Logbooks Lab Maintenance Evaporator_1 Evaporator_2 Laser cutter Target Production Test-Stand RH-ISAC RH-Cyclotron RH-Meson Hall RH-Beamlines RH-ARIEL
  RH-ISAC, Page 87 of 138  Not logged in ELOG logo
Entry  Tuesday, September 01, 2015, 14:54, David Wang, ITW, Standard Operation, TM2, , TM2 has been connectec in ITW. 

TM2 has been connected in ITW. During the connection, Anders and I  found the TM2  high current cables used in ITE and CS are short in ITW.  Anders and Grant found the original TM2 ITE high current cables in target hall. We replaced them. They works fine. But, a little bit longer on cable length would be easy to connect them. All other connections and HV cover in ITW work for the TM2 so far.

Entry  Tuesday, September 01, 2015, 10:38, David Wang, ITW, Maintenance, TM2, , ITW top tank flange clean up and r-ring replacement. ITW_o-ring_replacement_2015-09-01_008.JPGITW_o-ring_replacement_2015-09-01_007.JPGITW_o-ring_replacement_2015-09-01_006.JPG

During last run, ITW dump circuit had a water leak on an adaptor below the pressure gauge. The top tank flange, slot, and O-ring were water contaminated by the leak. I removed the old o- ring, cleaned up the flange and o-ring slot, and put a new o-ring into the flange. Some  pictures will be attached in this mail later.

Entry  Tuesday, September 01, 2015, 10:32, Travis Cave, ITW, Standard Operation, TM2, ZrC #7, Module moved 

TM#2 with ZrC#7 has been moved from the conditioning station  to the west target station.

Entry  Tuesday, September 01, 2015, 06:25, David Wang, Conditioning Station, Standard Operation, TM2, ZrC, Argon venting TM2 at CS 

Argon venting TM2 at CS.

Entry  Thursday, August 27, 2015, 10:10, Anders Mjos, Conditioning Station, Standard Operation, TM2, ZrC#7, Conditioning new Source Tray 2015-08-31_Service_Cap_Sparking_on_Rubber_Plug.pdfTM2_Source_Tray_with_ZrC#7.docxVacuum_gague_calibration.xlsx

Thursday, August 27, 2015, 10:10: Started water system. TK2 level reduced from 24.9 to 23.5 in. 

IG2 not working. Force is ON.


EE in conditioning mode.

 Friday, August 28, 2015, 08:39: BIAS/EL 10 / 5 kV

Friday, August 28, 2015, 08:49: BIAS/EL 20 / 10 kV

Friday, August 28, 2015, 09:18 BIAS OFF. Ramping to 200/100 A at 2/1 A/min

Friday, August 28, 2015, 15:46: Target at 76 / 38 A. Changed ramping to 100/40 at 1/0.5 A/min

Friday, August 28, 2015, 22:20: Ramping down heaters.


Saturday, August 29, 2015, 09:50: RGA off. PNG1 7.85E-6 / 5.0E-6 T (EPICS / local)

Saturday, August 29, 2015, 10:11: BIAS/EL 20 / 10 kV

Saturday, August 29, 2015, 10:28: BIAS/EL 30 / 15 kV. Some sparking around 29 kV

Saturday, August 29, 2015, 10:43: 10 min w/o sparking

Saturday, August 29, 2015, 10:55: BIAS/EL 32 / 15 kV. Small vacuum responses for every 100 V increase

Saturday, August 29, 2015, 11:03: Sparking at 33 kV

Saturday, August 29, 2015, 11:12: BIAS/EL 34 / 15 kV

Saturday, August 29, 2015, 14:22: Power has returned after site-wide power outage, but no communication with IOC yet.

Saturday, August 29, 2015, 15:13: IOC restarted.

Saturday, August 29, 2015, 15:14: Starting turbos

Saturday, August 29, 2015, 15:22: Turbos at speed.

