Logbooks Lab Maintenance Evaporator_1 Evaporator_2 Laser cutter Target Production Test-Stand RH-ISAC RH-Cyclotron RH-Meson Hall RH-Beamlines RH-ARIEL
  RH-ISAC, Page 54 of 138  Not logged in ELOG logo
ID Date Author Categorydown Type Module Target/Number Subject
  2723   Tuesday, November 26, 2024, 14:52 Aaron TamSouth Hot-CellStandard OperationTM3UCx#47 UC#47 LP-SIS w/ gas Install

 November 26, 2024 - Aaron Tam 

Handover from TPO and inspection

  • Completed
  • Some modification to the center Inner-Outer conductor had to be made (hole enlarged as tab was slightly short)

Target Insertion:

  • Successful 

Target Mounting:

  • Upon fully seating UC#47 on service tray locating pins, the gas line VCR gasket came off 
    • Operator doesn't have line-of-sight to this area, so there has to be healthy clearance (Foreshadowing) 
    • Gas line VCR gasket reinstalled using manipulators  
  • 2nd seating of UC#47 on service tray locating pins, the gas line VCR gasket came off again
    • Some alignment interference with the gas line coupling is the cause of the gasket falling off during placement (photo attached)
    • Gas line on service tray was loosened, raised to highest position and fastened (Photo attached)
    • Failed to re-install VCR gasket (Plastic separated from gasket material)
  • Target removed from Hot cell to reinstall gaskets and make modifications to the gas-line coupling
    • Gas line coil plastically deformed to give less of a spring action so the coupling can stay down under friction until it is time to couple
    • Target carefully inserted into hot cell without disturbing spring/friction of gas-line coupling. 
      • This had to be repeated several times. Once for the waterline gaskets coming off, and a few other times to insert the target/tray without disturbing sprung coupling
  • Target mounted without issue after the above steps successfully 

Gas and Water Services:

  • VCR connections coupled 
  • Leak test passed
    • leak test faster today because module had been left in silo for a long time to dry out. 
  • Gas line no-longer needed, so was not checked

Electrical Services:

  • Conductor bolts installed
  • All bolts (including mounting bolts) checked for fit with mirror
  • Coil conductor bolts torqued to at least 130inch-lbs 
  • Electrical test completed 

Containment box panel reinstalled 

Cleared area around module for craning out. 

 

Attachment 1: Gas_line_interference.jfif
Attachment 2: Gas_line_Gasket_reinstalled.jfif
Attachment 3: Gas_line_moved_to_highest_position.jfif
Attachment 4: Target_Installed_photo.jfif
Attachment 5: Inside_of_containment_box_panel.jfif
Attachment 6: Completed_photo_(module_with_panel_on).jfif
  2724   Thursday, November 28, 2024, 16:13 Aaron TamSouth Hot-CellStandard Operation TiC#9 ParasiticsTiC#9 Parasitics Leak Check and removal from hotcell

 November 27th, 2024 - Aaron Tam with Farran & David 

Parasitic Assembly Leak Check (Aaron, Farran, David)

-Note that the furthest upstream (right of the target) parasitic top cap screws had been loosened and retightened in error when attempting to remove it off TiC#9

-This puts this data point into question 

-Leak check starting from upstream to down stream 

-First parasitic had no leak 

-Second parasitic had some leak 

-Third parasitic was not pumping down at all

-First parasitic checked on test hose again with same success

Parasitic Dis-assembly (Aaron) 

-First parasitic had good tension in all 3 screws

-second parasitic had 2 screws with a perceptible breaking-loose of the screws, but one was imperceptible 

-Third parasitic had lower (than first parasitic), but okay tension in all 3 screws 

In an attempt to move the PEEK seal into a safe spot with tweezers, this one was accidentally sprung across the hotcell in the direction of the tool port 

A lengthy attempt to find it was conducted, but no PEEK seal was recovered 

This may effect our ability to do work during hot cell entries coming up. 

PEEK Seal extraction (Aaron, Farran) 

-A labeled bag was inserted into the hotcell via the tool port and onto an existing tray in the Hotcell

-PEEK seal placed inside bag, placed back on tray, and moved back to the tool port for extraction

-With tool port open, the draft was able to push the bag across the lift table. Changing the cross section exposed to the draft works to keep the bag from moving

-Farran used picker to extract the bag into the tool port where he wiped and placed into separate bag.

