Logbooks Lab Maintenance Evaporator_1 Evaporator_2 Laser cutter Target Production Test-Stand RH-ISAC RH-Cyclotron RH-Meson Hall RH-Beamlines RH-ARIEL
  RH-ISAC, Page 19 of 138  Not logged in ELOG logo
ID Date Author Category Type Module Target/Numberdown Subject
  33   Monday, October 03, 2011, 11:54 chad fisherSouth Hot-CellStandard OperationTM1UCx#2 - TaC#1Target change UCx#2-TaC#1

UCx#2 has been removed from Tm1 and put in a bucket with a slow argon feed and a lid placed lossely on top.

 

TaC#1 ITW has been installed and is awaiting testing at the cell.

  21   Thursday, August 18, 2011, 14:09 Bevan MossSouth Hot-CellStandard OperationTM1UCx#2Leak and Electrical Check plus Remote Move to Conditioning Station

 TM1 with UC#2 had the target installed, the heat shield line was pumped on and achieved a vacuum of 0.0 x 10^-4 Torr and a  leak rate of 0.0 x 10^-9 atm cc / sec with no response when sprayed with helium. An electrical check was completed by David and myself all values were withing tolerance.  The module was then moved from the south hot cell to the conditioning station where it will start pump down. The move was uneventful every operated as it should and there were no crashes minor or large. It was attempted to fill the containment box with argon prior to closing it but assuming that didn't work I estimate the target was exposed to air for a total of ~4 hours during installation and move. 

  22   Thursday, August 18, 2011, 16:07 Bevan MossConditioning StationStandard OperationTM1UCx#2Pump Down

 Pump down in the conditioning station started at ~2:40 for rough down. The turbo pumps were turned on at ~3:30 and at 3:52 the pressures were reading as follows:

IMG in the containment box 9.2 x 10^-5 T

IMG in the secondary 2.0 x 10^-3 T

ION in the service cap 4.6 x 10^-5 T

Note that the cross has been installed on the vacuum vessel which now includes a turbo pump and the IMG 100.

Leak check will occur tomorrow.

  23   Friday, August 19, 2011, 14:52 Bevan MossConditioning StationRepairTM1UCx#2Leak Check

 A leak check was performed on the module when it was in the conditioning station today. There were no external leaks found. When the coolant lines were check a small leak was found in the heat shield circuit. Base leak rate was 6.7 x 10^-9 atm cc /sec and rose to 4.1 x 10^-9 atm cc /sec quickly (~3 seconds) and remained there for the 2 minute test. The remaining lines had small responses as usual but the highest response was in the low 10^-8 atm cc /sec range. The pressures were recorded as 1.2X10^-6 T, 2.7 x 10^-6 T and 1.1 10^-5 T in the service cap, containment box, and secondary respectively. The module was then vented with argon which took ~1.5 hours, vessel was pressurized to ~ 1 psi. A panel was then removed to leak check the feed through stem of the heat shield pressure of the line was recorded to be 0.0 x 10^-4 T and a leak rate of 1.3 x 10^-8 atm cc/sec was achieved. The stem was sprayed and no response was found. Swipes of the were taken of the panel (150 counts) and the containment box (3000 counts). The panel was then returned and the vessel roughed out for the weekend, it will be vented and moved to the south hot cell on Monday where the VCR fittings will be checked again and then tightened.  

