above lead me to conclude that the extra work required for two module moves for one set of partial leak checks is not a value-added exercise: In other words, the module will have to go back to the CS, regardless of what we do over the next week for more tests.  The time savings of trying to squeeze it in next week are really negligible and it makes for a tight schedule for not much benefit.

 

Chad:  Please prepare a detailed work plan for your hot cell jobs including a list of the tools required and what leak checks you will do specifically after you have installed the blank-offs.  You may refer to existing procedures if you already have these written.  I would like to review this plan and I am expecting that an e-log will be filed daily and this work plan should be referred to as an attachment.

 

Proposed Schedule Jun 20 to 29

 

Wednesday Jun 20 (1 working day)

-          Setup for TM3 move from Silo to HC (Travis, David)

 

Thursday Jun 21 (1 working day)

-          TM3 moved from silo to HC (Travis, Don Dale, David)

 

Friday Jun 22 to Wednesday Jun 27 (4 working days)

-          Chad performs the following HC work on TM3:

·         Removes containment box

·         Installs water-line blank-offs

·         Checks Sliding Tray Removal Tool Fit

-          Vacuum leak checks of blanked-off lines at the HC (Chad, David, VG)

-          Chad buttons up TM3

-          In parallel - David performs block moves as required

 

Thursday Jun 28 (1 working day)

-          TM3 moved from HC to Silo (Travis, Don Dale, David)

 

Friday Jun 29 (1 working day)

-          Contingency

 

RH Group: Please move ahead with the work as outlined above.  Please comment if you have any concerns or proposed changes to this plan.  Thanks very much to all for your assistance,

 

Grant

 

-------------------------------------------------

Grant Minor, M.A.Sc., P.Eng.

TRIUMF Remote Handling Group Leader

Nuclear Engineer

4004 Wesbrook Mall, Vancouver

BC, Canada, V6T2A3

gminor@triumf.ca

(604) 222-7359

http://www.triumf.ca/profiles/4557

-------------------------------------------------

Entry  Tuesday, June 19, 2012, 16:18, David Wang, ITW, Standard Operation, TM1, Ta38, TM1connected in ITW 

 We moved TM1 to ITW today, I connected TM1 to ITW, and started all turbo pumps this afternoon. TP4s is very difficult to bring to 38 KRMP now. I have to use soft start model and tried twice to get this pump started (1.5 hours). This pump always had a difficult start time during the past 2-3 runs. I talked with Friedhelm and we think it should be replaced after this run. I will issue an e-fault on this pump and try to get a new pump from vacuum group. It will take 2 hours to change this pump. I could do this job with another person help. Or, vacuum group could do it. Don can schedule a time for this job before next run. Anyway, it should work fine for this run.  The water interlock check related to TM1 is done. I will do the rest before blocks on. All TM1 water signals are strong and good. All vacuum gauge readings are good so far(below5.0xe-5 torr).

 

Entry  Tuesday, June 19, 2012, 10:35, Travis Cave, ITW, Standard Operation, TM1, Ta#38, module move 

TM#1 with Ta#38 moved from the conditioning station to the west target station. Move went well.

Entry  Monday, June 11, 2012, 14:41, David Wang, Conditioning Station, Standard Operation, TM1, Ta38, Heat shield helium pressure test 

Connected leak detector to TM1 and CS vacuum system. The vacuum readings on TM1 and CS:PNG1 1.3 xE-6 Torr, IG1 4.7xE-7torr, IG4(diagnostic box)1.5xE-6 Torr. Leak detector base pressure:0.0xE-4 torr, base leak rate: 0.0xE-9 atm.cc/sec. Applied 80 psi helium to heat shield circuit for 5 mins . There is no response on leak detector. The heat shield circuit is leak tight.

Entry  Monday, June 11, 2012, 14:14, Travis Cave, Conditioning Station, Standard Operation, TM1, Ta#38, Electrical check TM#1_Ta38_at_constat_elec_check.PDF

Electrical check of TM#1 with Ta#38 at the conditioning station under vacuum. See attached file for details.

Entry  Monday, June 11, 2012, 10:52, Travis Cave, Spent Target Vault, Standard Operation, , Nb#6, Spent target move Vault_Storage_June_11_2012.pdf

The Nb#6 target has been moved from the south hot cell into storage. It was place in pail #95 and is in slot 5C of the vault. See attached file for more details.

Entry  Friday, June 08, 2012, 15:03, Don Jackson, South Hot-Cell, Standard Operation, TM1, Ta38, Electrical Check on new Ta38 at hot cell Ta38_New_Target.JPG

Megger checks were exceptionally high (good).  Readings taken less than 2 hours after reading low values from end of run on Nb#6.  Tests on Ta38 will be repeated at conditioning station later.

Entry  Friday, June 08, 2012, 15:00, Don Jackson, South Hot-Cell, Standard Operation, TM1, Nb#6, Electrical Check Nb#6 at end of run Nb#6_End_of_Run.JPG

Megger check values were low but still within operational range.

Entry  Friday, June 08, 2012, 11:07, David Wang, Conditioning Station, Standard Operation, TM1, Ta38, conditioning staion and TM1 is under TP1 and TP2 pumping now. 

I connected vacuum system to TM1 and conditioning station and started two turbo pumps yesterday. The pumping an d vacuum readings  are verg good so far(all below 5xE-6 torr). Helium pressure test on heat shield circuit will be fulfilled next week.

Entry  Thursday, June 07, 2012, 11:58, Bevan Moss, Conditioning Station, Standard Operation, TM1, Ta38, Module Move from SHC to TCS 

TM1 was moved from SHC to the TCS. The mode took roughly 1 hour. During the move the north east corner of the containment box caught slightly on the flange of the vacuum vessel and then slipped off. The contact was minimal but should none the less be noted. After sliding off of the flange the module did not crash into the other sides of the vacuum vessel, this is why I believe the contact was minimal. It should be noted that the corner of concern is the one that is most difficult to see.

Entry  Wednesday, June 06, 2012, 14:33, David Wang, South Hot-Cell, Standard Operation, TM1, Ta38, leak check heat shield circuit 

Chad and I did a leak check on heat shield circuit after target is installed on TM1.The leak detector pumping down is smooth. The base leak rate is 0.0xE-9 atm.cc/sec. The base pressure is 0.0xE-4torr. Chad checked helium flow downstairs and sprayed helium to each joints for 2 seconds.The first joints is good and there is no any response on leak detector.we double checked it again and got the same result. On the second joint, Chad sprayed helium 2second. After 15 second of spraying,the leak detector got a response which climbed to 3.2xE-8 atm.cc/sec max,and back to 2.5 XE-8 atm.cc/sec. Chad tried to tighten the fitting. During his tight, the leak rate response to 7.5x E-8 atm.cc/sec momentarily. After the tightening ,the leak rate back to 0.0x E-9atm.cc/sec whic is the base.So we sprayed the helium to the joint again.This time ,there is no any response on leak detector. We checked this joint  again and got the same result which is no response. Finally, Chad flush the helium around the target for 10 second ,and during 45 sec observation time there is no any response on leak detector. I would say the heat shield circuit is leak tight so far. I will do a helium pressure test on it once the TM1 is moved the CS.

Entry  Wednesday, June 06, 2012, 13:36, chad fisher, South Hot-Cell, Standard Operation, TM1, Ta#38, Target Change Nb#6 - Ta#38 

Nb#6 was removed from TM1...it looked very clean.

Ta#38 was installed onto TM1...fit well.

Isaac Earle did this change with supervision in an effort to cross train.

TM1 containment box was checked for damage from the "bump" it got during yesterday's move. There was new scratches on the shutter side panel. Picture to follow.

The front containment box panel was "difficult" to remove...it required a good pull to get off.

 

Entry  Wednesday, June 06, 2012, 08:21, David Wang, ITW, Standard Operation, TM1, , TM1 disconnected in ITW 

I disconnected TM1 in ITW yesterday morning.The general radioactive level in ITW over the TM top (300mm) is about 350 usv/hr. contacting level on TP1 and TP2 are 1.0-1.2 msv/hr. I took 0.22 msv dose .The module is moved to

south hot cell later and a shielding plug is put back to ITW. Everything is fine.

Entry  Tuesday, June 05, 2012, 15:06, Bevan Moss, ITW, Standard Operation, TM1, Nb#6, Module move from ITW to SHC 

 TM1 has been moved from ITW to the SHC. The move did encounter some issues, one of the railings for preventing people from falling into the MAA was hit with the containment box. This caused the module to rotate. The module rotated ~90 degrees before the problem was noticed. The module was backed off from the post once noticed but had already freely rotated. The box was inspected with the cameras prior to being inserted into the SHC. No damage was detected. The error came as a result of over confidence. It did appear it was going to be hit but as the module moved closer I believed that there would be clearance. The angle of the camera has caused the module to appear it was going to hit thing before in the past but it actually (once the module was closer to the object) had several feet of clearance. This is not a mistake I will make again.

Chad Fisher, Grant Minor, and Don Jackson, have been alerted about this. Chad will complete another visual inspection in the hot cell. David will take swipes of the pole to ensure there is no contamination. 

Entry  Tuesday, June 05, 2012, 12:20, Bevan Moss, South Hot-Cell, Standard Operation, TM1, Ta#38, Target inserted into HC 

Ta#38 has been placed into the south hot cell. Swipes of the tool port were taken there was a count of 600 on the floor and 150 on the walls and top. 

Entry  Monday, May 28, 2012, 13:05, David Wang, ITE, Standard Operation, , , I moved 5 shielding blocks from ITW to ITE . 