-This process was repeated for the second PEEK seal 

-Bags were wiped and swiped, put in another bag, swiped and brought over to Hot cell Service area Lab 

 

 

 

Attachment 1: Leak_Test.jpg
Leak_Test.jpg
Attachment 2: Dissassembly.jpg
Dissassembly.jpg
Attachment 3: Seal_Seat.jpg
Seal_Seat.jpg
Attachment 4: PEEK_seal.jpg
PEEK_seal.jpg
Attachment 5: PEEK_Seal_Closer_look.jpg
PEEK_Seal_Closer_look.jpg
  2726   Tuesday, December 03, 2024, 10:51 Adam NewsomeSouth Hot-CellStandard OperationTM2 TM2 move - ITE to SHC

TM2 was moved from ITE to SHC with Ta#68 target. During the move, a railing was lightly bumped by the corner of the module - no obvious damage or issues have been observed. Otherwise, the move was smooth.

  2727   Tuesday, December 03, 2024, 12:28 Adam NewsomeSouth Hot-CellStandard OperationTM2 TM3 move - TCS to ITE

TM3 was moved with UCx#47 from TCS to ITE. The move was smooth.

  2728   Tuesday, December 03, 2024, 15:53 Aaron TamSouth Hot-CellStandard OperationTM2Ta#68Ta#68 Removal

  Note: Ta#68 had a difficult install. See E-log ID# 2698 for more info 

First look:

  • Containment box cover looks the same as previous (See:ID: 2697)
  • Target shows large amount of soot-like deposits (See photos for locations)
  • Deposits seem to have been left on parts of the service tray as well ie.: Multipin connector 

Removal:

  • Removal was smooth
  • Water-line bracket fixing bolts seemed loose even before I put a tool to them 

Eyes of sides:

  • Better photos of where deposits are 
  • Everything else seems normal 
Attachment 1: Containment_Cover_Internal.jpg
Containment_Cover_Internal.jpg
Attachment 2: First_Look.jpg
First_Look.jpg
Attachment 3: First_look_Water_Lines_and_bracket.jpg
First_look_Water_Lines_and_bracket.jpg
Attachment 4: First_look_Water_Lines_and_bracket.jpg
First_look_Water_Lines_and_bracket.jpg
Attachment 5: First_Look_water_line_bracket_closer.jpg
First_Look_water_line_bracket_closer.jpg
Attachment 6: First_Look_Triplet_Conductos.jpg
First_Look_Triplet_Conductos.jpg
Attachment 7: Triplet_conductors_2.jpg
Triplet_conductors_2.jpg
Attachment 8: Multi_Pin.jpg
Multi_Pin.jpg
Attachment 9: Top.jpg
Top.jpg
Attachment 10: Top_Closer.jpg
Top_Closer.jpg
Attachment 11: Top_Closer_(2).jpg
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Attachment 12: Right.jpg
Right.jpg
Attachment 13: Left.jpg
Left.jpg
Attachment 14: Bottom.jpg
Bottom.jpg
Attachment 15: Bottom_Closer.jpg
Bottom_Closer.jpg
Attachment 16: Extraction_electrode.jpg
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Attachment 17: Extraction_electrode2.jpg
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Attachment 18: Extraction_electrode3.jpg
Extraction_electrode3.jpg
Attachment 19: Extraction_electrode4.jpg
Extraction_electrode4.jpg
Attachment 20: Deposit.jpg
Deposit.jpg
Attachment 21: Deposit2.jpg
Deposit2.jpg
Attachment 22: Deposit_3.jpg
Deposit_3.jpg
  2731   Wednesday, December 04, 2024, 10:40 Adam NewsomeSouth Hot-CellStandard OperationTM2 TM2 move - SHC to silo

TM2 was remotely moved from the South Hot Cell to SW Silo. Reading at SHC = 89.8 mSv/h. The move was smooth.

