Logbooks Lab Maintenance Evaporator_1 Evaporator_2 Laser cutter Target Production Test-Stand RH-ISAC RH-Cyclotron RH-Meson Hall RH-Beamlines RH-ARIEL
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Entry  Wednesday, February 15, 2017, 11:57, chad fisher, T-Hall Crane, Development, Jason's Remote Crane Test Boxes 

On Tuesday, February 14th I finished modifying Jason's boxes for the remote crane tests by adding shelves to mount cameras... Apart from given the edges a quick sanding (so no one gets slivers)...which I will try and do tomorrow.

Entry  Wednesday, August 02, 2023, 09:13, chad fisher, Hot Cell 1, Repair, Leak Rate Testing 

On August 1, 2023 HC1 was pumped down to -1200 Pa (gauge) and then valved off to test the leak rate after turntables had been sealed with backer rod in the gaps.

The sealing with backer rod allowed the cell to reach the test pressure of 1000 Pa. The cell pressure equalized within 30-40 seconds which is an improvement but still not sufficient to meet the goals we have set.

Next step is to pump down to -500 Pa and use smoke generator and perform thorough investigation to identify any leaks.

Entry  Tuesday, November 04, 2014, 16:58, John Wong, 100KW Beam Dump, Maintenance, Testing Elog 

Tuesday, November 04, 2014, 16:58

This is a test.


 

Entry  Friday, March 31, 2017, 19:39, Jason Kapalka, T-Hall Crane, Development, ARIEL Target Hall overhead crane faults (Test Mode) history_201703311454.csvDataLogging_201703311520_Table.csvphoto_1.JPGphoto_2.JPG
On March 29, 2017, a 9 tonne steel shield block was transferred from the ARIEL Target Pit and placed into a 
wood container on the Target Hall B1 level with the overhead crane main hoist in Local Mode without incident. 
Afterwards, the overhead crane was switched into Test Mode (which is the same as Remote Mode but without the 
Target Hall interlocked) and an attempt was made to transfer the shield block from the wood container on the B1 
level to a wood container in the Target Pit remotely with the main hoist. At 11:51:09, after lifting the shield 
block ~1 m above the B1 level, a "136. Main Hoist West Drum South Motor Drive Fault (900 VFD)" alarm pop-up was 
shown on the overhead crane HMI in the crane control room which disabled the controls on the remote console. 
The reset button on the remote console was pressed and the remote lifting operation was resumed briefly until 
the same fault occurred at 11:51:42 and the reset button was pushed once again. While attempting to lower the 
shield block back down to the ground this fault-reset sequence reoccurred at 11:57:25, 11:58:16, 11:58:28, 
11:58:43, 11:59:27, and 12:00:27, at which point the remote crane operation was aborted and the shield block 
was lowered down to the Target Pit floor with the main hoist in Local Mode, without incident. The Test Mode 
faults did not appear to depend upon the speed/acceleration of the lift, nor did they appear to be spaced apart 
by a fixed time interval. Upon closer inspection of the alarm history screen in the HMI (shown below) and the 
exported alarm log (attached below), almost every time the fault #136 occurred, the following three additional 
faults were logged simultaneously in the alarm history (but were not displayed as a pop-up on the main HMI 
screen):
"103. Main Hoist East Drum North Motor Drive Fault (700 VFD)" 
"104. Main Hoist East Drum South Motor Drive Fault (800 VFD)" 
"135. Main Hoist West Drum North Motor Drive Fault (1000 VFD)" 

On March 31, 2017, the overhead crane main hoist was operated once again in Test Mode; however, no load was 
connected to the hook block to determine if the faults that occurred two days earlier could depend on the load. 
The main hoist hook block was remotely lowered ~3 m below the upper 'home' position, and then remotely raised 
as high as possible to function test the upper limit switch in remote mode; at 14:21:05 immediately after 
initiating the 'hoist up' motion, the same four faults occurred simultaneously. This incident shows that these 
specific faults do not depend on what load is connected to the hook block. Note: the crane position data from 
March 31 is attached below, however the times shown are 1 hour fast due a DST adjustment error.

Follow up with the crane supplier, COH, is required to obtain a index and troubleshooting guide for these (and 
all other) fault codes.