5 shielding blocks have  been transferred from  ITW to ITE. ITE ventilation is opened, and ITW closed. All ITE water  signals have been checked for frequency and strength.They are all good. ITE is ready for taking proton beam.

Entry  Friday, May 25, 2012, 10:48, Travis Cave, Spent Target Vault, Standard Operation, , , Moving the spent targets to mini storage. Mini_Vault_Storage_May_25_2012.pdfVault_Storage_May_25_2012.pdf

Five targets were moved to the mini storage today in preparation for transfer of the targets to the F308s later next week. The moves went well. See the attached files for the vault and mini storage details.

Entry  Tuesday, May 22, 2012, 15:19, David Wang, ITE, Standard Operation, TM4, sic 27, TM4 in ITE under pumping 

  I started 6 turbo pumps this afternoon. The TM4 and ITE are under pumping now. The vacuum is fine so far. We will see a better picture tomorrow morning. In order to keep the system pressure at 90 psi, I just turned on all the water to TM4 circuits. The water interlock check which related to TM4 water circuits is all done. I will do the rest part (XTpage related to 2A beam) next week once I turn on all the water to ITE. The ITE and TM4 will be ready for HV conditioning once the vacuum is ok.

                    

Entry  Tuesday, May 22, 2012, 12:36, David Wang, ITE, Standard Operation, TM4, sic 27, TM4 connection in ITE 

All TM4 connections in ITE is done. The station and TM4 is under roughing now.

Entry  Tuesday, May 22, 2012, 10:50, Travis Cave, ITE, Standard Operation, TM4, SiC#27, module moved 

Module has been moved from conditioning station to the east target station. Move went well.

Entry  Tuesday, May 22, 2012, 10:00, David Wang, Conditioning Station, Standard Operation, TM4, sic 27, helium pressure test on heat shield circuit 

I did a helium pressure test on heat shield circuit. The leak detector is concected to the TM4 primary vacuum system.The IG1 is 1.1xe-6 torr,PNG4 is 1.5 x E-6torr,and IG4 is 2.1 XE-6torr.leak detector base leak rate:0.0xE-9 atm.cc/sec, base pressure is 0.0x E-4 torr.Applied 80psi helium to heat shield circuit for 4 mins .There is no any response on leak detector during 4mins time. There is no pressure change during the test time. The heat shield circuit is leak tight.

Entry  Tuesday, May 22, 2012, 08:33, Travis Cave, Conditioning Station, Standard Operation, TM4, SiC#27, Electrical check TM#4_SiC#27_pre_beam_under_vac.PDF

Electrical check of TM#4 with SiC#27 under vacuum at that conditioning station. See attached PDF for details.

Entry  Friday, May 18, 2012, 08:37, David Wang, South Hot-Cell, Standard Operation, TM4, sic 27, leak check on heat shield circuit 

Chad and I leak checked the heat shield circuit after sic 27 target  installed. It took 20minutes  to pump down the circuit to the leak detector bottom scales. The leak detector is calibrated today,and all the vacuum lines and connections are leak checked by spraying helium. Chad sprayed helium to each vc fittings for 2 seconds. There is no any response on leak detector . The test repeated one time and the result is same. Chad flushed  helium around the target for 10 second .This time leak detector also have no respone.  The heat shield circuit is leak  tight at this stage . We will move TM4 to conditioning station and pressure helium test the circuit.

Entry  Friday, May 18, 2012, 08:29, Travis Cave, South Hot-Cell, Standard Operation, TM4, SiC#27, Electrical check TM#4_SiC#27_pre_beam.PDF

TM#4 with SiC#27 has had its electrical check. See attached PDF for details.

Entry  Friday, May 18, 2012, 08:17, chad fisher, South Hot-Cell, Standard Operation, TM4, SiC#27, SiC#27 Installed 

SiC#27 has been installed onto TM4. Fit was very good. All electrical connections double checked with mirror.

Pictures can be found at: http://documents.triumf.ca/docushare/dsweb/View/Collection-8530
 

Entry  Thursday, May 17, 2012, 14:08, Travis Cave, South Hot-Cell, Standard Operation, TM4, no target, module move 

TM#4 has been moved from the north east silo to the south hot cell for target installation.  No problems with the move.

Entry  Wednesday, May 16, 2012, 10:35, Travis Cave, Spent Target Vault, Standard Operation, , SiC#26, Spent target move Vault_Storage_May_16_2012.pdf

SiC #26 was moved from the south hot cell into storage today. The target was is in pail # 94 and was placed in slot 1B in the storage vault. The fields of the pail at the hot cell were 118mSv/hr upon pail been removed from the hot cell. Attached is the current status of the storage vault.

Entry  Tuesday, May 15, 2012, 14:29, Travis Cave, South Hot-Cell, Standard Operation, TM4, no target, module move 

TM#4 moved from the south hot cell to the north east storage silo. No issues with the move.

Entry  Tuesday, May 15, 2012, 12:14, chad fisher, South Hot-Cell, Standard Operation, TM4, SiC#26, SiC#26 removal TM4 degredation 19x

SiC#26 was removed from target module #4 this morning. Target shows the now standard arc marks on the 9 pin connector housing...pictures to follow.

Of greater concern is the amount of "plating out" or "arc" marks on both the insulators and connductor of the TM4 source tray. I will again warn that the source trays historically have a life expectancy, and that TM4 continues to show visual signs that the current source tray is rapidly approaching the end of its useful life!

I understand that one of this years goals is to retrofit TM3; however I fear TM4(and possibly TM1) may fail before this can be released. With the current absence of backup source trays and modules I fear we leave the ISAC program in a very vulnerable position.

 

 

 

Entry  Tuesday, May 15, 2012, 11:45, Travis Cave, South Hot-Cell, Standard Operation, TM4, SiC#26, Electrical check TM#4_SiC#26_FEBIAD_post_beam.PDF

Results of the electrical check of TM#4 with SiC#26 attached post beam.

Entry  Monday, May 14, 2012, 12:37, Travis Cave, ITE, Standard Operation, TM4, SiC#26, module move 

TM#4 with SiC #26 was moved from the East Station to the South Hot Cell. Bevan was at the helm of the PLC. There was no issue with the move.

Entry  Tuesday, May 08, 2012, 10:28, David Wang, ITE, Standard Operation, TM4, , Disconnected TM4 in ITE. 

I disconnected TM4 in ITE. The heat shield water circuit is purged. I  closed the water supply to ITE.Now, the water system only supply water to ITW and the system pressure is 110 psi which is good.I visually checked S-tank sight glass,and the water level is stable comparing to last week. Also, I visually checked the ITW water signals  strength and stability on electrical panel from electrical room.Everything looks fine.

Entry  Wednesday, May 02, 2012, 11:27, David Wang, ITW, Standard Operation, TM1, , ITW is ready for taking proton beam. 

 I moved 5 shielding blocks from ITE to ITW .  I checked  all ITW water signals strength and frequency in electrical room, and everything looks fine.The ventilation system is set up for ITW. MAA is locked. ITW is ready for taking proton beam.

Entry  Thursday, April 26, 2012, 13:01, David Wang, ITE, Repair, TM4, , Replaced TM4 EE water flow wheel in ITE. 

Due to weak magnetic field on TM4 EE water flow wheel, we have two times intermittent water signal on this circuit this morning. I replaced the old wheel with a new one in ITE. I checked the signal frequency and strength.It looks fine now.

Entry  Thursday, April 26, 2012, 09:23, David Wang, ITE, Repair, TM4, , changed flow wheel on ITE TM4 contaiment box water circuit 

The the magnetic field on ITE TM4 flow wheel  was gone yesterday.So there is no water signal on this circuit. The water flow is fine ,and the wheel is rotating. I removed 1 shielding block on ITE and replaced the old wheel with a new one.Now the containment box water signal is normal.The problem is fixed.The shielding block is back.

Entry  Tuesday, April 24, 2012, 10:38, David Wang, Conditioning Station, Standard Operation, TM1, LP SIS Nb6, TM1 heat shield circuit leak check with Nb5 

 The pumping down on TM1 and conditioning station is fine over the weed end. The PNG 1(containment box) is 2.4xe-6 Torr, the IG1 (top service cap) is 9.0 xE-7 Torr, and the IG4 is 1.9xE-6Torr (diagnostic box). At this pressure, I connected the leak detector to the system and applied 80psi helium to the heat shield circuit. The leak rate and base pressure on leak detector are 0.0xE-9 Atm.cc/sec and 0.0xE-4Torr. There is no any response on leak detector during 4mins helium applying time. So the heat shield and Nb5 target water circuit is completely leak tight.

Entry  Tuesday, April 24, 2012, 10:36, Bevan Moss, Conditioning Station, Standard Operation, TM1, Nb#6, HV test April 23 

 A HV test was complete on TM1 with Friedhelm, David, and Myself. The module behaved as it has in other tests. The vacuum achieved was 1.6 x 10^-6 in the diagnostics box, 2.3 x 10^-6 in the containment box, and 8.6 x 10^-7 in the service cap. Maximum voltage without continuous sparking achieved was 27kV. Current was unstable varrying from 40 to 300 uA. This voltage was held for 10 minutes. 

Entry  Tuesday, April 24, 2012, 10:02, Travis Cave, ITW, Standard Operation, TM1, Nb#6, module move 

TM#1 with Nb#6 from the conditioning station to the west target station, move was uneventful. Mike LaRoss was there today for move in place of Don Dale working the PLC.

