ID |
Date |
Author |
Category |
Type |
Module |
Target/Number |
Subject |
332
|
Wednesday, May 08, 2013, 10:12 |
chad fisher | South Hot-Cell | Repair | TM3 | | TM3 9 pin wiring removal |
The 9 pin wiring has successfully been removed from TM3. |
1348
|
Thursday, September 08, 2016, 16:30 |
David Wang | Conditioning Station | Repair | TM3 | | TM3 vacuum system have been connected at TCS. |
start of roughing now.
start of TCS and TM3 turbo-pumps. Everything is good so far. |
1412
|
Wednesday, November 30, 2016, 16:31 |
David Wang | Conditioning Station | Repair | TM3 | | TM3 vacuum system have been connected at TCS. |
All water circuits are by passed on the top of TM3. Water pumps and vacuum turbo- pumps are started. Everything is ready for TM3 camera sparking check. |
1414
|
Monday, December 05, 2016, 10:04 |
Aurelia Laxdal | Conditioning Station | Repair | TM3 | | TM3 vacuum system have been connected at TCS. |
David Wang wrote: |
All water circuits are by passed on the top of TM3. Water pumps and vacuum turbo- pumps are started. Everything is ready for TM3 camera sparking check.
|
Wednesday November 30st: <br>
- 3 cameras (1 UV and 2 regular cameras) were installed in the Service cap and the module was pumped down. 1 UV and 1 regular were placed on the East side of the module, aiming to water lines entering the Service Tray; 1 regular camera was placed on the South side of the module, aiming at the bottom of the blue insulators.
- started pumping down. <br>
Thursday, December 1st: <br>
- 1st HV test done. TM3 started sparking above 20kV. The cameras responses were consistent with the sparks. However, the screens were flickering and it was not clear if the responses were due to electromagnetic interferences; or due to cameras' gain change caused by high intensity light due to sparking.<br>
- added helium using the regulating valve. same results were found; <br>
Friday, December 2nd: <br>
- vented the module. <br>
- shielded the cameras' cables with aluminum tape. <br>
- removed 2 blue insulator (EE and HS) and shortened them by 1". They were found too long: HS blue insulator touching the horizontal HV water line; and the EE blue insulator at 2-3mm far from the HV water line; re-installed both shortened blue insulators.<br>
- changes the location of the cameras: 1 regular camera taped to the UV camera were placed South, aiming at the bottom of the blue insulators; 1 regular camera was kept on the East side of the module, also aiming at the bottom of the blue insulators. <br>
- started pumping down. <br>
Saturday, December 3rd: <br>
- 2nd HV test was done, with cameras' installed as mentioned above. results were consistent with the first test results. <br>
- added helium. results were the same. <br>
- vented and changed the location of the cameras: 1 regular camera taped to the UV camera were placed at the top of the Service Tray (South-West corner) aiming down the Service Tray; 1 regular camera was kept (its setup was not touched at all) on the East side of the module, aiming at the bottom of the blue insulators. <br>
- attempted to pump down, but the module was leaking. reopened the flanges, cleaned them, attempted again to pump down, but it showed a bigger leak. <br>
Sunday, December 4th: <br>
- the third attempt to pump down was successful (without reopening the module!). <br>
Monday, December 5th: <br>
- did the 3rd HV test with the cameras installed as described on December 3rd. same results as before were seen. <br>
- again helium was added and same results were noticed. <br>
- stopped pumps and prepared for venting to relocate the cameras lower in the Service Tray.
|
1417
|
Friday, December 09, 2016, 18:05 |
Aurelia Laxdal | Conditioning Station | Repair | TM3 | | TM3 vacuum system have been connected at TCS. |
Aurelia Laxdal wrote: |
David Wang wrote: |
All water circuits are by passed on the top of TM3. Water pumps and vacuum turbo- pumps are started. Everything is ready for TM3 camera sparking check.
|
Wednesday November 30st: <br>
- 3 cameras (1 UV and 2 regular cameras) were installed in the Service cap and the module was pumped down. 1 UV and 1 regular were placed on the East side of the module, aiming to water lines entering the Service Tray; 1 regular camera was placed on the South side of the module, aiming at the bottom of the blue insulators.
