Logbooks Lab Maintenance Evaporator_1 Evaporator_2 Laser cutter Target Production Test-Stand RH-ISAC RH-Cyclotron RH-Meson Hall RH-Beamlines RH-ARIEL
  RH-ISAC, Page 92 of 138  Not logged in ELOG logo
ID Datedown Author Category Type Module Target/Number Subject
  932   Wednesday, June 03, 2015, 13:51 David WangConditioning StationStandard OperationTM4SiC #31TM4 is connected at CS

TM4 has been connected at CS. CS HV cover is installed.I made a pair of new cooling lines for TM window cooling at CS. The TM4 containment box window cooling line is connected to the HVC spare circuit now. I checked water flow visually, and it is good. The TM4 is ready for conditioning.See attachment for window cooling modification.

 

Attachment 1: 007.JPG
007.JPG
Attachment 2: 009.JPG
009.JPG
Attachment 3: 008.JPG
008.JPG
Attachment 4: 010.JPG
010.JPG
  931   Wednesday, June 03, 2015, 13:01 Anders MjosConditioning StationStandard OperationTM4SiC#31Conditioning SiC#31

PNG1 connected to PNG in service cap (as per David W)

 Wednesday, June 03, 2015, 12:59: Water on

Wednesday, June 03, 2015, 13:04: Staging enabled.

Wednesday, June 03, 2015, 14:02: Auto-ramping to 580 and 200 A at 2 and 1 A/min.

Wednesday, June 03, 2015, 14:03 : BIAS/EL/EE to 20/10/1.5 kV


ISAC operations monitored TCS from Wednesday to Monday


Monday, June 08, 2015, 08:55 : Started cool-down of target

Monday, June 08, 2015, 09:19: BIAS/EL/EE off

Monday, June 08, 2015, 09:32: EE configured to conditioning mode

Monday, June 08, 2015, 10:12 : TGHT and TBHT off

Monday, June 08, 2015, 10:25: BIAS/EL to 20/10 kV

Monday, June 08, 2015, 10:32: BIAS/EL to 30/15 kV

Monday, June 08, 2015, 10:45: BIAS/EL to 40/20 kV. Some bias sparking from ~39 kV

Monday, June 08, 2015, 13:40: BIAS/EL to 47.5/20 kV

Monday, June 08, 2015, 14:35: BIAS/EL to 50/20 kV

Monday, June 08, 2015, 14:39: BIAS/EL to 50/25 kV

Monday, June 08, 2015, 16:54: BIAS/EL to 53/25 kV

Monday, June 08, 2015, 17:03: BIAS/EL/EE off


Tuesday, June 09, 2015, 08:02: BIAS/EL to 30/15 kV

Tuesday, June 09, 2015, 08:07: BIAS/EL to 40/20 kV.

Tuesday, June 09, 2015, 08:13: BIAS/EL to 50/25 kV

Tuesday, June 09, 2015, 08:27: BIAS/EL to 53/25 kV 

Tuesday, June 09, 2015, 08:57: BIAS/EL to 55/25 kV  

Tuesday, June 09, 2015, 09:31: Power supplies tripped on IG2 vacuum after a spark at ~57.5 kV

Tuesday, June 09, 2015, 09:40: BIAS/EL to 40/20 kV.

Tuesday, June 09, 2015, 10:00 : BIAS/EL to 55/25 kV  

Tuesday, June 09, 2015, 10:09: BIAS/EL to 57.5/25 kV

Tuesday, June 09, 2015, 10:22: Sparking activity at 58 kV. Tripped TP2 and BV2. Reduced to 50 kV. Leakage current increased.

Tuesday, June 09, 2015, 10:33: Sparking activity at 55 kV. Reduce to 45 kV. Increased BIAS current limit from 0.25 to 0.30 mA

Tuesday, June 09, 2015, 10:41: BIAS/EL to 50/25 kV. BIAS RDCUR 0.17 mA, was 0.08 mA at 8:13 this morning.

Tuesday, June 09, 2015, 11:28 : Restarted TP2. Tripped.

Tuesday, June 09, 2015, 11:50:  Increased BIAS current limit from 0.30 to 0.35 mA

Tuesday, June 09, 2015, 11:55 : BIAS/EL to 54.5/25 kV for 5 min, 0.12 mA . Reducing to 40 kV for lunch break.

Tuesday, June 09, 2015, 13:07: BIAS/EL to 50/25 kV 

Tuesday, June 09, 2015, 13:27: BIAS/EL to 55/25 kV 

Tuesday, June 09, 2015, 13:40: BIAS/EL to 57/25 kV 

Tuesday, June 09, 2015, 13:49: BIAS/EL to 57.5/25 kV. Increased BIAS current limit from 0.35 to 0.40 mA

Tuesday, June 09, 2015, 14:30: IG1 tripped after spark. Controller seems to be broken. Forced IG1. Fault report submitted June 10th.