Entry  Friday, April 20, 2012, 14:07, Travis Cave, Conditioning Station, Standard Operation, TM1, Nb#6, module move 

TM#1 with Nb#6 is now in the conditioning station. The fields of the module at the south cell was 15.8mSv/hr. The move was uneventful. Don Dale was present for the move locking out parts of the code so only one movement of the crane could be done at a time.

Entry  Thursday, April 19, 2012, 09:48, David Wang, South Hot-Cell, Standard Operation, TM1, LP SIS Nb 6, leak check heat shield circuit 

Chad and I did a leak check on TM1 Nb5 target heat shield circuit. The leak detector was connected to heat shield circuit.The pumping down  of the  circuit is very smooth.Base leak rate is 0.0xE-9atm.cc/sec,and the base pressure is 0.0xE-4 torr. Chad checked the helium flow downstairs .He sprayed helium to both up and down VCR joints 2seconds each time. There is no any response on leak detector(30 seconds waiting time). Both joints did the same test twice, no response . Finally, he flushed helium around the target for 10 seconds,and i didnt see any response on leak detector either.The heat shield circuit on TM1 Nb5 target is leak tight at this stage.

Entry  Thursday, April 19, 2012, 09:36, Travis Cave, South Hot-Cell, Standard Operation, TM1, Nb#6, Electrical check Elec_Check_TM1_Nb6.PDF

Electrical check has been completed of TM#1 with Nb#6 attached. Our new micro-ohm meter was also used for the first time for this test.

Entry  Tuesday, April 17, 2012, 11:30, Travis Cave, South Hot-Cell, Standard Operation, TM1, no target, module moved 

TM#1 moved from conditioning station to the south hot cell, the module had a field of 16mSv/hr.  The move was not without excitement as the crane decided on its own to move 2 inches west on two occasions during the move.On the second time that the errant moved happened I hit the E-stop on the crane kill the power, the first time it happen it stopped the errant movement on its own.

Entry  Tuesday, April 17, 2012, 10:15, chad fisher, South Hot-Cell, Standard Operation, TM1, Nb#6, Target inserted into south hot cell 

Nb#6 has been inserted into the south hot cell in preparation for ionstallation onto TM1. During the pre-insertion inspection I noticed that I could see the foil installed into the ionizer tube and that in did not seem to be seated or concentric to the tube itself. I had Anders and Friedhelm check this and they deemed that it was ok.

Entry  Monday, April 16, 2012, 16:17, Bevan Moss, Conditioning Station, Standard Operation, TM1, No Target, High Voltage Test 

 A high voltage test was completed on a target free TM1 in the conditioning station. Only the turbo pumps on the target module were operational due to phase 2 construction. Testing started at 2:51PM with the following vacuum gauge readings, 1.6 x 10^-6 Diagnostics Box, 7.4 x 10^-7 Service Cap, 2.0 x 10^-6 Containment Box. Voltage was increased ~3kV at a time every minute until 21 kV was reached with a current of 0 uA. Voltage was then increased in ~1.5kV steps every 2 minutes until 30 kV was reach at a current of 60uA. This was held for 7 minutes until a spark occurred and the current spiked to 300uA and the voltage dropped. The voltage was dropped back to zero. The vacuum gauges had increased and read the following  1.6 x 10^-6 Diagnostics Box, 7.9 x 10^-7 Service Cap, 2.1 x 10^-6 Containment Box. Testing was restarted 2 minutes later (the vacuum gauges were still recovering for ~ another 2 minutes) and the voltage was quickly increased to 24kV reaching a current of 100uA. at 3:22 The current then fluxuated but trended up for the next 12 minutes peaking at a total current of 240uA. After this point the current started deceasing, at 3:41 the testing was concluded and the average current was ~170uA. The vacuum gauge readings were 1.6 x 10^-6 Diagnostics Box, 7.4 x 10^-7 Service Cap, 2.0 x 10^-6 Containment Box. It was deemed that this is "not ideal but good enough" to put the target on.  The maximum known required voltage will be ~22kV for Berillium which TM1 should be capable of providing.

Entry  Friday, April 13, 2012, 12:31, David Wang, Conditioning Station, Development, TM1, , TM1 and conditioning station leak check. 

  I hooked up the leak detector to the TM1 and conditioning station vacuum system, and did the air to vacuum leak check on TM1 and station. The leak detector base leak rate 0.0x-9Eatm.cc/sec,base pressure 0.0x -4E torr. I sprayed helium around all water quick connectors (especially heat shield),gasline and valves, all gauges, turbo-pumps, bellow,  flanges, and blank-offs. There is no any response on leak detector. The TM1 is leak tight on air to vacuum seal. All   water lines on this module had been pressurized with 80psi helium when module was located in ITW on this January, and they are all leak tight. Bevan and I did a leak check on new installed diagnostic box and all vacuum lines, gauges, and turbo pump last week, and they are all leak tight. So I would say the whole vacuum system on TM1 and conditioning station now is leak tight. Right now, the PNG1(inside containment box ) is 6.5 xE-6Torr, the IG1 (top service cap which close to turbo) is 2.1xE-6 torr, and the IG4 (inside diagnostic box) is 4.1xE-6 torr.  

Entry  Thursday, April 12, 2012, 14:40, David Wang, Conditioning Station, Development, TM1, , conditioning staion and TM1 is under TP1 and TP2 pumping now. 

TM1 moved to conditioning station to today. After moving, I connected the vacuum system which include all gauges ,vacuum lines , controllers,and fans.I started roughing the station through two turbo pumps(on TM1) . After 2 hours roughing, the station vacuum went to 100 mtorr. I started TP1 and TP2 on TM1 and turned on 3 gauges (png1 on service cap, ig1 on service cap ,and png4 on emittance box) . All  turbo pumps and high vacuum gauges work fine .The pumping down of the station is smooth so far. With only 1 hour turbo pump on all three gauges readings are at low -5 torr range. The fans for cooling the turpump are also turned on. Everything is fine.

Entry  Thursday, April 12, 2012, 09:38, Travis Cave, Conditioning Station, Standard Operation, TM1, no target, Move ot TM#1 

TM#1 has been moved from the NE silo to the Conditioning Station.

Entry  Thursday, April 05, 2012, 10:30, David Wang, ITE, Standard Operation, TM4, , I moved 5 shielding blocks back to ITE this morning. 

 MAA is secured .The ITE and MAA are ready for taking proton beam now.

Entry  Tuesday, April 03, 2012, 12:11, David Wang, Conditioning Station, Development, , , leak check on conditioning station vacuum system 

I did a leak check on conditioning station vacuum system today.The vacuum system had been roughed over night . This morning before the leak check,the convectron gauge  reading on emittance box is 20m torr which is reasonable. I hooked the  leak detector to system (without turbo pump  on) . The leak detector showed base LR 6.3xE-8 atm.cc/sec. At this base LR, I found 2 leaks up to low E -6range on that cross tube flange to small turbo pump, and the cross tube flange to vessel. I found some of the bolts on the flanges could be tightened more ½ to ¾ turn without difficulty. I checked all the fasteners on the box, cross tube, and turbo pump, tightened some of them. By doing it, the base leak rate dropped to 3.0x E-8 atm,cc/sec, base pressure still 0.0XE-4 torr. I sprayed helium again, the response I found before now disappeared. I waited for about 1hour, and let the leak detector base leak rate dropped to 1.3 xE-8 atm.cc/sec, and base pressure still at 0.0xE-4 torr. At the same time, i only use leak detector as back up pump for whole sysytem and shut off the valve to the scroll pump.By doing this , the leak detector is much stable on the base leak rate. With the help of Bevan, i sprayed the helium to all the vacuum  equipments again.This time,no any tiny response has been found on leak detector.The leak rate stayed at 1.2x E-8atm.cc/sec, and no change on pressure also. I checked helium bubble several times during the spray. The conditioning station vacuum system is leak tight.

Entry  Monday, April 02, 2012, 08:17, David Wang, Conditioning Station, Development, , , conditioning station IMC pump down. 

I pumped down conditioning station IMC today. The inside bellow pressure is -20 psi on the gauge.Visually checked the bellow before and after pump.The bellow is in retracted condition now.

Entry  Tuesday, March 13, 2012, 09:42, chad fisher, South Hot-Cell, Standard Operation, TM1, UCx#3, UCx#3 Autopsy 

An autopsy was performed on UCx#3 yesterday afternoon. This autopsy followed the plan written by Anders. Indeed, both sides of the target oven had seperated from the central block.Pictures were taken by Anders and Pierre.

After the disection the target was placed back in a can under argon. Any small piece were placed in a zip lock bag and also put in the can under argon.

    Reply  Tuesday, March 13, 2012, 12:24, Anders Mjos, South Hot-Cell, Standard Operation, TM1, UCx#3, UCx#3 Autopsy Inspection_of_UCx#3_in_the_South_Hot_Cell.docx

chad fisher wrote:

An autopsy was performed on UCx#3 yesterday afternoon. This autopsy followed the plan written by Anders. Indeed, both sides of the target oven had seperated from the central block.Pictures were taken by Anders and Pierre.

After the disection the target was placed back in a can under argon. Any small piece were placed in a zip lock bag and also put in the can under argon.

Pictures are available on DocuShare:

https://documents.triumf.ca/docushare/dsweb/View/Collection-8189

ISAC e-log entries:

https://web.accel.triumf.ca/isac_elog/Elog_shift_view.pl?shiftid=10803

See attachment for autopsy plan.

