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  RH-ISAC, Page 138 of 138  Not logged in ELOG logo
  ID Date Author Category Type Module Target/Number Subject
  14   Wednesday, July 27, 2011, 14:34 Travis CaveSouth Hot-CellStandard OperationTM1 Module move

TM#1 has been moved from the Conditioning Station to the South Hot Cell for the installation of Ta#37.

  13   Monday, July 25, 2011, 14:49 Travis CaveSpent Target VaultStandard Operation Ta#35Spent target move

Ta#35, in pail #88, has been place into spent target storage, in spot 6C. Upon removal from the South Hot Cell it was 411mSv/hr our hottest target to be placed into storage to date. There are 8 free slots for targets left in the vault.

  12   Friday, July 22, 2011, 10:30 Bevan MossConditioning StationRepairTM1 TM1 Ground Electrode, Thermocouple line, Stem, panel, repairs

Bevan Moss wrote:

Over the period of July 20-21st TM1 had several repairs completed and tested. The easiest of the repairs was the installation of a gasket and a blank off. The next repair was to replace the 2 oring on the side panels that were removed for inspection and repair. The instrument panel oring was replaced again and the previous one measured. Both were found to have the correct diameter of 0.131 inches for the seal groove. When attempting to cut the thermocouple line back to an acceptable distance it detached from the stainless tube running down the high voltage chase. It was discovered that it was only being held in place with heat shrink and that the bend consisted of a hand made copper tube that was flared slightly, a truly poor electrical and mechanical connection. Also discovered was the thermocouple wire was left in the tube, this too was removed. The stainless steel tube was then secured to the tube heater (C) lines with a PEEK tie wrap. The port where the thermocouple line was then blanked off. The extraction electrode and mounting plate feed through stem repair went as practiced and no unexpected events occurred. One thing of note is that because the lines are twisted and some of the tube was removed the quick connects are no longer facing the same direction they were before. During these repairs the Ion gauge screen contacted a filament and caused a fault, this was repaired by edi who rotated the gauge. Roughing was started at ~10 am on July 21st and the turbo pumps turned on at 10:45.  At 13:20 all of the lines and external seals were tested and no leaks were found. The module was at a pressure of 2.9 x 10^-5 Torr (IMG) and 1.4 x 10^-5 Torr (ION). The leak test cart was at a pressure of ~2.7 x 10^-2 Torr and a leak rate of 1.1 x 10^-2 atm cc/sec for the external leak test and the repaired lines. A small response was found in the Tube heater (D) where the leak increased to 2.1 x 10^-8 atm cc/sec. The leak test cart would then no longer drop below 1.9 x 10^-8 atm cc/sec and there was no response measured for lines C, B, and A. Over all very positive results! After 6 hours of pumping down the pressures were 2.0 X 10^-5 Torr (IMG) and 9.7 x 10^-6 Torr (Ion).  

 

 

 I again checked the TM this morning (July 22) at 10:00 am (24 hours of pumping), There is no external leaks carts pressure was 0.0x10^-4 Torr and leak rate was 0.0X10^-9 atm cc/sec. The IMG gauge was reading 6.8 x 10^-6 Torr and ION gauge was reading 3.1 x 10^-6 Torr. The lowest we have yet to record on the IMG gauge was 6.6 x10^-6 Torr and that was when the ION gauge was reading 1.2 x 10^-6 Torr and there were several leaks. This is a very good sign. I will continue to check the vacuum throughout the day. 

One more thing of note is that the copper feed thru stems have a design flaw, the holes for the locating pins are too large. As such a custom step pin had to be made. It work functionally the same but is not as intended.

  11   Thursday, July 21, 2011, 17:39 Bevan MossConditioning StationRepairTM1 TM1 Ground Electrode, Thermocouple line, Stem, panel, repairs