Tuesday, June 09, 2015, 14:58: BIAS/EL to 45/25 kV

Tuesday, June 09, 2015, 15:46: BIAS/EL to 55/25 kV

Tuesday, June 09, 2015, 15:55: BIAS/EL to 56/25 kV

Tuesday, June 09, 2015, 17:30: BIAS/EL to 57/25 kV 

Tuesday, June 09, 2015, 17:46: BIAS/EL to 57.5/25 kV 

Tuesday, June 09, 2015, 18:00: BIAS/EL to 58/25 kV

Tuesday, June 09, 2015, 18:30: No sparks for 30 min

Tuesday, June 09, 2015, 18:55: One spark observed. BIAS/EL off.

Tuesday, June 09, 2015, 18:56: Turbos stopped. Stopped water circuit.


Thursday, June 11, 2015: IG1 seems to work again after a power cycle. Controller tested with another IG. Closing Fault report

Attachment 1: SiC#31_Conditioning.docx
  930   Wednesday, June 03, 2015, 11:22 David WangConditioning StationStandard Operation  Target Hall Scheduled Activities April 07 - July 21 2015

I revised the Target Hall schedule to July 21 2015. It is the time new TM2 with ZrC target started at ITW.

2015-06-04, Updated the schedule with   new PDF view. See attachments 3, 4

Attachment 1: Target_Hall_Scheduled_Activities__Apr_07_to_July_21__2015.pdf
Target_Hall_Scheduled_Activities__Apr_07_to_July_21__2015.pdf
Attachment 2: Target_Hall_Scheduled_Activities__Apr_07_to_July_21_2015.mpp
Attachment 3: Target_Hall_Scheduled_Activities__Apr_07_to_July_21_2015.pdf
Target_Hall_Scheduled_Activities__Apr_07_to_July_21_2015.pdf
Attachment 4: Target_Hall_Scheduled_Activities__Apr_07_to_July_21_2015.mpp
  929   Tuesday, June 02, 2015, 14:39 David WangConditioning StationStandard OperationTM4SiC #31TM4 and CS turbo- pumps are started .

TM4 and CS turbo-pumps are started this afternoon. Everything is good so far.

  928   Tuesday, June 02, 2015, 14:38 David WangConditioning StationRepairTM4 replace broken TM4 IG1

 TM4 IG1 filament was broken during last run  at ITE.  The broken filament is replaced with a new one today when TM4 is located at CS.

2015-06-03 , Leak checked the new 25 conflat gasket today. No leak. See attachments

Attachment 1: 002.JPG
002.JPG
Attachment 2: 006.JPG
006.JPG
  927   Tuesday, June 02, 2015, 14:32 David WangSouth Hot-CellStandard OperationTM4SiC #31Leak check on TM4 HS water line with new SiC #31 target. at SHC

Chad and I leak checked TM4 HS water line with SiC #31 target installed. leak rate:0.0xE-9atm.cc/sec.  No leak.  The line will be helium pressurized at CS later.

2015-06-03, helium pressure test the line at CS. 70psi 3 minutes. leak rate 0.0xE-9 atm.cc/sec. No leak.   See attachments

Attachment 1: 003.JPG
003.JPG
Attachment 2: 005.JPG
005.JPG
Attachment 3: 001.JPG
001.JPG
  926   Tuesday, June 02, 2015, 11:54 Travis CaveConditioning StationStandard OperationTM4SiC#31Module moved

TM#4 with SiC#31 has been moved from the south hot cell to the conditioning station.

  925   Tuesday, June 02, 2015, 10:39 Travis CaveSouth Hot-CellStandard OperationTM4SiC#31Electrical Check

Electrical check on TM#4 with SiC#31. See attached PDF for details.

Attachment 1: TM4_SiC31_elecchk_SHC.PDF
TM4_SiC31_elecchk_SHC.PDF
  924   Tuesday, June 02, 2015, 09:43 chad fisherSouth Hot-CellStandard OperationTM4SiC#31SiC#31 installed

Ta #45 has been removed from TM4 and SIC#31installed.

  923   Tuesday, June 02, 2015, 06:51 David WangSouth Hot-CellStandard OperationTM4 Target Hall Scheduled Activities April 07 - June 26 2015

Target Hall schedule weekly update. All jobs are finished on time so far.

