ID |
Date |
Author |
Target Material |
Target Oven W.O# |
Source |
Status |
Subject |
145
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Monday, July 28, 2014, 15:06 |
Laura Lambert | | 40282-3 | LP-SIS | In progress | Sintering ZrC# 6 target | Monday, July 28, 2014, 14:41
Total number of foils: 445 discs
Total mass of materials [incl graphite foils]: 49.027 g
Total length packed: 11.2 cm
Container has no Ta heat shields.
Currently being pumped down.
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146
|
Tuesday, July 29, 2014, 11:23 |
John Wong | | 40282-3 | LP-SIS | In progress | Sintering ZrC# 6 target |
Laura Lambert wrote: |
Monday, July 28, 2014, 14:41
Total number of foils: 445 discs
Total mass of materials [incl graphite foils]: 49.027 g
Total length packed: 11.2 cm
Container has no Ta heat shields.
Currently being pumped down.
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Tuesday, July 29, 2014, 11:19
Chamber was pumped down overnight to ~5.5e-7 torr.
HS water valve opened; no leaks were detected.
Stepped up TGHT/TBHT to 40A. IG went up 8e-6 Torr and stabilized.
Initiated auto-ramping TGHT @ 580A, TBHt @ 230A at 0.2A/min
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147
|
Friday, August 01, 2014, 11:47 |
Peter Kunz | | 40282-3 | LP-SIS | In progress | ZrC #6 conditioning | The maximum current of 580A was reached at 9:15.
TGHT:RDCUR 578 A
TGHT:RDVOL 9.87 V
IGP1:RDVAC 3.8e-6
The temperature was measured with the Minolta 2-color pyrometer:
from the side - inside target container : ~1200 deg C
from the front trough hole in the heat shield : ~1800 deg C
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148
|
Friday, August 01, 2014, 13:27 |
Peter Kunz | | 40282-3 | LP-SIS | In progress | ZrC #6 conditioning | Target was conditioned for 4 hours at 580A.
Initiating ramp-down sequence @ 2A/min
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Attachment 1: zrc6_conditioning.png
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149
|
Tuesday, August 05, 2014, 12:01 |
Laura Lambert | | 40282-3 | LP-SIS | Done | ZrC #6 conditioning |
Peter Kunz wrote: |
Target was conditioned for 4 hours at 580A.
Initiating ramp-down sequence @ 2A/min
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Tuesday, August 05, 2014, 12:00
target vented in air and taken out this morning
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155
|
Thursday, September 11, 2014, 14:23 |
Laura Lambert | | 40282-3 | TARGET BOAT | Failed | Sintering TaC coated end caps | Thursday, September 11, 2014, 13:14
The target container end caps were coated with TaC spray and let dry.
The caps are inserted in the target boat wrapped in graphite foil with 3 x Ta-heat shields.
The chamber is currently pumping down.
Friday, September 12, 2014, 14:17
Chamber was pumped down overnight.
HS cooling water valves opened, no leaks detected.
IGP1 = 7.2e-7 Torr.
TGHT stepped up to 35A, TBHT at 0A.
Waited ~30min, current stabilized, vacuum started to drop, auto-ramp initiated at 0.2A/min.
Will ramp TGHT to 580A with a max 10V.
Good vacuum: 3.00e-5 Torr; Bad vacuum: 4.00e-5 Torr.
Monday, September 15, 2014, 11:31
TGHT stopped at 500A due to not high enough voltage max.
Increased max voltage to 12V
Monday, September 15, 2014, 14:17
IGP1 = 6.3e-7 Torr
Increasing ramping rate to 1.0A/min
Tuesday, September 16, 2014, 09:04
TGHT reached 577A and finished auto-ramping, then proceeded to drop down to 560A overnight.
Increased max voltage to 13.05A and TGHT to 580A.
Tuesday, September 16, 2014, 13:52
TGHT reached 580A and sat there for ~5hrs.