  2732   Wednesday, December 04, 2024, 14:30 Aaron TamSouth Hot-CellStandard Operation Ta#68Ta#68 PIE

 Abstract:
This target has seen some irregular beam patterns 
Possibility that the beam hit the walls of the target tube or even the cooling fins
This PIE we want to investigate how the irregular beam physically affected the target 

Related ELOGS: 
ID: 2728
ID: 2698

PIE was performed by Aaron Tam, Directed by Aurelia Laxdal, Observed by Lucas Backes, Special help from Chad Fisher 

External views:

  • Windows are clear of any irregularities 
  • More pictures of this can be found in RH-ISAC E-log 2728

Internal Views:

  • Heatshield internal
    • Some discolouration from heat and soot deposits.
    • This seems to be fairly clean to normal amounts - not concerning 
  • Target tube
    • tube is bent with the middle higher than the sides
    • Target tube was not removed 9/64ths allen wrench could not be located for this operation 
  • Target tube Exit
    • Heatshield windows were punctured to reveal the target tube entraces/exits
    • Entrance is waterline side (ITE)
  • Extraction electrode parts were removed from the back off the target
    • These parts look normal
    • some of the extraction electrode would not pull out due to tight fitting parts and the investigation stopped here.

Conclusion: Target physical condition is normal as far as we could investigate 

Attachment 1: Waterline_disconnect.jpg
Waterline_disconnect.jpg
Attachment 2: Heatshield_inside.jpg
Heatshield_inside.jpg
Attachment 3: Target_tube_first_look.jpg
Target_tube_first_look.jpg
Attachment 4: Heatshield2.jpg
Heatshield2.jpg
Attachment 5: Heatshield3.jpg
Heatshield3.jpg
Attachment 6: Target_tube_2.jpg
Target_tube_2.jpg
Attachment 7: Target_tube_3.jpg
Target_tube_3.jpg
Attachment 8: Couldn't_undo_this_bolt.jpg
Couldn't_undo_this_bolt.jpg
Attachment 9: Exit_tube.jpg
Exit_tube.jpg
Attachment 10: Exit_tube2.jpg
Exit_tube2.jpg
Attachment 11: Exit_tube3.jpg
Exit_tube3.jpg
Attachment 12: Exit_tube4.jpg
Exit_tube4.jpg
Attachment 13: Exit_tube5.jpg
Exit_tube5.jpg
Attachment 14: Exit_tube6.jpg
Exit_tube6.jpg
Attachment 15: Exit_tube7.jpg
Exit_tube7.jpg
Attachment 16: Exit_tube8.jpg
Exit_tube8.jpg
Attachment 17: Exit_tube9.jpg
Exit_tube9.jpg
Attachment 18: Exit_tube10.jpg
Exit_tube10.jpg
Attachment 19: entrance_tube.jpg
entrance_tube.jpg
Attachment 20: entrance_tube2.jpg
entrance_tube2.jpg
Attachment 21: entrance_tube3.jpg
entrance_tube3.jpg
Attachment 22: entrance_tube4.jpg
entrance_tube4.jpg
Attachment 23: Exit_tube5.jpg
Exit_tube5.jpg
Attachment 24: entrance_tube6.jpg
entrance_tube6.jpg
Attachment 25: entrance_tube7.jpg
entrance_tube7.jpg
Attachment 26: entrance_tube8.jpg
entrance_tube8.jpg
Attachment 27: entrance_tube9.jpg
entrance_tube9.jpg
Attachment 28: entrance_tube10.jpg
entrance_tube10.jpg
Attachment 29: entrance_tube11.jpg
entrance_tube11.jpg
Attachment 30: Extraction_electrode.jpg
Extraction_electrode.jpg
Attachment 31: entrance_tube1.jpg
entrance_tube1.jpg
Attachment 32: Extraction_electrode2.jpg
Extraction_electrode2.jpg
  2733   Thursday, December 05, 2024, 11:43 Aaron TamSouth Hot-CellStandard Operation Ta#68 Pail loading - Ta#68 & Others into Pail#300

December 5, 2024 - Aaron Tam w/ help from Chad, Peter and Adam at the Crane  

Hot Cell Prep:

  • Tools organized, working space cleared, spot for clean tool to sit placed, Air tool is open and spinning clockwise for tightening 

Loading:

  • Ta#68 was loaded into pail# 300
  • PEEK seal parasitic assemblies loaded (PEEK seals were removed in ID: 2724)
  • Farran had some old samples that also went in (More details to come when Farran sends the info)

Lid/latching:

  • This went smoothly

Bail attachment:

  • Some difficulty in attaching the Lifting Bail, but went on smoothly with the help of Chad

Notes:

