Logbooks Lab Maintenance Evaporator_1 Evaporator_2 Laser cutter Target Production Test-Stand RH-ISAC RH-Cyclotron RH-Meson Hall RH-Beamlines RH-ARIEL
  RH-ISAC, Page 70 of 138  Not logged in ELOG logo
  ID Date Author Categorydown Type Module Target/Number Subject
  1638   Tuesday, October 10, 2017, 10:38 David WangITWStandard Operation   5 shielding blocks have been transferred from ITE to ITW .

ITW is configured to take proton beam.

  1661   Tuesday, November 14, 2017, 10:01 Travis CaveITWStandard OperationTM2Ta#55Module move

 TM#2 with Ta#55 has been moved from the conditioning station to the west target station. The field was measured on the access panel to the service chase and the field was found to be 430uSv/hr at one meter from the module.

  1662   Tuesday, November 14, 2017, 14:34 David WangITWStandard OperationTM2Ta#55TM2 has been connected in ITW.

TM2 has been connected in ITW. All turbo-pumps are started. Everything works fine.

  1670   Friday, December 22, 2017, 11:09 Anders MjosITWStandard OperationTM2 Shut down High Active Cooling water

Stopped MP1 today in preparation for the power outage over the holidays. both P-25 and P-26 breakers have been switched off to prevent inadvertent start of system

  1686   Tuesday, February 13, 2018, 13:56 Anders MjosITWStandard OperationTM2Ta#55Target module disconnected

TM disconnected by David and Yasmine Feb 8th. One of the water couplings were leaking for a short while when disconnected. NCR 10836 submitted by Max

  1687   Wednesday, February 14, 2018, 10:06 Anders MjosITWMaintenanceTM2 Replaced parker couplings on Window cooling line

By Anders & David. Couplings will be taken apart for inspection.

  1688   Friday, February 16, 2018, 13:46 Anders MjosITWMaintenanceTM2 Parker coupling inspection

Findings and photos from the inspections attached. The inspection was conducted by Anders, David and Maico.

Attachment 1: Used_Parker_FS251_Inspection.pdf
Used_Parker_FS251_Inspection.pdf Used_Parker_FS251_Inspection.pdf
  1691   Tuesday, March 06, 2018, 09:53 David WangITWStandard OperationTM2 Tm2 and Tm4 vacuum disconnection

The job is done. See attachment.

Attachment 1: TM2_TM4_disconnection_Vacuum.pdf
TM2_TM4_disconnection_Vacuum.pdf TM2_TM4_disconnection_Vacuum.pdf
  1692   Wednesday, March 07, 2018, 10:18 David WangITWStandard Operation  Oil leak on target station vacuum primary back pump.

I can not see oil in sight window of the primary pump during visual inspection. The aluminum tray underneath the pump is filled with oil. The performance on this pump start to drop by watching ITH CG4 reading. A fault report with suggestion is issued to vacuum group.  Everything on secondary pump looks fine.

  1694   Thursday, March 08, 2018, 14:10 David WangITWMaintenance  Two small water leak has been found in ITW.

Two small water leaks have been found on ITW High active water system. One is from an unused 1/4" copper valve stem. another is on supply 1.5" supply line valve body top sealing. Both of them are seeping water from seal. 1/4" copper valve will be replaced with a new one. 1.5" supply line valve will be replaced by an old valve with all new seals. I have all spare parts in hand.  At present, water supply to ITW are stooped to reduce leak rate. Two aluminum flat tray are put underneath leak valves to hold small amount leak water. Both leak will be fixed in April  mostly.

  1696   Thursday, April 05, 2018, 11:29 David WangITWMaintenance  ITH MP1 replacement

ITH MP1 is replaced today with a new style pump.The new pump is 0.75 inch higher than  old pump on inlet and exhaust so a new solid inlet adapter  (KF50-25) has to been used. For future secondary pump ITH MP1S replacement, we need a new adapter 0.75 inches shorter as well.   The new pumps is started . Everything works fine. Old pumps is drained , bagged, and stored in TH B2 level. All radioactive garbage produced during the job are bagged , tagged, and stored in TH as well.

  1697   Monday, April 09, 2018, 06:36 David WangITWStandard Operation  ITW Turbo -pumps switch off

I asked MCR to switch off ITW TP3,4 TP1s,2s this morning.

  1701   Tuesday, April 17, 2018, 11:05 David WangITWRepair  Disconnect ITW entrance module

ITW entrance module has been disconnected.  All connections are labelled before or during disconnection. The 24VDC electrical plug on ITW TP1S is broken . It will be replaced with a new plug. The lift yoke is installed onto module without difficulty.   

  1702   Thursday, April 19, 2018, 10:27 Travis CaveITWMaintenance  Entrance module move

 The west entrance module has been moved from the west target station to the silo.

  1703   Friday, April 20, 2018, 15:33 Keith C NgITWRepair  ITW beam tube repair job

2A2 window has been removed from ITW and beamlines has removed the beamtube from the penetration. The penetration has been sealed with plastic sheeting and duct tape to maintain the ventilation depression between the 2A tunnel and the Target Pit.

