Wednesday, April 13, 2022, 11:54, Carla Babcock, South Hot-Cell, Maintenance, TM2, , EZL cable change
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Chad changed the EZL cable and plugs on TM2. New cable runs along the cable trays. |
Friday, July 29, 2022, 12:05, Carla Babcock, North Hot-Cell, Repair, TM2, UCx#38, Repair of UCx#38 EE short in ante room 
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UCx#38 developed a short between the plasma electrode and the extraction electrode about 30mins after reaching full temperature in the conditioning station. The decision was made to bring it into the anteroom and try to clean it there.
To do this, it was uninstalled, the parasitic attachments were removed and it was brought into the ante room.
I removed the EE and the PE, and cleaned quite a lot of material from them both with methanol. I think put the ionizer foil bar down the ionizer to help dislodge any material there, and I also turned the target over and tapped gently to get any material out. The first two times some flakes came out, the third time nothing came out. I then reinstalled the electrodes using the EE alignment tool (not sure how successfully, didn't push it into the ionizer too much because I was worried about catching the Rh foil).
The taret was meggered at 500V then reinstalled and electrical checks were done. Everything looks back to normal. Conditioning in ITW was successful. |
Tuesday, August 23, 2022, 10:51, Carla Babcock, ITE, Repair, TM4, SiC#44, TBHT to HV common short on SiC#44-TM4
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TM4 with SiC#44 installed developed a short TBHT to HV common during its first heating in ITE. Was fine before installation. Now with everything cold TBHT to HVC is 25kOhms. Removed short in electrical room, will rely on short in the module. |
Tuesday, August 23, 2022, 11:33, Carla Babcock, ITE, Repair, , , ITE:ANODE swapped with TCS:ANODE
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ITE:ANODE supply reading strange currents - 17mA with the power supply on and no voltage. Checked anode circuit from electrical room:
Anode wire in electrical room shows 0L at 250V
Circuit with 50kOhm resistor mostly looks good (49-52kOhms) but a couple times read 28kOhms, no idea why. Tried jiggling all cables, unplugging and replugging and everything looks fine.
But power supply still seems to be giving out signal for 17mA readback. Decided fastest to swap with TCS power supply and troubleshoot this one on the bench. |
Wednesday, October 19, 2022, 12:00, Carla Babcock, North Hot-Cell, Standard Operation, TM4, SiC#44, PIE on SiC#44  
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Conducted PIE on SiC#44, which failed online. It had a cathode short, a target short and an anode short by the time we called the experiment off. In the post irradiation examination, two clear marks where the target legs touched the heat shield were found (see attachments 1 and 2). No marks were found to indicate where the cathode short would have been. The fibreglass sheath covering the anode wire where it passes over top of the coil was destroyed, must have been a result of sparking (see attachment 3). No other issues noticed, grid looked fine, though close inspection is difficult. |
Wednesday, October 19, 2022, 12:04, Carla Babcock, Conditioning Station, Repair, , , TCS:TBHT taken as replacement for ITE:TBHT
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During the last ITE run with the SiC#44 target, the ITE:TBHT controls card was fried twice. The first time we put in our spare, and the second time we just continued to run without controls readback. For the C#4 run starting Oct. 19, we used the conditioning station supply. As soon as one of the other supplies is fixed, we will install it in the conditioning station. The equipment list (https://triumfoffice365-my.sharepoint.com/:x:/g/personal/cbabcock_triumf_ca/EQPffP4p1P9JqEDWIHGRPfsBVDSQjMCv-M8ZNg4ngkyGHw?e=fnLVYe) tracks these movements. |
Thursday, November 03, 2022, 16:41, Carla Babcock, North Hot-Cell, Standard Operation, , UCx#39, Post irradiation inspection UCx#39
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Did the PIE on UCx#39-IGLIS on Thursday Nov. 2 2022, couple pictures uploaded to docushare. Did not remove the target, just the heat shield cover.
Final electrical check on the module showed a dead short from TGHT/TBHT to HV common, which we did not see online. Seems like it must have occurred after ramp down? It persisted on the target after we removed it from the module. We couldn't find any obvious contact points, because it seems it did not happen while current was running in the target. Possible locations are the bottom support leg for the TBHT and the top of the right side target leg, though it was difficult to confirm with the camera.
Otherwise the only thing to note was a blacker-than-usual spot on the inside of the Cu heat shield, downstream in the proton direction.
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Tuesday, November 22, 2022, 14:53, Carla Babcock, North Hot-Cell, Maintenance, TM4, , Multipin connector alignment pin on TM4 module loose
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The pin on TM4 has become loose again, making it very difficult to remove the multipin connector with the last target, C#4. For the installation of the next target, UCx#41, we will drill out the hole on the target side bracket so that it doesn't contact the multipin pin. Will try to remove this pin by force in January, or if needed change out the whole multipin bracket. |
Thursday, December 01, 2022, 13:45, Carla Babcock, North Hot-Cell, Standard Operation, TM4, C#4, Post irradiation inspection C#4  
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Post irradiation inspection of C#4 which was running in TM4/ITE was conducted at the NHC on Nov. 22 2022.