 

 

Entry  Tuesday, March 13, 2012, 09:43, chad fisher, South Hot-Cell, Standard Operation, TM1, UCx#3, UCx#3 to spent vault Vault_Storage_March_13_2012.pdf

UCx#3 was packaged into a spent can, double bagged and the bag and cans filled with argon as much as possible. Lid was attached and can moved to the storage vault. The target was placed in in Pail 93, and placed into slot 1C of the vault, it was 11.7mSv/hr when removed from the south hot cell. See attached file for latest vault details

Entry  Monday, March 12, 2012, 11:54, Travis Cave, South Hot-Cell, Standard Operation, TM1, no target, module moved 

TM#1 has been moved from the south hot cell to the north east silo, move went well.

Entry  Monday, March 12, 2012, 10:03, chad fisher, South Hot-Cell, Standard Operation, TM1, UC#3, UC#3 Removal IMG_0610.JPGIMG_0616.JPG

UC#3 was removed from TM1 this morning. Upon removing the oven heater bolts BOTH legs fell demonstrating that both sides of the oven tube have broken off from the central block.

Target was put into a can under argon for disposal after the module is removed from the cell.

The source tray looked to be in very good, clean condition.

IMG_0610.JPG

Entry  Monday, March 12, 2012, 09:19, Travis Cave, South Hot-Cell, Standard Operation, TM1, UCx#3, module move 

TM#1 with UC#3 was moved from the west maa to the south hot cell, move went well

Entry  Wednesday, February 01, 2012, 09:54, David Wang, ITW, Maintenance, TM1, , ITW and TM1 winter shut down vacuum leak check 

ITW and TM1 winter shut down vacuum leak check had been finished yesterday.All ITW primary vacuum vessel, secondary vacuum vessel, and TM1water lines had been leak checked.No any leak has been found .The ITW and TM1 are both leak tight.Some detail information below:

TM1 and ITW primary vacuum vessel and water lines:   The leak detector was hooked on BV2 after TP2.  Calibrate leak detector.leak detector BL 0.0xe-9atm.cc/sec,BP0.0xe-4 torr.

Sprayed helium to all primary vacuum vessel seals, flanges, turbo pumps,gauges, blank offs, bellows, and insulation blocks on TM1 and ITW. No any response had been found on leak detector.Also applied 60 psi helium to all water lines in TM1 for 5minutes each,no any response on leak detector.The leak rate stayed at 0.0xe-9 to 0.3 xe-9 atm.cc/sec all the time. All waterlines in TM1 are leak tight.

ITW secondary vacuum vessel:the leak detector was hooked on BV4s after TP4.Leak detector BL 0.0xe-9 atm.cc/sec ,BP 0.00xe-4 torr.  Sprayed helium to all secondary vacuum seals which include all bellows, tank to tank flange seals,tank flange to modules seals,beam diagnostics, gauges,turbo pumps, and EXIT 2 top service cap seals.No any response had been found on leak detector during the check. The secondary vacuum vessel is leak tight on ITW. 

All high vacuum gauges were read at 2-3xe -7 torr range  during the test time and no change during the test.

Entry  Monday, January 16, 2012, 09:30, David Wang, ITE, Maintenance, , , Changed all old inducion coils for flow sensors in ITE 

I had changed all old induction coils for flow sensors in ITE .I checked all ITE water signals on control boards in electrical room.They are all very stable and constant.All ITE inductions coils work fine now.

Entry  Thursday, January 12, 2012, 14:32, David Wang, ITE, Repair, TM4, , TP2 on TM4 has been replaced  

TP2 on TM4 has been replaced with a new turbo pump , I didnt  reset the controller in electrical room.So this new pump start to run at 8083 hours on ITE TP2 controller. The new TP2 pump properly  started. It works fine now.

Entry  Thursday, January 12, 2012, 08:43, Travis Cave, Spent Target Vault, Standard Operation, , , Spent targets to F-308s 

All targets in the mini storage have been moved to F-308s and those flasks have been moved over to rad waste. The transfer of target occurred on January 10th and the flasks were moved to rad waste on January 11th.  Contamination was found on the bottoms of some of the pails and was removed, some of the contamination was difficult but not impossible to remove from the pail bottoms.

Entry  Tuesday, January 10, 2012, 11:51, Grant Minor, Conditioning Station, Repair, , , IMC at Cond. Station is VENTED - DO NOT PUT MODULE IN IMC_Installation_and_Leak_Check_April_28_2011_011.jpg

Hi Remote Handling,

The guage on the IMC circuit in the Target Hall is reading atmosphere, and the bellows is currently relaxed (i.e. expanded), whereas it should be reading about -20inHg and the bellows should be contracted (i.e. compressed).

I've attached a photo of what the guage and fittings should look like when pumped down to -30inHg.

Either the IMC circuit has been vented, disturbed, or it has some kind of leak.  When I was in the Target Hall this morning, I saw the gauge bent around the railing at an awkward angle with a pretty severe bend in the copper line, it appeared to have been disturbed by the temporary glove box sitting at that level used by Rob Walker for nuclear ventilation work.

I will co-ordinate pump-down and leak check of the circuit, but the Conditioning Station cannot be used until this is repaired.

Cheers,

Grant

 IMC_Installation_and_Leak_Check_April_28_2011_011.jpg

Entry  Monday, January 09, 2012, 14:44, David Wang, ITE, Maintenance, TM4, , ITE and TM4 2012 winter shut down leak check is completed. 

I did a vacuum leak check on all ITE primary vacuum vessel and secondary vessel.I also did a helium pressure test(80psi ) on all TM4 water lines. There is no leak has been found.ITE and TM4 are both leak tight now.

ITE primary vacuum vessel and TM4 waterlines:

Hooked leak detector after TP1 between BV1. leak detector base pressure :0.0xe-4 torr. base leak rate:1.8x e-8 atm.cc/sec.sprayed helium around all TM4 and exit 1 ,2 module primary vessel including all flanges,  gauges, bellows,turbos,blank offs,etcThere is no  any response  on leak detector. All water lines  had been pressurized with 80 psi helium  for 5 minutes. The leak rate always stayed at 1.8xe-8 atm.cc/sec which is the base leak rate  on ITE this time, and no vacuum pressure change also.The TM4  water lines and ITE primary vacuum vessel are leak tight.

ITE secondary vacuum vessel:

Hooked leak detector after TP1S between BV1S. Leak detector base pressure :0.0xe-4 torr.Base leak rate:0.0xe-9 atm.cc/sec. Sprayed helium around all TM4,EXIt 1,2  module secondary vessel including alll flanges,gauges, air cylinders , valves, and blank-offs.There is no any response on leak detector . tThe late rate  kept at 0.0XE-9 ATM.CC/SEC, and no pressure change either.The ITE secondary vacuum vessel is leak tight.

Entry  Thursday, January 05, 2012, 11:40, Travis Cave, Spent Target Vault, Standard Operation, , , Target swapping  Vault_Storage_January_5_2012.pdfMini_Vault_Storage_January_5_2012.pdf

Looks like the UC target s #1 and #2 were found invalidprize winners for their all inclusive trip to Chalk River and have thus been placed back in to storage for the next draw. In their place a pair of lucky Ta targets won, seems to be Ta lucky draw this year, Ta#28 and #29 have been placed in the mini storage for several fabulous day and wondrous nights, before being whisked away on their all inclusive one way trip to Chalk River. See attachments for the status of both vaults.

Entry  Wednesday, January 04, 2012, 13:49, Travis Cave, Spent Target Vault, Standard Operation, , , Moving the spent targets to mini storage. 

Well the first of this year's lucky winners to win a fabulous one way trip to Chalk River are as follows. UC#1, UC#2, Ta#25, Ta#26, and Ta#37. First these lucky winners will get to stay several days and night in the lovely all inclusive mini vault before being loaded in to their very own private F-308 flasks to be whisked away off to fabulous Chalk River.

Entry  Thursday, December 15, 2011, 13:08, Travis Cave, Spent Target Vault, Standard Operation, , , Spent Target Assay Vault_Storage_December_14_2011.pdf

Spent target assay completed. A total of 16 target were looked at, 13 were low enough to be assayed and those 13 are at shippable levels, the other 3 of the 16 looked at were too hot to ship and assay. See attached pdf for complete details.

Entry  Thursday, November 24, 2011, 10:40, Travis Cave, ITW, Standard Operation, TM1, UCx#3, Module move 

TM#1 with UCx#3 moved from the conditioning station to the west target station.

Entry  Thursday, November 24, 2011, 10:39, Travis Cave, ITW, Standard Operation, TM1, UCx#3, Module move 

TM#1 with UCx#3 moved from conditioning station to west target station. Move went well.

Entry  Tuesday, November 22, 2011, 15:07, Bevan Moss, Conditioning Station, Standard Operation, TM1, UCx #3, HV testing UCx_#3_HV_testing.JPG

 High Voltage (HV) testing was completed on TM1 today. Vacuum was very good 1.9 x 10^-7 T in the service cap, 3.2 x 10^-7 in the containment box, and 2.0 x 10^-6 in the secondary. The voltage was successfully brought up to 27kV with a current draw of 0.12mA and o sparking. At the next step, 30 kV, the current draw was above 0.3mA and sparking was beyond 20 sparks per minute. The module should not be taken above 27kV. There is the possibility this voltage can be increased with conditioning but it is very unlikely. See attached for a graph of the testing. These results are comparable to the results without the source tray (see previous elog)

Entry  Monday, November 21, 2011, 13:49, David Wang, Conditioning Station, Standard Operation, TM1, , TM1 full leak check in conditioning station 

TM1 full leak check in conditioning station has been fulfilled this morning.Both air to vacuum leak check and waterlines helium 80psi pressure test are fine.The result:

Air to vacuum helium spray:base leak rate on leak detector 1.6x E-9 atm .cc/sec.base pressure0.0xE-4 torr. sprayed helium around all flanges, turbo pumps,panels,bellow,insulation stands, gauges. No Response on leak detector. Air to vacuum seals on TM1 is leak tight.

