Friday, August 12, 2016, 09:58, chad fisher, South Hot-Cell, Maintenance, , , Manipulator Maitenance
|
Disassembled the master side of the right manipulator this morning to check the wrist cable. The cable on the master side shows no sign of wear or fraying suggesting that the slave side cable may be the item that is wearing. during disassembly of the master I did notice some loose parts that could have been the source of the audible concern but should not have contributed to the slippage felt in the gripper. I will try and schedule Tuesday for entry into the hot cell to address the slave cable. |
Thursday, August 11, 2016, 10:37, David Wang, Conditioning Station, Repair, TM3, , TM3 service tray cover plate ITA2108 has been removed.
|
Requested by Aurelia, and approved by Friedhelm, TM3 service tray cover plate ITA2108 has been remove out of the module. The plated is checked for active and contamination after removal. Then,It is double bagged, sealed , tagged, and placed downstairs in TH between south wall and green block . The ram contact reading on the plate is about 10 usv/hr. We will do anther TM3 HV test at TCS without this cover plate. |
Wednesday, August 10, 2016, 14:38, Isaac Earle, North Hot-Cell, Development, , , North Hot Cell Ventilation Test Results
|
Testing was performed on August 9th on the ISAC nuclear ventilation system to determine if the existing ventilation system can achieve the required cell depressions for both SHC and NHC under all expected configurations and if a proposed modification to the DDC control system can provide acceptable stability and response time for the system. The proposed control system observes the lower of the SHC depression or the NHC depression + 10% (to avoid stability issues), and adjusts the dampers to try to achieve 250Pa (1.00" WC) depression in the area it is observing. With the proposed control system the SHC and NHC dampers are programmed to be at the same position, but can be tuned with a bias between them if required to achieve all ventilation requirements. The NHC and SHC dampers are programmed with a limit at 90% of the fully-open position. There is a damper in the ducting system in the section of duct after the SHC and NHC legs join together; this is set at 50% open, and was not adjusted during the the tests. Test summary and results are listed below:
1. Prior to switching to SHC+NHC control mode, the flow rate and depression of the SHC was measured with the lid on: 266Pa cell depression, damper 47% open, duct flow 417cfm. The lid was opened and the measurements repeated: 35Pa, damper 90% open, duct flow 630cfm (results in 83ft/min, 0.42m/s average flow velocity across HC module opening)
2. The control system was switched to the new SHC+NHC single control loop system. Measurements were taken with both hot cell lids closed. SHC: 246Pa, damper 72% open, 350cfm flow rate. NHC: 257Pa, damper 72% open, 510cfm flow rate. The ventilation fan speed was then increased from 53Hz to 57Hz (maximum speed is 60Hz). Measurements were taken with both hot cell lids closed. SHC: 257Pa, damper 51% open, 353cfm flow rate. NHC: 257Pa, damper 51% open, 515cfm flow rate.
3. The SHC module port lid was opened and the NHC lid left closed. SHC: 37Pa, damper 90% open, 462cfm (results in 61ft/min, 0.31m/s average flow velocity across HC module opening). NHC: 249Pa, damper 90% open, 551cfm.
4. The NHC module port lid was opened and the SHC lid closed. SHC: 203Pa, damper 90%, 360cfm. NHC: 33Pa, damper 90%, 648cfm (results in 85ft/min, 0.44m/s average flow velocity across HC module opening). The fan speed was then increased to 60Hz (max speed) to see if the depression setpoint for the SHC could be achieved in this configuration. SHC: 231Pa, damper 90%, 389cfm. NHC: 29Pa, damper 90%, 705cfm (results in 93ft/min, 0.47m/s average flow velocity across HC module opening)
5. Both SHC and NHC module port lids were opened and the fan was left at 60Hz. SHC: 31Pa, damper 90%, 448cfm (results in 59ft/min, 0.30m/s average flow velocity across HC module opening). NHC: 29Pa, 90% damper, 669cfm (results in 88ft/min, 0.45m/s average flow velocity across HC module opening)
For all tests the control system arrived at a stable depression value in less than 5 minutes, and thereafter exhibited only minor fluctuations.
It was observed that when the fan speed was increased to 57Hz, and for the duration of the tests, there was negligible change in the depression and damper positions for the mass separator room and target pit area.
The HEPA filter in the SHC leg of ducting has not been changed since commissioning of the facility (~15 years), and the SHC charcoal filters have not been changed since installation approximately 5 years ago. The SHC pre-fitler located inside the cell was changed in January 2016. When these are changed (which should be done before commissioning of the NHC ventilation system), the difference between SHC and NHC flow rates should decrease, and the SHC depression with NHC open should increase (likely up to the 250Pa setpoint).
