Logbooks Lab Maintenance Evaporator_1 Evaporator_2 Laser cutter Target Production Test-Stand RH-ISAC RH-Cyclotron RH-Meson Hall RH-Beamlines RH-ARIEL
  RH-ISAC, Page 113 of 138  Not logged in ELOG logo
ID Date Author Category Type Module Target/Number Subject
  509   Friday, October 18, 2013, 13:43 chad fisherSouth Hot-CellRepairTM4 C2 Circuit Removal

The C2 circuit (coil 2) water lines and blocks have been revoed from TM4.

Water block jig could not be used as the window water block connection was nowhere near fitting into the jig (IMG_1224 image below) and therefore caused an interference causing the rest of the blocks to not mate with the jig. A different tool that has never been used was implimented and sucessful (IMG_1227 below).

 Sorry about the picture numbering format...new format will be implimented next time.

Attachment 1: IMG_1224[1].JPG
IMG_1224[1].JPG
Attachment 2: IMG_1227[1].JPG
IMG_1227[1].JPG
Attachment 3: IMG_1230[1].JPG
IMG_1230[1].JPG
  508   Friday, October 18, 2013, 10:17 Bevan MossITWRepair  Paddle Wheel

 Yesterday I visually inspected the paddle wheel and noticed that it was spinning freely and constant. As the signal was intermittent replaced the coil at the back of the wheel only. This does not require access to the high active water. With the coil replaced the signal looked strong. I asked operations to keep and eye on it and advise if the problem has been resolved. I also discussed with David this morning and he informed me that this is the same procedure he would have followed.

  507   Thursday, October 17, 2013, 17:16 Grant MinorITERepair  Pre-Separator-area (ITE Harp 9) Blocks Replaced

The pre-separator-area blocks were replaced today by Bevan and Travis, with Grant present for photos and observation.

Photos are attached of each block replacement.

Some difficulty was encountered in replacing the "Layer #3" blocks (photo 9 attached).  An interference occurred between the outside of the west "Layer #3" block and an aluminum channel directly beside the rubber pad that supports the block.  The block was initially resting on this channel but slipped off, breaking off some concrete at the edge.   See photo 12 attached and notice crumbled concrete inside this channel around the area where the interference occurred. Photo 14 shows the damaged block edge.

It should be noted that when these two blocks are resting flat, there should be a gap between them (i.e. they should NOT be touching as shown in photo 9).

 

Attachment 1: PreSeparatorHarp9Blocks_17Oct2013.JPG
PreSeparatorHarp9Blocks_17Oct2013.JPG
Attachment 2: PreSeparatorHarp9Blocks_17Oct2013-008.JPG
PreSeparatorHarp9Blocks_17Oct2013-008.JPG
Attachment 3: PreSeparatorHarp9Blocks_17Oct2013-009.JPG
PreSeparatorHarp9Blocks_17Oct2013-009.JPG
Attachment 4: PreSeparatorHarp9Blocks_17Oct2013-012.JPG
PreSeparatorHarp9Blocks_17Oct2013-012.JPG
Attachment 5: PreSeparatorHarp9Blocks_17Oct2013-017.JPG
PreSeparatorHarp9Blocks_17Oct2013-017.JPG
Attachment 6: PreSeparatorHarp9Blocks_17Oct2013-020.JPG
PreSeparatorHarp9Blocks_17Oct2013-020.JPG
Attachment 7: PreSeparatorHarp9Blocks_17Oct2013-021.JPG
PreSeparatorHarp9Blocks_17Oct2013-021.JPG
Attachment 8: PreSeparatorHarp9Blocks_17Oct2013-014.JPG
PreSeparatorHarp9Blocks_17Oct2013-014.JPG
  506   Thursday, October 17, 2013, 10:24 chad fisherSouth Hot-CellRepairTM4 Coil Line Removal

The containment box was removed from TM4 earlier this morning in preparation for removal of the C2 circuit water lines, their respective water blocks and conductor block.

