Logbooks Lab Maintenance Evaporator_1 Evaporator_2 Laser cutter Target Production Test-Stand RH-ISAC RH-Cyclotron RH-Meson Hall RH-Beamlines RH-ARIEL
  RH-ISAC, Page 48 of 139  Not logged in ELOG logo
New entries since:Wed Dec 31 16:00:00 1969
Entry  Tuesday, February 26, 2019, 10:33, Travis Cave, Conditioning Station, Standard Operation, TM2, no target, Module move 

 TM#2 with no source tray has been moved from the south hot cell to the conditioning station.

Entry  Tuesday, February 26, 2019, 08:51, chad fisher, South Hot-Cell, Repair, TM2, , TM2 containment box 

The containment box has been reinstalled onto TM2 in prepatation for testing in the conditioning station.

Entry  Monday, February 25, 2019, 09:44, chad fisher, South Hot-Cell, Repair, TM2, , Water block jig 

module side water block jig has been removed in preparation for electrical checks.

Entry  Friday, February 22, 2019, 10:31, chad fisher, South Hot-Cell, Repair, TM2, , TM2 Source tray removal 6x

The source tray has been removed from TM2.

Entry  Thursday, February 21, 2019, 15:10, Isaac Earle, Safe Module Parking, Development, , , Seismic requirements for SMP 

Dragan Mitrovic, TRIUMF structural engineer, was consulted earlier this week regarding seismic requirements for the SMP assembly.  Installation location, overall dimensions, total weight, and the center of mass for assembly IRH1670 were provided to him by e-mail.  On Feb 20th he communicated verbally that he had analyzed the assembly for seismic loads, and concluded that this equipment does not require anchoring or any other form of seismic restraint.

Update (May 30, 2019): Confirmed with Dragan that the approach he used for analysis was that specified in the BC Building Code (both 2012 edition and updated 2018 edition).

Entry  Wednesday, February 20, 2019, 09:07, chad fisher, South Hot-Cell, Repair, TM2, , Module side waterblock jig 

I have installed the module side water block jig.

Entry  Tuesday, February 19, 2019, 11:56, chad fisher, South Hot-Cell, Repair, TM2, , Optics tray removal 

Aaron has removed the optics tray in TM2 in preparation for source tray removal.

Entry  Tuesday, February 19, 2019, 10:20, chad fisher, South Hot-Cell, Repair, TM2, , Containment box removed 

Containment box has been removed from TM2 in preparation for source tray removal. I will walk Aaron through removal of the optics tray today also.

Entry  Friday, February 15, 2019, 12:09, David Wang, ITE, Maintenance, TM4, , ITE water system maintenance. 

The ITE water system maintenance job is done. Changed all paddle wheels and coils on ITE flow sensors. All using water poly-tubes in ITE are replaced .  Started high active water pump, and checked ITE water signals. They are good. No leak has been found on  replaced tubes and related fittings.

Entry  Friday, February 15, 2019, 12:05, David Wang, ITE, Maintenance, TM4, , ITE annual vacuum leak check.  

Helium pressure test on all water lines: 70psi , 3 minutes. HS has a quick response to 9Xe-9atm.cc/sec for 20 seconds. No response on other lines. All water lines are good. Air to vacuum  leack check on ITE and TM4: TM4 IG1 / Steers side panel has a low E-6 atm.cc/sec leak. The o-ring need to be changed when TM4 is located at TCS. All other air to vacuum seals are good on both primary and secondary vacuum vessel.

Entry  Thursday, February 14, 2019, 14:02, Travis Cave, South Hot-Cell, Standard Operation, TM2, no target, Module move 

 TM#2 has been moved from the conditioning station to the south hot cell.

Entry  Thursday, February 14, 2019, 07:13, David Wang, Conditioning Station, Standard Operation, TM2, , TCS vacuum pumps have been stopped. 

Preparation on TM2 move from TCS to SHC.