Conclusion: The new SHC+NHC single control loop system effectively controls the system under all conditions tested. The existing ventilation system achieved the required NHC depression (250Pa, from RS 50, Document #131915) with both cells closed, and with SHC open only. The same depression for SHC with both cells closed was achieved with both cells closed, but only reached 231Pa w/ NHC open (203Pa at 57Hz fan speed). It is expected that 250Pa can be easily achieved in the final system because the NHC will be better sealed than in its current condition, the damper in the shared SHC/NHC leg can be opened further, there will be greater flow through the SHC leg after changing the HEPA and charcoal filters, and the system can be tuned to better balance the SHC and NHC flow rates. RS51 states "the ventilation system should maintain an average air flow velocity of 0.5m/s across the opening into the hot cell". This is almost achieved with the NHC open, but SHC only had 0.3m/s average flow velocity. It should be possible to increase both to > 0.5m/s by further opening the shared leg damper and tuning the system to have more balanced flow rates. At the very least, both SHC and NHC should have > 0.42m/s average flow velocity to match what is currently achieved in SHC only mode (measured in test step #1), which to date has not allowed contamination to escape out the top of the hot cell. Depending on what flow velocity is deemed acceptable, after commissioning it may be possible to have both the SHC and NHC open concurrently based on the results of Test 5. At the time of commissioning, the SHC/NHC damper bias and NHC air inlet damper should both be tuned to achieve as similar depression and flow rate conditions as possible for both cells, and to meet all requirements in the RS document.
Notes:
Duct flow rate was calculated assuming that measured flow velocity at the center of the duct is 90% of average duct velocity. The duct ID at the sample location is 7.75", the hot cell opening size used for SHC and NHC module opening flow velocity calculations was 33" x 33".
Duct flow velocity measurements were taken using a thermal anemometer (Model number: 9555-P, Serial number: 9555:1108059 Rev. 2.11.0, Last calibrated by Rob Walker on April 29, 2016).
After completion of the tests the system was restored to it's original configuration and the ISAC target hall was swiped for contamination: none found. No EF12 trips occurred during these tests. |
Wednesday, August 10, 2016, 12:18, chad fisher, South Hot-Cell, Maintenance, , , Anteroom clearing
|
Black "radio active" materials cabinet has been emptied, items bagged and removed from the anteroom. Cabinet itself has been swiped inside and out and also been removed from the anteroom. Most items have been removed from the anteroom now save some cardboard, rolls of plastic etc. |
Wednesday, August 10, 2016, 11:30, David Wang, ITE, Standard Operation, TM4, UC#17, TM4 has been connected at ITE
|
Dan and I connected TM4 in ITE yesterday. It is pumping down at ITE now. Everything is fine so far. |
Wednesday, August 10, 2016, 09:44, Travis Cave, Conditioning Station, Standard Operation, TM3, no target, module moved
|
TM#3 has been moved from the north east silo to the conditioning station. |
Tuesday, August 09, 2016, 11:36, Anders Mjos, Conditioning Station, Maintenance, , , RGA and CG1S moved
|
The locations (ports) for the RGA and CG1S was swapped today by Anders and Isaac to provide clearance for the North Hot Cell ventilation. Attached photos show old and new locations. |
Tuesday, August 09, 2016, 10:05, Travis Cave, ITE, Standard Operation, TM4, UC#17, module moved
|
TM#4 with UC#17 is now in the east target station. |
Tuesday, August 09, 2016, 07:15, David Wang, Conditioning Station, Standard Operation, TM4, UCx17, TM4 has been disconnected at TCS
|
I stopped TCS water pumps this morning . The argon venting for TCS is in processing. |
Monday, August 08, 2016, 11:24, chad fisher, South Hot-Cell, Maintenance, , , Anteroom Clean-up - Waveguide
|
The wave guide from TM3 has been surveyed, swiped and removed from the anteroom and transported to rad waste for disposal. The wave guide has been stored in the anteroom since its removal. |
Friday, August 05, 2016, 14:13, Isaac Earle, North Hot-Cell, Development, , , Preparations for NHC Ventilation Test
|
A hole was drilled in the NHC exhaust duct in the east end of the target hall above the hatch to the Ante Room. This will be used for measuring NHC exhaust flow rate with a thermal anemometer. The hole was tapped and plugged with an NPT tap.
Flow was measured in the existing hole in the SHC exhaust duct in approximately the same location. Flow velocity was measured to be 1415 ft/min with the lid on the SHC. Using duct ID 7.75", and assuming the average flow velocity is 90% of the flow at duct center, the flow rate was found to be 417cfm. We will attempt to match this figure for the NHC when the ventilation tests are performed. The tests have been scheduled for the maintenance day on Tuesday August 9th.