Attachment 1: TM4_C2_circuit.pdf
TM4_C2_circuit.pdf TM4_C2_circuit.pdf TM4_C2_circuit.pdf
  505   Wednesday, October 16, 2013, 18:53 Grant MinorITERepair  ITE Harp 9 Removed & Blanked-Off - blocks NOT YET replaced

The blocks above the pre-separator section of the ISAC beam lines were removed today in the Target Hall by Bevan Moss and Chad Fisher with Lynne LeMessurier present from RPG.

The two blocks in the layer below the top layer above the pre-separator were damaged on removal (see attached photos).  This was due to an attempt to lift them in the incorrect sequence caused by misinterpretation of the labeling / numbering system drawn on the top of the blocks.  The blocks are labelled for the replacement sequence, but not for the removal sequence.  An attempt was made to lift a block that had an overlap with an adjacent block that was not visible, causing damage to two blocks.  A note was added in black marker to the critical block to indicate that it should be removed last (shown in attached photo).  The block replacement sequence will be photographed and a procedure document will be written by Bevan, with a bound copy of the procedure provided in the Target Hall, in order to prevent such an incident from occurring again.  Broken pieces of the blocks were collected and placed in a 5-gallon pail.

The removal of all of the blocks caused the depression in the target station to fluctuate around the trip point (17 inches of water column), which caused the ventilation alarm to trip on and off constantly.  Operations contacted me to ask if this could be remedied.  Bevan closed the damper to ITW, which brought the depression to a low enough value so that the alarm could be defeated properly.  This was around 2pm.

Preliminary co-ordination of the ITE Harp 9 removal job was discussed by Scott Kellogg and Ron Kuramoto around lunch time.  Keith Ng (RH) and Scott searched for the blank-off that was used during the last Harp 9 repair (removed from B/L in March 2013) but they could not locate it.  I was later able to find the blank-off bagged in a grey rubbermaid bin at the bottom of the stairs in the target storage vault pit (under the SHC / NHC ventilation and filters).  The blank-off was found bagged and tagged as surveyed at 100 counts @ 0.5m on March 27, 2013.  I gathered Scott, Ron Kuramoto, and Danka Krsmanovic to co-ordinate the Harp 9 removal and blank-off installation, starting at around 2:30 pm.

For the Target Hall Harp work, Ron Kuramoto and Scott prepared the required tools and plastic coverings / bags.  I acted as crane operator.  Danka was the surveyor present.  Anders Mjos joined the group for photos and moral support.

Scott disconnected services from the Harp device, and prepared it for lift.  I called operations to confirm that the section of B/L had been vented.  Ron and Scott used the RH tools to disconnect the 2 vacuum flange bullet bolts.  Ron directed the crane with signals and I lowered the chain rigging to the Harp, it was connected and removed from the BL with the main hoist.  (I made the mistake of directing the rigging of the harp to the main 20T hoist, when in fact the 3T Aux hoist should have been used, as the main hoist can't reach to the vacuum / storage pit on the west side of the hall.)

Danka performed several swipes and measurements of the Harp after removal.  Alpha contamination was discovered on the bottom of the Harp flange.

Ron and Scott installed the blank-off flange, then I called operations to indicate that pumping should start.

Ron and Scott retrieved the vacuum test flask jig / support structure from the West storage pit and brought it down to the pre-separator pit.  I lowered the Harp into this flask jig, and Scott used the side-wall location bolts from the top of the harp assembly to fasten the flanges of the Harp and the jig.

I had trouble at first activating the Aux hoist but soon realized that it's necessary to press the Aux pendant "ON" button down for several seconds before the power actually turns on to this hoist.

We then removed the main hoist hook and attached the Aux hoist to the Harp / flask.  The assembly was transported to the West storage pit.

