Monday, June 27, 2016, 13:45, David Wang, ITE, Standard Operation, , , 5 Shielding blocks have been transferred from ITW to ITE.
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ITE is configured to take proton beam. |
Thursday, June 30, 2016, 13:33, Dan McDonald, Spent Target Vault, Maintenance, , , F308's
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The five spent target F308 flasks where gone through in accordance with Nordion guidelines, the sixth spare is remains in the Hot Cell area. All flasks where in reasonable shape with two needing weld repairs on the pallets. I replaced all the 3/4" pallet to flask fasteners with new Grade 8 bolts nut and washer combo. Flasks have been moved into the Hot Cell area awaiting movement into the Target Hall. |
Wednesday, July 06, 2016, 07:03, David Wang, ITW, Standard Operation, TM2, , TM2 was connected in ITW.
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TM2 was disconnected in ITW and moved to SHC. |
Wednesday, July 06, 2016, 07:06, David Wang, Conditioning Station, Standard Operation, , , venting TCS with argon.
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I switched off the vacuum pumps and vented TCS with argon. The TCS will be ready to accept TM2 this afternoon. |
Wednesday, July 06, 2016, 14:25, David Wang, Conditioning Station, Standard Operation, TM2, , TCS and TM2 turbo-pumps have been started.
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The TCS and TM2 are pumping down. |
Friday, July 08, 2016, 08:20, David Wang, Conditioning Station, Standard Operation, TM2, , TM2 has been connected at TCS
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I connected TM2 to TCS and started water system. |
Friday, July 08, 2016, 16:56, Anders Mjos, Conditioning Station, Repair, , , VFD21 OL1 fault on Chiller
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Plant Services group (Tony) will contact a service tech on Monday.
Water system will be switched off over the weekend. |
Tuesday, July 12, 2016, 12:40, David Wang, ITW, Standard Operation, TM2, , TM2 has been connected in ITW
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All turbo-pumps are started. Everything is good so far. |
Tuesday, July 12, 2016, 12:42, David Wang, Conditioning Station, Standard Operation, , , Target Hall schedule for beam schedule 130 (Apr- Sep) 
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Update schedule weekly.Attachment 1,2 |
Thursday, July 14, 2016, 10:54, David Wang, Conditioning Station, Standard Operation, TM2, , Target Hall schedule for beam schedule 130 (Apr- Oct, 2016)   
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Update TH schedule 130 according to mini-shut down change.See attachment 1,2,3,4 |
Thursday, July 14, 2016, 13:25, Anders Mjos, Conditioning Station, Repair, , , VFD21 OL1 fault on Chiller
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Anders Mjos wrote: |
Plant Services group (Tony) will contact a service tech on Monday.
Water system will be switched off over the weekend.
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Thursday, July 14, 2016, 13:24: Claus from Daikin is on site to troubleshoot.
The VFD driven fan motor has failed. Temporarily blocked air-flow through failed fan to improve air-flow to radiator. A new motor will be ordered (Curtis).
Thursday, July 14, 2016, 15:39: Stopped cooling system for the day
Friday, July 15, 2016, 08:16: Cooling system started
Friday, July 15, 2016, 15:00; Cooling system stopped. |
Monday, July 18, 2016, 14:14, David Wang, Conditioning Station, Repair, TM3, , TM3 leak checked at TCS
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Last Friday July-15, TM3 was leak checked at TCS. All air to vacuum seals on service cap are good. Helium pressure test on TM3 water lines(except GE, HS, and Window) were done. Leak detector has no response at 0.0xE-9 atm.cc/sec. They are leak free. |
Tuesday, July 19, 2016, 14:35, Aurelia Laxdal, Conditioning Station, Repair, TM3, , TM3 leak checked at TCS
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David Wang wrote: |
Last Friday July-15, TM3 was leak checked at TCS. All air to vacuum seals on service cap are good. Helium pressure test on TM3 water lines(except GE, HS, and Window) were done. Leak detector has no response at 0.0xE-9 atm.cc/sec. They are leak free.
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Friday July 15: did HV tests (with no target installed and with the anode wire removed ). <br>
TM3 went up to 22.5kV. At this voltage it started sparking. The EL was kept at 1/2 with respect to the HV BIAS. <br>
Also HV tests were done while the EL was kept at zero V. In this case, the EL voltage was once in a while spiking up (up to 4kV). <br>
During sparking we saw responses in the vacuum. Checked the Service Cap (with the HV Cover) in the Target Hall: we couldn't hear/see sparks there. <br>
The HV was turned off in the same day, after 5:30pm. |
Friday, July 22, 2016, 10:57, David Wang, Conditioning Station, Repair, TM3, , TM3 has been moved and connected at TCS
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I started vacuum system.
