Logbooks Lab Maintenance Evaporator_1 Evaporator_2 Laser cutter Target Production Test-Stand RH-ISAC RH-Cyclotron RH-Meson Hall RH-Beamlines RH-ARIEL
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Entry  Monday, January 25, 2016, 13:20, Allon Messenberg, T-Hall Crane, Maintenance, Possible oil leak 20160122_161849.jpg20160122_161830.jpg20160125_100929.jpg

Two small (approx. 5 cm across) puddles of green fluid were discovered on the floor, directly below the crane trolley.  The hook block was lowered and inspected.  No fluid found on hook block.
The plant group (Neil Wong) was notified and asked to schedule an inspection when the maintenance crew is on site to inspect the ISAC target hall crane.

The crane bridge and trolley were moved to another position on Friday evening and parked over the weekend.  The floor directly below the crane trolley was inspected on Monday morning.  Three very small (1-3cm diameter) puddles of green fluid were found.

Entry  Wednesday, February 15, 2017, 11:57, chad fisher, T-Hall Crane, Development, Jason's Remote Crane Test Boxes 

On Tuesday, February 14th I finished modifying Jason's boxes for the remote crane tests by adding shelves to mount cameras... Apart from given the edges a quick sanding (so no one gets slivers)...which I will try and do tomorrow.

Entry  Friday, March 31, 2017, 19:39, Jason Kapalka, T-Hall Crane, Development, ARIEL Target Hall overhead crane faults (Test Mode) history_201703311454.csvDataLogging_201703311520_Table.csvphoto_1.JPGphoto_2.JPG
On March 29, 2017, a 9 tonne steel shield block was transferred from the ARIEL Target Pit and placed into a 
wood container on the Target Hall B1 level with the overhead crane main hoist in Local Mode without incident. 
Afterwards, the overhead crane was switched into Test Mode (which is the same as Remote Mode but without the 
Target Hall interlocked) and an attempt was made to transfer the shield block from the wood container on the B1 
level to a wood container in the Target Pit remotely with the main hoist. At 11:51:09, after lifting the shield 
block ~1 m above the B1 level, a "136. Main Hoist West Drum South Motor Drive Fault (900 VFD)" alarm pop-up was 
shown on the overhead crane HMI in the crane control room which disabled the controls on the remote console. 
The reset button on the remote console was pressed and the remote lifting operation was resumed briefly until 
the same fault occurred at 11:51:42 and the reset button was pushed once again. While attempting to lower the 
shield block back down to the ground this fault-reset sequence reoccurred at 11:57:25, 11:58:16, 11:58:28, 
11:58:43, 11:59:27, and 12:00:27, at which point the remote crane operation was aborted and the shield block 
was lowered down to the Target Pit floor with the main hoist in Local Mode, without incident. The Test Mode 
faults did not appear to depend upon the speed/acceleration of the lift, nor did they appear to be spaced apart 
by a fixed time interval. Upon closer inspection of the alarm history screen in the HMI (shown below) and the 
exported alarm log (attached below), almost every time the fault #136 occurred, the following three additional 
faults were logged simultaneously in the alarm history (but were not displayed as a pop-up on the main HMI 
screen):
"103. Main Hoist East Drum North Motor Drive Fault (700 VFD)" 
"104. Main Hoist East Drum South Motor Drive Fault (800 VFD)" 
"135. Main Hoist West Drum North Motor Drive Fault (1000 VFD)" 

On March 31, 2017, the overhead crane main hoist was operated once again in Test Mode; however, no load was 
connected to the hook block to determine if the faults that occurred two days earlier could depend on the load. 
The main hoist hook block was remotely lowered ~3 m below the upper 'home' position, and then remotely raised 
as high as possible to function test the upper limit switch in remote mode; at 14:21:05 immediately after 
initiating the 'hoist up' motion, the same four faults occurred simultaneously. This incident shows that these 
specific faults do not depend on what load is connected to the hook block. Note: the crane position data from 
March 31 is attached below, however the times shown are 1 hour fast due a DST adjustment error.

Follow up with the crane supplier, COH, is required to obtain a index and troubleshooting guide for these (and 
all other) fault codes.