Some of the handrails had to be removed to facilitate initial movements of the Harp assembly.  These handrails should be replaced tomorrow morning.

Scott also submitted a Work Order for a back-up blank-off today, job number 40303.

The pre-separator blocks have NOT been replaced yet, we will do this tomorrow morning.

It was a busy day, thanks to all for their efforts and for staying a bit late to get the blank-off installed.

Best regards,

Grant

Attachment 1: Damaged_Pre-Separator_Blocks_(ITEHarp9)_16Oct2013.JPG
Damaged_Pre-Separator_Blocks_(ITEHarp9)_16Oct2013.JPG
Attachment 2: Damaged_Pre-Separator_Blocks_(ITEHarp9)_16Oct2013-001.JPG
Damaged_Pre-Separator_Blocks_(ITEHarp9)_16Oct2013-001.JPG
Attachment 3: Damaged_Pre-Separator_Blocks_(ITEHarp9)_16Oct2013-002.JPG
Damaged_Pre-Separator_Blocks_(ITEHarp9)_16Oct2013-002.JPG
Attachment 4: Damaged_Pre-Separator_Blocks_(ITEHarp9)_16Oct2013-004.JPG
Damaged_Pre-Separator_Blocks_(ITEHarp9)_16Oct2013-004.JPG
Attachment 5: Damaged_Pre-Separator_Blocks_(ITEHarp9)_16Oct2013-007.JPG
Damaged_Pre-Separator_Blocks_(ITEHarp9)_16Oct2013-007.JPG
Attachment 6: Damaged_Pre-Separator_Blocks_(ITEHarp9)_16Oct2013-009.JPG
Damaged_Pre-Separator_Blocks_(ITEHarp9)_16Oct2013-009.JPG
Attachment 7: Closing_Damper_for_ITE_16Oct2013.JPG
Closing_Damper_for_ITE_16Oct2013.JPG
Attachment 8: ITE_Harp_9_Remove_and_Blank_16Oct2013-012.JPG
ITE_Harp_9_Remove_and_Blank_16Oct2013-012.JPG
Attachment 9: ITE_Harp_9_Remove_and_Blank_16Oct2013-021.JPG
ITE_Harp_9_Remove_and_Blank_16Oct2013-021.JPG
Attachment 10: ITE_Harp_9_Remove_and_Blank_16Oct2013-031.JPG
ITE_Harp_9_Remove_and_Blank_16Oct2013-031.JPG
Attachment 11: ITE_Harp_9_Remove_and_Blank_16Oct2013-038.JPG
ITE_Harp_9_Remove_and_Blank_16Oct2013-038.JPG
  504   Wednesday, October 16, 2013, 10:12 Travis CaveSouth Hot-CellStandard OperationTM4no targetmodule move

TM#4 with no target has been moved from the south west silo to the south hot cell.

  503   Tuesday, October 15, 2013, 16:44 Grant MinorCraneRepair  Target Hall Crane - operational with temporary thermal sensor bypass

E-mail correspondence on the Target Hall crane fault diagnosis between October 11th and 15th:

On 15/10/2013 3:34 PM, Grant Minor wrote:

Hello all,

Mike Smith from Norelco arrived this morning and spent some time with Travis from RH and Mike Rowe from Controls group examining the crane controls and electrical schematics.  A common understanding of the wiring and control signal scheme for the thermal sensor circuits was reached.  A scanned copy of Norelco / Seattle Crane drawing E5 - 1/1 with markups by Dave Morris (Oct 11th) and Mike Smith (Oct 15th) is attached.

The group then worked on top of the crane bridge to systematically isolate the thermistor circuits in each drive motor.  The thermistor readings were all normal / as-expected (about 180 Ohms for 3 in series), i.e. there was no indication of failure in any of the motor thermistors.  Fall arrest equipment was used to access the motors where required.