Saturday, August 29, 2015, 15:22 : MP3 not running. Investigating

Saturday, August 29, 2015, 15:47: Reset MP3 breaker (wait 5 min for capacitors to empty)

Saturday, August 29, 2015, 15:48: Water system running


Sunday, August 30, 2015, 09:38: BIAS/EL 10 / 5 kV

Sunday, August 30, 2015, 09:54: BIAS/EL 20 / 10 kV 

Sunday, August 30, 2015, 10:01: BIAS/EL 30 / 15 kV 

Sunday, August 30, 2015, 10:12: No sparking

Sunday, August 30, 2015, 10:27: BIAS/EL 35 / 15 kV 

Sunday, August 30, 2015, 10:37: No sparking

 Sunday, August 30, 2015, 10:52:  BIAS/EL 37.5 / 15 kV 

Sunday, August 30, 2015, 11:00:  BIAS/EL 37.5 / 20 kV. No sparks

Sunday, August 30, 2015, 11:22:  BIAS/EL 40 / 20 kV 

Sunday, August 30, 2015, 11:34: No sparks

Sunday, August 30, 2015, 12:00: BIAS/EL 42 / 21 kV

Sunday, August 30, 2015, 12:32: Sparking at 43.5 kV. Tripped off PS on conductivity (spark response)

Sunday, August 30, 2015, 12:44:  BIAS/EL 40 / 20 kV. ISAC Ops will monitor over lunch

Sunday, August 30, 2015, 14:20: BIAS/EL 43 / 20 kV

Sunday, August 30, 2015, 14:41: Sparking at 43.5 kV. lowered to 43 kV

Sunday, August 30, 2015, 15:56: Sparking every 5-10 min at 43.4 kV not able to increase to 43.5 kV. Sparking is causing signal response on water conductivity and drop in IG1 and IG1S readings during sparking.


Monday, August 31, 2015, 08:33: BIAS/ EL to 40 / 20 kV in 9 min w/o any sparking

Monday, August 31, 2015, 08:44: No sparking

 Monday, August 31, 2015, 08:46: BIAS/ EL to 42 / 20 kV

Monday, August 31, 2015, 08:53: BIAS/EL 43 / 20 kV. Two vacuum/current responses

Monday, August 31, 2015, 09:47: BIAS off to investigate spakring.

David observed sparking coming from under the HV cover on TM2 twice. When the cover was removed, spark marks on a rubber plug for the water lines was observed. The plug with marks and one more plug was removed from the service cap as it is not used. See attached PDF.

Monday, August 31, 2015, 10:09: BIAS/ EL to 40 / 20 kV in 8 min w/o any sparking

Monday, August 31, 2015, 10:15 BIAS/EL 43.5 / 22 kV. One small spark

Monday, August 31, 2015, 10:30: No sparks

Monday, August 31, 2015, 10:35: BIAS/EL 44 / 22 kV.

Monday, August 31, 2015, 11:00: BIAS/EL 45 / 22 kV.

Monday, August 31, 2015, 11:31: PNG1 taken out by a spark

Monday, August 31, 2015, 12:04: Reset power to PNG1 controller. PNG1 back online.

Monday, August 31, 2015, 12:25: BIAS tripped on IG1 after a spark at 47.1 kV

Monday, August 31, 2015, 12:39: BIAS/EL 47 / 24 kV. No sparks for 5 min

Monday, August 31, 2015, 12:54: PNG1 taken out by spark at 47.7 kV

Monday, August 31, 2015, 13:02: BIAS/EL 48 / 24 kV

Monday, August 31, 2015, 13:07: No sparks

Monday, August 31, 2015, 13:25: BIAS/EL 49 / 24 kV

Monday, August 31, 2015, 13:30: No sparks

Monday, August 31, 2015, 13:37: PNG1 returned after a spark

Monday, August 31, 2015, 14:06: BIAS/EL 50 / 25 kV

Monday, August 31, 2015, 14:45: No sparks.

Monday, August 31, 2015, 15:15: BIAS/EL 51 / 25 kV

Monday, August 31, 2015, 15:38: BIAS/EL 51 / 30 kV

Monday, August 31, 2015, 16:01: Tested XCB0 and YCB0 to 5 kV. Some sparking. Tested CCB0 to 4 kV. No sparking.

