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Entry  Tuesday, December 20, 2022, 10:03, Adam Newsome, T-Hall Crane, Standard Operation, Overhead crane powered off for the holidays 

[edit 2023-01-03] The crane was powered back on this morning - there do not appear to be any faults on the HMI and it seems that the crane was unaffected by the power outage.

The ARIEL target hall overhead crane was powered off for the holidays. In the new year, throw the main disconnect in the crane control room to power back on.

Entry  Friday, January 13, 2023, 13:57, Adam Newsome, T-Hall Crane, Repair, Crane light (west) not working 

It was observed today that the crane's west light was not functioning.

Entry  Friday, January 20, 2023, 14:48, Adam Newsome, T-Hall Crane, Standard Operation, Pendant/Receiver Communication Issue (Repeated) 

An issue was observed in which the pendant did not work to control the crane. This is the second time in recent memory this has happened. See e-log 55 for details. The same sequence of steps outlined in e-log 55 was followed, and the pendant control was re-established. It is still unclear what the root cause of this issue is, but it is suspected that the crane pendant loses communication with the receiver for some reason, and even though communication can be re-established, the reset button on the crane control console does not clear the fault message, and the system must be power-cycled in order to fully reset. This is just speculation based on what is observed. Further investigation required.

Entry  Thursday, March 16, 2023, 14:41, Adam Newsome, T-Hall Crane, Development, ARIEL Target Hall Crane - Spare Pendant Procured, Tested PXL_20230316_204047237.jpg

A spare pendant for the overhead crane was procured from COH. The pendant's functionality is the same as the original one's. The pendant was tested today by Adam Newsome - all functions behave as expected.

Important - to change to the spare pendant in the case of failure of the original one, insert a battery into it, and transfer over the small black transmitter card shown in the attached picture. The pendant will not pair with the receiver without this card. There is nothing else that needs to be set up for it to work.

The spare pendant is kept in a labeled box on top of the electrical cabinets located in the crane control room (L1 floor).

Entry  Tuesday, March 21, 2023, 10:47, Adam Newsome, Hot Cell 1, Repair, Circuit breaker replacement - telemanipulators 

There was an issue with a 20 A circuit breaker used to control motor assist functions for the telemanipulators (specifically, the rightmost CB in the panel for the right (East) manipulator set). This circuit breaker was moved to the panel for the left (West) manipulator set in the rightmost position, and then subsequently replaced with a new one, which is functioning correctly. It is suspected that the former CB which was not working was calibrated towards the low end from the factory, based on discussions with the manufacturer and extensive testing of multiple scenarios.

Entry  Tuesday, April 25, 2023, 12:28, Adam Newsome, T-Hall Crane, Standard Operation, ARIEL Target Hall Crane - Drives Fault MicrosoftTeams-image_(10).png

Today while operating the crane with load, the crane stopped moving. Upon investigating, all safety signals appeared to be OK. Fault messages regarding drive faults for various VFDs were present, which seemed to stem from an ethernet adapter card fault (see attached photo). It is unknown how this occurred, but suspected that it was due to a brief blip in network communications or the external drive power supply control signal. It is worth noting that the diesel generator tests took place today, and there could have been some affect from a power surge because of this.

The crane was power-cycled using the main disconnect, and safety system reset. The faults disappeared. The crane was operational again.

If this issue occurs again, it should be investigated more thoroughly. It would be worth checking if there were any generator tests or other things which could cause some sort of power surge.

Entry  Wednesday, April 26, 2023, 16:06, Adam Newsome, T-Hall Crane, Maintenance, Target Hall Crane - Hoist Wire Wrapping 20230131_120303.jpg

It was observed recently that the main hoist's wires seemed skewed, and there was occasionally some noise heard when raising and lowering the hook block. It was suspected that this was due to wires having jumped in their tracks at some point. This is typically caused by side loading. It is possible that wire wrap skew occurred during the incident outlined in e-log 46

 

Gordon Crane was contacted for a service call. Crane inspector Ali from Gordon Crane was supervised/assisted by Maico Dalla Valle. They lowered the hoist down into the target pit and supported it on saw horses, then let the wires run all the way out. Ali confirmed that there was a wire wrapping issue, and re-seated the wires properly. The crane is now functioning normally. It is recommended to re-apply lubrication as soon as possible.  