Helium pressure test on all water lines.with 80 psi helium 3minutes test:

        PNG1 :2.4XE-7torr .PNG4 :2.6x E-6torr . IG1 :5.1xE-7torr.

A :target oven(+)  BL:2.0xE-9 atm.cc/sec .First minute no response,then climbed to1.9xE-8 atm.cc/sec. Stabled at 1.9xE-8 atm.cc/sec to 3 minutes.

B:target oven(-)    BL:5.5x E-9 atm.cc/sec.First 80 seconds no response, then climbed to 1.8xE-8atm.cc/sec. Stabled at 1.8xE-8atm.cc/sec to 3 minutes.

C:tube heater(-)   BL:8.0xE-9 atm.cc/sec .First minute no response ,then climbed to 2.7xE-8 atm.cc/sec. Stabled at 2.7x E-8 atm.cc /sec to 3 minutes.

D: tube heater(+) BL: 1.0xE-8 atm.cc/sec. First minute no response , then climbed to 1.8xE-8 atm.cc/sec. Stabled at 1.8x E-8 atm.cc/sec to 3minutes.

G:EE  BL:1.0xE-8 atm.cc/sec .First 1.5 minutes no response , then climbed to 1.7x E-8 atm.cc/sec. Stabled at 1.7x E-8atm.cc/sec to 3minutes.

F:heat shield   BL:1.2x E-8 atm.cc/sec. First  1.5 minutes no response , then climbed to 1.9 xE-8 atm.cc/sec. Stabled at 1.9 xE-8 atm.cc/sec to 4 minutes. Total test time 4 minutes.

I: mounting plate    BL:1.2 x E-8 atm.cc/sec.     NO RESPONSE on leak detector  in 3minutes.

M: window   BL:1.2x E-8 atm.cc/sec First 1.5 minutes  no response,then climbed to 2.0xE-8 atm.cc/sec . Stabled at 2.0xE-8 atm.cc/sec to 3minutes.

The base pressure on leak detector stayed at 0.0x E-9 torr through all the test, and no pressure response on high vacuum gauges.

Entry  Friday, November 18, 2011, 16:29, Bevan Moss, Conditioning Station, Standard Operation, TM1, N/A, High Voltage (HV) testing TM1_High_Voltage_Test_Nov_16_2011.JPG

 TM1 was high voltage tested without a target on November 16, 2011 with Don Jackson, Pierre Bricault, and Bevan Moss. The module was able to hold up to 25 kV but between that and 32 kV there was lots of discharge which could be measured in the vacuum. See the attached plot for the voltage current and sparks.

Entry  Friday, November 18, 2011, 11:09, Travis Cave, Conditioning Station, Standard Operation, TM1, UCx#3, Module move 

TM#1 with UCx#3 has been moved from the south hot cell to the conditioning station. Move went well.

Entry  Friday, November 18, 2011, 09:56, chad fisher, South Hot-Cell, Standard Operation, TM1, UCx#3, UCx#3 Installation 

UCx#3 has been installed on TM1.

Leak check also complete.

Base Leak Rate 0.0 x 10-9

Pressure 0.0x10-4

Two checks on upper heat shield joint - no response (2 sec spray/check)

Two checks on lower heat shield joint - no response(2 sec spray /check)

10 sec flood of all heat shield joints - no response

Electrical check coomplete.

Entry  Friday, November 18, 2011, 09:44, Travis Cave, South Hot-Cell, Standard Operation, TM1, UCx#3, Electrical check ITW_UC#3_Elec_check.PDF

Electrical checks of TM#1 with UCx#3 have been completed. They all appear to be with in operational range. All megger checks were done at 500 volts. See attached file for details.

Entry  Thursday, November 17, 2011, 11:52, Travis Cave, Conditioning Station, Standard Operation, TM1, no target, Module move 

TM#1 moved from the conditioning station to the south hot cell. Move went well.

Entry  Thursday, November 17, 2011, 11:51, Travis Cave, Spent Target Vault, Standard Operation, , TaC#1, Spent target move 

TaC#1 was moved from the south hot cell to the storage vault. It was placed in pail#92 and put in vault slot 7B. It was 239mSv/hr upon removal from the south hot cell.

Entry  Wednesday, November 16, 2011, 07:46, chad fisher, South Hot-Cell, Standard Operation, TM1, TaC#1, Inspection of TaC#1 

Inspection of TaC#1 showed that the oven was indeed broken on the A+ (left oven leg) side of the central block.

See the following for pictures.

https://documents.triumf.ca/docushare/dsweb/View/Collection-7438

Entry  Wednesday, November 16, 2011, 07:44, chad fisher, South Hot-Cell, Standard Operation, TM1, TaC#1, TaC#1 Removal and inspection 

November 15, 2011 removed TaC#1 from TM1 and inspected TM1 for any obivous signs of trouble (Problems with EE at end of run).

Upon starting removal of the high current conductor fastener on A+ (Left oven leg) it became clear right away that the oven of the target was broken as the leg moved as soon as the fasten was loosened.

Inspection of TM1 with the target removed yeilded no obvious signs of trouble, save a piece of capton tape found on the sliding tray directly below the service tray.

 

Entry  Tuesday, November 15, 2011, 13:08, Travis Cave, Conditioning Station, Standard Operation, TM1, , Move ot TM#1 

TM#1 has been moved from the south hot cell to the conditioning station. Move went well.

Entry  Monday, November 14, 2011, 14:07, Travis Cave, ITW, Standard Operation, TM1, TaC#1, Module move 

TM#1 with TaC#1 from the west target station to the south hot cell. Move went well.

Entry  Thursday, November 10, 2011, 14:33, Travis Cave, Spent Target Vault, Standard Operation, , , Spent Target Assay 

For the week of November 7th 2011, four of a possible ten targets that are in storage were assayed. Targets are as follows:

Target             General average field @ 1 metre from edge of pail

SiC#24           1.99 mSv/hr

Nb#4               3.89 mSv/hr

Ta#25              4.57 mSv/hr

Ta#37              0.47 mSv/hr

 

These four are all viable spent targets to be shipped. We still need another couple of days of "UNINTERRUPTED" time to assay the remaining six targets, for us to have enough to make a ship of five to Chalk River.

Entry  Friday, November 04, 2011, 11:12, Travis Cave, Conditioning Station, Standard Operation, TM4, SiC#26 High Powered, Module move 

TM#4 with SiC#26 HP move from the conditioning station to the East Target Station, move went well.

Entry  Wednesday, November 02, 2011, 13:12, Bevan Moss, Conditioning Station, Standard Operation, TM4, SiC#26 High Powered, High Voltage (HV) testing 

 The silicon carbide targets voltage was raised to 42 kV today before continuous current draw was observed. It took roughly 10 minutes to raise the module to this voltage with only the occasional spark. The ION gauge reading was 2.0 x 10^-6 T, The service cap IMG 3.6 x 10^-6 T, and the secondary vacuum was 4.5 x 10^-6 T. Setup check and conditioning was performed by Pierre.

Entry  Tuesday, November 01, 2011, 11:50, David Wang, Conditioning Station, Standard Operation, TM4, , TM4 leak test on conditioning station 

 I did a leak check again on TM4 today. This time, the leak detector pump to the bottom on both base pressure(0.0xE-4 torr) and base leak rate(0.0xE-9 atm.cc/sec). All high vacuum gauges on TM4 and conditioning station at -6torr range.IG1 is 3.3-6torr,PNG5(top of service cap)is 6.5-6 torr, and the PNG4(bottom of the vessel )is 8.7-6torr. For air to vacuum leak checking, I checked the panel we moved last week on service cap by spraying helium around the panel. There is no any response on leak detector. The panel is leak tight. Also I sprayed helium around the tube heater (+) water cap and blue nylon stand. They are also leak tight. Then, I put 80 psi pressure air to the “D” circuit first. With 80 psi pressure air for 5 minutes, the leak detector has no any response on it. Also all high vacuum gauges stayed at same level .Then I checked it with 80 psi pressure helium for 3 minutes. The leak detector has a response on leak rate with pressure helium same as last time. It climbed from the 0.0xE-9 atm. cc/sec quickly to high -8 range then slow down. The leak rate finally climbed to 2.0 X E-7 atm.cc/sec this time. There is no base pressure change on leak detector. All high vacuum gauge readings no change during the test time. There is a small helium leak at 80 psi pressure test on “D” circuit. But we can not locate it at this stage. Also I don’t want to disturb this circuit any more before the febiad run since this time I saw a little bit increase on leak rate comparing to last time when I checked it. If we really like to find this small helium leak, I would suggest we do it after the febiad run.    Thank you.

Entry  Monday, October 31, 2011, 08:51, Travis Cave, South Hot-Cell, Standard Operation, TM4, SiC#26 High Powered, Module move 

TM#4 with SiC#26 HP moved from the south hot cell to the conditioning station.