  • One of the PEEK seal parasitic Target assembly lids was missed in the loading. This will have to be loaded next time. 
  • All parasitic type targets remain in the yellow container shown in photos below. 
Attachment 1: Pail_Landing.jpg
Pail_Landing.jpg
Attachment 2: Loaded_Pail.jpg
Loaded_Pail.jpg
Attachment 3: Parasitic_Lid_that_was_missed.jpg
Parasitic_Lid_that_was_missed.jpg
Attachment 4: Location_of_all_parasitic_type_targets_and_fasteners.jpg
Location_of_all_parasitic_type_targets_and_fasteners.jpg
Attachment 5: Parastics_and_Target_stuff_that_went_inside_this_pail.jpg
Parastics_and_Target_stuff_that_went_inside_this_pail.jpg
  2743   Wednesday, January 08, 2025, 07:37 chad fisherSouth Hot-CellStandard OperationTM4UCx#46UCx#46 removal

UCx#46 removed from TM4 and placed into a pail back-filled with argon. Nothing visually unusual; no issues.

Attachment 1: TM4_UCx46_07012024.jpeg
TM4_UCx46_07012024.jpeg
Attachment 2: TM4_UCx46_2_07012024.jpeg
TM4_UCx46_2_07012024.jpeg
  2748   Tuesday, January 14, 2025, 10:00 David WangSouth Hot-CellStandard OperationTM3UCx#47after operation electrical check, Tm3 UCx 47

TM3 UCx#47 after operation electrical check  is done at SHC. The result is normal. See attachment.

Attachment 1: TM3_UCX_47_after_operation_electrical_check.pdf
TM3_UCX_47_after_operation_electrical_check.pdf
  1857   Friday, January 11, 2019, 13:59 Isaac EarleSafe Module ParkingDevelopment  SMP motor selection decision

SMP drivetrain design work is currently underway.  Alejandro has selected a suitable 1200:1 reducer which will give a vessel rotation speed of 0.21rpm with a 1725rpm motor (deemed sufficiently close to the SHC rotation speed of 0.17rpm).  The reducer however is only rated for 0.33hp, and Allon's analysis recommended we use a motor of at least 0.4hp

 
From his calculations the expected power required to turn the loaded vessel is 0.2hp (see Document-161943, p3).  The higher figure of 0.4hp in his final recommendations comes from the power rating of a 40 tooth sprocket (the driver sprocket) with a No. 50 roller chain operating at 10rpm (the lowest speed shown on the table) - meaning this driver sprocket arrangement can handle up to 0.4hp.  We discussed this on the phone on January 4th and agreed that a 1/3hp motor could be used which will match the reducer Alejandro selected, and will supply sufficient power given that calculations indicate only 0.2hp is required.
 
Once the vessel is installed in the shield box a test will be performed to determine the actual torque (and power) required to turn the vessel.  If the value differs significantly from the calculated value the design will be revisited.
  1865   Monday, February 11, 2019, 10:26 Isaac EarleSafe Module ParkingDevelopment  SMP shield box and vacuum vessel moved to Target Hall

  On February 8th the SMP shield box (IRH1675) and the vacuum vessel (IRH1806) were both raised from a horizontal to vertical orientation in the ISAC-1 Experimental Hall.  Hamilton "Mini-Mite" S-MM2-43FS caster wheels were then installed on the base of the shield box and it was lowered down the hatch to the B2 level.  The vacuum vessel was then lowered into the shield box, supported by the rollers, as designed.  The shield box and vessel combination were then moved south along the steel plated floor until positioned under the hatch leading to the Target Hall.  Movement along the floor was achieved by pushing the back of the vessel with an electric fork truck and pulling from the front with a cable winch attached to a plate mounted in the floor in the SHC service area, centered east/west between the Ante Room doors.  The fork truck alone was sufficient to move the assembly on the smooth section of the plates, but the winch was needed on the section paitned with textured grit.  The vacuum vessel was then lifted into the Target Hall and placed in a temporary storage location in the silo area.  The shield box was then lifted, casters removed, and then lifted up into the Target Hall.  It was a very tight fit with the tubing which has been installed on the SHC and NHC ducting for the new flow meters, but the move was completed without causing damage.  The shield box was placed on the B2 level in the Target Hall where some final tapped holes will be added on the exterior before moving to the final installation location.

