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New entries since:Wed Dec 31 16:00:00 1969
ID Date Author Category Type Module Target/Number Subject
  568   Wednesday, December 04, 2013, 11:15 David WangITERepairTM4 New bolts are installed on ITE TP3.

I installed 8 new bolts(3/8-16 UNC x1.25  STL) on the ITE TP3. The ITE TP3 replacement job is done. Everything is connected back to the pump. and it is ready for starting.

  567   Wednesday, December 04, 2013, 11:05 David WangITWStandard OperationTM4Ta41#I disconnected TM4 in ITW

I disconnected TM4 in ITW .The job took about 20minutes and I got 0.11 msv dose.

  566   Wednesday, December 04, 2013, 10:44 Travis CaveSouth Hot-CellStandard OperationTM4Ta#41module move

TM#4 with Ta#41 has moved to the south hot cell, the move it self was uneventful but, the fields on the module are extremely high when lowering it down into the south hot cell the module had a maximum field of about 392mSv/hr. The shield plug was also installed remotely as well due to the 12mSv/hr field at the top of the west target station due to shine from the dump.

  565   Tuesday, December 03, 2013, 14:14 Bevan MossConditioning StationStandard OperationTM2 HV conditioning

 It was attempted to HV condition TM2 to 55kV and leave it operating there for an hour to demonstrate stability. Unfortunately at 52.65kV a spark destroyed the canbus controller. This controller had shown issues in the past but seemed to magically fixed itself. I will contact Hubert for another card. Attached  is is a screen shot of the stip tools. 

  564   Tuesday, December 03, 2013, 10:35 Travis CaveITWStandard Operation  fields above and in the target station with blocks off

The blocks have been removed from the west target station. The fields at the top of the target pit at the railing at waist level is about 80uSv/hr, Turbo pumps are about 805uSv/hr, backing lines for the turbos about a 1mSv/hr and the average field in the area of work down in the pit is about 600 to 750uSv/hr. The proton beam went off at 10:45 on December 2nd, these measurements were done at 09:00 on December 3rd.

 

Another set of field measurement was done at the west target station. At the top of the west target station at the railing the field ranged from 50 to 70 uSv/hr. The turbo pumps had field of about 650uSv/hr, the area over the dump was about 750uSv/hr, the area over the HV cover and the south side was about 450uSv/hr. These measurements were done at 13:15 on December 3rd.

  563   Tuesday, December 03, 2013, 09:58 David WangITWStandard OperationTM4 I moved 5 shielding blocks from ITW to block storage area.

I moved 5 shielding blocks from ITW to block storage area.

  562   Monday, December 02, 2013, 11:29 Travis CaveSouth Hot-CellStandard OperationTM3no targetmodule move

TM#3 with no target has been moved from the south hot cell to the northeast silo.

  561   Friday, November 29, 2013, 11:57 Bevan MossSouth Hot-CellRepairTM3 Steerer short investegation

chad fisher wrote:

Using in cell camera and transit the suspect line on the steerers was inspected as best as possible. An existing photo of the complete steerers before installation was used for comparison. The wiring and beading inspected today showed no obvious problems, breaks or spots where there may be a short. In comparison to the photo from construction, what we could see of the steerers looked identical to the original installation.

 The test was repeated to confirm that there was a short.

  560   Friday, November 29, 2013, 11:54 chad fisherSouth Hot-CellRepairTM3 Steerer short investegation

Using in cell camera and transit the suspect line on the steerers was inspected as best as possible. An existing photo of the complete steerers before installation was used for comparison. The wiring and beading inspected today showed no obvious problems, breaks or spots where there may be a short. In comparison to the photo from construction, what we could see of the steerers looked identical to the original installation.

  559   Wednesday, November 27, 2013, 15:24 Bevan MossSouth Hot-CellMaintenanceTM3 Wiring Harness Electrical Test

 Maico removed the containment box today allow Travis and I to further test the wiring harness. I disconnected the junction block and Travis and I repeated the test from yesterday. The all lines except the PNG tested OL. The module was then lowered and the twisted pair connected to the pin that corresponds to the steerer labeled BTM (it is likely this is not labeled correctly). This testing showed showed that the source of the short found yesterday is in the wiring harness or the source tray. The PNG gauge was then tested again. When beeping out the harness to find the location of the pin it was found that the short had gone away. This circuit was then tested with the megger at 500V and showed OL. Don Jackson has suggested looking at the SHV feed through. It is difficult to determine where the source of the problem is as it is intermittent. The source tray side wiring harness for the steerers was then disconnected from the steerers and tested to OL. Finally the connections on the source tray were tested. It was determined that the third socket down (see attached picture) has a short somewhere to ground. When Chad returns on Friday I will have him complete a visual inspection and if the source can be found we may be able to deflect the line. Failing that to repair this connection a new steerer cone assembly will need to be installed.

  558   Wednesday, November 27, 2013, 12:50 Bevan MossSouth Hot-CellStandard OperationTM3 Ground devices wiring check

 Travis and I completed an electrical check on the wiring harness for the devices on the ground plane. All lines passed 500V with the megger except for PNG and the BTM steerer. Those devices had a short to ground. of ~1.4ohm.