Attachment 1: Target_Hall_Scheduled_Activities__Apr_07_to_June_26_2015.mpp
Attachment 2: Target_Hall_Scheduled_Activities__Apr_07_to_June_26_2015.pdf
Target_Hall_Scheduled_Activities__Apr_07_to_June_26_2015.pdf Target_Hall_Scheduled_Activities__Apr_07_to_June_26_2015.pdf Target_Hall_Scheduled_Activities__Apr_07_to_June_26_2015.pdf Target_Hall_Scheduled_Activities__Apr_07_to_June_26_2015.pdf
  922   Monday, June 01, 2015, 14:24 Travis CaveSouth Hot-CellStandard OperationTM4Ta#45Electrical Check

Post beam electrical check on the Ta#45 target installed on TM#4. See attached PDF.

Attachment 1: TM4_Ta45_elecchk_postbeam.PDF
TM4_Ta45_elecchk_postbeam.PDF
  921   Monday, June 01, 2015, 11:23 Travis CaveITEStandard OperationTM4Ta#45Module moved

TM#4 with Ta#45 has been moved from the east target station to the south hot cell.

  920   Friday, May 29, 2015, 09:16 Travis CaveConditioning StationStandard OperationTM2no targetModule moved

TM#2 with no source tray has been moved from the conditioning station to the north east silo.

  919   Wednesday, May 27, 2015, 08:57 Travis CaveConditioning StationStandard OperationTM2 Module moved

TM#2 with no source tray has been moved from the south hot cell to the conditioning station.

  918   Tuesday, May 26, 2015, 14:34 chad fisherSouth Hot-CellRepairTM2 Shutter replacement

The shutter in TM2 was successfully replaced today.

New lock washer and nut were installed onto shutter and nut torqued to 120 ft lbs.

Shutter guide alignment tool was used to insure tapped shutter guide holes were concentric with thru holes in shutter side mounting panel, button head screws replaced and torqued to 110 ft-lbs.

The shutter was manually cycled open and closed by David and everything is to operate well.

Attachment 1: Shutter.jpg
Shutter.jpg
  917   Tuesday, May 26, 2015, 11:49 Grant MinorAssembly/Bench TestRepairTM2 TM2 New Source Tray - Braze & Solder Report - 22 May 2015

Hello,

For reference, I have attached a list of all solder joints in the TM2 Source Tray, and the alloys used for the most recent build (as per ITA6144).   I have also provided data sheets for the alloys, and PDF copies of all the drawings calling out the joints.

Certanium 34 C (222 deg C melt point) was used for all low-temperature solder applications, except for the steel inserts in the water blocks.  Previous revisions of the Source Tray drawings called out a higher-temperature McMaster lead-based solder (304 deg C melt point).  The change to Certanium 34 C on the prints was made in Bevan's era, during the transitional update of the source tray drawings between the TM1 and TM3 source tray projects, just before I took over updating the drawing packages.  I believe Bevan made this change on general advice from Guy Stanford, who stated that Certanium 34 C is a much easier solder to work with and makes a more mechanically reliable joint.  However, the change really should have had more review and validation testing before being implemented.

This said, we now have a source tray that uses Certanium 34 C, and rework of every joint would set us back too far in the schedule to meet the deadline, so we will have to run with it as it is.

Of particular concern are the joints on the target oven and coil heating blocks, which are now using a lower temperature solder (222 deg C melt vs 304 deg C melt).  We have experienced a coil block failure on TM4 due to a failed solder joint, although the failure mode is not known for certain.  We also had two recent failures on the test stand of a coil joint soldered with Certanium 34 C, but this was due to an error in the connection of cooling water to the joints (i.e. the joints had no coolant flow and the solder melted... this is expected!).

Anders and I have performed independent thermal analysis on the joints due to the radiative and electric heating from the target, and have concluded that even with a lower temperature solder, there is a lot of margin, so the risk seems to be low.  This work will be published in a separate report to be circulated later.