IGP1 = 6.1e-7 Torr.
Initiating auto-cool at 2.0A/min.
Wednesday, September 17, 2014, 13:03
Vented in air.
Opened up....looked 'deceivingly' ok.
then i took a layer of Ta off....grrrr
the 1st layer of Ta was holding the boat together. as soon as that layer was taken off the target boat broke.
see attached photos.
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Attachment 1: IMG_20140917_142605683.jpg
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Attachment 2: IMG_20140917_143120141.jpg
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Attachment 3: IMG_20140917_143343399_HDR.jpg
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Attachment 4: Capture.JPG
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Attachment 5: Capture2.JPG
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293
|
Wednesday, May 04, 2016, 13:45 |
Laura Lambert | | 40282-3 | TARGET BOAT | In progress | Conditioning Nb samples for Tobias | Wednesday, May 04, 2016, 13:28
Target boat has a layer of niobium foil on the bottom of the boat.
A niobium foil has been made with slots to hold samples [similar to when sintering endcaps] *See attached photos
Larger niobium samples are placed in the slots, holding in place, to avoid warping; smaller niobium sample sitting inside the boat by itself.
Smaller sample closest to OMEGA IR reading [right side]
Boat is wrapped with 1 large layer of Ta foil, wrapped around the boat 3x, careful to avoid touching samples.
Loaded into evap2 yesterday.
Vacuum pump bearings gone - pump replaced this morning by vacuum group.
Pumping down now...
Friday, May 06, 2016, 13:36
HS water valves opened, no leaks detected.
Tapped up manually to 35A.
IGP1 = 2.4e-7 Torr
Setting auto-ramp rate at 0.2A/min to 250A over the weekend.
Will tap up manually monday to final desired temperature of 1400C.
Monday, May 09, 2016, 09:38
OMEGA = 1128C
IGP1 = 1.3e-7 Torr
TGHT = 250A, 3.7V
Tapping up manually to 1400C...
Monday, May 09, 2016, 14:05
Evap2 has reached ~1405C
TGHT = 341A, 5.34V
IGP1 = 1.9e-7 Torr
Will remain at max setpoints for min 4hrs then initiate cool down.
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Attachment 1: Nb_samples_in_boat_(2).jpg
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294
|
Monday, May 09, 2016, 18:19 |
John Wong | | 40282-3 | TARGET BOAT | In progress | Conditioning Nb samples for Tobias |
Laura Lambert wrote: |
Wednesday, May 04, 2016, 13:28
Target boat has a layer of niobium foil on the bottom of the boat.
A niobium foil has been made with slots to hold samples [similar to when sintering endcaps] *See attached photos
Larger niobium samples are placed in the slots, holding in place, to avoid warping; smaller niobium sample sitting inside the boat by itself.
Smaller sample closest to OMEGA IR reading [right side]
Boat is wrapped with 1 large layer of Ta foil, wrapped around the boat 3x, careful to avoid touching samples.
Loaded into evap2 yesterday.
Vacuum pump bearings gone - pump replaced this morning by vacuum group.
Pumping down now...
Friday, May 06, 2016, 13:36
HS water valves opened, no leaks detected.
Tapped up manually to 35A.
IGP1 = 2.4e-7 Torr
Setting auto-ramp rate at 0.2A/min to 250A over the weekend.
Will tap up manually monday to final desired temperature of 1400C.
Monday, May 09, 2016, 09:38
OMEGA = 1128C
IGP1 = 1.3e-7 Torr
TGHT = 250A, 3.7V
Tapping up manually to 1400C...
Monday, May 09, 2016, 14:05
Evap2 has reached ~1405C
TGHT = 341A, 5.34V
IGP1 = 1.9e-7 Torr
Will remain at max setpoints for min 4hrs then initiate cool down.
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Monday, May 09, 2016, 18:18
TGHT at 341A/5.34V for over 4 hours. Vac stables at 1.78e-7 Torr.