Window is currently stored in a lead flask in the target hall. Window fields are 26 mSv/h OC, 1.2 mSv/h at .5m. There is a 10 uSv/h field outside the flask with the window inside it.

Clamp is currently sitting bagged in ITW Station Pit, it is quite corroded.

Tank flange was video inspected but still needs to be cleaned, currently there is a slip on dust cover over the flange to protect it.

Work will resume after the nuclear ventilation comissioning is completed.

 

 

 

Attachment 1: 20180420_2a2beamtuberepair_P1040034.JPG
20180420_2a2beamtuberepair_P1040034.JPG
Attachment 2: 20180420_2a2beamtuberepair_P1040030.JPG
20180420_2a2beamtuberepair_P1040030.JPG
Attachment 3: 20180420_2a2beamtuberepair_P1040029.JPG
20180420_2a2beamtuberepair_P1040029.JPG
Attachment 4: 20180420_2a2beamtuberepair_P1040036.JPG
20180420_2a2beamtuberepair_P1040036.JPG
  1704   Friday, April 27, 2018, 15:06 Keith C NgITWRepair  ITW beam tube repair

Vacuumed out remainder of debris from the wall penetration, removed cradle and checked condition. Down stream support bracket sees advanced stages of material loss (OBO 20-30% loss). See attached photos.

RPG reports that the removed beam tube has 15k CPM on the interior of the beam tube.

Tank flange was cleaned as per 2009 repair report, looks OK. Video capture of flange inspection attached as .zip file.

.03" shim was inserted into the clamp indexing block.

 

Attachment 1: 20180427_2a2windowbeamline_P1040042.JPG
20180427_2a2windowbeamline_P1040042.JPG
Attachment 2: 20180427_2a2windowbeamline_P1040043.JPG
20180427_2a2windowbeamline_P1040043.JPG
Attachment 3: 20180427_2a2windowbeamline_P1040044.JPG
20180427_2a2windowbeamline_P1040044.JPG
Attachment 4: 20180427_2a2windowbeamline_P1040046.JPG
20180427_2a2windowbeamline_P1040046.JPG
Attachment 5: 20180427_2a2windowbeamline_P1040041.JPG
20180427_2a2windowbeamline_P1040041.JPG
Attachment 6: 2018_2a2windowinspection.zip
  1705   Tuesday, May 01, 2018, 10:54 Keith C NgITWRepair  2a2 window installation and beamtube repair

Yesterday we installed the 2a2 window, the drive screw was torqued until 70 ft-lbs and we stopped, the yoke is not fully closed to its hard stop with roughly 7/8" to 3/4" still to go. Similar to identical conditions to 2a3 beamline window install, see https://elog.triumf.ca/TIS/RH-ISAC/647 for that install. Otherwise clamp looks centered and installed correctly.

 

2018_2a2window00017.jpg

 

 

Concerns with the cooling lines for the window WRT to the base of the shielding plug: There is no jog bend indicated on drawings for the transition of the window cooling lines from beamline center to the corner of the shield plug penetration. See photo for cooling line position on initial removal of shielding plug. It was decided to not add a jog for the shield plug and to carefully reinsert it being mindful of the cooling lines.  The shielding plug has a chamfer on the corner to allow the cooling lines to be routed to the top.

 

20180420_2a2beamtuberepair_P1040025.JPG

 

 

A new beam tube cradle is being manufactured where the old one will removed and the new one swapped with the beam tube in situ. Both sides of the window still need to be leak checked.

  1710   Friday, May 04, 2018, 11:21 David WangITWRepair  2A2 winodw leak check in TH

Anders and I leak checked new 2A2 window seal on ITW side. Leak detector was connected  to ITW TP4.  Base  leak rate 0.0Xe-9 atm.cc/sec. base pressure 0.0xe-4 torr.  Sprayed 15-20 psi directly underneath 2A2 window by using exist 2a2 window leak check copper tube. The leak detector got response in 5 seconds when helium was applied. the leak rate was 5xe-6 atm.cc/sec. Once the helium source was closed, the leak rate dropped quickly back to base level. To confirm the leak is at window , I sprayed 15 psi helium around all top flange seals of TM and entrance module.  There was no direct response during the spray( about 1.5- 2 minutes). There was a weak slow up response (up to 1.0 xe-7 atm.cc/sec) which was started after 1.5 minutes of spray. The weak response is cause by helium drift in my view.   Our conclusion is the 2A2 window seal on ITW side is not perfectly sealed.  The elak we saw on LD is ture , and it is located on window.  The station will be vented soon for shielding plug moving back. .

  1712   Wednesday, May 09, 2018, 08:48 David WangITWRepair  2A2 winodw leak check on ITW vacuum vessel.

Leak detector is connected to ITW TP4. LD Base leak rate 0.0XE-09 atm.cc/sec. Helium line is connected to existing window leak check 1/8 " copper tube. Applied 18psi helium for 1 minute. No response on LD. The window seal is good on ITW vacuum vessel. 

  1716   Thursday, May 17, 2018, 13:17 Travis CaveITWStandard Operation  Entrance module move

 The west entrance module has been moved from the silo to the west target station.

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