2017-04-06 update: Sylvain Raymond of COH has been assigned to resolve these crane faults by Maxime Dubé-Blanchet 
of COH.
Entry  Wednesday, April 12, 2017, 10:52, Jason Kapalka, T-Hall Crane, Repair, ARIEL Target Hall crane oil leaks & inspection plan IMG_3111.JPGIMG_3112.JPGIMG_3113.JPGIMG_3114.JPGIMG_3115.JPG
On March 29, 2017, a 9 tonne load was transferred in the ARIEL Target Hall with the overhead crane (TRIUMF crane #44). On April 3, 2017, several drops of green oil were observed on the floor and hookblock directly beneath the single equalizing sheave. The Remote Handling department millwrights were notified and an inspection of the crane using a man-lift was performed to verify the source of the oil leak. Upon inspection, it was confirmed that the green oil leak was coming from the bearing on the single balancing sheave. This sheave wheel is rarely moved since it's primary purpose is to equalize the wire rope between the hook block and the two hoists; however both hoists have remained relatively synchronized since the crane installation in the summer of 2015. The millwrights suspect that the grease inside the sheave bearing has separated due to inactivity and the low viscosity fluid slowly weeps out. The leak rate was estimated at less than one oil drop per day. During the inspection to find the source of the green oil leak, black oil was observed on top of both crane bridge girders. The apparent source of the black oil is the redundancy (aka failed drive bypass) system gearbox on the north and south side of the trolley. This black oil leak was significantly larger than green oil leak, and the question was raised about whether it was noticed during the annual inspection of the crane. Upon review, it was discovered that this crane was not yet added to the list of TRIUMF cranes that are inspected annually (typically performed during January-March), presumably due to its infrequent use. A request was made and this crane was added to the inspection list. Both leaks will be investigated further when the crane receives its annual inspection in April or May (which will be conducted by a third party service company) and the findings and recommended actions will be documented in this E-Log entry.
Entry  Tuesday, April 18, 2017, 19:28, Jason Kapalka, T-Hall Crane, Development, ATH overhead crane fault investigation 8x
On April 18, 2017, an investigation was initiated to determine the cause of the ARIEL Target Hall overhead crane faults that occurred while attempting to perform remote lifting operations in Test Mode on a 8.6 tonne SEG block (see E-Log #30). Hugo Lapointe (Automation Technician, REEL-COH) requested pictures of the HIM (Human Interface Module) displays, located inside the electrical panels in the crane control room, immediately after a fault to assist with the troubleshooting process.

An unsuccessful attempt was made to trigger a fault in Test Mode with no load on the hook block. A 8.6 tonne load was then attached to the hook block and three separate fault incidents were quickly triggered, which are summarized below:

2017-04-18 2:12:57 PM 103. Main Hoist East Drum North Motor Drive Fault (700VFD) Fault Code: 211 Fault Description: Safety Brd Fault
2017-04-18 2:13:00 PM 104. Main Hoist East Drum South Motor Drive Fault (800VFD) Fault Code: 4 Fault Description: UnderVoltage
2017-04-18 2:13:00 PM 136. Main Hoist West Drum South Motor Drive Fault (900VFD) Fault Code: 4 Fault Description: UnderVoltage
2017-04-18 2:13:01 PM 135. Main Hoist West Drum North Motor Drive Fault (1000VFD) Fault Code: 4 Fault Description: UnderVoltage

2017-04-18 2:19:57 PM 136. Main Hoist West Drum South Motor Drive Fault (900VFD) Fault Code: 211 Fault Description: Safety Brd Fault
2017-04-18 2:20:00 PM 103. Main Hoist East Drum North Motor Drive Fault (700VFD) Fault Code: 4 Fault Description: UnderVoltage
2017-04-18 2:20:00 PM 104. Main Hoist East Drum South Motor Drive Fault (800VFD) Fault Code: 4 Fault Description: UnderVoltage
2017-04-18 2:20:00 PM 135. Main Hoist West Drum North Motor Drive Fault (1000VFD) Fault Code: 4 Fault Description: UnderVoltage

2017-04-18 2:23:07 PM 136. Main Hoist West Drum South Motor Drive Fault (900VFD) Fault Code: 211 Fault Description: Safety Brd Fault
2017-04-18 2:23:10 PM 103. Main Hoist East Drum North Motor Drive Fault (700VFD) Fault Code: 4 Fault Description: UnderVoltage
2017-04-18 2:23:10 PM 104. Main Hoist East Drum South Motor Drive Fault (800VFD) Fault Code: 4 Fault Description: UnderVoltage
2017-04-18 2:23:10 PM 135. Main Hoist West Drum North Motor Drive Fault (1000VFD) Fault Code: 4 Fault Description: UnderVoltage