Cooling down at 2A/min
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295
|
Tuesday, May 10, 2016, 11:57 |
Laura Lambert | | 40282-3 | TARGET BOAT | Done | Conditioning Nb samples for Tobias |
John Wong wrote: |
Laura Lambert wrote: |
Wednesday, May 04, 2016, 13:28
Target boat has a layer of niobium foil on the bottom of the boat.
A niobium foil has been made with slots to hold samples [similar to when sintering endcaps] *See attached photos
Larger niobium samples are placed in the slots, holding in place, to avoid warping; smaller niobium sample sitting inside the boat by itself.
Smaller sample closest to OMEGA IR reading [right side]
Boat is wrapped with 1 large layer of Ta foil, wrapped around the boat 3x, careful to avoid touching samples.
Loaded into evap2 yesterday.
Vacuum pump bearings gone - pump replaced this morning by vacuum group.
Pumping down now...
Friday, May 06, 2016, 13:36
HS water valves opened, no leaks detected.
Tapped up manually to 35A.
IGP1 = 2.4e-7 Torr
Setting auto-ramp rate at 0.2A/min to 250A over the weekend.
Will tap up manually monday to final desired temperature of 1400C.
Monday, May 09, 2016, 09:38
OMEGA = 1128C
IGP1 = 1.3e-7 Torr
TGHT = 250A, 3.7V
Tapping up manually to 1400C...
Monday, May 09, 2016, 14:05
Evap2 has reached ~1405C
TGHT = 341A, 5.34V
IGP1 = 1.9e-7 Torr
Will remain at max setpoints for min 4hrs then initiate cool down.
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Monday, May 09, 2016, 18:18
TGHT at 341A/5.34V for over 4 hours. Vac stables at 1.78e-7 Torr.
Cooling down at 2A/min
|
Tuesday, May 10, 2016, 08:45
Vented in air and opened up this morning.
Samples look good!
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339
|
Tuesday, November 22, 2016, 15:58 |
Laura Lambert | Nb | 40282-3 | TARGET BOAT | Done | Conditioning Nb samples for Doug | Tuesday, November 22, 2016, 15:53
Target boat has a layer of niobium foil on the bottom of the boat.
A niobium foil has been made with slots to hold samples [similar to when sintering endcaps] *See attached photos
Niobium samples are placed in slots, holding in place, to avoid warping.
Smaller samples closest to MIKRON IR reading [left side]
Boat is wrapped with 1 large layer of Ta foil, wrapped around the boat 3x, careful to avoid touching samples.
Loaded into evap2 today.
Pumping down now...
Wednesday, November 23, 2016, 11:45
HS water valves opened, no leaks detected.
Tapped up manually to 35A.
IGP1 = 6.4e-7 Torr
Setting auto-ramp rate at 0.2A/min to max setpoint of 250A.
Will tap up manually to final desired temperature of 1400C.
Wednesday, November 23, 2016, 13:17
IGP1 = 5.9e-7
TGHT = 66A, 0.51V
Vacuum stable.
Increasing ramping rate to 1.0A/min
Thursday, November 24, 2016, 08:46
IGP1 = 3.9e-7 Torr
TGHT = 250A, 3.41V *NOTE: the current set reads 243.8A but the readout is 250A
OMEGA = 1013C
MIKRON has no reading yet
Tapping up manually to 1400C
Thursday, November 24, 2016, 15:42
Samples have remained at ~1400C for 5hrs.
IGP1 = 5.8e-7 Torr
TGHT = 420A, 6.5V
OMEGA = 1410C
MIKRON = 1420C
Initiating auto-cool at 2.0A/min
Friday, November 25, 2016, 11:39
Vented in air and opened up this morning.
Samples look good!
