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Entry  Thursday, January 16, 2014, 08:46, maicodallavalle, Trolleys serviced, Maintenance, Pre Cyclotron work servicing and checking 

This is a list of all the trolleys and other equipment witch were checked and serviced prior to work in the Cyclotron.

- Video Trolley cleaned and checked (no adjustments needed)

-Lift Trolley cleaned and checked (no adjustments needed)

- Left Outrigger cleaned and checked

 All of the bearings in the festooning wheels  were changed.

  Drive chain needed adjustment. (modification to wheel mounting bracket so that chain could be adjusted)

-Right Outrigger cleaned and checked

 All of the bearings in the festooning wheels were changed.

 Drive chain needed adjustment. (modification to wheel mounting bracket so that the chain could be adjusted)

-Tool Trolley cleaned and checked

 One of the support wheels was checked and found to be out of alignment. (an adjustment was made to correct the problem) 

-Upper Resonator Trolley cleaned and checked (no adjustments needed)

-Service Bridge cleaned and checked

  Center post mount was rotated by hand. (no adjustment needed)

-Service Bridge Carrier cleaned and checked

 The two hydraulic cylinders witch lift the Service Bridge into the Cyclotron leaked last year.They were rebuilt last year and are not leaking.

 The two drive chains witch run the Carrier North and South were found to be too tight. (an adjustment was made to correct the problem)

 

 

Entry  Friday, January 17, 2014, 07:53, Travis Cave, Trolleys serviced, Standard Operation, Trolley checks 

All trolleys work electrically and control wise. One encoder was found non functioning on the upper resonator trolley for the vertical drive it was replaced, we've no move replacements of those current type of encoders so a wholesale replacement of all the trolley's encoders will have to be done post shutdown. Also the wiring for the outrigger is in need of replacement but will work for this shutdown it will also have to be replaced post shutdown as well. The upper resonator trolley has also been setup to remove X2C.

Entry  Tuesday, February 17, 2015, 07:10, Dan McDonald, Trolleys serviced, Maintenance, Pre shut down trolley service 

Routine maintenance as per Mike Gallop's written procedure took place in December with the only non routine service being the changing of shaft seals on Vacuum trolley drive reduction box.

Trolleys maintained - Lift trolley

                                     - Vacuum trolley / Tool trolley

                                     - Camera trolley

                                     - Upper resonator trolley

                                    

Entry  Friday, February 26, 2021, 08:29, Adam Newsome, Trolleys serviced, Maintenance, First Turn Radial Flag (FTRF) Jig - Pneumatic Upgrade PXL_20210216_202019350.jpg

Old fittings and broken pneumatic tubing on the FTRF jig have been replaced with new push-connect fittings and polyurethane tubing. The jig was previously not in a functioning state due to damaged tubing. A pneumatic diagram was created in the process of the upgrade. The tubing will be cleaned up within the next few days and the jig tested.

Entry  Friday, February 26, 2021, 13:00, Adam Newsome, Trolleys serviced, Maintenance, Lower Resonator Trolley - Radial Drive Failure Issue 

On Feb. 24 while practising a training exercise, the lower resonator trolley unexpectedly experienced a radial drive failure. The trolley did not move in either radial direction (this occurred after approx. 5 minutes in the tank, near the centre post, with FTRF jig installed). The trolley was retrieved from the tank manually for investigation. Upon retrieval and testing on the mockup, the radial drive began to work again.

Investigation consisted of:

  • Verifying controls signals reaching motor controller
  • Verifying power to motor
  • Verifying all connectors and cables intact
  • Verifying drive components installed and free of damage (shafts, keys, set screws, etc.)
  • Disassembly and inspection of gearbox
  • Running the motor for approximately 3 hours with no load to verify no issues

 

The cause of the issue cannot be found, however it is suspected a thermal shutdown of the motor or motor controller may have occurred, and after a short delay, the circuit was reset back to a functioning state on its own.

 

In the future prior to using this trolley it is recommended to test run it, with load, in the mockup to verify radial drive functionality.