2017-04-06 update: Sylvain Raymond of COH has been assigned to resolve these crane faults by Maxime Dubé-Blanchet 
of COH.
Entry  Wednesday, April 12, 2017, 10:52, Jason Kapalka, T-Hall Crane, Repair, ARIEL Target Hall crane oil leaks & inspection plan IMG_3111.JPGIMG_3112.JPGIMG_3113.JPGIMG_3114.JPGIMG_3115.JPG
On March 29, 2017, a 9 tonne load was transferred in the ARIEL Target Hall with the overhead crane (TRIUMF crane #44). On April 3, 2017, several drops of green oil were observed on the floor and hookblock directly beneath the single equalizing sheave. The Remote Handling department millwrights were notified and an inspection of the crane using a man-lift was performed to verify the source of the oil leak. Upon inspection, it was confirmed that the green oil leak was coming from the bearing on the single balancing sheave. This sheave wheel is rarely moved since it's primary purpose is to equalize the wire rope between the hook block and the two hoists; however both hoists have remained relatively synchronized since the crane installation in the summer of 2015. The millwrights suspect that the grease inside the sheave bearing has separated due to inactivity and the low viscosity fluid slowly weeps out. The leak rate was estimated at less than one oil drop per day. During the inspection to find the source of the green oil leak, black oil was observed on top of both crane bridge girders. The apparent source of the black oil is the redundancy (aka failed drive bypass) system gearbox on the north and south side of the trolley. This black oil leak was significantly larger than green oil leak, and the question was raised about whether it was noticed during the annual inspection of the crane. Upon review, it was discovered that this crane was not yet added to the list of TRIUMF cranes that are inspected annually (typically performed during January-March), presumably due to its infrequent use. A request was made and this crane was added to the inspection list. Both leaks will be investigated further when the crane receives its annual inspection in April or May (which will be conducted by a third party service company) and the findings and recommended actions will be documented in this E-Log entry.
Entry  Tuesday, April 18, 2017, 19:28, Jason Kapalka, T-Hall Crane, Development, ATH overhead crane fault investigation 8x
On April 18, 2017, an investigation was initiated to determine the cause of the ARIEL Target Hall overhead crane faults that occurred while attempting to perform remote lifting operations in Test Mode on a 8.6 tonne SEG block (see E-Log #30). Hugo Lapointe (Automation Technician, REEL-COH) requested pictures of the HIM (Human Interface Module) displays, located inside the electrical panels in the crane control room, immediately after a fault to assist with the troubleshooting process.

An unsuccessful attempt was made to trigger a fault in Test Mode with no load on the hook block. A 8.6 tonne load was then attached to the hook block and three separate fault incidents were quickly triggered, which are summarized below:

2017-04-18 2:12:57 PM 103. Main Hoist East Drum North Motor Drive Fault (700VFD) Fault Code: 211 Fault Description: Safety Brd Fault
2017-04-18 2:13:00 PM 104. Main Hoist East Drum South Motor Drive Fault (800VFD) Fault Code: 4 Fault Description: UnderVoltage
2017-04-18 2:13:00 PM 136. Main Hoist West Drum South Motor Drive Fault (900VFD) Fault Code: 4 Fault Description: UnderVoltage
2017-04-18 2:13:01 PM 135. Main Hoist West Drum North Motor Drive Fault (1000VFD) Fault Code: 4 Fault Description: UnderVoltage

2017-04-18 2:19:57 PM 136. Main Hoist West Drum South Motor Drive Fault (900VFD) Fault Code: 211 Fault Description: Safety Brd Fault
2017-04-18 2:20:00 PM 103. Main Hoist East Drum North Motor Drive Fault (700VFD) Fault Code: 4 Fault Description: UnderVoltage
2017-04-18 2:20:00 PM 104. Main Hoist East Drum South Motor Drive Fault (800VFD) Fault Code: 4 Fault Description: UnderVoltage
2017-04-18 2:20:00 PM 135. Main Hoist West Drum North Motor Drive Fault (1000VFD) Fault Code: 4 Fault Description: UnderVoltage

2017-04-18 2:23:07 PM 136. Main Hoist West Drum South Motor Drive Fault (900VFD) Fault Code: 211 Fault Description: Safety Brd Fault
2017-04-18 2:23:10 PM 103. Main Hoist East Drum North Motor Drive Fault (700VFD) Fault Code: 4 Fault Description: UnderVoltage
2017-04-18 2:23:10 PM 104. Main Hoist East Drum South Motor Drive Fault (800VFD) Fault Code: 4 Fault Description: UnderVoltage
2017-04-18 2:23:10 PM 135. Main Hoist West Drum North Motor Drive Fault (1000VFD) Fault Code: 4 Fault Description: UnderVoltage