Next, the shunt circuit in each temperature sensor module was measured (terminals T1 and T2 on each module, on drawing E5 - 1/1).  The shunt in the operational module was measured at 500 kOhms.  The shunt in the suspected faulty module was measured at 79 kOhms.

It was concluded that there is most likely a fault in the module with the low shunt resistance.  The suspect module was left wired in bypass (shorted from terminals 14 to 11).  Mike Smith advised at that point that it would be safe to operate the crane in this mode temporarily until a replacement module can be installed.  I discussed this with him and Don Dale, and we agreed the risk is low, as we have not ever experienced a motor overheat scenario in the operating lifetime of the crane.

Mike Smith called me around 1pm to advise that he has located a replacement unit from their supplier in the US and I asked him to order 2 units on expedited overnight.  Mike expects the components to arrive Friday this week or Monday next week latest, factoring in delays at customs and local delivery times.  The units will be sent to Norelco first, then to TRIUMF locally.

Remote Handling is now continuing with Target Hall operations, using the crane as normal with the thermal module bypassed until the replacement module arrives.

Thanks to Dave Morris / Mike Lowe for their assistance in diagnosing this fault.

Here is a short summary of the Fault:

Cause of fault
- Most likely a failed thermal sensor module for one of the two pairs of bridge drive motors

Diagnosis
- Crane company (Norelco) consulted, with on-site inspections by tech Mike Smith on October 9th and October 15th
- Controls group / Mike Smith measured resistances in motor thermistors and sensors to systematically isolate fault to thermal sensor

Remedy actions taken

- Thermal sensor bypassed to temporarily restore crane function
- Risk of operating without sensor determined to be low through discussions with Norelco / Don Dale / Grant Minor
- Replacement thermal sensor + 1 spare (~ $300 ea + shipping) ordered from parts supplier through Norelco - expected delivery Monday October 21st

How could this fault have been prevented?
- Cause of failure within thermal sensor module unknown at this time
- Annual crane inspection performed by Norelco in March 2013 did not indicate any problems with this sensor (crane drive system functioned as normal)
- Suggested for future: routine inspection of sensor module shunt resistance to determine if there are any long-term signs of slow degradation

What can be done to prevent the fault in the future?
- The ISAC crane controls were designed in the late 1990's by Norelco sub-contractor Seattle Crane (now defunct)
- The crane is supposed to have two pairs of independent motors with separate thermal sensors, each capable of driving the crane if the other fails due to thermal trip
- My understanding is that the controls logic design should have been designed so that failure of one pair of motors does not prevent crane operation... it does not seem to be the case with the current design
- The design of the control logic related to these sensors could be re-evaluated and modified so that a trip from one thermal module does not prevent operation of the bridge if the other module is OK
- This is a project that will require some time and some controls and engineering resources
- In the interim, if the same failure occurs again, it may be possible to jumper the thermal sensor from the crane control room and continue operating normally - I will confirm with controls group / Norelco
- However, this is not advisable as it would be difficult in some cases to determine if the trip was due to a faulty thermal module, or an actual motor overheat scenario
- I will discuss further actions with Don Dale

Thanks and best regards,

Grant


On 11/10/2013 4:29 PM, Grant Minor wrote:

Hello all,

I spoke with the Norelco tech Mike Smith this afternoon regarding the failed thermal sensor component / circuit.  He will call Kone on holiday Monday (their office is not closed for Canadian Thanksgiving) and determine if they have a replacement module.

I explained (to the best of my understanding) the diagnosis performed by Dave Morris / controls group and the test that was done to isolate the thermal sensor unit.  Unfortunately, Mike Smith's drawings from Seattle crane contain notes and revisions that don't match the drawing that Dave Morris provided me (Seattle Crane dwg E5 - 1/1 revision 1 02-10-99), and he was unable to confirm in his opinion whether the bypass performed by Dave Morris has correctly isolated the problem components.  In addition, he believes that the bypass he performed on Wednesday isolated portions of circuitry that are inconsistent with this thermal sensor circuit.