I started TCS water system. The chiller does not work properly still. But, It will not affect the TM3 HV conditioning. HV cover is installed on TM3 in TH. The module is ready for HV conditioning. |
Monday, July 25, 2016, 08:15, Anders Mjos, Conditioning Station, Repair, TM3, , HV Test  
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Monday, July 25, 2016, 08:14: Enabled staging for chiller
Monday, July 25, 2016, 08:33: Disabled staging. Fault 2. Staging does not work at this point.
Monday, July 25, 2016, 08:34: Running CP1 manually to cool down water.
Monday, July 25, 2016, 09:15: Bias current limiting at 150 V. Investigating short.
Monday, July 25, 2016, 09:51: EE cable was shorting the BIAS on the TCS side.
Monday, July 25, 2016, 09:57: BIAS/ / EL at 20 / 10 kV
Monday, July 25, 2016, 10:08: Sparking at 24 kV. Lowered to 22 kV
Monday, July 25, 2016, 10:44: BIAS at 25 kV
Monday, July 25, 2016, 11:00: Sparking at 25.5 kV. Lowered to 25 kV
Monday, July 25, 2016, 12:03: 25.5 kV. No sparking for 10 min. Lower to 20 kV for lunch break.
Monday, July 25, 2016, 12:51: 26 kV
Monday, July 25, 2016, 13:00: Sparking at 27.3 kV. Lowered to 27 kV. EL at 14 kV
Monday, July 25, 2016, 13:04: More sparking. Lowered to 25 kV
Monday, July 25, 2016, 13:39: 25 kV
Monday, July 25, 2016, 14:21: A spark tripped the PS on water resistivity
Monday, July 25, 2016, 14:31: 25 kV
Monday, July 25, 2016, 15:34: ~20 sparks for the last 60 min
Monday, July 25, 2016, 16:28: ~10 sparks for the last 60 min. BIAS an EL off
Monday, July 25, 2016, 16:36: Stopped water cooling system.
Tuesday, July 26, 2016, 08:20: Started water cooling system.
Tuesday, July 26, 2016, 08:24: Ran CP1 manually for 3 min. Enabled staging.
Tuesday, July 26, 2016, 08:31: BIAS / EL at 25 / 0 kV
Tuesday, July 26, 2016, 08:39: EL float to 300 V. Set to 500 V
Tuesday, July 26, 2016, 08:45: BIAS to 25.5 kV
Tuesday, July 26, 2016, 09:07: 26 kV
Tuesday, July 26, 2016, 09:12: Lost contact with EPICS. Scheduled maintenance
Tuesday, July 26, 2016, 10:26: 6 sparks for the last 60 min
Tuesday, July 26, 2016, 10:33: BIAS to 27 kV
Tuesday, July 26, 2016, 10:43: Sparking at 27.8 kV. Lowered to 23 kV
Tuesday, July 26, 2016, 10:51: BIAS back at 27 kV. A spark tripped the BIAS on water resistivity
Tuesday, July 26, 2016, 11:08: BIAS at 27 kV
Tuesday, July 26, 2016, 11:22: BIAS at 28 kV
Tuesday, July 26, 2016, 11:42: BIAS at 27 kV after trip due to water resistivity (spark)
Tuesday, July 26, 2016, 12:00: BIAS / EL off for lunch break
Tuesday, July 26, 2016, 14:10: EL to 10 kV
Tuesday, July 26, 2016, 14:14: El to 20 kV
Tuesday, July 26, 2016, 14:20: EL to 25 kV
Tuesday, July 26, 2016, 14:27: First spark at 27.6 kV
Tuesday, July 26, 2016, 14:29: EL to 28 kV (BIAS at 0 kV)
Tuesday, July 26, 2016, 14:43: RGA on
Tuesday, July 26, 2016, 14:49: No sparking for 20 min
Tuesday, July 26, 2016, 16:02: No sparks for 90 min.
Tuesday, July 26, 2016, 16:06: PS and water off.