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Attachment 1: samples.jpg
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Attachment 2: evap2.jpg
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Attachment 3: heating_up.xlsx
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Attachment 4: visual_of_MIKRON_pointing_at_samples.JPG
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135
|
Friday, June 13, 2014, 14:57 |
Laura Lambert | Ta | 40282-2 | LP-SIS | In progress | Conditioning Ta#43 target | Friday, June 13, 2014, 14:53
Container is filled with 400 discs of Ta foils; target length = 5.2cm;
Total mass ( Ta foils + wire) = 45.92g
No Ta foil heat shield.
No caps inserted.
Chamber pumped down this morning.
HS cooling water valves opened, no leaks detected.
IG @ 5.8e-6 Torr.
TGHT max = 580A
TBHT max = 230A
Ramping rate 0.2A/min.
Monday, June 16, 2014, 11:46
TGHT and TBHT reached their respective 580A and 230A over the weekend.
IGP1 currently at 3.2e-7 Torr.
Internal temp [measured using mikron, right side of EVAP2, pointed at discs inside] = 1375C
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136
|
Monday, June 16, 2014, 17:42 |
John Wong | Ta | 40282-2 | LP-SIS | In progress | Conditioning Ta#43 target |
Laura Lambert wrote: |
Friday, June 13, 2014, 14:53
Container is filled with 400 discs of Ta foils.
No Ta foil heat shield.
No caps inserted.
Chamber pumped down this morning.
HS cooling water valves opened, no leaks detected.
IG @ 5.8e-6 Torr.
TGHT max = 580A
TBHT max = 230A
Ramping rate 0.2A/min.
Monday, June 16, 2014, 11:46
TGHT and TBHT reached their respective 580A and 230A over the weekend.
IGP1 currently at 3.2e-7 Torr.
Internal temp [measured using mikron, right side of EVAP2, pointed at discs inside] = 1375C
|
Monday, June 16, 2014, 17:21
Further stepping up TGHT to 650A.
Temperature measured on target discs = 1542C. Vac @ 3.28e-7 Torr.
Initiate cooling down process; 2A/min for TGHT; 1A/min for TBHT
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Attachment 1: Ta#43_3.JPEG
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137
|
Tuesday, June 17, 2014, 10:14 |
Laura Lambert | Ta | 40282-2 | LP-SIS | Done | Conditioning Ta#43 target |
John Wong wrote: |
Laura Lambert wrote: |
Friday, June 13, 2014, 14:53
Container is filled with 400 discs of Ta foils.
No Ta foil heat shield.
No caps inserted.
Chamber pumped down this morning.
HS cooling water valves opened, no leaks detected.
IG @ 5.8e-6 Torr.
TGHT max = 580A
TBHT max = 230A
Ramping rate 0.2A/min.
Monday, June 16, 2014, 11:46
TGHT and TBHT reached their respective 580A and 230A over the weekend.
IGP1 currently at 3.2e-7 Torr.
Internal temp [measured using mikron, right side of EVAP2, pointed at discs inside] = 1375C
|
Monday, June 16, 2014, 17:21
Further stepping up TGHT to 650A.
Temperature measured on target discs = 1542C. Vac @ 3.28e-7 Torr.
Initiate cooling down process; 2A/min for TGHT; 1A/min for TBHT
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Tuesday, June 17, 2014, 10:08
TGHT and TBHT reached 0A last night.
Turned off EVAP2
Venting chamber
Process Complete
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357
|
Thursday, April 06, 2017, 13:16 |
Laura Lambert | Empty | 40282-2 | TARGET BOAT | Done | Sintering TaC coating on evap1 target boat |
Laura Lambert wrote: |
Laura Lambert wrote: |
Laura Lambert wrote: |
Wednesday, April 05, 2017, 15:36
Coated container with TaC coating using spray technique this morning and let dry.
Wrapped with one long layer of Ta heat shield, wrapped around boat 3x
No ends to target boat
Installed in evap2 and pumping down now...