Entry  Friday, October 28, 2011, 14:42, Bevan Moss, South Hot-Cell, Maintenance, TM4, , Leak check on service cap feed through IMG_1906.JPGIMG_1905.JPGIMG_1908.JPG

 After Chad and Davids leak check results from the containment box it was decided to perform a leak check on the feed through stem in the service cap. This is a known point of failure on TM1 and the same design flaw is likely in TM4. Once the service cap was open a visual inspection was performed and some oxidization of the copper line on the tube heater (+) circuit was observed (see attached pictures). The leak check was performed with the cart at a base pressure of 0.0 x 10^-4 Torr and base leak rate of 0.0 10 x 10^-9 atm cc/sec. A total of 4 joints were checked and no response was found. The service cap was then flooded with helium and once again no response was found. It was decided to give the module a clean bill of health, make note of the baseline test from the conditioning station, and continue to monitor the circuit.  

Entry  Friday, October 28, 2011, 14:29, Bevan Moss, Conditioning Station, Standard Operation, TM4, , Leak Check on October 27/10/2011 

A leak check was performed on the module on October 27/10/2011 by David Wang and was reported to Bevan Moss but it never made it into the Elog system. This entry is to summarize the results of that testing. All circuits were pressurized to 80 psi with helium and every line except the tube heater (+) showed no or small responses as experienced before. The tube heater line had a slightly larger response under the conditions summarized below:

Varian 959

Base Pressure                   7.0 x 10^-3 Torr

Base Leak Rate                  7.5 x 10^-9 atm cc/sec

Gauges

IG1                                         2.0 x 10^-6 Torr

PNG5                                    9.6 x 10^-6 Torr

PNG4 (C.S.)                        2.4 x 10^-5 Torr

Convectron (Back line) 20mTorr

 The leak rate quickly climbed to 3.0 x 10^-8 atm cc/sec then constantly climbed to 1.4 x 10^-7 atm cc/sec for 2 minutes. David repeated this test again at the end of the leak test and found the same results. In the past we have called this a leak and attempted to find its location and repair it. David believes that this isn’t a real leak as we have been able to achieve very good vacuum on TM4 all year and that we do not normally touch the feed through stem on this circuit. This result makes me nervous as the total differential is roughly the same as that we found on the UCx#2 run(which was at a higher vacuum).

The result of this test caused the module to move back to the hot cell for further more localized leak checking.

 

 

 

 

 

 

 

 

 

 

Entry  Friday, October 28, 2011, 09:37, chad fisher, South Hot-Cell, Standard Operation, TM4, SiC#26 HP Febiad, SiC#26 installed on TM4 

HP febiad target SiC#26 was installed onto Tm4 on Monday morning.

"JP's" connector required lossing of the two mounting fasteners. Connector was pushed tight to its mating half on the source tray and both fasteners retightened, and the mating checked; it was good.

Two new 7/8 long 3/8-16 fasteners were used for the febiad coil connections.

Installation went well.

Leak check was performed:

 

Base Pressure: 0.0x10-4

Stable leak rate 0.0x10-9

Left vcr joint was checked two times with a 2 second spray of helium with a 60 second waiting time between sprays; no response.

Right vcr joint was checked two times with a 2 second spray of helium with a 60 second waiting time between sprays; no response.

Fllod of system with a 6 second spray; no response.

Entry  Friday, October 28, 2011, 09:30, chad fisher, South Hot-Cell, Repair, TM4, , Tube Heater + Leak Check C.B. 

Base Pressure: 0.0x10-4

Stable Leak Rate: 0.0x10-9

Leak check of tube heater circuit, containment box side was performed.

Initail check at tube heater block on source tray yeilded a response 60 sec after the 2 second spray of helium. The response was very small and recovered immediately.

This area was checked twice more but the reponse could not be recreated.

Joint at the waterblocks was tested with an intial 2 sec spray. No response after 60 sec.

Waterblock joint was tested again with a 4 second spray. No response after 60 sec.

 

 

 

Entry  Friday, October 28, 2011, 08:24, Travis Cave, Conditioning Station, Standard Operation, TM4, SiC#26 High Powered, Module move 

TM#4 moved from conditioning station to south hot cell. For further leak checking.

Entry  Tuesday, October 25, 2011, 16:57, Bevan Moss, Conditioning Station, Standard Operation, TM4, , Turbo Pump 1 issues 

Roughing on TM1 started at ~15:00 today by ~16:30 the module had reached a pressure of ~200 mTorr and the turbo pumps were turned on. TP1 failed to achieve normal operation and we running at approximately 4KRPM and 50W with 6.1 A of current draw. TP2 was able to achieve normal operation. The controller for TP1 was then powered off and back on but that failed to resolve the issue. The controllers for TP1 & 2 were then switched at which point TP1 again failed normal operation and TP2 achieved it, thus eliminating the controller as the issue. The turbo pumps have been turned off and the roughing pump left on for overnight in case Vacuum group wishes to do any additional diagnosis. 

Entry  Tuesday, October 25, 2011, 11:58, Travis Cave, South Hot-Cell, Standard Operation, TM4, SiC#26 High Powered, Module move 

TM#4 with SiC#26 HP has been moved from the south hot cell to the conditioning station.

Entry  Tuesday, October 25, 2011, 08:47, Travis Cave, South Hot-Cell, Standard Operation, TM4, SiC#26 High Powered, Electrical check 

TM#4 with SiC#26 HP has been checked electrically it has passed. It was noted that the Megger check of the Oven to Chassis (earth ground) and Oven to 60kV Common is low but will not hinder running, according to Don Jackson.  Also yesterday the transition piece that sits on the 55 pin connector was damaged from excessive handling, it was removed and repaired and it now back in place.

Entry  Wednesday, October 05, 2011, 09:41, Travis Cave, Spent Target Vault, Standard Operation, , UCx#2, Spent target move 

The spent UCx #2 target has been moved into storage. It was placed in tray 5A and is in Pail #91, it was 8.91mSv/hr upon removal from the south hot cell. There are 5 free slots left in the storage vault.

Entry  Tuesday, October 04, 2011, 14:13, Travis Cave, ITW, Standard Operation, TM1, TaC#1, Move ot TM#1 

Move of TM#1 with the TaC#1 target has been moved from the south hot cell to the west target station.

Entry  Monday, October 03, 2011, 14:52, Travis Cave, South Hot-Cell, Standard Operation, TM1, TaC#1, Electrical check 

TM#1 with TaC#1 installed passed the electrical test. With a value of 882MOhms that was meggered from the heat shield to the chassis, all other measurements are within spec.

Entry  Monday, October 03, 2011, 11:54, chad fisher, South Hot-Cell, Standard Operation, TM1, UCx#2 - TaC#1, Target change UCx#2-TaC#1 

UCx#2 has been removed from Tm1 and put in a bucket with a slow argon feed and a lid placed lossely on top.

 

TaC#1 ITW has been installed and is awaiting testing at the cell.

Entry  Monday, October 03, 2011, 11:00, Travis Cave, ITW, Standard Operation, TM1, UCx#2, Move from west station to south hot cell 

TM#1 with UCx#2 has been moved from the west station to the south hot cell. Move went well.

Entry  Thursday, September 29, 2011, 11:11, Travis Cave, Spent Target Vault, Standard Operation, , Ta#36, Spent target move 

The spent Ta#36 has been moved to the storage vault. It was placed in pail #90, and placed into slot 3B, it was 111mSv/hr upon removal from the south hot cell. There are 6 free slots left in the storage vault.

Entry  Wednesday, September 28, 2011, 11:59, Travis Cave, South Hot-Cell, Standard Operation, TM4, no target, TM#4 moved from South Hot Cell to to North East Silo. 

TM#4 moved from South Hot Cell to to North East Silo, move went well.

Entry  Wednesday, September 28, 2011, 10:06, chad fisher, South Hot-Cell, Standard Operation, TM4, Ta#36, Ta#36 Removal 

Ta#36 was removed from target module 4.

The standard, unexplained, un-investegated, un-resolved "arc" were again present on "JP's connector", otherwise no apparent problems visible.

 

Chad

 

 

Entry  Wednesday, September 28, 2011, 09:07, Travis Cave, ITE, Standard Operation, TM4, Ta#36, Move of TM#4 from East target station to south hot cell. 

Move of TM#4 with Ta#36 from East target station to south hot cell, move went well.

Entry  Wednesday, September 14, 2011, 10:32, Travis Cave, Spent Target Vault, Standard Operation, , Ta#37, Spent target move 

Ta#37 has been moved from the south hot cell into the storage vault. The target is in pail #89 and in spot 6A in the vault. It was 840uSv/hr upon removal from the south hot cell. There are 7 free spots left in the vault.

Entry  Thursday, September 01, 2011, 09:11, Don Jackson, ITW, Standard Operation, TM1, UCx#2, Argon Venting West Station 

West target station is setup to use argon for tank venting.  There is 1200 PSI remaining on argon bottle in electrical room.  That is sufficent for venting west target station to atmosphere twice.  ISAC Operations has been previousily contacted and their procedures for venting remain the same except that they can not rely on ITW:CG4S to determine when at atmospheric pressure.  I have asked them to contact me if an unscheduled vent is required.