 

Note: Ali from Gordon Crane has advised that it is acceptable for some degree of wire skew to occur - they can handle the abrasion if there's a small angle between them. However, wires should not be rubbing across each other at a large angle (ex. more than approx. 10 degrees). 

Entry  Wednesday, February 14, 2024, 09:02, Adam Newsome, T-Hall Crane, Maintenance, Target Hall Crane: Trolley Encoder Homing PXL_20240214_160748765.jpg

The main trolley's E/W motion was observed to be slowed on 2024-02-13.
Upon investigation, the following faults were present:
- 200. Rotating Hook Velocity Difference between SSI Encoder and Drive Speed Feedback
- 82. Main Hoist Slack Rope

It is suspected that these faults are irrelevant in this situation. Upon inspection of the main trolley status screen, it was evident that both the SLOW EAST and SLOW WEST indicators were on (which matches observations). Clicking one of these status icons showed "Main Trolley Encoder Not Homed 2253ENC".

Logging in as an administrator allowed for homing the encoder.

The trolley was moved all the way East, to the limit, and the encoder was homed at position 0.389m (encoder count = 6886940). Note: the alignment arrows were not used as this would have required gaining access to the crane which was difficult at the time. It is suggested to properly home it in the future.

The E/W motions were fully tested to confirm proper slow down and stopping at the expected positions. The crane appears to be operational as of 2024-02-14.

 

Entry  Wednesday, April 24, 2024, 09:17, Adam Newsome, T-Hall Crane, Repair, Target Hall Crane: VFD DC bus undervoltage fault [root cause: encoder board failure on 900VFD] DC_bus_voltage.jpegPXL_20240422_225858594.jpg

On 2024-04-22 around 3:30 pm it was discovered that the crane's main hoist was in a faulted state. The operator (Adam Newsome) experienced the fault after performing a safety reset and attempting to lower the hoist. There were no visible signs of any issues, mechanically. This fault had not been previously reported by any other crane operators. The crane was previously unused, sitting idle. Note: the auxiliary hoists appeared to function normally.

Fault messages on the HMI indicated:

"135. Main Hoist West Drum North Motor Drive Fault (1000VFD)"
"104. Main Hoist East Drum South Motor Drive Fault (800VFD)"
"103. Main Hoist East Drum North Motor Drive Fault (700VFD)"
"138. Main Hoist West Drum South Motor Drive Not Ready (900VFD)"
"136. Main Hoist West Drum South Motor Drive Fault (900VFD)"

It is clear from this that there is either some sort of common issue seen across all these main hoist VFDs, or one issue with one of them which caused a cascading series of faults.

 

On 2024-04-23, upon investigation of these faults by going online with the PLC to determine fault logic, it was clear that all faults were indeed present, but there was no obvious indication as to what it was. Inspection of the VFDs in the control panel showed that all of the aforementioned drives displayed a fault code. This was fault code 4 which indicates DC bus undervoltage.

After researching this fault online, it appears this is typically caused by an issue with the input mains supply (480VAC @ 3 phase in this case), or by the drive's input DC filter/buffer circuitry. When measuring the DC bus voltage, it is expected for it to be approximately 1.414 times the AC supply voltage. In this case, 1.414*480 = 678 VDC. The first troubleshooting step was to measure to confirm the DC bus voltage on a known working and not working drive.

The bus voltage was probed on drive 500VFD which, based on lack of fault message, was expected to be functioning properly. With the safety off due to E-stop condition, the voltage was nearly zero. When a safety reset was pressed to enable the drive, the voltage changed to 690 VDC. This is close enough to the expected 678 VDC. The voltage did not change, even when the fault message for the other drives appeared again.