Over the period of July 20-21st TM1 had several repairs completed and tested. The easiest of the repairs was the installation of a gasket and a blank off. The next repair was to replace the 2 oring on the side panels that were removed for inspection and repair. The instrument panel oring was replaced again and the previous one measured. Both were found to have the correct diameter of 0.131 inches for the seal groove. When attempting to cut the thermocouple line back to an acceptable distance it detached from the stainless tube running down the high voltage chase. It was discovered that it was only being held in place with heat shrink and that the bend consisted of a hand made copper tube that was flared slightly, a truly poor electrical and mechanical connection. Also discovered was the thermocouple wire was left in the tube, this too was removed. The stainless steel tube was then secured to the tube heater (C) lines with a PEEK tie wrap. The port where the thermocouple line was then blanked off. The extraction electrode and mounting plate feed through stem repair went as practiced and no unexpected events occurred. One thing of note is that because the lines are twisted and some of the tube was removed the quick connects are no longer facing the same direction they were before. During these repairs the Ion gauge screen contacted a filament and caused a fault, this was repaired by edi who rotated the gauge. Roughing was started at ~10 am on July 21st and the turbo pumps turned on at 10:45.  At 13:20 all of the lines and external seals were tested and no leaks were found. The module was at a pressure of 2.9 x 10^-5 Torr (IMG) and 1.4 x 10^-5 Torr (ION). The leak test cart was at a pressure of ~2.7 x 10^-2 Torr and a leak rate of 1.1 x 10^-2 atm cc/sec for the external leak test and the repaired lines. A small response was found in the Tube heater (D) where the leak increased to 2.1 x 10^-8 atm cc/sec. The leak test cart would then no longer drop below 1.9 x 10^-8 atm cc/sec and there was no response measured for lines C, B, and A. Over all very positive results! After 6 hours of pumping down the pressures were 2.0 X 10^-5 Torr (IMG) and 9.7 x 10^-6 Torr (Ion).  

 

 

  10   Wednesday, July 20, 2011, 09:55 Travis CaveITEStandard OperationTM4Ta#36Move of TM#4 from South Hot Cell to East Target Station.

Move completed, move went well.

  9   Tuesday, July 19, 2011, 13:51 chad fisherSouth Hot-CellStandard OperationTM4Ta#36TM4 Ta#36 Leak Check Results

Tm4 w/ Ta#36 has been vacuum leak checked using the standard leak check procedure.

At 1:45pm RH was contacted to notify them that TM4 is ready to move.

  8   Tuesday, July 19, 2011, 12:25 maicodallavalleSouth Hot-CellStandard OperationTM4Ta36TM4 Ta36 Target was put into the south hot cell.

Ta36 was check by Maico and Chad.It was then carried into the anteroom.From the anteroom it was transferred into the south hot cell.

  7   Tuesday, July 19, 2011, 12:02 Travis CaveSouth Hot-CellStandard OperationTM4Ta#36Electrical check

See attached PDF for the details.

  6   Tuesday, July 19, 2011, 11:52 chad fisherSouth Hot-CellStandard OperationTM4Ta#36New target Ta#36 Installed on TM4

Ta#36 has been installed on TM4 and is awaiting leak and electrical check.

A small piece of the standard top insulator ITA3376 broke off during removal of Ta#35 (indicated with a blue circle on attached pictures).

"JP's connector, ITA2493 showed the usual and as yet undiagnosed "arc" mark (picture to follow).

The plastic retainers on the new torqtite gaskets showed rad damage.

  5   Tuesday, July 19, 2011, 11:17 Travis CaveSouth Hot-CellStandard OperationTM4Ta#35Move of TM#4 from East target station to south hot cell.

Move went well no problems readings at East Target Station were very high at 500mSv/hr.

  4   Thursday, June 30, 2011, 16:04 Pierre BricaultConditioning StationRepairTM1 TM1 status

Friday June 24 2011

The target module has been moved to the Conditioning Station (CS)

Pumping overnight

Saturday June 25 2011

Pressure Service Cap (SC) 3E-6 T

Pressure Containment Box (CB) 6.6E-6 T

High voltage test to 40 kV, unfortunately, the pressure is not great so we stop at 40 kV

Pressure at the end of the day: 1650H was, P SC 2.6E-6T

P CB 6.6E-6 T

Sunday June 26 2011

Pressure P SC 1.6E-6T

P CB 6.6E-6 T

It seems we have a leak. The pressure does not drop in the CB over one day.

Today June 27 2011

 Pressure P SC 1.2E-6T

P CB 6.6E-6 T

We leak check the target module and found two leaks, one on the ground electrode and one on the mounting plate cooling circuit.

This is a new one. We had test this line three times before and it was ok.

Action for tomorrow.

After CS vent, 

Move TM1 to SHC

Survey 

Connect LD to Mounting plate cooling circuit

Open Side panel and leak check.

Meeting at 0830H

ELOG V2.9.2-2455