Entry  Wednesday, August 24, 2011, 17:11, Bevan Moss, Conditioning Station, Standard Operation, TM1, UCx#2, Leak Check, HV conditioning and Module Move 

Today a leak check on TM1's external seals and the heat shield line was completed by David Wang. After 16 hours of the turbo pumps running on the conditioning station stations pressures were 3.6 x 10^-6 T, 1.2 x 10^-5 T, and 1.8 x 10^-6 T for the containment box, secondary vacuum, and service cap respectively. This is a significantly quicker pump down after the cross with small turbo pump was installed on the vacuum vessel. The base pressure of the leak testing cart was 0.0 x 10^-4 T and the leak rate was 1.2 x 10 x 10^-8 atm cc / sec. There was no response from the external test where the module was sprayed with helium. The heat shield line was pressurized with 80 psi helium which caused the leak rate to climb to a maximum of 2.5 10 ^-8 atm cc / sec but dropped to 1.9 x 10^-8 atm cc / sec and was stable there, the total test time was 2 minutes. This test was repeated another time and had similar results.  These results although showing a slight increase in the detected leak rate are withing acceptable and indicate that the module is leak tight. 

At 9:30 the HV check and conditioning started (~17 hours turbos on), the secondary vacuum, containment box and service cap had the following pressures in Torr respectively, 1.0 x 10^-5, 3.2 x 10^-6, 1.6 x 10^-6.  The voltage was steadily raised with virtually no current up to 28.5 kV which was achieved at 9:50. When raised to 30 kV the current increased significantly to ~300 uA and a large amount of sparking occurred. The voltage was dropped to 0 volts for 2 minutes and then was returned to 30 kV at 10:03, the current draw was around 200 uA and climbing. After a few sparks and time the current had dropped to 120 uA. This indicates that the module is still conditioning and matches what is observed by the control room when the module is in ITW. The module was deemed acceptable for this current run and was then vented with argon this took about 2 hours.

The module was then remotely moved from the conditioning station to ITW. When first attempting to transfer the controls to the remote control room they were not transferred and when testing the up command as per standard procedure the module dropped down slightly. David Wang went to lock out the target again and the controls were successfully transferred. A note of this was made in the log book. Apart from this the move went smoothly.  

Entry  Wednesday, August 24, 2011, 16:35, Bevan Moss, South Hot-Cell, Repair, TM1, UCx#2, Move, inspection and repair 2011-08-23-17-41-40.UCx_Leak_August_22_2011.jpg

 On August 22nd TM1 was vented with Argon in the conditioning station. It had been pumping with just the roughing pump over the weekend so the UCx#2 target would not be exposed to oxygen. The move went without incident and took roughly an hour to complete. Once at the hot cell the panel was removed by Tom Lyth and a leak check completed with Bevan, David Wong, Grant Minor, and Tom Lyth present. The connections to source tray were checked starting at the top. Each connection was checked on either side of the VCR and at the center through the hole in the nut. For both connections on the source tray there was no response from the leak cart which was at a pressure of 0.0 x 10^-4 T and had a baseline leak rate of 0.0 x 10^-9 atm cc / sec. The leak check then proceeded to VCR connections on the Target. A leak was found on the upper VCR connection of the target and was repeatable. This leak was detected at the hole of the VCR nut connection by priming the line with helium and placing it next to the hole in the VCR connection. Response time was between 5 and 10 seconds to a maximum of 2.6 x 10^-8 atm cc / sec. The lower connection also appeared to have a small leak rate of 4.4 x 10^-9 atm cc/ sec but could be a result of helium drift. Unfortunately the target is not design to be repaired with manipulators and required the target to be removed from the south hot cell and repaired in the anteroom. The anteroom was prepared for the target by lining much of it with plastic so to prevent the spread of contamination. Once the target was in the anteroom it was leak checked again, the base pressure was 0.0 x 10^-4 and the base leak rate was 0.0 x 10^-9. A response from the upper connection again was detected in the 10^-8 range but no leak was found in the lower connection. It was attempted to tighten the joint to stop the leak but this caused it to increase to the 10^-7 range. This increase in leak rate is as expected from past experience because copper gaskets are used rather than silver plated ones. The heat shield cover was loosened and the gaskets from from both joints were replaced with the silver plated ones. The target was then leak check and passed with no response once again with a full pump down. The target was had an electrical checked with the megger and was within spec. The target was then placed in an argon bag and returned to the hot cell. The bag was damaged went placing it in the hot cell and there were not any acceptable options for leaving the target over night. The target was removed and and placed in 2 bags filled with argon for over night.

On August 23rd the target was removed from the argon bags that were still inflated and returned to the hot cell. The target was re-installed on the target module by Grant Minor, Tom Lyth, an Bevan Moss. One VCR gasket fell off during the first attempt and it appeared that the right target leg may have been slightly bent at some point. Other than that the installation went smoothly but slowly. The heat shield line was then leak checked once again by Grant, Tom, David, and Bevan and no response was detected from the source tray or target VCR connections, the base leak rate and pressure once again achieved the minimum detectable levels. The target module passed the electrical check with the megger, this test was completed by Bevan and Pierre Bricault. The module was then moved from the south hot cell to the conditioning station. Roughing was started at 3:00 and the turbo pumps were turned on at 3:45. The module was left to pump over night.     

Entry  Friday, August 19, 2011, 14:52, Bevan Moss, Conditioning Station, Repair, TM1, UCx#2, Leak Check 

 A leak check was performed on the module when it was in the conditioning station today. There were no external leaks found. When the coolant lines were check a small leak was found in the heat shield circuit. Base leak rate was 6.7 x 10^-9 atm cc /sec and rose to 4.1 x 10^-9 atm cc /sec quickly (~3 seconds) and remained there for the 2 minute test. The remaining lines had small responses as usual but the highest response was in the low 10^-8 atm cc /sec range. The pressures were recorded as 1.2X10^-6 T, 2.7 x 10^-6 T and 1.1 10^-5 T in the service cap, containment box, and secondary respectively. The module was then vented with argon which took ~1.5 hours, vessel was pressurized to ~ 1 psi. A panel was then removed to leak check the feed through stem of the heat shield pressure of the line was recorded to be 0.0 x 10^-4 T and a leak rate of 1.3 x 10^-8 atm cc/sec was achieved. The stem was sprayed and no response was found. Swipes of the were taken of the panel (150 counts) and the containment box (3000 counts). The panel was then returned and the vessel roughed out for the weekend, it will be vented and moved to the south hot cell on Monday where the VCR fittings will be checked again and then tightened.  

Entry  Thursday, August 18, 2011, 16:07, Bevan Moss, Conditioning Station, Standard Operation, TM1, UCx#2, Pump Down 

 Pump down in the conditioning station started at ~2:40 for rough down. The turbo pumps were turned on at ~3:30 and at 3:52 the pressures were reading as follows:

IMG in the containment box 9.2 x 10^-5 T

IMG in the secondary 2.0 x 10^-3 T

ION in the service cap 4.6 x 10^-5 T

Note that the cross has been installed on the vacuum vessel which now includes a turbo pump and the IMG 100.

Leak check will occur tomorrow.

Entry  Thursday, August 18, 2011, 14:09, Bevan Moss, South Hot-Cell, Standard Operation, TM1, UCx#2, Leak and Electrical Check plus Remote Move to Conditioning Station 

 TM1 with UC#2 had the target installed, the heat shield line was pumped on and achieved a vacuum of 0.0 x 10^-4 Torr and a  leak rate of 0.0 x 10^-9 atm cc / sec with no response when sprayed with helium. An electrical check was completed by David and myself all values were withing tolerance.  The module was then moved from the south hot cell to the conditioning station where it will start pump down. The move was uneventful every operated as it should and there were no crashes minor or large. It was attempted to fill the containment box with argon prior to closing it but assuming that didn't work I estimate the target was exposed to air for a total of ~4 hours during installation and move. 

Entry  Thursday, August 18, 2011, 13:12, chad fisher, South Hot-Cell, Standard Operation, TM1, UCx #2, UCx #2 Installation 

UCx #2 has been installed onto TM1.

Installation went well except the left leg got bent slightly sometime between testing on the jig and installation onto the module (probably during removal for the argon filled bag). Leg was gentle offered into place and its clearance with the heat shield double checked with both a mirror and goose neck camera. Leg was close to ther heat shield but appeared to have clearance. Anders and John Wong viewed this and deemed it ok. Video images of this clearance were recorded.

Leak checking was also completed successfully:

Base pressure on the leak detector was a constant 0.0 x 10-4, Stable leak rate was an unwavering 0.0 x 10-9.

Both heat sheild circuits were checked twice (starting with the highest gland) and sprayed with a 2 second burst of helium into the test hole in the nut. No reponses were seen after 1 minute an any of the circuits.

Bevan Moss and David Wang performed an electrical check which they relayed to me that the module with target installed had passed.

 

Entry  Wednesday, August 17, 2011, 13:09, Bevan Moss, ITW, Standard Operation, TM1, Ta #37, TM1 move from ITW to Hot Cell 

 TM1 with Ta #37 target was moved from ITW to the south hot cell. The rotation of TM1 may have been off slightly during the final removal from ITW but it was minimal. Entry into the south hot cell went with out incident. This was my first time moving the module without the presence of Travis Cave. 

Entry  Wednesday, August 03, 2011, 11:24, Travis Cave, ITW, Standard Operation, TM1, Ta#37, Module move 

TM#1 with Ta#37 has been moved from the conditioning station to the the west target station, move went well.

Entry  Tuesday, August 02, 2011, 09:41, Pierre Bricault, Conditioning Station, Repair, TM1, ITW-TM1-Ta#37-LP-SIS, Test high voltage on TM1 

 TM1 has received the Ta#37-LP and has been pumping since thursday. This morning the pressure gauges read, IMG1: 1.6x10^-6 T and IG1: 7.4x10^-7 T.

The high voltage power supply has been connected to all high voltage feedthroughs and the voltage raise to 42 kV. 

High voltage conditioning started around 20 kV and after few minutes we were able to go up to 40 kV. 