- started pumping down. <br>
Thursday, December 1st: <br>
- 1st HV test done. TM3 started sparking above 20kV. The cameras responses were consistent with the sparks. However, the screens were flickering and it was not clear if the responses were due to electromagnetic interferences; or due to cameras' gain change caused by high intensity light due to sparking.<br>
- added helium using the regulating valve. same results were found; <br>
Friday, December 2nd: <br>
- vented the module. <br>
- shielded the cameras' cables with aluminum tape. <br>
- removed 2 blue insulator (EE and HS) and shortened them by 1". They were found too long: HS blue insulator touching the horizontal HV water line; and the EE blue insulator at 2-3mm far from the HV water line; re-installed both shortened blue insulators.<br>
- changes the location of the cameras: 1 regular camera taped to the UV camera were placed South, aiming at the bottom of the blue insulators; 1 regular camera was kept on the East side of the module, also aiming at the bottom of the blue insulators. <br>
- started pumping down. <br>
Saturday, December 3rd: <br>
- 2nd HV test was done, with cameras' installed as mentioned above. results were consistent with the first test results. <br>
- added helium. results were the same. <br>
- vented and changed the location of the cameras: 1 regular camera taped to the UV camera were placed at the top of the Service Tray (South-West corner) aiming down the Service Tray; 1 regular camera was kept (its setup was not touched at all) on the East side of the module, aiming at the bottom of the blue insulators. <br>
- attempted to pump down, but the module was leaking. reopened the flanges, cleaned them, attempted again to pump down, but it showed a bigger leak. <br>
Sunday, December 4th: <br>
- the third attempt to pump down was successful (without reopening the module!). <br>
Monday, December 5th: <br>
- did the 3rd HV test with the cameras installed as described on December 3rd. same results as before were seen. <br>
- again helium was added and same results were noticed. <br>
- stopped pumps and prepared for venting to relocate the cameras lower in the Service Tray.
|
Monday, December 5th (Con't): <br>
- vented and changed the location of the cameras;<br>
- the UV camera was placed (tapped on an aluminum spacer and on the grounded water lines) at the middle of the Service Tray (right below the first Mykroy insulator-plate) aiming down the Service Tray (at the second Mykroy insulator-plate and water lines) ; <br>
- 1 regular camera was placed right below the UV camera, also using a spacer (taped with the camera on grounded water lines) and also aiming down the Service Tray (at the second Mykroy insulator-plate and water lines); The spacer for this camera had 300counts on it after it was removed from TM3, after the test;<br>
- NOTE: when installing the 1st regular camera: dropped a small allen key in the Service Tray. It landed on last insulator with the epoxi and water lines, between the first HV line and the wall of the grounded Service Tray. This insulator is down below in the Service tray. Used a magnet stick to recuperate the allen key. <br>
- the 2nd regular camera was placed at the top of the Service Tray (tapped on the grounded water lines) looking down at the first Mykroy insulator-plate and water lines. NOTE: this camera had a filter applied to its lens. <br>
- pumped down <br>
Tuesday, December 6th:<br>
- did the 4th HV test with the cameras installed as described on December 5rd Tuesday morning very early . Same results as before were seen, except that the top camera (2nd regular camera) with the filter applied to its lens was flickering less than the other 2 cameras, and for small sparks this camera was not reacting at all. <br>