The yields from this target had been dropping and its behaviour was erratic, with the voltages on the tube and target jumping all over the place sometimes. The ion current on the FCs followed the voltages. We took this to mean the target container was breaking down.
Upon inspection we found the container looked pretty damaged - highly crystallized and distorted. The container had gone banana-shaped, but not in the usual direction. It had curved in the direction of the ion source (see photos). The heat shield and other surrounding components were super clean, no deposits or marks at all. |
Wednesday, February 22, 2023, 09:22, Carla Babcock, ITE/ITW, Standard Operation, , , HV testing of ITE/ITW  
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Feb. 16 2023: HV tests done on ITE station. Ramped up to 59kV but was not stable there, current draw was very unstable and was sparking every ~6mins. Ramped down to 58kV and it was stable there for 3 hours drawing 285uA.
Feb. 24 2023: HV tests done on ITW station. Ramped easily to 60kV with no sparking - suspicious. Has been stable at 60kV for 45mins with no sparks and current draw of 200uA. Cannot find any reason that things aren't connected properly... |
Monday, March 13, 2023, 11:25, Carla Babcock, ITE/ITW, Development, , , 10kOhm resistors installed in ITE/ITW faraday cages
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On Sept. 14 2022, a 10kOhm 30W resistor was installed in each target station faraday cage, in line with the HV bias supply. This was an effort to reduce the current draw from the BIAS supply and protect the power supply controls cards which have been repeatedly breaking due to HV sparks (we think). In the end we still broke cards after the installation, so it doesn't seem to have helped. See below for details on the electrical side:
At 30kV, HV currents are around 100-150uA, meaning the voltage drop over the resistor is around 1.5V. When operating at higher voltages, with higher current draw, the voltage across the resistor could be over 2V and we could get into a situation where it would have an effect outside the normal adjustments needed on the mass separator. We made this decision based on the fact that the power supply's setting resolution is on the order of 1 x 10-4.
When the resistance of the water changes, this affects the current draw from the power supply and this in turn affects the voltage over this resistor. Based on some sample numbers of running times, there is not much variation in the current except from sparks and if there is some issue, like water leaking between HV and ground. During normal running, the voltage change across the resistor should be less than 0.5V during normal operation. This is on the same order as the 8 hour stability of the power supply.
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Monday, May 22, 2023, 15:06, Carla Babcock, ITE, Standard Operation, TM4, TiC#5, Module conditioning
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Yesterday and today module conditioning was done on Tm4 in ITE. This is the first ramp up after the shutdown and ITE is planned to run at high voltages for the first weeks. The module is behaving well - went up to 40kV yesterday, stayed there for an hour, and up to 46kV today. Current draw is 113uA at 46kV. No serious sparking.
Tuesday, May 23, 2023, 09:32 : Ramping up again, easy to 45kV. Drawing 132uA at 49kV. Still behaving quite well. |
Wednesday, May 24, 2023, 17:25, Carla Babcock, ITE, Repair, TM4, TiC#5, Issues with anode short
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When I tried to raise the anode voltage in cathode bias mode on May 23 evening, I found the target or tube shorted to HV common. Investigations in the faraday cage today showed the same. I removed all the new electronics (resistors, gemovs, etc) from the power supply to no effect, so I disconnected the TGHT supply and pushed it away from the busbars. There was still a short. David Frank and I then went down to the pit and disconnected everything to measure the module. The module itself showed no short, and the bus bars in the chase for TGHT showed no short, though the ones for TBHT still showed the short.
David and Frank reconnected the module and I disconnected the TBHT supply in the faraday cage, then I found no shorts to TGHT/TBHT. When I reconnected everything there were still no shorts. There must have been a short in the TBHT line in the faraday cage, and another short in the TGHT line in either the faraday cage or on the module top. Both these shorts got resolved by taking everything apart. Still not sure how it happened.