  557   Tuesday, November 26, 2013, 14:10 Travis CaveCraneMaintenance  Thermal relay replaced

The bad thermal motor protection relay for the crane has been replaced with a new unit. Crane was tested in pendant(local) operation and all drives worked.

  556   Monday, November 25, 2013, 11:48 Travis CaveSouth Hot-CellStandard OperationTM3no targetmodule move

TM#3 with no target has been moved from the north east silo to the south hot cell.

  555   Friday, November 22, 2013, 10:29 Travis CaveSpent Target VaultStandard Operation NiO#2Spent target move

NiO#2 has been moved from the south hot cell into spent target storage. It was placed in pail 111 in slot 3C of the storage vault. It was 76.4mSv/hr upon removal from the south hot cell.

  554   Thursday, November 21, 2013, 12:12 Anders MjosSouth Hot-CellStandard OperationTM3NiO#2End of beam target inspection - ANODE does not hold 250V

The target was inspected by Chad and Anders in the Hot Cell. Electrical megger tests were done during the assembly. It was found that Insulators No 3 (ITD0311) and No 2 (ITD0310) failed to hold voltage after the run.

  [V] [kOhm]
ANODE - HS 40 21
ANODE - TGT 100 55
HS - TGT 100 55
Lid removed    
ANODE - HS 40 21
ANODE - TGT 90 41
HS - TGT 100 55
Target removed    
ANODE - HS 245 139
No 3 Ins - TBHT 0 0
No 2 Ins 110 64
No 2 Ins removed    
ANODE - HS 540 OL

EE to HS was measured OL at 1000  V.

Photos can be found on DocuShare

 

 

  553   Wednesday, November 20, 2013, 13:52 Bevan MossConditioning StationStandard OperationTM2 HV testing of TM2

 HV testing without the cover continued today. With the EINZEL lens at 30kV the target module was able to achieve 58.7kV. At this voltage any spark was reeking havoc on the electronics of the TCS. Vacuum gauges signals were occasionally lost, the thermocouple reading would occasionally be lost, turbo pump would turn off. All of these events caused the interlocks to trip resulting in the power supplies to be turned off. As a result I bypassed majority of the interlocks to prevent this from happening. Ultimately as spark took out the CANBUS controller first for the EINZEL lens and then for the BIAS. David Morris has been contacted to have them replaced. The damage of the CANBUS controller for these power supplies is becoming a common problem and should be investigated for if there is a better solution. During testing I experimented with raising the BIAS to near its limit followed by the EINZEL lens and vise versa. From this it was determined that the EINZEL must be raised to high voltage before the BIAS otherwise sparking occurs. Even a step from 0 to 500 volts on the ENIZEL lens with the BIAS at 55kV caused sparking. There are a few combinations of testing along this line I would like to continue with but initially my though is that the BIAS and ENIZEL do not have sufficient clearance for the BIAS to operate above 55kV. Attached is a screen shot of the strip tool and the data. I have not heard from David yet but I do not expect the TCS to be operational today. 

  552   Wednesday, November 20, 2013, 09:52 Travis CaveSouth Hot-CellStandard OperationTM3no targetmodule move

TM#3 with no target has been moved from the south hot cell to the north east silo.

  551   Wednesday, November 20, 2013, 08:50 chad fisherSouth Hot-CellStandard OperationTM3NiO#2NiO#2 removed

NiO#2 has been removed from TM3

  550   Tuesday, November 19, 2013, 16:55 Bevan MossConditioning StationStandard OperationTM2 HV conditioning

 HV conditioning of TM2 continued today. At ~53.5kV the module started to spark externally to the HV cover. This is the first time the cover has been tested to this high of a voltage due to the limitations of the modules. As such for the conditioning station to achieve 60kV while keeping the target hall open of personnel the cover and cage will need to be modified. To continue with HV testing of TM2 the cover was removed and the target hall locked out as per the procedure covered in Document 70039 "ISAC Conditioning Station: First Lock-Out and High-Voltage "ON". With the cover off the module was able to achieve ~56.7kV without the Einzel lens on. Eliminate the Einzel lens as a potential source of sparking it was brought to 25kV while the module continued conditioning. Maximum voltage achieve under this configuration was 57.1kV. Increments are now 50V steps. The Canbus continues to be very sensitive to any sparking and is slowing the process down considerably. It does however appear that the module is continuing to condition. I will continue tomorrow after the module moves to attempt to reach 60kV and hold it for 1 hour.

  549   Tuesday, November 19, 2013, 14:24 David WangITERepair  ITE TP3
Hi all, The old  ITE TP3 pump is moved out and the new pump is  in postion .Since this time I used a new holding ring(1 piece) insead of old 2 pieces holding ring which are thicker than new ring, the old holding  bolts are a little bit too long for the thread holes on the  ITE exit 1. I have to find the right length bolts for this new holding ring. The pump is in position,and all connection are done except the holding bolts. I will put the new bolts on and tight them when I connect the TM4 in ITE next time. So, If I am not here at that time and you need to connect TM4 and start the pumps in ITE, please check all the bolts are tighted before you do anything.
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