Entry  Monday, February 11, 2019, 10:26, Isaac Earle, Safe Module Parking, Development, , , SMP shield box and vacuum vessel moved to Target Hall 6x

  On February 8th the SMP shield box (IRH1675) and the vacuum vessel (IRH1806) were both raised from a horizontal to vertical orientation in the ISAC-1 Experimental Hall.  Hamilton "Mini-Mite" S-MM2-43FS caster wheels were then installed on the base of the shield box and it was lowered down the hatch to the B2 level.  The vacuum vessel was then lowered into the shield box, supported by the rollers, as designed.  The shield box and vessel combination were then moved south along the steel plated floor until positioned under the hatch leading to the Target Hall.  Movement along the floor was achieved by pushing the back of the vessel with an electric fork truck and pulling from the front with a cable winch attached to a plate mounted in the floor in the SHC service area, centered east/west between the Ante Room doors.  The fork truck alone was sufficient to move the assembly on the smooth section of the plates, but the winch was needed on the section paitned with textured grit.  The vacuum vessel was then lifted into the Target Hall and placed in a temporary storage location in the silo area.  The shield box was then lifted, casters removed, and then lifted up into the Target Hall.  It was a very tight fit with the tubing which has been installed on the SHC and NHC ducting for the new flow meters, but the move was completed without causing damage.  The shield box was placed on the B2 level in the Target Hall where some final tapped holes will be added on the exterior before moving to the final installation location.

 

 

Entry  Thursday, January 31, 2019, 14:16, Isaac Earle, North Hot-Cell, Development, , , NHC grounding approval NHC_grounding.pdf

 Franco Mammarella was consulted regarding electrical grounding of the NHC design (RS103 of Document-131915).  After discussing the design, and having grounding inspected by Randy Boehm, Franco approved the design and advised that the grounding system should be inspected periodically.  This task has been added to the Remote Handling inspection index on an annual schedule.  A PDF copy of the e-mail correspondence with Franco is attached.

Entry  Monday, January 28, 2019, 10:41, David Wang, Conditioning Station, Repair, TM2, , TM2 water lines helium pressure test at TCS 

leak detector base LR: 0.0Xe-9atm.cc/sec. helium 70 psi. test time : 3 minutes for each circuit.The results in atm.cc/sec are Ta+(A):1.8  XE-8. TA-(B):0.0xE-9. Tu-(C):1.2XE-7. TU+(D):1.6XE-7. Coil 2 (PQ):0.0XE-9. Coil 1 (RU):0.0XE-9. MSP:2.2XE-7. EE:1.0XE-7. HS:N/A. Window:5.8XE-9

Entry  Thursday, January 24, 2019, 10:34, David Wang, ITW, Maintenance, , , Changed 24VDC plugs of TP solenoid valves in ITW 

3 damaged 24VDC plugs of TP solenoid valves are replaced. Inspected other plugs. All of them are in good condition now.

Entry  Tuesday, January 22, 2019, 09:56, David Wang, ITW, Maintenance, TM2, , ITW water system maintenance. 

ITW water system maintenance is done. All working paddle wheels and coils are replaced. ITW water system polyurethane tubes are replaced as well. Two 3/8" leak small valves on return lines are replaced. 85 liters of tritium water are transferred from storage tank to B2 level holding tank. LALC water are refilled into S-tank. Restarted pump and checked system. Everything works fine now. No water leak has been found so far.  

Entry  Monday, January 21, 2019, 16:27, Isaac Earle, North Hot-Cell, Development, , , NHC in-cell camera wired to right side monitor 20190121_154407.jpg

 The NHC right side monitor has been wired to display the signal from the in-cell camera.  This was tested using a snake camera on both of the CPC-4 connectors.

20190121_154407.jpg

Entry  Friday, January 18, 2019, 10:26, Isaac Earle, North Hot-Cell, Development, , , NHC sealing improvements and repeat of RH test for LED lights 

The following NHC development work was completed under WP I2019-01-09-4:

  • Location of RH feature on operator level LED lighting updated to match IRH1800 Rev B design
  • Remote Handling test of the LED fixtures was repeated using a 9' pole with hook attachment through the manipulator slave hatch from the Target Hall: both LED fixtures were removed and reinstalled successfully with relative ease
  • Tool port seal replaced to address an audible air leak: the 1/4" foam seal was removed and replaced with adhesive backed 5/8" wide hollow foam rubber seal (McMaster Carr PN: 93085K81). Prior to the change DPG4 was at 0.63"wc, after the change wit was 0.73"wc with all system variables constant.
  • NHC manipulator access block seal was replaced, likewise to address an audible air leak: the 1/4" foam seal was removed and replaced with adhesive backed 1/2" thick BunA-N rubber strip (McMaster Carr PN: 9023K85).  DPG4 was at 0.94"wc prior to the change, and 1.07"wc after with all system variables constant
Entry  Monday, January 14, 2019, 07:07, David Wang, Conditioning Station, Maintenance, TM2, , Restarted TCS vacuum system . 

No issue.

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