Next I found I could not raise the anode voltage above 230V, it looked like it was current limiting but since the current limit was high, I figured it had something to do with the new electronics installed. I disconnected them all the in cage and that solved the problem, and then reconnecting the gemovs that go from the PSU terminals to HV common caused the problem again, so I left those disconnected. |
Tuesday, June 06, 2023, 17:36, Carla Babcock, ITW, Standard Operation, TM2, TiC#6, Module conditioning
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Conditioned TM2 up to 48kV in ITW. Some sparks and current is not very stable. Drawing about 178uA at 48kV. |
Wednesday, July 12, 2023, 22:21, Carla Babcock, North Hot-Cell, Standard Operation, , TiC#5, TiC#5 post irradiation inspection results
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The TiC#5 post irradiation inspection was done on Wed. June 14 and Mon. June 19. This target didn't have any obvious issues but it didn't produce much beam. The inspection revealed that the container was quite embrittled and showed significant damage, though it was not broken. The FEBIAD grid looked fine, despite the large anode current draw (indicating that current was flowing elsewhere). The gas line looked fine though the gas injection to this target looked as if it wasn't connected. But there was a plug on the unused line, so it must have been correct. No other obvious signs that would explain the poor performance. Pictures are can be found here https://documents.triumf.ca/docushare/dsweb/View/Collection-37913 |
Tuesday, July 25, 2023, 16:25, Carla Babcock, North Hot-Cell, Standard Operation, , SiC#45, SiC#45 post irradiation inspection
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Looked at SiC#45 in the hot cell. Looked very clean, no deposits on the heat shield or other components. Target also looked very straight. Only issue we saw was sparking marks on the EE side that faces the ground electrode, in several spots. This target had a bout of sparking when ramping up the protons, so I guess that was the location. Will look for matching spark marks on the ground electrode next time TM4 is in the hot cell. Forgot to take picutres... |
Wednesday, August 09, 2023, 13:43, Carla Babcock, North Hot-Cell, Standard Operation, TM2, TiC#6, TiC#6 PIE
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PIE on TiC#6 was done in the NHC. The target assembly looked brand new when we took it out, no heating spots or deposits (pictures on docushare). Online we measured a 400kOhm connection between TGHT-TBHT-COIL to HV common (TGHT and COIL shorted in TM2 service tray) and anode was unstable above ~300V. After the module move and before the target removal David found TGHT-TBHT-COIL was a dead short to HV common and the anode was at 39kOhms to HV common.
1. Wanted to see if the TGHT-TBHT-COIL short was on the COIL. Measured with ohmmeter the COIL lines to HS and got about 700Ohms. But with the target lying down the COIL lines drop and touch the heat shield so to do this measurement Chad had to lift the lines, which could cause them to touch something else. So not sure how reliable this measurement was. It jumped around a lot, saw 0L occasionally.
2. Measured both target legs and tantalum gas line to HS, got about 5kOhms repeatedly using the ohmmeter.
3. Meggered across the gas line insulator to the gas line going into the target and got open circuit at 250V, so the gas line wasn't coated.
4. Target container looked vaguely red in the areas where the target material was, otherwise still no deposits on the inside. The container was not overly crystalized as seen on the legs and end caps.
5. Some sparking marks on the EE and some slightly asymmetric deposits
Continuing Aug. 22 2023:
6. Found what looks like a hole in the insulation on the COIL, maybe the cause of our short? Found a corresponding line mark on the copper plates that hold the coil down but not sure if it is related. Pics on docushare.
7. Grid looks perfectly new. Where was that current going?
8. Copper plates that hold coil were loose and bolts that hold coil in just fell out as well.
9. What can be seen of the anode wire looks good. |
Wednesday, November 29, 2023, 12:45, Carla Babcock, ITE, Standard Operation, , , gas lines pumped down
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Pumped down the gas lines in ITE on Tuesday Nov. 28 2023 and opened the CF4 bottle valves. Missed the small section between the regulator and SV2 though, so will probably redo it.
Pumped down again on Dec. 12 2023. Was taking a long time so might not be as good as earlier. Maybe there is a leak in there... |
Tuesday, January 02, 2024, 16:01, Carla Babcock, Conditioning Station, Development, TM3, , TM3 service tray HV testing and conditioning 
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Tuesday, January 02, 2024, 15:58 :
Started HV ramp up on TM3 service tray about 3pm today. Had to bypass TCS:BIAS interlocks to make it work - there are some flow restrictions on the water lines that are causing the flow interlock to periodically trigger. The water flow it not very important for this test as long as the water is moving. Turned out that it was also conveninent to have all the interlocks bypassed because sparks tripped off the IG1 gauge and this did not cause the HV bias supply to turn off. Should use same setup next time.
Some sparking around 35-44kV, tripped off turbos/IG1/IG1S 3 times and so decided to ramp down.
Tried again while standing outside TH door to hear if sparking is outside the vacuum. Went to 48kV very slowy with multiple trips of the turbos, mostly TP2. Lots of sparks but easy to ramp back up to previous high point, so likely just a painful conditioning process. Current draw 167uA at 48kV. No sparks audible outside door, and vacuum response looks too large to be electrical noise.
Continued on Wednesday January 03 - went up to 53kV in the same way as before, lots of TP2 trips making its current a bit unstable... data was dumped as TM3_servicetray_conditioning_jan32023. Tried limiting the current on the power supply to very near the drain current to see if that reduces the number of trips. Didn't notice a significant effect.