Next, the bus voltage on two known faulted drives, 900VFD and 1000VFD, was probed. In both cases, after the safety reset, the bus voltage started at 690 VDC but then slowly dropped down towards nearly zero (somewhere around 18 V) over a period of 3-5 seconds. It was during this transition when the voltage dropped off that the undervoltage condition became true, which triggered the fault.

As of 2024-04-24, the root cause of this issue is unknown. It will be investigated further and this e-log will be updated when a solution is found.

 

Update 2024-04-24: the root cause has been identified. The undervoltage fault was just a symptom as a result of the input contactors for these drives switching off, causing the DC bus voltage to drop slowly due to capacitance in the input filtering circuit. The reason for the input contactors switching off is attributed to safety signals dropping out due a fault observed specifically on 900VFD. When looking at the drive itself, a fault with code 4030 was displayed: Enc1 open wire.
This fault implies the encoder may be disconnected. The encoder wiring was checked: OK. The encoder cable was swapped with a unknown working one from an adjacent drive - the issue remained with 900VFD, which suggested the problem is with the drive itself. The encoder board (20-750-DENC-1) was swapped with an adjacent drive and the problem followed the board. The encoder board was then switched with a brand new spare (note: jumpers needed to be set!).
Upon power-cycling the system, the fault did not persist. Therefore, it is suspected that the encoder board had failed (in fact this happened previously with the same drive - see e-log 42). Upon inspection, one of the capacitors on the board appeared to be cracked - this will be investigated further to see if replacing it fixes the problem.

A spare encoder board will be ordered. This issue should be monitored in the future - it seems as if the drive itself is perhaps causing the encoder boards to fail.

Note: upon powering the system on again, another issue was noticed: 500VFD shows "drive not ready" fault. This is not displayed on the HMI though - it was just not possible to reset the safety system and this was only discovered from going online with the PLC. This will be investigated further.

 

Update 2024-04-26: the 500VFD "drive not ready fault" was investigated. It was determined that the SP+ (safety power +) signal wire was loose, which meant the safety signals to the drive were not getting through, causing it to remain in a "not ready" state. The wiring issue was corrected. Performing a safety reset resulted in successful drive enables across all drives. However, upon attempting to move the crane, even though all safety signals were green and it appeared to be able to move, it did not.
It turned out that there was a crane pendant fault: "Fault 305. Radio Control Receiver in Fault (3700RC)". This is exactly what happened previously in a similar situation (see e-log 55). The steps mentioned in that e-log were followed (power cycle, reconnect antenna/connector). Upon powering back up, everything worked as normal. The crane was tested in local mode - all three hoists up/down (main hoist run to upper limit), all trolley travels in each direction, and bridge travel in each direction.

 

As of now, everything is operating normally and all issues are considered to be resolved. A spare encoder board has been ordered.

Entry  Wednesday, July 17, 2024, 15:07, Adam Newsome, Hot Cell 1, Standard Operation, Safety Walkaround Complete - B2 Level 

A safety walkaround for July 2024 was completed for the B2 level by A. Newsome. No deficiencies to report.

Results can be found in the master spreadsheet

Entry  Tuesday, September 10, 2024, 12:52, Adam Newsome, T-Hall Crane, Standard Operation, Drive not ready faults observed on power-up 

Upon powering on the crane today and attempting to use the main hoist, the following faults were present:

1. Main Hoist East Drum North Motor Drive Fault (700VFD)
2. Main Hoist West Drum South Motor Drive Fault (900VFD)
3. Main Hoist East Drum North Motor Drive Not Ready (700VFD)

Note that the auxiliary hoists functioned as normal.

Upon power cycling the crane to reset, the faults disappeared, and the main hoist functioned normally again. The root cause of the issue is unknown. It is suspected to be related to either prolonged inactivity, improper safety reset sequence, or the battery being removed from the pendant. This issue will be monitored for re-occurrence.

Entry  Tuesday, September 10, 2024, 13:03, Adam Newsome, Hot Cell 1, Development, Spacer flange installation 

The spacer flanges were installed on both turntables today.