Monday, August 31, 2015, 16:50: No sparks for 1 hour at 51 / 30 kV.

Monday, August 31, 2015, 17:00: HV off.

 Monday, August 31, 2015, 17:07: EE at 2 kV, R= 1 MOhm

Monday, August 31, 2015, 17:08 : EE off.

Monday, August 31, 2015, 17:10: Water off.

Monday, August 31, 2015, 17:12 : Vacuum gauges off. Turbos off. Roughing pump off.

Entry  Thursday, August 27, 2015, 08:43, Travis Cave, Conditioning Station, Standard Operation, TM2, ZrC #7, Electrical Check TM2_elec_chk_ZrC7_CS.PDF

Electrical check of TM#2 at the conditioning station under vacuum. The resistance value of the target to 60kV common is a bit lower then what it was at the south hot cell.

Entry  Wednesday, August 26, 2015, 14:52, David Wang, Conditioning Station, Standard Operation, TM2, ZrC, Helium pressure test on TM2 HS and window lines at CS 

LD base LR 0.0xE-9 atm.cc/sec , 80 psi helium 2 minutes on HS and window circuits. No leak. Also, the reinstalled(after rewiring job) TP2 and PNG1(steers) side panel have been leak checked. No leak.

Entry  Wednesday, August 26, 2015, 14:30, David Wang, Conditioning Station, Standard Operation, TM2, ZrC, TM2 and Cs vacuum sysyem has been connected at CS. 

Turbo-pumps are started . The pumping down is good so far.

Entry  Wednesday, August 26, 2015, 14:28, David Wang, Conditioning Station, Standard Operation, TM2, ZrC, Leak check on TM2 HS and windowwater line with new ZrC target at SHC 

Chad and I leak checked TM2 HS and window circuit VCR joints with ZrC target and containment box installed at SHC. No leak has been found. They will   be helium pressurized  at CS later.

Entry  Wednesday, August 26, 2015, 11:12, Travis Cave, Conditioning Station, Standard Operation, TM2, ZrC #7, Module moved 

TM#2 with ZrC#7 has been moved to the conditioning station from the south hot cell.

Entry  Wednesday, August 26, 2015, 10:55, chad fisher, South Hot-Cell, Repair, TM2, ZrC#7, New wiring and target 20150826_090047.jpg

New wiring was installed yesterday as well as ZrC#7 which had its high current fasteners torqued to 130 in lbs.

 

Entry  Wednesday, August 26, 2015, 09:54, Anders Mjos, Conditioning Station, Maintenance, , , Topped up water in TCS:TK2 

 Filled to 24.9 in

Entry  Wednesday, August 26, 2015, 09:20, Travis Cave, South Hot-Cell, Standard Operation, TM2, ZrC #7, Electrical Check TM2_elec_chk_ZrC7_SHC.PDF

Electrical check of TM#2 with ZrC #7 installed

Entry  Tuesday, August 25, 2015, 13:54, Grant Minor, South Hot-Cell, Repair, TM2, ZrC#7, TM2 - Electrical / HV Short Repair and Current Status (ZrC target) TM2_Loose_Wires_Touching_Febiad_Gas_Line_notes_21Aug2015.jpgTM2_Wire_Bundle_Clear_of_Febiad_Gas_Line_notes_25Aug2015.jpg

Hello all,

TM2's first performance in the Conditioning Station with the new source tray was not great, with sparking and HV degradation beginning to occur at 30kV:
https://elog.triumf.ca/TIS/RH-ISAC/1039

This is perplexing, because the module without the source tray performed well at the TCS:
https://elog.triumf.ca/TIS/RH-ISAC/829

AND the new source tray performed well at the test stand (i.e. not inside the module):
https://elog.triumf.ca/TIS/Test-Stand/447

Upon inspection back at the Hot Cell last week after the failure, David Wang was observant enough to notice that one of the steerer coax wires (ground plane) was essentially touching one of the FEBIAD gas lines (HV plane) in the new source tray installation (photo attached).  Closer inspection by a group consisting of Anders, Alex, and myself revealed some apparent tracking and damage to the wire sheath.
https://elog.triumf.ca/TIS/RH-ISAC/1045

We believed at this point that the bad HV performance of TM2 was due to this problem.  The wires were originally arranged loose as it was believed it would be easier to install them in the Hot Cell this way.  However, it turned out to be a bad decision, as the wires at ground ended up becoming stray and touching the HV surface.