It appears as though one motor causes the initial fault (Safety Brd Fault) and then the other three motors react to a safety trip fault (UnderVoltage). Upon further review of all the fault incidents from March and April it was observed that:
- 136. Main Hoist West Drum South Motor Drive Fault (900VFD) caused the initial “Safety Brd Fault” on 8 of 10 fault incidents
- 103. Main Hoist East Drum North Motor Drive Fault (700VFD) caused the initial “Safety Brd Fault” on 2 of 10 fault incidents

Pictures showing the 700, 800, 900, and 1000VFD HIM displays in FAULTED and normal mode were send to Hugo (COH) for review and are attached below.
Entry  Tuesday, May 16, 2017, 17:30, Jason Kapalka, T-Hall Crane, Development, ARIEL Target Hall Overhead Crane Measurements ARIEL_Target_Hall_Overhead_Crane_Measurements_(20170505).pdfEmail_-_Michael_Vogel_-_ARIEL_B1_&_Target_Pit_floor_heights_(20170519).pdf
On May 5, 2017 the Beamlines and Remote Handling groups recorded distances in the ARIEL Target Hall from the Target Pit floor and B1 Target Hall floor elevations up to the overhead crane girders and main hoist rotation plate using a laser measurement device (see attached file). On May 19, 2017, the Beamlines Group measured the B1 and Target Pit floor elevations relative to the Cyclotron centre (see attached file).
Entry  Monday, July 17, 2017, 15:32, Jason Kapalka, T-Hall Crane, Repair, Target Hall Crane modifications and repairs 
 
Entry  Friday, December 22, 2017, 12:42, Jason Kapalka, T-Hall Crane, Standard Operation, Powered down ARIEL Target Hall Crane 

 Powered down ARIEL Target Hall Crane today by switching off main power switch on B1 level in preparation for site-wide BC Hydro power outage on Dec. 27-29.

Entry  Tuesday, August 13, 2019, 11:43, Jason Kapalka, T-Hall Crane, Development, Installed surge protector 908355.pdf
Background: On 2019-06-25 a Pri VelFdbk Loss fault was discovered on the Main Hoist East Drum South Motor of the ARIEL Target Hall Crane. The crane was used previously on 2018-08-22 without incident. The main hoist of the crane was unavailable until the Hugo Lapointe (Automation Technician) from the crane manufacturer (REEL-COH) replaced the Allen-Bradley 20-750-ENC-1 Incremental Encoder board in the 800VFD with a new one, and replaced the Motrona cross switcher and splitter with a terminal block on 2018-08-22. The cause of the damage to the board and splitter could not be determined. Hugo Lapointe recommended that a DEHNguard DG MU 3PD 480 3W+G R (908355) pluggable surge arrester be installed in order to protect the system from voltage surges, which may of been the cause of the fault on 2019-06-25. Datasheet for surge arrester is attached. Sylvain Raymond said that the device should be installed downstream of the motor disconnect switch and fuse in the electrical enclosure.

Date: 2019-08-09

Participants:
- Jason Kapalka (mechanical engineer)
- Marshal Faragher (electrician)

Operation:
- Locked and tagged out 480 V Target Hall Crane breaker on panel P-703 in ARIEL Penthouse
- Verified that ARIEL Target Hall Crane has powered down
- Locked and tagged out 480 V Target Hall disconnect switch
- Locked and tagged out 480 V motor disconnect switch on PR electrical enclosure in ARIEL Crane Control Room
- Opened PR electrical enclosure in ARIEL Crane Control Room
- Verified that 480 V power supply wires were de-energized
- Installed DEHNguard DG MU 3PD 480 3W+G R (908355) pluggable surge arrester according to crane manufacturers (REEL-COH) recommendations
- Closed PR electrical enclosure in ARIEL Crane Control Room
- Removed lock and tag from 480 V motor disconnect switch in ARIEL Crane Control Room
- Removed lock and tag from 480 V Target Hall disconnect switch
- Removed lock and tag from 480 V Target Hall Crane breaker on P-703 breaker panel in ARIEL Penthouse and closed the breaker
- Closed the motor disconnect switch on PR electrical enclosure and waited 1-2 minutes until the ARIEL Target Hall Crane had completely powered up
- Function tested ARIEL Target Hall Crane: all movements functioned as expected
Entry  Tuesday, November 19, 2019, 10:31, Adam Newsome, T-Hall Crane, Repair, 900VFD Encoder Board Replacement IMG_20191106_140016.jpgIMG_20191106_153311.jpgIMG_20191112_114042.jpgHoist_Sync_3.jpgHoist_Sync_5.jpg
An issue arose in which the ARIEL crane hoist could not be moved. It was determined that the East and West drums were out of synchronization (by more than 0.2 m, which the limit) and the encoder board inside the 900VFD had failed.