See photos and information in the following DocuShare Collection: Collection-39816

Important note: the fitment was quite tight due to interference with universal joints and grease nipples. The flanges were still able to be installed with a bit of difficulty. They are not posing any immediate issues, but it is predicted that the adapter flanges will certainly interfere with drive system components. It is necessary to change the design of the adapter flanges to allow for the appropriate clearance.

Entry  Thursday, October 10, 2024, 12:22, Adam Newsome, Hot Cell 1, Standard Operation, Safety Walkaround Complete - Hot Cell area 

A safety walkaround was completed for the ARIEL Hot Cell area.

The resulting spreadsheet can be found on DocuShare as Document-242733.

No major deficiencies identified.

Entry  Thursday, November 28, 2024, 09:04, Adam Newsome, Hot Cell 1, Repair, Hot Cell turntables not rotating, access hatch not moving 

It was reported that the hot cell turntables would not rotate and the access hatch could not be operated. The turntables' elevation motion was working normally, and other cell functions were working.

Upon investigation, after going online with the PLC and checking the interlocks for the turntable, it was determined that motion was being prevented because the turntables were in the "critical position" in which they could interfere with the access hatch raising/lowering. However, the access hatch was fully closed, so this logic should not have been actively preventing motion. After inspecting the target access hatch limit switches, it was determined that the upper limit switch's Normally Open contacts were behaving normally, but the Normally Closed ones were not. When the switch was toggled, the NO contacts did not switch over. Thus, the sensor was in an unknown state causing conflicting logic in the PLC (the program thought the access hatch was in an intermediate state between opened and closed, thus preventing motion... and the access hatch could not move because the turntables were in the "critical position"). After testing the switch multiple times, jiggling the wiring/contacts, and rewiring one of the screw terminals, the NO contacts started working normally again. It is suspected that a wire was loose. 

The issue has been resolved and tested - the access hatch logic is functioning regularly and both turntables can fully rotate and elevate.

Entry  Friday, November 29, 2024, 15:23, Adam Newsome, Hot Cell 1, Maintenance, 1000 kg crane: y axis position display not functioning PXL_20241202_204356508.jpg

After a recent power cycle, the y-axis referencing was lost for the 1000 kg crane. The position readout was also incorrect, somewhere on the order of > 30,000 mm. On 2024-11-29, A. Newsome re-referenced the y-axis. The position readout correctly reset to zero, and both +y and -y motion is functioning correctly, but the y-axis position readout on the HMI constantly displays 0 and does not change. To be investigated.

 

Update 2024-12-02:

After going online with the PLC, it was determined that the reason for the display of 0 as the position is that the two values used for calibration of the +y and -y limits were actually the same, meaning the scaling factor (the difference between these two values) was 0, which resulted in the displayed value being 0. The root cause of this is that the encoder was not functioning correctly so its value was not changing when the crane moved and it was stuck at one value. Upon investigation of the encoder input card, the red "ERR" light was on. This indicates the encoder signals are not properly reaching the input card. Once this was discovered, it was remembered that this happened in July 2024 as well (no e-log was written). In July, the root cause was identified as being a loose encoder signal wire in a junction box. Junction box CJB1-BC, located on the bridge crane near its disconnects, was opened and investigated. Upon checking each wire, it was determined that the red wire seemed not to be making full contact. The wire was removed and re-inserted, and the "ERR" indicator on the encoder card turned off. The crane's +y and -y limits were re-referenced. The crane is functioning normally after re-referencing. (Note: if something like this happens again, during the re-referencing process, the displayed value on the HMI will be incorrect.. this is because the PLC's scaling factor is not fully adjusted until both +y and -y limits are reached. The actual encoder measurement taken at those limits is used for the scaling factor. This is not an ideal way to program the system, but this is how it works with all ARIEL hot cell subsystems. So incorrectly displayed values can be ignored, in general, until full referencing is completed).