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Thursday, April 06, 2017, 08:56
Problems with IGP2
Won't turn on, has low voltage output.
See screenshot attached.
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Thursday, April 06, 2017, 11:12
Turns out it was just a bad connection.
See attached photos.
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Thursday, April 06, 2017, 13:16
HS water valves opened, no leaks detected.
Tapped up manually to 35A
Waited almost 2hrs
IGP1 = 9.9e-7 Torr
Initiating auto-ramp at 0.2A/min to 400A
Final desired temperature = 1900C
OMEGA slope = 0.98
Good vac at 3.0e-5, bad vac at 4.0e-5 Torr.
Monday, April 10, 2017, 09:26
IGP1 = 1.79e-7 Torr
TGHT = 400A, 6.47V
OMEGA = 1505C
Tapping up manually to 1900C...
Monday, April 10, 2017, 11:46
TGHT tripped off at 410A, ~1530C
Water is still on and good flow.
Vacuum was stable ~1.8e-7 Torr.
No power trips according to controls.
Not sure of reasoning behind trip.
Initially tried tapping back-up, no current was being applied.
Turned off and back on TGHT power supply - this restarted things and now works again.
Have tapped back up to 35A, vacuum still good.
Restarting auto-ramp to 400A at 1.0A/min
Monday, April 10, 2017, 13:13
Vacuum looks good.
IGP1 = 1.1e-7 Torr
TGHT = 127A, 1.30V
Increasing ramping rate to 2.0A/min
Monday, April 10, 2017, 16:08
IGP1 = 1.5e-7 Torr
TGHT = 400A, 6.24V
OMEGA = 1510V
Increasing auto ramp setpoint to 450A at a rate of 0.2A/min
Wednesday, April 12, 2017, 11:06
IGP1 = 2.96e-7 Torr
TGHT = 555A, 9.74V
OMEGA = 1935C
Has remained at max setpoints overnight.
Initiating auto-cool at 2.0A/min
Thursday, April 13, 2017, 11:59
vented in air and opened up this morning.
container looks good.
see photo attached.
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Attachment 1: IMG_1653.JPG
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274
|
Tuesday, February 16, 2016, 14:02 |
Laura Lambert | Empty | 40202-5 | TARGET BOAT | In progress | sintered TaC coating on target boat [container style with no ionizer tube] | Tuesday, February 16, 2016, 14:19
coated with TaC yesterday and let dry overnight.
wrapped with one long Ta heat shield - wrapped around tube 3x, with Ta wire to offset Ta foil away from container
loaded into evap2 and currently pumping down.
Wednesday, February 17, 2016, 10:51
HS water valves opened, no leaks detected.
Tapped up manually to 35A.
Waited ~20min, vacuum stable.
IGP1 = 5.9e-7 Torr.
Initiating auto-ramp at 0.2A/min to a final setpoint of 400A.
Final desired temperature = 1900C
Thursday, February 18, 2016, 09:16
IGP1 = 6.6e-7 Torr.
TGHT = 303A, 4.3V
OMEGA = 1311C
Increasing ramping rate to 1.0A/min.
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275
|
Thursday, February 18, 2016, 13:22 |
John Wong | Empty | 40202-5 | TARGET BOAT | In progress | sintered TaC coating on target boat [container style with no ionizer tube] |
Laura Lambert wrote: |
Tuesday, February 16, 2016, 14:19
coated with TaC yesterday and let dry overnight.
wrapped with one long Ta heat shield - wrapped around tube 3x, with Ta wire to offset Ta foil away from container
loaded into evap2 and currently pumping down.
Wednesday, February 17, 2016, 10:51
HS water valves opened, no leaks detected.
Tapped up manually to 35A.
Waited ~20min, vacuum stable.
IGP1 = 5.9e-7 Torr.
Initiating auto-ramp at 0.2A/min to a final setpoint of 400A.
Final desired temperature = 1900C
Thursday, February 18, 2016, 09:16
IGP1 = 6.6e-7 Torr.