The pressure increases on both locations, IG1 went up to 8.1x10^-7T and IMG1 went up to 1.8x10^-6T.

The module is good to go. 

Entry  Thursday, July 28, 2011, 14:07, Travis Cave, Conditioning Station, Standard Operation, TM1, Ta#37, Module move 

Tm#1 with Ta#37 moved from the south hot cell to the conditioning station. Move went well.

Entry  Thursday, July 28, 2011, 12:02, Travis Cave, South Hot-Cell, Standard Operation, TM1, Ta#37, Electrical check Electrical_Check_for_TM_1_with_Target_attached_Ta37.pdf

TM#1 has passed the the electrical check.

Entry  Wednesday, July 27, 2011, 14:34, Travis Cave, South Hot-Cell, Standard Operation, TM1, , Module move 

TM#1 has been moved from the Conditioning Station to the South Hot Cell for the installation of Ta#37.

Entry  Monday, July 25, 2011, 14:49, Travis Cave, Spent Target Vault, Standard Operation, , Ta#35, Spent target move 

Ta#35, in pail #88, has been place into spent target storage, in spot 6C. Upon removal from the South Hot Cell it was 411mSv/hr our hottest target to be placed into storage to date. There are 8 free slots for targets left in the vault.

Entry  Thursday, July 21, 2011, 17:39, Bevan Moss, Conditioning Station, Repair, TM1, , TM1 Ground Electrode, Thermocouple line, Stem, panel, repairs IMG_1681.JPGIMG_1662.JPGIMG_1686.JPGIMG_1695.JPG

Over the period of July 20-21st TM1 had several repairs completed and tested. The easiest of the repairs was the installation of a gasket and a blank off. The next repair was to replace the 2 oring on the side panels that were removed for inspection and repair. The instrument panel oring was replaced again and the previous one measured. Both were found to have the correct diameter of 0.131 inches for the seal groove. When attempting to cut the thermocouple line back to an acceptable distance it detached from the stainless tube running down the high voltage chase. It was discovered that it was only being held in place with heat shrink and that the bend consisted of a hand made copper tube that was flared slightly, a truly poor electrical and mechanical connection. Also discovered was the thermocouple wire was left in the tube, this too was removed. The stainless steel tube was then secured to the tube heater (C) lines with a PEEK tie wrap. The port where the thermocouple line was then blanked off. The extraction electrode and mounting plate feed through stem repair went as practiced and no unexpected events occurred. One thing of note is that because the lines are twisted and some of the tube was removed the quick connects are no longer facing the same direction they were before. During these repairs the Ion gauge screen contacted a filament and caused a fault, this was repaired by edi who rotated the gauge. Roughing was started at ~10 am on July 21st and the turbo pumps turned on at 10:45.  At 13:20 all of the lines and external seals were tested and no leaks were found. The module was at a pressure of 2.9 x 10^-5 Torr (IMG) and 1.4 x 10^-5 Torr (ION). The leak test cart was at a pressure of ~2.7 x 10^-2 Torr and a leak rate of 1.1 x 10^-2 atm cc/sec for the external leak test and the repaired lines. A small response was found in the Tube heater (D) where the leak increased to 2.1 x 10^-8 atm cc/sec. The leak test cart would then no longer drop below 1.9 x 10^-8 atm cc/sec and there was no response measured for lines C, B, and A. Over all very positive results! After 6 hours of pumping down the pressures were 2.0 X 10^-5 Torr (IMG) and 9.7 x 10^-6 Torr (Ion).  

 

 

    Reply  Friday, July 22, 2011, 10:30, Bevan Moss, Conditioning Station, Repair, TM1, , TM1 Ground Electrode, Thermocouple line, Stem, panel, repairs 

Bevan Moss wrote:

Over the period of July 20-21st TM1 had several repairs completed and tested. The easiest of the repairs was the installation of a gasket and a blank off. The next repair was to replace the 2 oring on the side panels that were removed for inspection and repair. The instrument panel oring was replaced again and the previous one measured. Both were found to have the correct diameter of 0.131 inches for the seal groove. When attempting to cut the thermocouple line back to an acceptable distance it detached from the stainless tube running down the high voltage chase. It was discovered that it was only being held in place with heat shrink and that the bend consisted of a hand made copper tube that was flared slightly, a truly poor electrical and mechanical connection. Also discovered was the thermocouple wire was left in the tube, this too was removed. The stainless steel tube was then secured to the tube heater (C) lines with a PEEK tie wrap. The port where the thermocouple line was then blanked off. The extraction electrode and mounting plate feed through stem repair went as practiced and no unexpected events occurred. One thing of note is that because the lines are twisted and some of the tube was removed the quick connects are no longer facing the same direction they were before. During these repairs the Ion gauge screen contacted a filament and caused a fault, this was repaired by edi who rotated the gauge. Roughing was started at ~10 am on July 21st and the turbo pumps turned on at 10:45.  At 13:20 all of the lines and external seals were tested and no leaks were found. The module was at a pressure of 2.9 x 10^-5 Torr (IMG) and 1.4 x 10^-5 Torr (ION). The leak test cart was at a pressure of ~2.7 x 10^-2 Torr and a leak rate of 1.1 x 10^-2 atm cc/sec for the external leak test and the repaired lines. A small response was found in the Tube heater (D) where the leak increased to 2.1 x 10^-8 atm cc/sec. The leak test cart would then no longer drop below 1.9 x 10^-8 atm cc/sec and there was no response measured for lines C, B, and A. Over all very positive results! After 6 hours of pumping down the pressures were 2.0 X 10^-5 Torr (IMG) and 9.7 x 10^-6 Torr (Ion).  

 

 

 I again checked the TM this morning (July 22) at 10:00 am (24 hours of pumping), There is no external leaks carts pressure was 0.0x10^-4 Torr and leak rate was 0.0X10^-9 atm cc/sec. The IMG gauge was reading 6.8 x 10^-6 Torr and ION gauge was reading 3.1 x 10^-6 Torr. The lowest we have yet to record on the IMG gauge was 6.6 x10^-6 Torr and that was when the ION gauge was reading 1.2 x 10^-6 Torr and there were several leaks. This is a very good sign. I will continue to check the vacuum throughout the day. 

One more thing of note is that the copper feed thru stems have a design flaw, the holes for the locating pins are too large. As such a custom step pin had to be made. It work functionally the same but is not as intended.

Entry  Wednesday, July 20, 2011, 09:55, Travis Cave, ITE, Standard Operation, TM4, Ta#36, Move of TM#4 from South Hot Cell to East Target Station. 

Move completed, move went well.

Entry  Tuesday, July 19, 2011, 13:51, chad fisher, South Hot-Cell, Standard Operation, TM4, Ta#36, TM4 Ta#36 Leak Check Results DOC.PDF

Tm4 w/ Ta#36 has been vacuum leak checked using the standard leak check procedure.

At 1:45pm RH was contacted to notify them that TM4 is ready to move.

Entry  Tuesday, July 19, 2011, 12:25, maicodallavalle, South Hot-Cell, Standard Operation, TM4, Ta36, TM4 Ta36 Target was put into the south hot cell. 

Ta36 was check by Maico and Chad.It was then carried into the anteroom.From the anteroom it was transferred into the south hot cell.

Entry  Tuesday, July 19, 2011, 12:02, Travis Cave, South Hot-Cell, Standard Operation, TM4, Ta#36, Electrical check TM#4_SIS_Elec_Check2.pdf

See attached PDF for the details.

Entry  Tuesday, July 19, 2011, 11:52, chad fisher, South Hot-Cell, Standard Operation, TM4, Ta#36, New target Ta#36 Installed on TM4 DSC_0897.JPGDSC_0899.JPGDSC_0901.JPGDSC_0905.JPG

Ta#36 has been installed on TM4 and is awaiting leak and electrical check.

A small piece of the standard top insulator ITA3376 broke off during removal of Ta#35 (indicated with a blue circle on attached pictures).

"JP's connector, ITA2493 showed the usual and as yet undiagnosed "arc" mark (picture to follow).

The plastic retainers on the new torqtite gaskets showed rad damage.

Entry  Tuesday, July 19, 2011, 11:17, Travis Cave, South Hot-Cell, Standard Operation, TM4, Ta#35, Move of TM#4 from East target station to south hot cell. 

Move went well no problems readings at East Target Station were very high at 500mSv/hr.

Entry  Thursday, June 30, 2011, 16:04, Pierre Bricault, Conditioning Station, Repair, TM1, , TM1 status 

Friday June 24 2011

The target module has been moved to the Conditioning Station (CS)

Pumping overnight

Saturday June 25 2011

Pressure Service Cap (SC) 3E-6 T

Pressure Containment Box (CB) 6.6E-6 T

High voltage test to 40 kV, unfortunately, the pressure is not great so we stop at 40 kV

Pressure at the end of the day: 1650H was, P SC 2.6E-6T

P CB 6.6E-6 T

Sunday June 26 2011

Pressure P SC 1.6E-6T

P CB 6.6E-6 T

It seems we have a leak. The pressure does not drop in the CB over one day.

Today June 27 2011

 Pressure P SC 1.2E-6T

P CB 6.6E-6 T

We leak check the target module and found two leaks, one on the ground electrode and one on the mounting plate cooling circuit.

This is a new one. We had test this line three times before and it was ok.

Action for tomorrow.

After CS vent, 

Move TM1 to SHC

Survey 

Connect LD to Mounting plate cooling circuit

Open Side panel and leak check.

Meeting at 0830H

ELOG V2.9.2-2455