The anemometer probe and SHC test port plug were checked for contamination: none found. |
Friday, August 05, 2016, 13:50, chad fisher, South Hot-Cell, Maintenance, , , Anteroom clean out
|
Some items have been removed from the anteroom in preparation for painting. Items have been placed on plastic in the south hot cell service area. No contamination found so far. |
Thursday, August 04, 2016, 08:56, Travis Cave, Spent Target Vault, Standard Operation, , UC#16, Spent Target move
|
The spent UC #16 have been moved from the south hot cell to the storage vault see attached PDF for details. |
Wednesday, August 03, 2016, 10:02, Travis Cave, South Hot-Cell, Standard Operation, TM4, UC#17, Electrical Check
|
The result of yesterdays electrical check on TM#4 with UC#17. |
Wednesday, August 03, 2016, 09:56, David Wang, Conditioning Station, Standard Operation, , , Target Hall schedule for beam schedule 130 (Apr- Oct, 2016)
|
Update schedule weekly. See attachments 1,2 |
Wednesday, August 03, 2016, 09:49, David Wang, Conditioning Station, Standard Operation, TM4, , TM4 is ready for conditioing at TCS.
|
I started TCS water system and installed HV cover onto TM4. The TM4 containment box is supplied with water also. TM4 is ready for conditioning at TCS. |
Wednesday, August 03, 2016, 09:45, David Wang, Conditioning Station, Standard Operation, TM4, UC#17, Helium pressure test on TM4 HS line at TCS
|
Helium pressure test on TM4 HS line at TCS is done.Leak detector 0.0X E-9atm.cc/sec. 5minutes, 70psi helium. No response on LD. |
Wednesday, August 03, 2016, 09:15, chad fisher, South Hot-Cell, Repair, , , Manipulator
|
East manipulator on the south hot cell is showing signs of eminent wrist/tong cable failure. Some slight slippage was noted yesterday and confirmed by a snapping sound and more slippage tomorrow. |
Wednesday, August 03, 2016, 08:08, Anders Mjos, Conditioning Station, Standard Operation, TM4, UC#17, Conditioning UC#17
|
Wednesday, August 03, 2016, 08:08: RGA on
Wednesday, August 03, 2016, 11:25: Configured EE to be connected to EE PS (not grounded)
Wednesday, August 03, 2016, 11:25: PS on
Wednesday, August 03, 2016, 11:32: BIAS / EL / EE to 20 / 10 / 1 kV
Ramping set to 40 / 20 A at 1 / 0.5 A/min. Good / bad vacuum at 2.0 / 2.2 E-6 T (IG2). Vacuum too high.
Wednesday, August 03, 2016, 13:02: BIAS / EL / EE to 30 / 15 / 1.5 kV
Wednesday, August 03, 2016, 15:59: BIAS / EL / EE to 35 / 17.5 / 1.5 kV. Some conditioning from 30 kV
Chiller staging stopped working around midnight. TGHT and TBHT ramped down by ISAC operators.
Thursday, August 04, 2016, 08:14: Ramping target to 50 / 25 A
Thursday, August 04, 2016, 08:22: Cycled power on chiller to reset alarm. Repeated again 5 min later
Thursday, August 04, 2016, 08:37: BIAS / EL / EE to 30 / 15 / 1.5 kV
Thursday, August 04, 2016, 09:36: Continue ramping to 100 / 50 A
Thursday, August 04, 2016, 11:32: Continue ramping to 120 / 60 A
Thursday, August 04, 2016, 14:50: ramping down
Friday, August 05, 2016, 07:09: Started cooling system
Friday, August 05, 2016, 07:56: Started ramping to 100 / 50 A
Friday, August 05, 2016, 14:27: TGHT / TBHT at 253 / 126 A.
Friday, August 05, 2016, 14:30: Ramping down at 2 / 1 A/min
Friday, August 05, 2016, 15:27: BIAS / EL / EE off
Monday, August 08, 2016, 08:15: Continue ramping. : BIAS / EL / EE to 30 / 15 / 1.5 kV
Monday, August 08, 2016, 14:36 TGHT / TBHT at 260 / 130 A. Ramping down at 2 / 1 A/min
Monday, August 08, 2016, 15:30: BIAS / EL off. EE remains at 1 kV.
Monday, August 08, 2016, 22:56: RGA off. Water system fault. Running CP1 manually
Monday, August 08, 2016, 22:57: EE off.
Monday, August 08, 2016, 22:58: Vacuum off |
Tuesday, August 02, 2016, 15:22, David Wang, Conditioning Station, Standard Operation, TM4, UC#17, TM4 with new target has been connected at TCS
|
It is being pumped now at TCS. |
|