Thank you and regards,

Grant

Attachment 1: TM2_Source_Tray_-_Braze_and_Solder_Report_File_-_22May2015.pdf
TM2_Source_Tray_-_Braze_and_Solder_Report_File_-_22May2015.pdf TM2_Source_Tray_-_Braze_and_Solder_Report_File_-_22May2015.pdf TM2_Source_Tray_-_Braze_and_Solder_Report_File_-_22May2015.pdf TM2_Source_Tray_-_Braze_and_Solder_Report_File_-_22May2015.pdf TM2_Source_Tray_-_Braze_and_Solder_Report_File_-_22May2015.pdf TM2_Source_Tray_-_Braze_and_Solder_Report_File_-_22May2015.pdf TM2_Source_Tray_-_Braze_and_Solder_Report_File_-_22May2015.pdf TM2_Source_Tray_-_Braze_and_Solder_Report_File_-_22May2015.pdf
Attachment 2: 1005_Bare_DS.pdf
1005_Bare_DS.pdf
Attachment 3: 1005_Bare_MSDS.pdf
1005_Bare_MSDS.pdf 1005_Bare_MSDS.pdf 1005_Bare_MSDS.pdf 1005_Bare_MSDS.pdf
Attachment 4: Certanium_34C_Data_Sheet.pdf
Certanium_34C_Data_Sheet.pdf Certanium_34C_Data_Sheet.pdf
Attachment 5: Certanium_34C_MSDS.pdf
Certanium_34C_MSDS.pdf Certanium_34C_MSDS.pdf Certanium_34C_MSDS.pdf Certanium_34C_MSDS.pdf Certanium_34C_MSDS.pdf Certanium_34C_MSDS.pdf
Attachment 6: mcmaster_carr_solder_7667A23.pdf
mcmaster_carr_solder_7667A23.pdf
  916   Friday, May 22, 2015, 15:44 David WangITWStandard OperationTM1UCx125 Shielding blocks have been transferred from ITE to ITW.

5 shielding blocks have been transferred from ITE to ITW. I  checked all ITW water signals, and they are good.  ITW is configured to take proton beam.

  915   Wednesday, May 13, 2015, 13:55 chad fisherSouth Hot-CellRepairTM2 Shutter removal

TM2 has been successfully de-shuttered.

All went pretty much according to plan except I had to remove one fastener out of the upper wiring harness (the one that has just been installed) to allow for enough clearance to rotated the shutter guide out of the way...I shutter to think what would have happened otherwise...anyways...

Close inspection of the shutter does show that the "thin" area isn't in very good shape; whether this is a result of removal or just the way it was is hard.Due to the ease of removal I would quess that it may have been a preexisting condition. That being said...I think we may want to consider replacing it.

 

Attachment 1: TM2_20150513_131339.jpg
TM2_20150513_131339.jpg
Attachment 2: TM2_20150513_134232.jpg
TM2_20150513_134232.jpg
  914   Monday, May 11, 2015, 11:20 David WangSouth Hot-CellStandard OperationTM2 Target Hall Scheduled Activities April 07 - June 26 2015

The schedule has some changes due to  new TM2 source tray coil cooling line leaking at test stand. Now,It is re-scheduled in such an estimation  that TM2 source tray could be ready at teat stand by this Friday(May-15th). see attachment 1,2.

2015-05-12,  Changed  and updated the TH activity schedule according to Dons new beam schedule which is re-arranged after the coil line leaking issue. See attachments 3,4. No major conflicts has been found on the new schedule.

2015-05 25, Updated the TH activity schedule according to present TM2 job processing. See attachment 5,6.

Attachment 1: Target_Hall_Scheduled_Activities__Apr_07_to_June_26_2015.mpp
Attachment 2: Target_Hall_Scheduled_Activities__Apr_07_to_June_26_2015.pdf
Target_Hall_Scheduled_Activities__Apr_07_to_June_26_2015.pdf Target_Hall_Scheduled_Activities__Apr_07_to_June_26_2015.pdf Target_Hall_Scheduled_Activities__Apr_07_to_June_26_2015.pdf
Attachment 3: Target_Hall_Scheduled_Activities__Apr_07_to_June_26_2015.mpp
Attachment 4: Target_Hall_Scheduled_Activities__Apr_07_to_June_26_2015.pdf
Target_Hall_Scheduled_Activities__Apr_07_to_June_26_2015.pdf Target_Hall_Scheduled_Activities__Apr_07_to_June_26_2015.pdf
Attachment 5: Target_Hall_Scheduled_Activities__Apr_07_to_June_26_2015.pdf
Target_Hall_Scheduled_Activities__Apr_07_to_June_26_2015.pdf Target_Hall_Scheduled_Activities__Apr_07_to_June_26_2015.pdf Target_Hall_Scheduled_Activities__Apr_07_to_June_26_2015.pdf Target_Hall_Scheduled_Activities__Apr_07_to_June_26_2015.pdf
Attachment 6: Target_Hall_Scheduled_Activities__Apr_07_to_June_26_2015.mpp
  913   Monday, May 11, 2015, 10:45 Anders MjosConditioning StationMaintenance  RGA electronics box installed

 The communications chip has been replaced. The electronics box has been grounded (see attached pdf).

Attachment 1: 2015-05_RGA_GND_connection.pdf
2015-05_RGA_GND_connection.pdf 2015-05_RGA_GND_connection.pdf 2015-05_RGA_GND_connection.pdf
ELOG V2.9.2-2455