To correct the problem, the old wires were removed, and a new steere wire bundle was made using a PEEK material sheath.  This new sheath bundle was installed over the last day or so.  The penning gauge wire was kept separate from the steerer wire bundle.  You can see the new wire bundle and penning gauge wire in the attached photo, now with a healthy clearance to the FEBIAD gas lines.

Chad has been instructed to re-install the Einzel lens wire, install the new ZrC target, and replace the containment box in preparation for transport back to the TCS for another HV test.  If anybody would like to see the source tray today before ~3pm, I have asked Chad to wait for my final OK to put the containment box back on the module.

I apologize for this problem.  We are hopeful the solution we have installed will improve the HV performance.  Much work over the last 2+ years was put into building and installing this source tray by many contributors inside and outside of Remote Handling, and we want this module to succeed more than anybody!

Thanks and best regards,

Grant

Entry  Friday, August 21, 2015, 11:38, Anders Mjos, South Hot-Cell, Repair, TM2, FEBIAD Test Target, Steerer wires found to be touching the gas lines 

Yesterday TM2 was inspected in the SHC. Spark marks were found both on the steerer wires and on the ANODE wire. The steerer wires (GND)  were touching the gas lines (60kV). This is likely the cause of the sparking observed at the Conditioning Station (e-log).

Photos are available on DocuShare

Entry  Thursday, August 20, 2015, 13:48, David Wang, Conditioning Station, Standard Operation, TM2, , Target Hall Scheduled Activities April 07 - Sep 08 2015 Target_Hall_Scheduled_Activities__Apr_07_to_Sep_08.pdfTarget_Hall_Scheduled_Activities__Apr_07_to_Sep_08.mppTarget_Hall_Scheduled_Activities__Apr_07_to_Sep_08.mppTarget_Hall_Scheduled_Activities__Apr_07_to_Sep_08.pdf

 Weekly update target hall schedule.See attachment 1,2

Spring and summer run is close to the end. This will be the last update on this old schedule. See attachment3,4.    A new schedule for TH activities after mini shut down will be posted next time.

Entry  Thursday, August 20, 2015, 11:00, Travis Cave, Conditioning Station, Standard Operation, TM2, Dummy Target, Electrical Check TM2_elecchkdummytgtatCS.PDF

TM#2 electrical check at the conditioning station. All pumps were off but the module was not vented.

Entry  Thursday, August 20, 2015, 10:15, Travis Cave, South Hot-Cell, Standard Operation, TM2, Dummy Target, Module moved 

TM#2 is now in the south hot cell.

Entry  Thursday, August 20, 2015, 09:38, David Wang, Conditioning Station, Repair, TM2, , TM2 was disconnected at CS 

TM2 was disconnected at CS. Travis and I did  electrical check before the venting. After,The module was vented and moved to SHC. The moving is smooth.

Entry  Wednesday, August 19, 2015, 14:52, David Wang, Conditioning Station, Repair, TM2, , TM2 at CS 

During the TM2 HV test at CS, It failed. In order to confirm there is no any water leak inside the module after the heaters and beam extraction test, I disconnected all the water lines on the TM2, and purged the water lines with pressure air. Leak detector was reconnected back to the TM2 service cap, and all water lines are pressurized with 80psi helium again each for 2 minutes.No any leak had been found during the test. All the water lines are still perfectly sealed. Also, I checked all the vacuum to air seals on the top of the module.They are good either.  Anders used the RGA  tracking the helium during the test. No leak.

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