Mike Smith will return Tuesday morning to review the bypass and schematics.  He recommended not operating the crane until he has a chance to confirm this thermal sensor issue.

From the drawings I have in hand and from discussions with Dave Morris, the failed component might be the thermistor sets inside the motor housing which are in series with the suspect module, or the module itself.  My understanding is that the crane is designed with two pairs of motors for the bridge drive, and each pair is protected by one of these thermal modules (thus there are two modules total).  Both modules would be the same age and both might be susceptible to the same failure mode.

As it is unclear to me the exact nature of the drive system failure, and I have a recommendation from Norelco to hold on operation of the crane, I must unfortunately state that the crane should not be used and we will have to wait until Tuesday to gather more information.

I am not so concerned about temporary loss of the thermal protection circuitry, as we have not had an overheating scenario in those motors in the lifetime of the crane (to my knowledge).  I am more concerned about getting 100% confirmation that we have addressed the problem.  If we attempt to use the crane and experience another failure during a lift that prevents us from placing the load down safely with the crane stuck in position over a target station, then we would be in much deeper trouble.

My apologies for this situation.

Best regards and have a good weekend,

Grant


On 11/10/2013 1:28 PM, Grant Minor wrote:
Thanks Dave,

I've contacted Norelco, Mike Smith and I are planning a path forward for further diagnosis and repair.

The crane MUST NOT be used to carry a load until it is identified whether the module or the sensors have failed, the reason for the failure, and the functionality of the thermal sensors has been restored.

Without the thermal sensor circuit we lose protection from motor overheat, an event which could have much more serious failure implications to the crane.

Cheers,

Grant

On 11/10/2013 1:04 PM, David Morris wrote:
The fault has been identified in the Target Hall Crane as a failed motor temperature module, or motor temperature sensor, on the East-West motion. The status contact in the module was bypassed allowing crane motion. There was no fault with the controls.

Dave

Attachment 1: ISAC_THall_Crane_elec_E5_1slash1_15Oct2013.pdf
ISAC_THall_Crane_elec_E5_1slash1_15Oct2013.pdf
  502   Tuesday, October 15, 2013, 15:34 Bevan MossITEStandard OperationTM3 Blocks moved from ITW to ITE

 Blocks 1-4 have been moved from ITW to ITE. Block 5 was moved to a storage area as it will be in the way of the harp repair. Danka took air samples and found 200 counts of alpha on the air samples but nothing on the swipes. It is recommended that resporators be worn while blocks are being lifted and lowered. She will check the monitor tomorrow to confirm it is behaving as it should.

  501   Wednesday, October 09, 2013, 19:33 Grant MinorCraneRepairTM4 Target Hall Crane not operational - likely controls / PLC hardware failure (not stuck wheel)

Grant Minor wrote:

Grant Minor wrote this e-mail today:

***

Hello all,

During our planned operation of transporting TM4 from a storage silo to the Hot Cell, we had a problem with the East-West bridge drive on the Target Hall crane.  The crane bridge is currently stuck in position over the silo area.  We were unable to complete the transport operation.  TM4 has been placed back down into the silo and the crane hook block has been disconnected from the module lifting yoke.

We have been on the phone with Norelco this afternoon and have determined the likely cause of the problem.  There is a splice joint in the crane rails at this position, where a small gap exists between the rail sections.  If the crane bridge is stopped during operation such that the wheel comes to rests in this gap, the crane motors have insufficient torque for the wheel to overcome the gap and ride back onto the rail.  The Norelco tech Mike Smith remembers encountering this problem several years ago (before my time) but cannot remember how it was overcome.  The fix likely involved moving the wheel out of the gap with pry bars.

Target Hall Survey Needed at or before 7:00 am, Wednesday Oct 9th (Lynne, Fiona, Danka, Max or Dano?)