TGHT = 303A, 4.3V
OMEGA = 1311C
Increasing ramping rate to 1.0A/min.
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Thursday, February 18, 2016, 13:10
TGHT reached to 450A, temp at 1800C. Stepped up TGHT 490A, temp measured at ~1900C.
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276
|
Thursday, February 18, 2016, 17:21 |
Laura Lambert | Empty | 40202-5 | TARGET BOAT | Done | sintered TaC coating on target boat [container style with no ionizer tube] |
John Wong wrote: |
Laura Lambert wrote: |
Tuesday, February 16, 2016, 14:19
coated with TaC yesterday and let dry overnight.
wrapped with one long Ta heat shield - wrapped around tube 3x, with Ta wire to offset Ta foil away from container
loaded into evap2 and currently pumping down.
Wednesday, February 17, 2016, 10:51
HS water valves opened, no leaks detected.
Tapped up manually to 35A.
Waited ~20min, vacuum stable.
IGP1 = 5.9e-7 Torr.
Initiating auto-ramp at 0.2A/min to a final setpoint of 400A.
Final desired temperature = 1900C
Thursday, February 18, 2016, 09:16
IGP1 = 6.6e-7 Torr.
TGHT = 303A, 4.3V
OMEGA = 1311C
Increasing ramping rate to 1.0A/min.
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Thursday, February 18, 2016, 13:10
TGHT reached to 450A, temp at 1800C. Stepped up TGHT 490A, temp measured at ~1900C.
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Thursday, February 18, 2016, 17:21
TGHT remained at max setpoint for 4hrs.
IGP1 = 6.6e-7 Torr.
OMEGA = 1913C
Initiating auto-cool for TGHT at 2.0A/min.
Friday, February 19, 2016, 14:17
evap2 vented and opened up this morning.
container looks good.
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90
|
Thursday, September 26, 2013, 15:17 |
John Wong | Empty | 39814-VI-? | LP-IG-LIS | Done | Sintering empty target oven coated with TaC for UCx#8 | Thursday, September 26, 2013, 13:04
The LP-IG-LIS target container is coated with TaC.
Container is wrapped with 3 layers of Ta heat shield and about to go through the sintering process.
A thermocouple is inserted to measure the temperature inside the tube (1st attempt ever).
Click on the link for detailed pictures:
https://www.dropbox.com/sh/6dc5arajg87mws9/6cU5OxjkZg
TGHT will be ramped up to 580A at 0.2A/min
TBHT will be ramped up to 230A at 0.2A/min.
Chamber has been pumped down. HS cooling H2O valves are opened, and no leaks are detected.
Currently IGP1 @ 5.9e-6 Torr.
Thursday, September 26, 2013, 15:44
TGHT stepped up to 30A. TBHT currently @ 0A.
Temp @ 35C, Vac @ 1.4e-5 Torr.
Monday, September 30, 2013, 14:54
The container was heated up to 580A TGHT/ 230A TBHT for a day (see attachment #1 for vac vs cur plot).
The temperature was measure at ~1780C. (see link for details: https://www.dropbox.com/sh/d8d9j2t60qlm3jk/nkMh7dx_R8 )
The target was cooled down and vented.
Proceed complete.
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Attachment 1: UCx#8_container_TaC_coat_sintering.PNG
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314
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Wednesday, August 17, 2016, 17:31 |
Laura Lambert | Empty | 39814-V2-1 | LP-IG-LIS | In progress | sintering TaC coating on SiC#34 container...round2 | Wednesday, August 17, 2016, 17:30
Container coated with TaC using 'flushing technique', cleaned ionizer tube with acetone, so no coating inside ionizer tube
Wrapped with 3 x Ta heat shields, incl center block
Currently pumping down in evap2
Thursday, August 18, 2016, 10:14
HS water valves opened...leak detected see attachment for photo from archives
Vented and opened up.