- vented shortly after the 4th test and relocated the cameras for the 5th HV test (last test); <br>
- placed only 2 regular cameras in the Service Tray;<br>
- 1 regular camera was placed right below the 2nd Mykroy insulator-plate, aiming down the Service Tray at the last insulator with the epoxi and water lines (this insulator is down below in the Service tray); <br>
- the 1st regular camera was placed a level up in the Service Tray, right below the 1st Mykroy insulator-plate, aiming down the Service Tray at the 2nd Mykroy insulator-plate; <br>
- NOTE: no spacers were used<br>
- pumped down and did the 5th HV test with the cameras installed as described above in the evening; <br>
- again same results as before were seen: the camera with the filter applied to its lens was flickering less than the other camera, and for small sparks this camera was not reacting at all. <br>
- NOTE: for this last test heard sparks outside (at atmosphere) when the HV was pushed at 26kV; <br>
Wednesday, December 7th:<br>
- vented and removed the cameras from TM3. No contamination was found on the cameras and wires. <br>
- TM3 was moved to the silo.<br> |
1288
|
Monday, July 18, 2016, 14:14 |
David Wang | Conditioning Station | Repair | TM3 | | TM3 leak checked at TCS |
Last Friday July-15, TM3 was leak checked at TCS. All air to vacuum seals on service cap are good. Helium pressure test on TM3 water lines(except GE, HS, and Window) were done. Leak detector has no response at 0.0xE-9 atm.cc/sec. They are leak free. |
1289
|
Tuesday, July 19, 2016, 14:35 |
Aurelia Laxdal | Conditioning Station | Repair | TM3 | | TM3 leak checked at TCS |
David Wang wrote: |
Last Friday July-15, TM3 was leak checked at TCS. All air to vacuum seals on service cap are good. Helium pressure test on TM3 water lines(except GE, HS, and Window) were done. Leak detector has no response at 0.0xE-9 atm.cc/sec. They are leak free.
|
Friday July 15: did HV tests (with no target installed and with the anode wire removed ). <br>
TM3 went up to 22.5kV. At this voltage it started sparking. The EL was kept at 1/2 with respect to the HV BIAS. <br>
Also HV tests were done while the EL was kept at zero V. In this case, the EL voltage was once in a while spiking up (up to 4kV). <br>
During sparking we saw responses in the vacuum. Checked the Service Cap (with the HV Cover) in the Target Hall: we couldn't hear/see sparks there. <br>
The HV was turned off in the same day, after 5:30pm. |
1349
|
Monday, September 12, 2016, 09:25 |
David Wang | Conditioning Station | Repair | TM3 | | TM3 leak checked at TCS |
After blue insulators replacement, TM3 service cap are leak checked. LD base leak rate 0.0xe-9 atm.cc/sec. I sprayed lots helium on all blue insulator seals. No leak has been found. Double checked them again, and got same result. All other seals on top of TM3 also have been checked. They are leak free. OVEN, TUBE, MSP, COIL, and EE water lines are pressurized with 70 psi helium for 3minutes each. They are good also. |
2101
|
Thursday, June 11, 2020, 12:36 |
David Wang | Safe Module Parking | Repair | TM3 | | TM3 containment box and service tray field measurement. |
At 15cm distance: Containment box window 21msv maximum. Service tray 8.0msv maximum.
At 0.5 meter distance 360degree rotation: containment box high 10msv, low 4.3msv.
Maximum 170 to 180 counts(44-2) on swipes taking from service cap inside.
0 to 20 counts(44-2) on air sample at 0.5 meter to containment box window panel.
80 counts(44-2) on air sample taking from service cap inside. The contamination level in service cap is low.
|
1745
|
Friday, June 29, 2018, 10:15 |
chad fisher | South Hot-Cell | Standard Operation | TM2 | | TM2 work and target install |
On Thursday, June 29th the containment box of TM2 was removed and the optics tray re-installed and reconnected. The box was then re-installed.