Mike Smith and possibly a few others from Norelco will come tomorrow morning at 7:00am, and require access to the Target Hall.  Since we have opened the Hot Cell in preparation for the module move, we will need a survey as early as possible to allow Mike and his crew to enter the hall without a suit and respirator.

Most of the Remote Handling group will be off-site for a Division meeting, but Travis and Maico will stay for the day to accompany the Norelco guys and help with the problem assessment.

Travis: Please take Mike to the control room when he arrives, one of the cameras is currently zoomed in on the wheel and problem rail section.

Maico: Scaffolding may be required to get access to the crane rail.  Unfortunately we don't have an operational crane to transport a man-lift into the hall ;)  Please see what you can do to get this ready in case we need it.  Max's leak check might have to go on hold until we get this resolved.  Please take responsibility for ensuring correct Fall Protection procedures are followed.  This means that nobody should be walking up on the crane rail unless they are tied in with harnesses, or there is scaffolding directly under them.

I can be reached on my cell phone at 778-319-4612.  The Division meeting is on UBC campus so I can return to TRIUMF fairly quickly if needed.

Thank you all for your assistance,

Grant

***

A photo of the THall camera view of the bridge wheel at the rail splice is attached, as well as Mike Smith's crane inspection report from March 2013.

E-mail from today:

Hello Dave, Jane, Franco, Michael, Don (controls + Franco), Remy,

We have lost the East-West bridge drive control functionality of the ISAC Target Hall crane, and unfortunately this very much prevents us from operating the ISAC facility.

The problem was originally thought to be a stuck bridge wheel but this was not actually the case.

Mike Smith from Norelco was on-site for most of today working with Michael Rowe in an attempt to diagnose the problem.

Mike believes the problem to be one of the following three items:
- input PLC board on the crane bridge
- output PLC board in the interface panel in B1 level Room 5 (ISAC remote crane control room)
- communication between the two boards (festooning hardware)

We are in a pretty dire situation without the ISAC target hall crane, and we lack the expertise within the Remote Handling group in PLC hardware to diagnose this on our own.  I need to ask for somebody's help from the controls group in diagnosing and repairing this problem.

I have notes from my telephone conversation with Mike Smith which I can discuss with a controls representative in the morning.  There is a pretty muddled history of the design and implementation of these controls but essentially Norelco outsourced the PLCs and festooning to a third party contractor, Seattle Crane in the US, which no longer exists anymore.  Neither Kone, Seattle Crane, or Norelco made appropriate as-built drawings of the wiring of the PLCs.  Mike Smith at Norelco had a stack of hand-written notes about the as-built configuration he made at the time of installation in the late 1990's but these notes have not been located yet.

The PLCs appear to be Allan Bradley but the modules are from approximately 1997 and we're not sure if spare units are available.

Mike Smith says the easiest thing to do at this point is install replacement PLC modules on the crane bridge and in the control room that have confirmed functionality.  If control is not restored then the problem is likely in the festooning.

Control of the crane bridge was temporarily attained by bypassing the controls (speed control / end limits, etc.) and sending drive signal directly to the drive motor controller in order to return the bridge to its home position at the access ladder.  This mode of operation is not safe as the crane has no speed reduction / limits to prevent driving the bridge into the walls at max speed.

Jane / Remy / Franco: please let me know who I should correspond with on the controls side and I will talk with them tomorrow morning.

Thanks,

Grant

  500   Tuesday, October 08, 2013, 18:12 Grant MinorCraneRepairTM4 Target Hall Crane Stuck in East-West Direction - Update

Grant Minor wrote this e-mail today:

***

Hello all,

During our planned operation of transporting TM4 from a storage silo to the Hot Cell, we had a problem with the East-West bridge drive on the Target Hall crane.  The crane bridge is currently stuck in position over the silo area.  We were unable to complete the transport operation.  TM4 has been placed back down into the silo and the crane hook block has been disconnected from the module lifting yoke.