Anders performed leak check, nothing found.
Replaced all seals with blue seals.
Pumping down now
Thursday, August 18, 2016, 16:12
HS water valves opened...leak detected again see attachment for photo of striptool
Vented and opened up.
working with Anders on finding leak...
Monday, August 22, 2016, 10:38
leaks FIXED!
HS water valves opened, NO leaks detected!
Tapped up manually to 70A
Vacuum stable, IGP1 = 2.5e-6 Torr
Initiating auto ramp for TGHT @ 0.2A/min to a max setpoint of 350A
Initiating auto ramp for TBHT @ 0.1A/min to a max setpoint of 230A
Once max setpoints achieved, will tap up manually to final desired temperature of 1900C
Monday, August 22, 2016, 14:58
TGHT = 115A, 1.3V
TBHT = 89A, 0.97V
IGP1 = 4.1e-7 Torr.
Increasing ramping rate to 1.0A/min and 0.5A/min for the TGHT and TBHT respectively.
Monday, August 22, 2016, 16:01
IGP1 = 1.25e-6 torr
TGHT = 174A, 2.2V
TBHT = 118A, 1.4V
Lowering ramping rate to 0.2A/min and 0.1A/min for the TGHT and TBHT respectively for overnight ramping.
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Attachment 1: leak.JPG
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Attachment 2: water_leak.JPEG
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316
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Tuesday, August 23, 2016, 12:15 |
John Wong | Empty | 39814-V2-1 | LP-IG-LIS | Done | sintering TaC coating on SiC#34 container...round2 |
Laura Lambert wrote: |
Wednesday, August 17, 2016, 17:30
Container coated with TaC using 'flushing technique', cleaned ionizer tube with acetone, so no coating inside ionizer tube
Wrapped with 3 x Ta heat shields, incl center block
Currently pumping down in evap2
Thursday, August 18, 2016, 10:14
HS water valves opened...leak detected see attachment for photo from archives
Vented and opened up.
Anders performed leak check, nothing found.
Replaced all seals with blue seals.
Pumping down now
Thursday, August 18, 2016, 16:12
HS water valves opened...leak detected again see attachment for photo of striptool
Vented and opened up.
working with Anders on finding leak...
Monday, August 22, 2016, 10:38
leaks FIXED!
HS water valves opened, NO leaks detected!
Tapped up manually to 70A
Vacuum stable, IGP1 = 2.5e-6 Torr
Initiating auto ramp for TGHT @ 0.2A/min to a max setpoint of 350A
Initiating auto ramp for TBHT @ 0.1A/min to a max setpoint of 230A
Once max setpoints achieved, will tap up manually to final desired temperature of 1900C
Monday, August 22, 2016, 14:58
TGHT = 115A, 1.3V
TBHT = 89A, 0.97V
IGP1 = 4.1e-7 Torr.
Increasing ramping rate to 1.0A/min and 0.5A/min for the TGHT and TBHT respectively.
Monday, August 22, 2016, 16:01
IGP1 = 1.25e-6 torr
TGHT = 174A, 2.2V
TBHT = 118A, 1.4V
Lowering ramping rate to 0.2A/min and 0.1A/min for the TGHT and TBHT respectively for overnight ramping.
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Tuesday, August 23, 2016, 12:14
Initiate TGHT autoramping to 400A at 2A/min. Vac 3.5e-7 Torr.
Tuesday, August 23, 2016, 14:48
TGHt tapped up to 420A/7.01V. Local temp read at ~1900C. Will sinter at this temp for a few hours before cooling down.
Tuesday, August 23, 2016, 17:20
TGHT at been at 420A/7.01V for over 4 hours. Vac at 4.8e-7 Torr.
Cooling TGHT and TBHT at 1A/min.
Wednesday, August 24, 2016, 10:35
TGHT/TBHT at 0A.
Venting chamber.
Container looks good.
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