Entry  Tuesday, August 31, 2021, 14:28, Adam Newsome, Trolleys serviced, Development, Upper Resonator Trolley - Finger Cylinders Replaced new_fingers.PNG

The two support fingers on the upper resonator trolley were bent due to excessive loading during cylinder toggling.

Fingers were bent back into position such that they are vertical when the cylinder is retracted.

The cylinders used to actuate these fingers were replaced (one was leaking) - replacement allowed for the opportunity for upgrade. The following changes were made:

  • Changing reverse spring-return cylinders to double-acting cylinders (formerly American Cylinder 750RVS-2.00, replaced with SMC NCDMB075-0200C)
  • Addition of in-line flow controls for both extension and retraction motions
  • Tuning of flow control to achieve smooth operation and prevent further damage to the fingers during actuation

 The new finger configuration has been tested and is working.

Entry  Tuesday, February 14, 2012, 15:40, Grant Minor, Trolley, Standard Operation, 2C Removal - all 4 QDLs were actuated remotely this year! 2C_probe_Feb_14_2012_labelled.JPG2C_probe_solenoid_5_Feb_14_2012_labelled.JPG

Today Remote Handling staff (Maico Dalla Valle, Travis Cave) used the Remote Handling 2C probe removal trolley to remove the probe assembly from inside the Cyclotron.  This is a regular yearly MRO task that is done every shutdown.

This task involves lining up the 2C trolley on the service bridge with the 2C probe assembly remotely with cameras, using a set of alignment markings on the trolley and probe assembly.  Once the trolley is lined up with the probe assembly, a set of solenoids are fired to disengage a corresponding set of four QDLs (quick disconnect latches) at different locations on the probe assembly.  A complete procedure is documented by Remote Handling staff.

The four QDLs are actuated by a set of four solenoid actuators on the 2C removal trolley, numbered 3, 4, 5, and 8.

Traditionally in the past, the QDL actuated by solenoid 8 has  jammed and does not automatically disengage when hit with the solenoid actuator.  A member of Probes or Remote Handling has had to suit up with a respirator, run into the Cyclotron tank, and tap this QDL by hand to free it from it's jammed state.  This has been done every year for quite some time, as long as Don Jackson can remember (around 30 years)!

However, today, Remote Handling staff (Travis and Maico) were able to disengage all four QDLs remotely using the solenoid actuators on the trolley!

 

A few things were done differently this year compared to previous years, which may have contributed to this success:

a.  The centre post bearing on the service bridge was disassembled, cleaned, and lubricated (see previous e-log from this shutdown)

b.  The "AXIAL A" alignment tab on the 2C removal trolley was intentionally misaligned with the felt pen markings on the 2C assembly (see attached picture that points out this "gap").

c.   The solenoids were fired in the following order: 8 (no success on disengagement), 5 (success), 4 (success), 3 (success), then 8 again (success).

 

After all four QDLs were disengaged, and the probe assembly was lowered away from its fixture points, it was observed that the assembly moved slightly laterally, indicating a slight stress or misalignment between all four QDL pins and their corresponding receptacles in the Cyclotron tank. The "gap" labelled in the attached picture, shrunk a small amount after this lateral movement.

Don Jackson remarked that in his entire tenure here, he had never witnessed successful remote disengagement of all four QDLs!  This is quite a positive result, as it lowers the expected dose and time required to remove the 2C probe assembly.  This approach to the task should be repeated next year and video documented (unfortunately we were not video recording the successful attempt this year).

Cheers,

Grant Minor, Remote Handling

 

Entry  Friday, February 17, 2012, 15:07, Don Jackson, Trolley, Repair, Video Trolley Failed in Cyclotron Tank Stuck_Video_Trolley_Feb_17_2012_005.jpgStuck_Video_Trolley_Feb_17_2012_001.jpg

All control to the video trolley was lost during remote photographing of components in the cyclotron. The control system and cameras on the trolley were still operational leading to the suspicion that a power cable was broken either on the trolley or the bridge festooning. Two trips into the tank were made to evaluate the problem and attempt to push the trolley out of the tank. Pushing the trolley only managed to move the trolley a few feet before jamming. A lift mechanism was used to raise the drive wheel without any success. This device was modified and used successfully to remove trolley completely from the tank.