Entry  Thursday, December 12, 2024, 15:57, Aaron Tam, Hot Cell 1, Development, Pistons Gas lines exchange 13x

December 12, 2024 - Chad Fisher, Albert Kong, Aaron Tam 

Tests:

Gas lines removal: 

  • Starting with the most exterior connection, VCR connection loosened off with open ended conventional wrench
  • Once loose, the nut can be un threaded with manipulator finger (rolling nut technique) 
  • Once gas line unhooked, gasket removed by bringing female end outside the service tray footprint and jiggling until the gasket was removed
    • Also possible to use a pick if needed
  • The same procedure was conducted for the interior VCR connection

Gas lines installation: 

  • Starting with the inner most connection
  • Gasket placed on 3D printed tool and clipped into position on VCR male end
  • At first an M10 bolt was inserted into the elbow below VCR connection, but without rotational authority, the makeshift handle is not worth using
  • Griping the elbow with one manipulator and rolling the nut onto the threads with the other proved successful
  • Nut was tightened using conventional open ended 19mm wrench

Observations/Notes:

  • Service Tray was not in a fully connected position, so even less space will be afforded.
    • This may affect the ability to get 2 manipulators on the same connection
  • Piston modules were missing some limit wires on the side. These constrain movement horizontally and will either need to be removed as part of the procedure or, make the procedure more difficult
  • Mass markers and various other connectors not installed, and these could slightly restrict movement as well
  • Service tray pin was restricting the movement of the left manipulator during install
  • Lighting was inadequate under the piston 

Recommendations/follow up items/questions:

  • All metal Parker VGR style gaskets to replace plastic retainer versions
    • This is so that the degraded plastic doesn't break off and end up in the gas lines (upside down connections)
  • A modified wrench with flats for handles and with more length would make the above procedures easier 
  • Along with raising and lower the service tray, the service tray pin being oriented towards the beam entry direction, would make life easier 
  • Still need to test gasket install on "other" Piston gas line connection
    • Chad will redesign some new gasket tools to be tested
      • side load and axial load gaskets, low and high clearance, aluminum construction 
  • Lighting positioned to flood the service tray area will be needed
  • labeling the gas lines with a more permanent solution will be needed
  • Once the high voltage feed-through parts have come in, we can re-test and see if the piston module can be lowered to aid in target removal situations
  • Aaron will test Parker style seals to see if they can be removed as easily once brought up to specified torque 

------------------------------------------------------------------------------------------------------------------------------------------------------------------

 December 16, 2024

  • Upon inspecting the piston modules on AETE in TISA, we became aware of how the wires are arranged for the limit switches, it may be a good idea to look into how these wires are handled when using the piston module jig.
Entry  Thursday, December 12, 2024, 16:20, Aaron Tam, Hot Cell 1, Development, Extraction Electrode Banana Plug (Show and Tell) 6x

 December 12, 2024 - Chad Fisher, Albert Kong, Aaron Tam, Austin Hagen

Tests:

Loose piece connection and removal 

  • By hand, the two connections were brought together and removed carefully

Observation/notes:

  • Copper extensions are fragile and can bend when removing extraction electrode. 
    • This makes this part fairly limited in its capacity to be re-used
    • Copper extensions will need to be tuned before inserting into hotcell for replacement 

Recommendations/follow up items/questions:

  • Bigger lead-ins would be appreciated
  • What is the exchange frequency?
  • the flexible nature of the copper extensions makes re-use limited
  • How many connections can we expect from the aluminum fingers?
  • Would a closer locating feature specific to the pins help?

December 12, 2024 - Michael Genix, Aaron Tam 

  • Guide pins for the extraction electrode contact before the banana plugs
    • As these pins are low tolerance, this will act as the guiding for the plugs
    • Copper extensions have a much smaller diameter than the plugs, so positioning can be less precise in this area 
  • Exchange frequency is still TBD
  • Pin and plug life is still TBD
  • Potentially the copper extensions can be tuned in the hotcell
ELOG V2.9.2-2455