 

 

Attachment 1: 20190208_091133.jpg
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Attachment 2: 20190208_095126.jpg
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Attachment 3: 20190208_105902.jpg
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Attachment 4: 20190208_112619.jpg
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Attachment 5: 20190208_113012.jpg
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Attachment 6: 20190208_114833.jpg
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  1873   Thursday, February 21, 2019, 15:10 Isaac EarleSafe Module ParkingDevelopment  Seismic requirements for SMP

Dragan Mitrovic, TRIUMF structural engineer, was consulted earlier this week regarding seismic requirements for the SMP assembly.  Installation location, overall dimensions, total weight, and the center of mass for assembly IRH1670 were provided to him by e-mail.  On Feb 20th he communicated verbally that he had analyzed the assembly for seismic loads, and concluded that this equipment does not require anchoring or any other form of seismic restraint.

Update (May 30, 2019): Confirmed with Dragan that the approach he used for analysis was that specified in the BC Building Code (both 2012 edition and updated 2018 edition).

  1903   Monday, April 01, 2019, 14:56 Isaac EarleSafe Module ParkingDevelopment  SMP shield box and vacuum vessel installed in final location

 Last week drilling of the additional required holes in the SMP shield box was completed in the Target Hall.  This morning the shield box (IRH1675) was moved to its final installation position in the silo area on the B2 level.  The vacuum vessel (IRH1806) was then installed inside the shield box.  The center of the vacuum vessel is 2-3" north of the south travel limit of the crane.  Photos as well as measurements of the final position are attached below.

 

20190401_101459.jpg

 

20190401_110353.jpg

 

20190401_110433.jpg

 

20190401_144133.jpg

 

 

  1904   Thursday, April 04, 2019, 14:49 Isaac EarleSafe Module ParkingDevelopment  SMP vacuum vessel support roller friction check

With the SMP vacuum vessel now installed inside the shield box, a test was performed to measure the torque required to rotate the vessel.  At a moment arm distance of 2.0m a force of 89N was required to rotate the vessel (with no module installed) resulting in a torque of 178Nm.  Based on this, the coefficient of rolling resistance (CRR) was calculated to be 0.007;  This is fairly close to available data for similar applications such as cast iron wheels on steel rail (https://en.wikipedia.org/wiki/Rolling_resistance).  The CRR used for design of the SMP drivetrain was 0.054 which was based on empirical data for a similar product.  Because this is significantly higher than the friction of the as-built system the drive-train components are stronger than required and should have no problem rotating the vessel when loaded with a module.

Further details and calculations included in the attached PDF.

Attachment 1: CRR_check_for_as-built_SMP_-_April_4_2019.pdf
CRR_check_for_as-built_SMP_-_April_4_2019.pdf
  1921   Wednesday, May 15, 2019, 16:06 Isaac EarleSafe Module ParkingDevelopment  SMP module support flange installed and leak checked

The SMP module support flange sub-assembly (IRH1755) was installed today according to drawing IRH1683.  Dow Corning 111 sealing compound was used to keep the o-ring adhered to the lower groove during transportation and installation.  The TCS shield plug (IRH1646) was then installed on the SMP module flange which has vacuum connections for leak checking.  Vacuum was pulled on the SMP vessel using the Varian 979 leak detector.  After approximately 3.5 hours of pumping the test port pressure was at 2.4E-2 Torr and leak rate was 7.9E-8atm*cc/s.  Helium was configured with the regulator set at 10psi and flow rate of >10 bubbles per second in Windex and then applied slowly around the perimeter of the vacuum flange (IRH1686) and it's mating components on both  the top and the bottom.  There was no response on the leak detector indicating the seals on both sides of the module flange are leak tight.

 

20190515_094730.jpg

 

20190515_094740.jpg

 

20190515_103253.jpg

 

20190515_103824.jpg

 

 

 

 

 

  1925   Friday, May 17, 2019, 16:46 Adam NewsomeSafe Module ParkingDevelopment  SMP Controls Installation Update

 

The following controls-related items were installed for the SMP project:

- Cable tray

- Main control panel

- Motor starter box

- Wiring from limit switches and rotation motor to main control panel

- Air fittings at supply (quick disconnect)

- Main air supply hose from supply to control panel (quick disconnect)

- Air tubing from lid control valve at control panel to lid cylinders

 

Air fittings stem off existing air supply lines on the South wall, below a manual shutoff valve. A quick disconnect was installed. When SMP is not in use, manual shutoff valve should be left off.