Three trips by two persons were required to remove the trolley. There was a total dose of 0.5 mSv was received by the two persons going into the tank. An additional 0.18mSv was receive by 3 persons outside of the tank.
 
The trolley will not be used in the cyclotron until the problem is diagnosed and repaired. This trolley is not critical to any upcoming remote handling operations.
Entry  Tuesday, July 28, 2015, 11:47, Dan McDonald, Trolley, Maintenance, Camera trolley service 

Serviced the Camera trolley this morning as per Mike Gallops service outline.

Entry  Thursday, June 30, 2016, 13:47, Dan McDonald, Trolley, Maintenance, Lift trolley 

Maintenance has been performed on the lift trolley, re sealed the main drive gear box it was quite dry inside and in need of new seals and lubrication. Inspected the vertical gear box and resealed it, re tensioned  the vertical drive chain after removing gear box and finding since last year the chain had become somewhat slack causing it to rub on the frame. Purchased a new LED light bar to replace the aging and failing flourescent light that was in place. greased all pillow block bearings and replaced old Zerk ( grease nipple) on some bearings to allow for easier lubrication.

Entry  Friday, February 02, 2018, 14:14, Don Jackson, Trolley, Repair, Overcurrent on radial drive motor 

 

Lower resonator trolley radial motor overcurrent was causing control system to drop out momentarily.  All controlled devices acted as expected and reverted to their fail-safe mode.  When system restarted 1-2 seconds later, all solenoids returned to their previous positions.

The cause was eventually traced to an unusual operation of the trolley.  In an attempt to limit trolley motion the drive switch on the control panel was repeatedly “tapped” in a rapid fashion.  This did not allow the motor to slow down enough to allow the starter winding to kick in which allowed large in-rush current.  The current was enough to load down the entire system including the power supply for the trolley controls, which caused the controls drop-out.

Later the same effect was observed to a lesser extent on the upper resonator trolley which used identical motors and controls.

Proposed solution is to either to limit large inrush current or preferably to replace the existing motor with a DC motor and controller.  A DC motor has the added benefit of now allowing true speed control.

 

 

No attempt is being made to modify the system until after the shutdown.  All trolley operators are being instructed to not use this method to attempt to control positioning of the trolley.  It is unlikely that it would help in positioning even if the system could handle the current overload.

Entry  Monday, February 19, 2018, 12:58, maicodallavalle, Trolley, Repair, Lift Trolley Repair 

We had just finished pulling out the ladders from the cyclotron with the lift trolley. We started to run the lift trolley into the cyclotron when it stopped moving. The radial drive gearbox was the problem. We pulled the gearbox off. Replaced  the key and the lift trolley is all repaired.

Entry  Wednesday, September 04, 2019, 15:29, Adam Newsome, Trolley, Maintenance, Connector faceplate and tubing upgrade 

Tool Trolley:

The connector faceplate was replaced with a new version to allow for more space for service, and consolidate video lines into a single 9-pin CPC connector. A model and drawing were created and are part of the overall tool trolley assembly (to be added to PDM later): TRH1394

Air tubing that previously ran to the connector faceplate on the tool trolley was replaced as it was very old. New tubing is in 3 different colours for easy identification: blue, black, green.

Fittings were replaced with more modern push-connect style (1/4" tube).

Entry  Wednesday, February 05, 2020, 15:04, Adam Newsome, Trolley, Repair, Upper resonator trolley: cylinders for Ex 2C tasks 
Cylinder 4 on the upper resonator trolley was not fully functional when removing Ex 2C during 2020 shutdown. It worked occasionally. Upon inspection it was determined that it was binding when extend was attempted. This cylinder was replaced Feb 5, 2020 (model: American Cylinder 562SVS-2.00).
The other three cylinders were inspected and all of their shafts appear significantly bent. Replacement cylinders will be ordered and these will be replaced to prevent further issues.
Edit: all cylinders have been replaced as of Oct 8, 2020

Note: the solenoid valves that control these cylinders are quite dated and are leaky. The layout, plumbing, and wiring could also be improved. One of the cylinders' default position is extended which suggests a wiring/plumbing issue. I will look into replacing these as well, and creating pneumatic circuit documentation.