  24   Wednesday, August 24, 2011, 16:35 Bevan MossSouth Hot-CellRepairTM1UCx#2Move, inspection and repair

 On August 22nd TM1 was vented with Argon in the conditioning station. It had been pumping with just the roughing pump over the weekend so the UCx#2 target would not be exposed to oxygen. The move went without incident and took roughly an hour to complete. Once at the hot cell the panel was removed by Tom Lyth and a leak check completed with Bevan, David Wong, Grant Minor, and Tom Lyth present. The connections to source tray were checked starting at the top. Each connection was checked on either side of the VCR and at the center through the hole in the nut. For both connections on the source tray there was no response from the leak cart which was at a pressure of 0.0 x 10^-4 T and had a baseline leak rate of 0.0 x 10^-9 atm cc / sec. The leak check then proceeded to VCR connections on the Target. A leak was found on the upper VCR connection of the target and was repeatable. This leak was detected at the hole of the VCR nut connection by priming the line with helium and placing it next to the hole in the VCR connection. Response time was between 5 and 10 seconds to a maximum of 2.6 x 10^-8 atm cc / sec. The lower connection also appeared to have a small leak rate of 4.4 x 10^-9 atm cc/ sec but could be a result of helium drift. Unfortunately the target is not design to be repaired with manipulators and required the target to be removed from the south hot cell and repaired in the anteroom. The anteroom was prepared for the target by lining much of it with plastic so to prevent the spread of contamination. Once the target was in the anteroom it was leak checked again, the base pressure was 0.0 x 10^-4 and the base leak rate was 0.0 x 10^-9. A response from the upper connection again was detected in the 10^-8 range but no leak was found in the lower connection. It was attempted to tighten the joint to stop the leak but this caused it to increase to the 10^-7 range. This increase in leak rate is as expected from past experience because copper gaskets are used rather than silver plated ones. The heat shield cover was loosened and the gaskets from from both joints were replaced with the silver plated ones. The target was then leak check and passed with no response once again with a full pump down. The target was had an electrical checked with the megger and was within spec. The target was then placed in an argon bag and returned to the hot cell. The bag was damaged went placing it in the hot cell and there were not any acceptable options for leaving the target over night. The target was removed and and placed in 2 bags filled with argon for over night.

On August 23rd the target was removed from the argon bags that were still inflated and returned to the hot cell. The target was re-installed on the target module by Grant Minor, Tom Lyth, an Bevan Moss. One VCR gasket fell off during the first attempt and it appeared that the right target leg may have been slightly bent at some point. Other than that the installation went smoothly but slowly. The heat shield line was then leak checked once again by Grant, Tom, David, and Bevan and no response was detected from the source tray or target VCR connections, the base leak rate and pressure once again achieved the minimum detectable levels. The target module passed the electrical check with the megger, this test was completed by Bevan and Pierre Bricault. The module was then moved from the south hot cell to the conditioning station. Roughing was started at 3:00 and the turbo pumps were turned on at 3:45. The module was left to pump over night.     

  25   Wednesday, August 24, 2011, 17:11 Bevan MossConditioning StationStandard OperationTM1UCx#2Leak Check, HV conditioning and Module Move

Today a leak check on TM1's external seals and the heat shield line was completed by David Wang. After 16 hours of the turbo pumps running on the conditioning station stations pressures were 3.6 x 10^-6 T, 1.2 x 10^-5 T, and 1.8 x 10^-6 T for the containment box, secondary vacuum, and service cap respectively. This is a significantly quicker pump down after the cross with small turbo pump was installed on the vacuum vessel. The base pressure of the leak testing cart was 0.0 x 10^-4 T and the leak rate was 1.2 x 10 x 10^-8 atm cc / sec. There was no response from the external test where the module was sprayed with helium. The heat shield line was pressurized with 80 psi helium which caused the leak rate to climb to a maximum of 2.5 10 ^-8 atm cc / sec but dropped to 1.9 x 10^-8 atm cc / sec and was stable there, the total test time was 2 minutes. This test was repeated another time and had similar results.  These results although showing a slight increase in the detected leak rate are withing acceptable and indicate that the module is leak tight. 

At 9:30 the HV check and conditioning started (~17 hours turbos on), the secondary vacuum, containment box and service cap had the following pressures in Torr respectively, 1.0 x 10^-5, 3.2 x 10^-6, 1.6 x 10^-6.  The voltage was steadily raised with virtually no current up to 28.5 kV which was achieved at 9:50. When raised to 30 kV the current increased significantly to ~300 uA and a large amount of sparking occurred. The voltage was dropped to 0 volts for 2 minutes and then was returned to 30 kV at 10:03, the current draw was around 200 uA and climbing. After a few sparks and time the current had dropped to 120 uA. This indicates that the module is still conditioning and matches what is observed by the control room when the module is in ITW. The module was deemed acceptable for this current run and was then vented with argon this took about 2 hours.

The module was then remotely moved from the conditioning station to ITW. When first attempting to transfer the controls to the remote control room they were not transferred and when testing the up command as per standard procedure the module dropped down slightly. David Wang went to lock out the target again and the controls were successfully transferred. A note of this was made in the log book. Apart from this the move went smoothly.  

  26   Thursday, September 01, 2011, 09:11 Don JacksonITWStandard OperationTM1UCx#2Argon Venting West Station

West target station is setup to use argon for tank venting.  There is 1200 PSI remaining on argon bottle in electrical room.  That is sufficent for venting west target station to atmosphere twice.  ISAC Operations has been previousily contacted and their procedures for venting remain the same except that they can not rely on ITW:CG4S to determine when at atmospheric pressure.  I have asked them to contact me if an unscheduled vent is required.