We have been on the phone with Norelco this afternoon and have determined the likely cause of the problem.  There is a splice joint in the crane rails at this position, where a small gap exists between the rail sections.  If the crane bridge is stopped during operation such that the wheel comes to rests in this gap, the crane motors have insufficient torque for the wheel to overcome the gap and ride back onto the rail.  The Norelco tech Mike Smith remembers encountering this problem several years ago (before my time) but cannot remember how it was overcome.  The fix likely involved moving the wheel out of the gap with pry bars.

Target Hall Survey Needed at or before 7:00 am, Wednesday Oct 9th (Lynne, Fiona, Danka, Max or Dano?)

Mike Smith and possibly a few others from Norelco will come tomorrow morning at 7:00am, and require access to the Target Hall.  Since we have opened the Hot Cell in preparation for the module move, we will need a survey as early as possible to allow Mike and his crew to enter the hall without a suit and respirator.

Most of the Remote Handling group will be off-site for a Division meeting, but Travis and Maico will stay for the day to accompany the Norelco guys and help with the problem assessment.

Travis: Please take Mike to the control room when he arrives, one of the cameras is currently zoomed in on the wheel and problem rail section.

Maico: Scaffolding may be required to get access to the crane rail.  Unfortunately we don't have an operational crane to transport a man-lift into the hall ;)  Please see what you can do to get this ready in case we need it.  Max's leak check might have to go on hold until we get this resolved.  Please take responsibility for ensuring correct Fall Protection procedures are followed.  This means that nobody should be walking up on the crane rail unless they are tied in with harnesses, or there is scaffolding directly under them.

I can be reached on my cell phone at 778-319-4612.  The Division meeting is on UBC campus so I can return to TRIUMF fairly quickly if needed.

Thank you all for your assistance,

Grant

***

A photo of the THall camera view of the bridge wheel at the rail splice is attached, as well as Mike Smith's crane inspection report from March 2013.

Attachment 1: THall_Crane_Bridge_Wheel_at_South_Rail_Splice_8Oct2013.JPG
THall_Crane_Bridge_Wheel_at_South_Rail_Splice_8Oct2013.JPG
Attachment 2: NORELCO_inv13045_joMS-064_31March2013.pdf
NORELCO_inv13045_joMS-064_31March2013.pdf NORELCO_inv13045_joMS-064_31March2013.pdf NORELCO_inv13045_joMS-064_31March2013.pdf NORELCO_inv13045_joMS-064_31March2013.pdf NORELCO_inv13045_joMS-064_31March2013.pdf NORELCO_inv13045_joMS-064_31March2013.pdf
  499   Tuesday, October 08, 2013, 14:58 Anders MjosSouth Hot-CellStandard Operation SiC#29Target to Heat Shield electrical short

The SiC#29 CTL target has been taken apart with the help of Isaac and Chad. Electrical measurements were done between Target and Heat Shield as the target was disassembled. Work was done on October 2nd, 4th, 7th and 8th.

The megger showed about 30kOhm at 50V with the following changes

  • Bolts for CTL block loosened
  • Above bolts removed
  • CTL block pulled away from Heat Shield
  • CTL block removed
  • Heat Shield lid removed
  • Bolts for target removed
  • Shims between target and insulators

The megger showed about 50kOhm at 100V with the following changes

  • Target removed. Measured between cathode restraint and HS.

The megger showed OL at 540V with No 3 insulator removed. A measurement on No 3 insulator while it was sitting on the HS showed 70kOhm at 120V confirming that the insulator can no longer hold voltage.

While taking off the coil retainer plate, Chad noticed that all bolts were not tight.

Photos are available on DocuShare.

  498   Tuesday, October 08, 2013, 14:55 Travis CaveSouth Hot-CellStandard OperationTM4no targetmodule move

TM#4 with no target was to be moved today but the move was aborted when the crane failed to move in the East - West direction. The crane does not preform this function in either remote or pendant operation.