This e-log will be updated when replacement is completed.
Entry  Saturday, April 04, 2020, 10:03, Dan McDonald, Trolley, Development, Addition of DC motor controller mounts 

Upper and lower resonator trolleys received mounting plates and brackets to accommodate DC motor controls for updated drive motors.

Entry  Monday, March 21, 2022, 13:14, Adam Newsome, Trolley, Repair, Video Trolley Mk 1 - Radial Limit Switch Replacement 

An issue was observed in which radial motion on the Video Trolley Mk 1 did not respond to commands. After troubleshooting, it was determined that this was due to the "OP LIMIT" interlock - the "OP LIMIT" pushbutton on the console was illuminated in red, and needed to be continuously held down in order to operate the radial in/out motion buttons.

 

It was determined that the root cause of the issue was a failed radial limit switch which was likely damaged during trolley transport. The limit switch was replaced, and functionality was restored.

Entry  Wednesday, May 04, 2022, 12:07, Adam Newsome, Trolley, Development, Tool Trolley: Brass air fittings replacement complete 

All of the old brass air fittings on the Tool Trolley have now been swapped over to push-connect style fittings. As these are plastic fittings, it is recommended to inspect them after ~5 years for degradation.

Entry  Thursday, August 03, 2023, 10:43, Adam Newsome, Trolley, Development, Previous generation video trolley decommissioned 

The "old" video trolley featuring scissor mechanism and DSLR camera has officially been decommissioned. Going forward, Video Trolley Mk 2 (TRH1089D) will be used.

Entry  Thursday, September 14, 2023, 13:51, Adam Newsome, Trolley, Maintenance, Lift Trolley: upgrades to camera tilt mechanism PXL_20230914_193143524.jpg

The two camera tilt mechanisms on the lift trolley have been upgraded. Upgrades include:

For the individual camera:

  • Replaced cylinder
  • Replaced fittings for cylinder
  • Replaced air tubing from flow control to cylinder
  • Visual inspection and fasteners tightened

For the overall platform containing the camera and lighting:

  • Replaced cylinder
  • Replaced fittings for cylinder
  • Replaced valve (5/3 centre closed style)
  • Replaced air regulator and set pressure (note: at the time of writing this e-log, it still needs to be fastened in place via its mounting bracket)
  • Replaced air tubing
  • Visual inspection and fasteners tightened

 

Entry  Friday, September 15, 2023, 10:15, Adam Newsome, Trolley, Maintenance, Lift Trolley: mirror actuation mechanism repair/upgrade PXL_20230915_164811247.jpg

The mirror actuation mechanism was observed to be "sticky" during 2023 winter shutdown - it occasionally did not function properly and needed some manual assistance. 

The following items were addressed to resolve the issue: 

  • Replacement of the Tyne Myte double acting valve which controls the cylinder (based on troubleshooting tests, it seemed this valve was not functional or intermittently functional)
  • Addition of a silencer and in-line flow control on the exhaust of the aforementioned valve - adjusted to allow for smooth operation of the mirror when toggled
  • Cleaning of the cylinder's shaft (it had a sticky residue build-up and was notably high friction) - this cylinder should likely be replaced in the near future 
  • Replacement of air tubing along the supply line to the valve, and between the valve and cylinder
  • Replacement of all fittings (push-connect style) on the valve and cylinders

The mirror actuation was tested after these changes and is behaving normally.

No further repairs required, although it is suggested to change the remainder of the tubing and fittings for the other valves which control different functions on this trolley, and to eventually upgrade the valves themselves to a low profile valve bank. 

 
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