Summary: The synchronization and encoder board issues were resolved, and the crane is now functional. The root cause of both of these issues is unknown.

The following is a timeline of events for record, in case a similar issue arises again:

Nov 6:

- Crane hoist not working
- Contact was made to COH to initiate troubleshooting
- Faults were observed: Drive fault for 700VFD, Drive fault for 900VFD and 900VFD not ready, Main Hoist Drum East and West Absolute Encoders Position Difference
- Logging in to the HMI as a maintenance user and viewing hoist feedback showed that: East drum absolute and incremental encoders agree with each other, West drum absolute and incremental encoders agree with each other, West drum and East drum encoder values do NOT agree with each other (approx 0.22 m difference, the threshold for faulting is 0.2 m)


Nov 12:

- Crane hoist mode was switched to operate only the East drum independently, and adjust it so that the encoder readout on the HMI of the difference between East and West drums was approximately 0... the red X indicators changed to a green checkmark, and the encoder difference fault was eliminated
- An attempt was made to operate both drums simultaneously again, but the drive faults persisted... contact was made to COH for further troubleshooting
- Hugo from COH suggested moving the encoder board within the VFD from 900VFD to 700VFD, to see if the "drive not ready" fault followed the board, to narrow down the issue. This swap was made, and it was determined that the issue was in fact due to a faulty encoder board. The VFD itself displayed fault code 4030 (Enc 1 open wire). A replacement as well as a spare were ordered (Allen Bradley 20-750-DENC-1).


Nov 18:

- The encoder board within 700VFD was replaced with a new one (this is the one that was previously in 900VFD)
- The fault messages were eliminated, and both drums could be run independently and simultaneously


Nov 19:

- Thomas Kauss, Travis Cave, and Adam Newsome tested the crane to verify functionality and check for synchronization of drums
- The drums are synchronized, as described in the operator's manual (visual verification of tick marks on hoists, 17 turns of rope when at upper limit)
- The crane was run to its upper limit and down a few times, and the hoists were observed: nothing out of the ordinary was noted
Entry  Thursday, February 13, 2020, 08:51, Adam Newsome, T-Hall Crane, Standard Operation, Remote mode door limit switch bypass 

The non-existent safety limit switch for the target hall door which prevents remote motion has been bypassed in the crane PLC control panel to allow for remote operation of the crane. This will be un-bypassed when a switch is installed. Specifically, a jumper was placed from terminal 18001 to 20121 and 20141 which will enable the hall lock safety relays 2012SR and 2014SR. The crane is currently operational in both local and remote mode.

Entry  Friday, July 03, 2020, 15:43, Adam Newsome, T-Hall Crane, Repair, North Aux Hoist: West Travel Motion Failure IMG_20200703_150700.jpg

An issue was observed in which the North Aux hoist failed to travel West when commanded to, but the East motion was functioning. The North Aux hoist Trolley was stuck in a position up against the East wall.

Present during troubleshooting: Adam N, Maico D, Tom K, Allon M, Travis C

After troubleshooting, it was determined that:

  • There were no fault messages on the HMI display relating to this issue
  • The HMI indicated "Bridge Not in North Limit and/or Auxiliary Trolley North Not in East or West Limit" - the Bridge was not in the north limit as described, and this message implies the PLC thought the North Aux hoist was somewhere along the middle of its travel
  • The West run signal was reaching the remote receiver from the crane pendant
  • The West and East run signals were correctly reaching their respective input pins on the VFD (DI1, DI2)... upon swapping wires and commanding it to run East, the West direction still did not function
  • The VFD was displaying the correct output frequency information on its display when commanded to run East, but not west
  • The limit switch was not related to this issue

Upon swapping out the VFD with the working one from the South Aux hoist, the North Aux hoist Trolley was able to move both East and West, as normal. It was therefore determined that the VFD had failed and must be replaced.