  32   Monday, October 03, 2011, 11:00 Travis CaveITWStandard OperationTM1UCx#2Move from west station to south hot cell

TM#1 with UCx#2 has been moved from the west station to the south hot cell. Move went well.

  36   Wednesday, October 05, 2011, 09:41 Travis CaveSpent Target VaultStandard Operation UCx#2Spent target move

The spent UCx #2 target has been moved into storage. It was placed in tray 5A and is in Pail #91, it was 8.91mSv/hr upon removal from the south hot cell. There are 5 free slots left in the storage vault.

  1469   Tuesday, March 28, 2017, 10:44 chad fisherSouth Hot-CellStandard OperationTM4UCx#19UCx#19 Installed

UCx#19 has been installed onto TM4. High current fasteners torqued to 130 in lbs. Has been leak and electrical checked and is ready to leave hot cell.

  970   Tuesday, June 30, 2015, 12:37 chad fisherSouth Hot-CellStandard OperationTM1UCx#12UCx #12 Removal

UCx#12 has been removed from TM1 and placed in a pail with argon.

Right leg (B) of target is clearly broken.

Containment Box cover re-installed and module ready to move.

  793   Wednesday, November 19, 2014, 08:49 chad fisherSouth Hot-CellStandard OperationTM4UCx#11Ta#44 Removed Ucx#11 Installed

Ta#44 has been removed from TM4 and UCx#11 has been installed and is ready for testing.

New fasteners were installed for all mounting and current connections.

High current fasteners were torqued to 130in lbs.

  2527   Monday, January 22, 2024, 10:16 David WangITEStandard OperationTM4UCx#Tm4 waterlines helium pressure test and TM service cap helium leak check.

Tm4 waterlines helium pressure test and TM service cap helium leak check was done last Friday. All water lines were pressurized with 70psi helium for 3 minutes each. The 3 minutes stable leak rate on all lines are less than 4.0 X E-9atm.cc/sec. some of lines had surging leak rate to 2xE-8 atm.cc/sec at the first 10 seconds of pressurization which should be a gas hammer result at the beginning. Based on the numbers, I would say all water lines are leak free still.  I did helium spray on TM4 service cap. There could be a small leak in high E-9 atm. cc/sec on ion gauge and steer service panel o-ring.  I will replace this o-ring when module is moved out of ITE. Other seals are leak free or less than 2.5X E-9 atm.cc/sec leak rate which are good. I am pretty confirm there is a small leak on ITE entrance module top. The leak rate and location will be confirmed when the rest of leak checks in ITE pit are done.

  2120   Monday, July 06, 2020, 07:54 David WangITEStandard OperationTM4UCx 30TM4 has been connected in ITE connection

TM4 has been connected in ITE. Vacuum pumping down is good so far.

  2018   Wednesday, October 30, 2019, 11:18 David WangITWStandard OperationTM4UCx 29UCx 29 connection checklist

See attachment

  2057   Monday, February 03, 2020, 09:14 David WangITWStandard OperationTM4UCx 29TM4 UCx 29 disconnection checklist

TM4 has been disconnected in ITW. See attachment checklist.

  2062   Wednesday, February 05, 2020, 11:03 David WangSouth Hot-CellStandard OperationTM4UCx 29UCx 29 post run electrical check

UCx 29 TM4 post run electrical check is done before target is removed. Everything is normal on measurements.

  1836   Tuesday, December 04, 2018, 12:36 David WangITEStandard OperationTM4UCx 26.TM4 has been connected in ITE/ Checklist.

TM4 has been connected in ITE. See attachment for connection checklist

  1815   Thursday, November 01, 2018, 11:42 David WangConditioning StationStandard OperationTM2UCx 25.TM2 HS line helium pressure test at TCS and helium spray at SHC..

Chad and I did  leak check on TM2 HS line at SHC yesterday. Base LR 0.0XE-9 atm.cc/sec.   No response on LD. during helium spray.   Today , I did helium pressure test at TCS. base LR 0.0xe-9atm.cc/sec. applied 70psi helium for 3 minute. leak rate slowly climbed to2.2 Xe-7 atm.cc/sec ate stopped there.  The result is close to before.

  1775   Tuesday, September 04, 2018, 08:18 David WangConditioning StationStandard OperationTM4UCx 24#Stppped TM4 and TCS vacuum and water system at TCS.

I stopped TM4 and TCS vacuum system at TCS. TCS and TM4 is venting with argon now.

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