Wednesday, July 27, 2016, 09:14: BIAS at 24 kV
Wednesday, July 27, 2016, 09:19: Lowered to 20 kV due to sparking
Wednesday, July 27, 2016, 09:28: BIAS at 22 kV
Wednesday, July 27, 2016, 15:30: BIAS and water off
Thursday, July 28, 2016, 08:43: RGA off |
Tuesday, July 26, 2016, 11:22, chad fisher, South Hot-Cell, Maintenance, , , Soth Hot Cell Waste Storage Vault Tunnel
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The two 45 gal (m) drums of waste removed from the south hot cell in December 2015 and January 2016 were transferred from the north hot cell to the shaft of the east vault tunnel on Monday, July 25th 2016 and subsequently to the east tunnel bunker in the vault tunnel on Tuesday, July 26th, 2016.The first drum (removed from the hot cell in December) containing both activated and contaminated metals was measured at 900 uSv/hr @ .5 m and the second drum (removed from the hot cell in January 2016) containing compressible items such as tank suits and plastic was measured at 150 uSv/hr @ .5 m.
Items were filed for storage/disposal with RPG under item number 1395 on the radioactive storage form.
Drums were transported to the vault tunnel using the 500 Mev Shield Flask (Drawing E-7097) with some minor modifications, namely a 1/4" thick Aluminum plate with four holes that line up with the holes in the bottom flange of the flask. This plate provided a bottom for the flask so that a drum could be contained within the flask during craning. Holes in the plate where countersunk for a 1/2" flat head bolt. Four bolts were also modified to accept 3/16 hair pins. 3 plates with clearances holes for the bolts were also manufactured to act as washers.
Procedure was as follows: With plate, washers and pins installed onto the flask, a modified drum dolly (5" spacers added to the casters) was placed inside the flask. Drum was craned into the flask using the automatic drum lifter. Flask with drum loaded was moved to the Meson Hall loading bay then craned to the B2 level of the Meson hall. Hair pins were pulled from the flask and the flask was then craned up leaving the drum (which was on the dolly firstly installed into the flask) and the plate. Drum on dolly was rolled to vault access shaft where it was craned off the modified dolly using the automatic drum lifter and down the access shaft to the vault tunnel level. A second drum dolly was waiting at the bottom level and drum lowered onto it. Procedure was repeated for the second drum
Was vault was open , drums were wheeled into the vault tunnel and into a bunker that had been modified to accept these drums. Drums were lifted off dollies and put in place in bunker which had blocks installed to cover the entrance provided for installation.
Pictures can be found on docushare http://documents.triumf.ca/docushare/dsweb/View/Collection-18072 (collection 18072)
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Friday, July 29, 2016, 14:27, Isaac Earle, North Hot-Cell, Development, , , North Hot Cell Measurements & Cleanup
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The North Hot Cell was accessed today via the Ante Room for inspection, measurements, and clean-up. There were no modules in the SHC or TCS, and no spent targets in the SHC. Under these conditions the maximum field in the NHC was approximately 2μSv/hr. The inside of the cell was cleaned and swept, followed by a floor swipe to check for contamination (none found). All areas of the ante room floor were also swiped: no contamination found.
The following measurements were taken in the NHC for comparison with the Soldiworks model:
SHC/NHC feedthrough panel fastener size: 1/4"-20, 1/2" long
NHC west wall to east edge of SEG block: 33-1/4" on south side, 33" on north side
NHC west wall to furthest extent of TCS (IRH1170): 40"
NHC west wall to wall indentation for viewing window: 46-7/8"
NHC west wall to end of existing ventilation duct: 4-1/8"
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Wednesday, August 03, 2016, 09:15, chad fisher, South Hot-Cell, Repair, , , Manipulator
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East manipulator on the south hot cell is showing signs of eminent wrist/tong cable failure. Some slight slippage was noted yesterday and confirmed by a snapping sound and more slippage tomorrow. |
Wednesday, August 03, 2016, 09:49, David Wang, Conditioning Station, Standard Operation, TM4, , TM4 is ready for conditioing at TCS.
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I started TCS water system and installed HV cover onto TM4. The TM4 containment box is supplied with water also. TM4 is ready for conditioning at TCS. |
Wednesday, August 03, 2016, 09:56, David Wang, Conditioning Station, Standard Operation, , , Target Hall schedule for beam schedule 130 (Apr- Oct, 2016) 
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Update schedule weekly. See attachments 1,2 |
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