 

Current state of system as of July 3, 2020:

  • The North Aux hoist is fully functioning (contains VFD from South one)
  • The South Aux hoist is disabled (no VFD, breakers shut off)
  • The North Aux hoist limit switch flag has been temporarily bypassed to allow for crane work in the target hall (not a safety issue - extended bumpers are installed and the regular bridge limit switches are functioning normally... this is only to allow the bridge to run its full length of travel when the North Aux hoist is at its fully East position)

 

Next steps:

  • Adam Newsome requested quote for replacement drive (Delta Electronics TDN007E1100WM0) - will advise when replacement arrives
  • Install replacement drive into South Aux hoist upon arrival (note: check EMC level modification)
  • Verify entire system functioning as normal
  • Reinstall North Aux hoist limit switch flag

 

Entry  Wednesday, September 09, 2020, 10:51, Adam Newsome, T-Hall Crane, Repair, North Aux Hoist Replacement (followup on E-Log 44) 

See E-Log 44 for details on North Aux Hoist failure.

A replacement VFD was ordered by Adam Newsome and installed by Tom Kauss.

Adam and Tom replaced the VFD in the South Aux hoist (which had been relocated to the North Aux hoist). The original braking resistor was used. No functionality changes to the system.

Both Aux hoists were tested: E/W travel, up/down travel. Each hoist is functioning correctly. E/W speeds were compared between the two hoists and found to be the same (~14 Hz for slow speed, ~95 Hz for fast speed).

The replacement job is complete and the issue outlined in E-Log 44 is resolved, although the original cause for failure has not been determined.

Current state of system as of Sept 9, 2020:

  • The North Aux hoist is fully functioning (contains original VFD from South one)
  • The South Aux hoist is fully functioning (contains newly replaced VFD with original braking resistor)
  • The North Aux hoist limit switch flag has been temporarily bypassed to allow for crane work in the target hall (not a safety issue - extended bumpers are installed and the regular bridge limit switches are functioning normally... this is only to allow the bridge to run its full length of travel when the North Aux hoist is at its fully East position)

Next steps:

  • Reinstall North Aux hoist limit switch flag (TBD when Target Hall installation work is done)
Entry  Wednesday, September 15, 2021, 15:10, Adam Newsome, T-Hall Crane, Maintenance, Hoist Broken Fault (actually: cable wrap issue) 

A fault occurred which presented as "114. Main Hoist Cable Broken (3200PX)". This occurred when a SEG block was suspended approximately 1 m off the ground.

Upon inspection, it was determined that the cable was in fact not broken, but wrapped around itself. There are no guides, and it is possible for the cable to double wrap if loaded in an usual fashion. This condition triggered the "Hoist Rocker Switch 1" sensor, 3200PX. The sensor is not visible or accessible from ground level, and could not be inspected, but it was confirmed that there was no 24 VDC PLC input at 30000EA:I.Data[7].0, as would be expected under normal operating conditions.

To rectify the issue:

  • The sensor was bypassed in the control panel by connecting wire 32001 directly to 24 VDC after confirming that there would be no adverse affects from doing this.
  • With careful supervision, the load was lowered, while watching the cabling.
  • The load was removed from the crane.
  • The hoist was then lowered to its extreme lower limit, and the cable unwrapped itself naturally as it was being lowered.
  • The sensor bypass was removed.
  • The sensor began functioning normally again when the wrapping issue was resolved.
  • The hoist was raised and lowered multiple times to confirm the cable wrapping issue was no longer present.

The crane is returned to its normally functioning state. Operators will keep a lookout for any more issues relating to the hoist cable. The crane will be inspected on Sept. 22, 2021.

Entry  Thursday, September 16, 2021, 09:37, Adam Newsome, T-Hall Crane, Maintenance, Bridge Encoder Homing PXL_20210916_161245978.jpgPXL_20210916_161205277.jpg

The bridge motion was slowed due to encoder homing issue. It is likely that the problem which occurred yesterday caused an velocity fault (mismatch between encoder speed and commanded speed), which unlatches the homing status for the bridge motion axis.