Friday the window waterlines were leak checked, Nb target installed (with new fasteners, high current torqued to 130 in*lbs) target leak and electrical checked and containment box cover installed with new fasteners. |
2253
|
Monday, October 04, 2021, 09:33 |
Frank Song | North Hot-Cell | Standard Operation | TM2 | C#3 | TM2 with target connection test |
the test was done when TM2 sit on NHC. |
2402
|
Monday, January 09, 2023, 14:19 |
Frank Song | ITW | Standard Operation | TM2 | UCx#40 | TM2 with UCx40 disconnection in ITW |
TM2 with target UCx40 was disconnected in ITW and moved to NHC. |
2658
|
Tuesday, August 13, 2024, 14:23 |
David Wang | ITE | Standard Operation | TM3 | Ta#67. | TM2 with Ta#target has been moved from SHC to ITE. |
TM2 with Ta#target has been moved from SHC to ITE. the move is smooth. |
2346
|
Tuesday, July 19, 2022, 11:47 |
Frank Song | ITW | Standard Operation | TM2 | SiC#43 Febiad | TM2 with SiC#43 disconnected in ITW |
the module was disconnected in pit and moved to NHC. |
1789
|
Friday, September 21, 2018, 10:07 |
David Wang | ITW | Standard Operation | TM2 | SiC nano | TM2 with SiC nano target was has been connected in ITW. |
Tm2 with SiC nano has been connected in ITW. See attachment for checklist |
1893
|
Monday, March 18, 2019, 07:23 |
David Wang | Conditioning Station | Repair | TM2 | | TM2 window line helium test |
New seals with a blank off cap are installed on TM2 window line water block. The seals are checked at TCS with 70 psi helium for 5 minutes with LD at 0.0xE-9atm/cc.sec. No response on LD during test. Seals are good. |
1726
|
Wednesday, May 30, 2018, 09:51 |
David Wang | Conditioning Station | Repair | TM2 | | TM2 water lines helium pressure test at TCS. |
I did a helium pressure test on TM2 water lines at TCS. We will remove the TM2 source tray soon so this test is a reference check for future new source. The result:
Helium 70 psi, 2 minutes to each circiut. Leak detector base LR.0.0x e-9atm.cc/sec, base pressure 0.0x e-4torr
Ta+(A) 0.0x e-9atm.cc/sec
Ta-(B) 0.0x e-9atm.cc/sec
Tu-(C) 7.8x e-7 atm.cc/sec
Tu+(D) 3.5x e-7 atm.cc/sec
Coil 2(PU) 0.0x e-9atm.cc/sec
Coil 1(RU) 0.0x e-9atm.cc/sec
EE 8.2 x e-9atm.cc/sec
MSP 0.0x e-9atm.cc/sec
Containment box window 0.0 xe-9atm.cc/sec
HS no target and opened. No test.
All water lines on module side in TM2 should be in good condition according to this test . The leak response we found on B and C lines are from water block seals mostly. |
1863
|
Monday, January 28, 2019, 10:41 |
David Wang | Conditioning Station | Repair | TM2 | | TM2 water lines helium pressure test at TCS |
leak detector base LR: 0.0Xe-9atm.cc/sec. helium 70 psi. test time : 3 minutes for each circuit.The results in atm.cc/sec are Ta+(A):1.8 XE-8. TA-(B):0.0xE-9. Tu-(C):1.2XE-7. TU+(D):1.6XE-7. Coil 2 (PQ):0.0XE-9. Coil 1 (RU):0.0XE-9. MSP:2.2XE-7. EE:1.0XE-7. HS:N/A. Window:5.8XE-9 |
1211
|
Thursday, April 14, 2016, 09:46 |
Anders Mjos | Conditioning Station | Standard Operation | TM2 | | TM2 water leak test |
Thursday, April 14, 2016, 07:50: RGA on
Friday, April 15, 2016, 08:09 : Ratio between water and air is higher than normal (indicating possible air leak). See attachment. 3.5 more H2O than N2. (Ratio in TM3 Nov 2015 was 82:1)
A leak was found on the o-ring between the module flange and TCS. This could be fixed by cleaning the o-ring and sealing surface. The Window line is not closed and was accidentally pressurized with He on April 25
Tuesday, April 26, 2016, 08:47: David started the water package.
Wednesday, April 27, 2016, 08:15: Switched off chiller / water cooling.
Wednesday, April 27, 2016, 14:41: Switched chiller / water cooling back on. |
2603
|
Thursday, May 30, 2024, 11:08 |
David Wang | Conditioning Station | Standard Operation | TM2 | | TM2 was moved from silo to TCS yesterday morning. |
TM2 was moved from silo to TCS yesterday morning. The move is smooth. TCS vacuum system was started after. TCS and TM2 pumping down is ok so far. |