  497   Tuesday, October 08, 2013, 13:11 Travis CaveSpent Target VaultStandard Operation SiC#29Spent target move

SiC#29 has been moved to the spent target vault. The target was placed in Pail #109 and placed into slot 2B it was 24.7mS/hr upon removal from the south hot cell. See attached PDF of the vault details.

Attachment 1: Vault_Storage_October_8_2013.pdf
Vault_Storage_October_8_2013.pdf Vault_Storage_October_8_2013.pdf Vault_Storage_October_8_2013.pdf Vault_Storage_October_8_2013.pdf
  496   Monday, October 07, 2013, 12:06 Travis CaveITEStandard OperationTM3NiO#2module move

TM#3 has been moved from the conditioning station to the east target station, move went well.

  495   Sunday, October 06, 2013, 20:28 Friedhelm AmesConditioning StationStandard OperationTM3NiO#2turbo pumps stopped

vacuum readings before stopping

IG1: 7.4e-7 T

IG2 3.8 e-6 T

IG1S 1.95 e-6 T

  494   Sunday, October 06, 2013, 17:08 Friedhelm AmesConditioning StationDevelopmentTM3NiO#2trip of all power supplies

All power supplies tripped on high conductivity of the cooling water < 5 MOhm, It is not clear if this was caused by a spark or vice versa. According to the strip tool for this signal the resistance of the water went up. There might be a fault in this signal. I do not have permission to force this signal so I keep the heaters off. We should revisit the interlock conditions, this signal should not be included in the interlocks for the heaters. Both target and tube seem to be still o.k. As I do not want to destroy the target I keep the heaters off and restart the high voltage only.

  493   Sunday, October 06, 2013, 15:39 Friedhelm AmesConditioning StationStandard OperationTM3NiO#2HEATERS STARTED

The high voltage was sparking several times during the night. It may be correlated with the cycling of the cooling water temperature and conductance.

vacuum levels at 11:00

IG1 7.5e-7 T

IG2 3.9e-6 T

IG1s 2.0 e-6 T

heaters have been ramped up to TGH 580 A, TBHT 250 A,

anode 100 V 5.3 mA, coil 50 A Faraday cup 50 nA bias 20 kV EL 6 kV

vacuum

IG1 7.9e-7

IG2 4.5e-6

IG1s 2.2e-6

  492   Sunday, October 06, 2013, 00:17 Friedhelm AmesConditioning StationStandard OperationTM3NiO#2high voltage conditioning

high voltage conditioning was carried out over the day up to 24 kV. i will leave it at 20 kV over night. Current is at 22 micro Amps, heaters off.

vacuum: IG1 7.7e-7

IG2 4.07 e-6

IG1sS 2.2 e-6

 

  491   Saturday, October 05, 2013, 14:45 Friedhelm AmesConditioning StationStandard OperationTM3NiO#2vacuum readings

IG1 8.0 e-7 T

IG1S 2.5 e-6 T

IG2 4.3 e-6 T

I will start the high voltage now

 

  490   Friday, October 04, 2013, 19:39 Grant MinorConditioning StationStandard OperationTM3NiO#2TCS vacuum improvement w/ heaters off - 2:20 pm to 7:17pm

Here is the change in the TCS vacuum after heaters were turned off earlier today:

2:20 pm readings

TCS:IG1 (service cap) 9.3 x 10^-7 Torr

TCS:IG2 (diagnostics box) 5.71 x 10^-6 Torr

TCS:IG1S (secondary vacuum) 4.0 x 10^-6 Torr

7:17 pm readings

TCS:IG1 (service cap) 8.69 x 10^-7 Torr

TCS:IG2 (diagnostics box) 5.0 x 10^-6 Torr

TCS:IG1S (secondary vacuum) 3.38 x 10^-6 Torr

ELOG V2.9.2-2455