 

Main control panel and motor starter box were mounted on the North wall. Wire duct runs from the main control panel to the grated floor. Cabling/air runs underneath the mezzanine platform, along existing and new cable tray, to the SMP.

 

Cable tray was installed on the South wall, from the corner to the SMP module. A cutout was made to accommodate for existing tubing. An additional ~1 ft. of tray will be added to the end, near the corner, at a future time.

 

Remainder of installation work to be done before commissioning:

- Mount and install new Opto-22 module
- Chain new Opto-22 module to existing one (power, comms) below mezzanine on North wall

Attachment 1: IMG_20190417_100838.jpg
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Attachment 2: IMG_20190417_100843.jpg
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Attachment 3: IMG_20190517_162230.jpg
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Attachment 4: IMG_20190517_162305.jpg
IMG_20190517_162305.jpg
  1944   Thursday, June 20, 2019, 15:09 Isaac EarleSafe Module ParkingDevelopment  SMP motor wiring inspected by electrician

The AC wiring for the SMP motor was inspected by Randy Boehm (TRIUMF electrician) as recommended by Franco Mammarella (TRIUMF electrical engineer).  After inspecting the system Randy required the following changes:

  1. AC wiring inside the control panel be increased to 16awg minimum (14awg preferred)
  2. Wiring between the control panel and motor control box be increased to 14awg
  3. Power cable to the motor be increased to 14awg
  4. Current rating for MS connectors be checked and replaced if below 10A
  5. Prefer that motor control box components be relocated to the control panel to reduce number of AC wires and connections (preferred but not mandatory)
  6. A dedicated ground wire is required in the cable going to the motor (if not already in place)

After these changes have been made the inspection will be repeated.

 

July 31, 2019 update:

Items 1, 2, 3, and 6 from above were completed.  14awg wiring was used for wiring inside the control panel (Item 1).  Current rating for the MS connectors was checked and is over 10A (Item 4).  Motor control box components were not relocated to the control panel at this time (Item 5).

Randy repeated his inspection today, and approved of the updated 120V wiring.

Adam updated the SMP electrical and control schematics (IRH1868-1874)

  1946   Thursday, July 04, 2019, 08:57 Isaac EarleSafe Module ParkingDevelopment  SMP vacuum system installed

 July 3:

- Assembled exhaust line flexible hose and fittings as per ISK0529 Rev D then leak checked: 1.4E-1 Torr test port pressure, 1.1E-7 atm-cc/s leak rate, no response to helium spray at both ends of flexible line (all vacuum fittings purchased from Kurt Lesker under Requisition #1046936)
- Connected exhaust of SMP vacuum pump to nuclear ventilation duct using flexible hose assembly as per ISK0529 Rev D
- Installed convectron gauges at pump inlet as per ISK0529 Rev D 
- Installed TCS plug block (IRH1646) in SMP
- Connected plug block vacuum port to SMP pump using flexible corrugated hose
- Connected SMP:CG1 to portable pressure display: ~700Torr 
- Turned on SMP:MP1 at 4:17pm, after approximately 25 minutes was down to 75 Torr, at 1hr 40 minutes was 90mTorr, left pumping over night
 
 
July 4:
- Pressure at 4mTorr at 8am, will leave pumping longer to see if it gets any lower
- Submitted Work Request #5239 to PLC Controls for wiring of the pump and convectron gauges and integrations with EPICS
 
20190703_122635.jpg
 
 
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20190703_122702.jpg
  1955   Friday, July 26, 2019, 15:43 Isaac EarleSafe Module ParkingDevelopment  SMP vacuum control system completed

 The SMP vacuum control system has been wired and setup to be controlled from EPICS.  Backing valve control (SMP:BV1) was tested by connecting to the turbo pump solenoid on TM3 located in the silo directly north of the SMP.  The SMP pump (SMP:MP1) was turned on and off through the EPICS interface and responded as expected.  Both convectron gauges (SMP:CG1 and SMP:CG2) responded as expected when the pump was turned on.  The readings from the two gauges were consistent throughout the mili-Torr range.


The work was done by Ray Mendoza under WP I2019-07-24-4 (work request #5239).

 

SMP_vacuum_system_EPICS_screen.png

ELOG V2.9.2-2455