When the bridge was in the southmost position (bumper pressed against wall), the position readback was: 0.353 m, encoder count = 5164003.

The bridge was moved to the "zero position" as indicated on the remote display - the tick was aligned with the zero.

The encoder was homed at this position. The home position readback was: 0.356 m, encoder count = 5164447. Note that this position is in alignment with the measuring tape zero mark, not pressed up against the wall.

 

The bridge was run to its full extreme positions in either direction to confirm proper slowdown and stopping behaviour. It appears to be functioning normally again.

Entry  Tuesday, November 23, 2021, 11:01, Adam Newsome, T-Hall Crane, Repair, Load Cell - Not Functioning 

The load cell which is located on the crane itself to display the load to operators was reported not working during the week of November 15. It is planned to investigate on Nov. 25 and this e-log will be updated with the status.

 

Edit (2022-02-02): the load cell is functioning again. No changes were made.

Entry  Thursday, January 06, 2022, 10:46, Adam Newsome, T-Hall Crane, Development, Modification of South Limits Untitled_picture.png

Edit: as of May 30, 2022, the modification has been reversed, and the crane is functioning normally as per the manufacturer's limits. 

 

Modifications have been made to the crane to allow for the South Aux Hoist to reach closer to the South wall during the ARIEL Hot Cell installation period. These modifications are temporary, and were considered to be a safer and simpler alternative to the modification proposed by the hot cell contractor workers, which involved installing a sort of come-along on the wall and pulling the hoist closer to obtain the desired reach. The following modifications were made:

  1. Removal of the bumpers on the south side (T. Kauss). There are no bumpers on the South side of the crane’s bridge currently.
  1. Modification of the PLC program to reduce the software limit by approximately 4 inches (A. Newsome). The previous soft limit was set at 0.36 m and it was reduced to 0.26 m (~3.9 inch reduction).

 

 These changes have been tested – the crane stops in the expected position. However, it is very close to the wall now. If you are using the crane anywhere near the South wall: exercise extreme caution. The crane automatically slows down when approaching the South wall, and there is plenty of time for the operator to react and further slow the motion by only holding the joystick down at about 20% speed. I strongly recommend operating at about 20% speed when close to the wall (on top of the automatic speed reduction I mentioned).  

  • These changes are based on Work Permit A2022-01-06-1
  • Changes have been noted in the crane’s logbook

See attached screenshot of PLC program indicating that the new limit has been reached.

Contact me (Adam Newsome) for more detailed information.

Entry  Tuesday, February 01, 2022, 08:29, Adam Newsome, T-Hall Crane, Repair, North Aux Hoist - West Motion Failure 

An issue was observed in which the North Aux hoist failed to travel West when commanded to, but the East motion was functioning. The up/down motion was also functioning. The North Aux Hoist Trolley failed during regular usage, seemingly randomly, when it was about 70% towards the West end of travel. Note that the West motion VFD inside the North Aux Hoist is the one previously taken from the South Aux Hoist (the same issue with the North Aux Hoist was observed last year, and the VFD was swapped, and a new one was installed in the South Aux Hoist).

 

A replacement VFD (Delta TDN007E1100WM0) will be ordered and installed, and this e-log will be updated.

Edit 2022-03-15: the replacement VFD has been installed and the system is operational. See e-log 52.

Entry  Friday, February 18, 2022, 09:26, Adam Newsome, T-Hall Crane, Maintenance, Potential grease leak observed MicrosoftTeams-image_(9).png

Naimat Khan noticed after using the crane that some grease dropped onto a spreader bar, and believes it is a leak from the main hoist (see attached photo). The hoist should be inspected.

 

Edit: Dan McDonald notes that this has been observed since the crane was installed and is likely due to excess grease dropping out. Perhaps not a major concern.

Entry  Tuesday, March 15, 2022, 10:03, Adam Newsome, T-Hall Crane, Repair, North Aux Hoist VFD Replaced 

The North Aux Hoist VFD which had failed (e-log 50) was replaced today by Tom Kauss and Adam Newsome on Work Permit A2022-03-15-1.

The hoist's motions were all tested - it is functioning normally again.

ELOG V2.9.2-2455