Thursday, January 04, 2024, 09:57 :
Restarting conditioning, starting at 180uA at 53kV. Got up to around 60kV with many trips of the turbos, and one restart of the IG1 controller needed. Added a grounding hook to the vacuum controller rack to see if that helps reduce the trips. (doesnt appear to have).
Friday, January 05, 2024, 09:51 :
Continuing conditioning. Starting by sitting at 50kV for 10mins. No sparks observed during this time.
Even though we got to 60kV last time, onset of conditioning started at 58.6kV with a trip at 58.9kV... got up to 70kV.
Got to 72kV on Monday January 08 2024.
On Monday Jan. 15, tried to improve the grounding on the vacuum services rack to reduce sparking through the turbo controllers. Added two welding cables from the vacuum rack ground busbar to the copper grounding strip on the ground. If the spark is travelling from the faraday cage to the rack through conduit or grounding cables, maybe this will help. If it is coming through the turbo cable then it likely won't. Tried to add grounding straps on the turbo controller chassis (there is a brass screw which I think is for this purpose) but couldn't get either of the screws out with any resonable force. They undo a bit then get stuck...
Wednesday, January 17, 2024, 20:39:
David vented TM3 with N, then opened the service cap to install new insulators. We pumped back down and Alexander and I ramped back up today - instabilities started around 55kV and we were back to slow conditioning in the high 50s. Got up to a set point of 65kV. Ray did some work on the TCS bias supply and now neither the set point or readback is correct. The PSU was reading 51.5kV at set point 50kV and 60kV at set point 58kV. Will continue later...
Wednesday, January 31, 2024, 16:23
Ramped up again, some slight instabiities around 56kV but could still go up pretty quick until about 65kV. Since Ray's testing of the TCS:BIAS supply both the readback and the set point are off from the powersupply display. Ran out of time and ramped down at set point 70.5.
Set point |
Readback |
PSU reading |
63 |
64 |
65.5 |
66.5 |
67.5? |
68 |
69.5 |
70.6 |
71.5 |
70.5 |
71.7 |
73 |
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Tuesday, February 06, 2024, 14:47
Testing again after venting the module with air. First tiny spark at 48, then some vacuum reactions starting at 49 but still no issues. Bit more reactive around 53.
Set point |
Read back |
PSU reading |
53 |
53883 |
55 |
57 |
57924 |
59 |
60 |
61 |
62 |
64 |
65 |
66.5 |
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stopped at 69.4
Wednesday, February 07, 2024, 15:28 :
Ramped easily to 60kV set point and let it sit there. Didn't spark at all then after 100mins, sparked TP2 off. Otherwise first sparking happened at set point 67.
Found at limit at around 72.5 on the PSU front output, set point 70.6. think it comes from EPICS. Will have to test the power supply.... stopped there.
Thursday, February 08, 2024, 15:03 :
Long term testing. ramped back up, first spark at set point 65.
Let it sit for 2hrs 20mins. Something like 6 sparks during this time. Current also dropped significantly from 0.32A to 0.27A.

EDIT 2024-11-25, Alexander Shkuratoff:
All the StripTool data related to the above tests are on the server as the following below. Those without "Alexander" in the name were dumped by Carla.
And the StripTool settings:
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Wednesday, January 10, 2024, 16:51, Carla Babcock, ITE, Standard Operation, TM4, UCx#43, UCx#43 failure
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To deliver stable beam to RadMol, started heating UCx#43 up again. Target was overheated during initial conditioning in Nov but then ran well for 4 weeks. During the run time, the TGHT voltage jumped around and this was reflected in the ion current, but yields seemed unaffected.
When re-heating it, the TGHT voltage was very unstable and once it got to 440A, it went into voltage limiting mode. We ramped down and it was still voltage limiting, but turning things off solved it. We ramped back up and it did about the same thing. TBHT voltage and current remained steady. Looks like a heat generated issue.
Measured the resistance in the lines from the electrical room. Resistance of the lines to ITE should be 1.19mOhms for TGHT and 1.95mOhms for TBHT. TBHT positive to negative had a resistance of 7.9mOhms from the electrical room today, and 5.7mOhms on module top when measured Nov. 8. This seems to track.
TGHT positive to negative was measured at 27.6mOhms today (and was jumping around), whereas it was 7.14m Ohms on Nov. 8.
10V @ 440A is 22.7mOhms, so it makes sense that it limited. Tried with increased voltage (up to limit of 16V) but this didn't help. Declared the target dead on Jan. 11.
David measured resistances on the module top and found (in mOhms):
A-B = 27 (TGHT)
A-C = 7.473
A-D = 6.380
B-C = 26.053
B-D = 25.569
C-D = 5.212 (TBHT)
So looks like the tube is broken on the B side. |
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