It appears as though one motor causes the initial fault (Safety Brd Fault) and then the other three motors react to a safety trip fault (UnderVoltage). Upon further review of all the fault incidents from March and April it was observed that:
- 136. Main Hoist West Drum South Motor Drive Fault (900VFD) caused the initial “Safety Brd Fault” on 8 of 10 fault incidents
- 103. Main Hoist East Drum North Motor Drive Fault (700VFD) caused the initial “Safety Brd Fault” on 2 of 10 fault incidents

Pictures showing the 700, 800, 900, and 1000VFD HIM displays in FAULTED and normal mode were send to Hugo (COH) for review and are attached below.
Entry  Tuesday, May 16, 2017, 17:30, Jason Kapalka, T-Hall Crane, Development, ARIEL Target Hall Overhead Crane Measurements ARIEL_Target_Hall_Overhead_Crane_Measurements_(20170505).pdfEmail_-_Michael_Vogel_-_ARIEL_B1_&_Target_Pit_floor_heights_(20170519).pdf
On May 5, 2017 the Beamlines and Remote Handling groups recorded distances in the ARIEL Target Hall from the Target Pit floor and B1 Target Hall floor elevations up to the overhead crane girders and main hoist rotation plate using a laser measurement device (see attached file). On May 19, 2017, the Beamlines Group measured the B1 and Target Pit floor elevations relative to the Cyclotron centre (see attached file).
Entry  Monday, July 17, 2017, 15:32, Jason Kapalka, T-Hall Crane, Repair, Target Hall Crane modifications and repairs 
 
Entry  Friday, December 22, 2017, 12:42, Jason Kapalka, T-Hall Crane, Standard Operation, Powered down ARIEL Target Hall Crane 

 Powered down ARIEL Target Hall Crane today by switching off main power switch on B1 level in preparation for site-wide BC Hydro power outage on Dec. 27-29.

Entry  Tuesday, August 13, 2019, 11:43, Jason Kapalka, T-Hall Crane, Development, Installed surge protector 908355.pdf
Background: On 2019-06-25 a Pri VelFdbk Loss fault was discovered on the Main Hoist East Drum South Motor of the ARIEL Target Hall Crane. The crane was used previously on 2018-08-22 without incident. The main hoist of the crane was unavailable until the Hugo Lapointe (Automation Technician) from the crane manufacturer (REEL-COH) replaced the Allen-Bradley 20-750-ENC-1 Incremental Encoder board in the 800VFD with a new one, and replaced the Motrona cross switcher and splitter with a terminal block on 2018-08-22. The cause of the damage to the board and splitter could not be determined. Hugo Lapointe recommended that a DEHNguard DG MU 3PD 480 3W+G R (908355) pluggable surge arrester be installed in order to protect the system from voltage surges, which may of been the cause of the fault on 2019-06-25. Datasheet for surge arrester is attached. Sylvain Raymond said that the device should be installed downstream of the motor disconnect switch and fuse in the electrical enclosure.

Date: 2019-08-09

Participants:
- Jason Kapalka (mechanical engineer)
- Marshal Faragher (electrician)

Operation:
- Locked and tagged out 480 V Target Hall Crane breaker on panel P-703 in ARIEL Penthouse
- Verified that ARIEL Target Hall Crane has powered down
- Locked and tagged out 480 V Target Hall disconnect switch
- Locked and tagged out 480 V motor disconnect switch on PR electrical enclosure in ARIEL Crane Control Room
- Opened PR electrical enclosure in ARIEL Crane Control Room
- Verified that 480 V power supply wires were de-energized
- Installed DEHNguard DG MU 3PD 480 3W+G R (908355) pluggable surge arrester according to crane manufacturers (REEL-COH) recommendations
- Closed PR electrical enclosure in ARIEL Crane Control Room
- Removed lock and tag from 480 V motor disconnect switch in ARIEL Crane Control Room
- Removed lock and tag from 480 V Target Hall disconnect switch
- Removed lock and tag from 480 V Target Hall Crane breaker on P-703 breaker panel in ARIEL Penthouse and closed the breaker
- Closed the motor disconnect switch on PR electrical enclosure and waited 1-2 minutes until the ARIEL Target Hall Crane had completely powered up
- Function tested ARIEL Target Hall Crane: all movements functioned as expected
Entry  Wednesday, November 19, 2014, 13:49, Isaac Earle, 100KW Beam Dump, Development, Decision on Modifications to Lower Center Block (TSH0225) 

I received a call today from Jim Adamson at Kaltech regarding modifications to shielding block TSH0225.

They had finished removing 19mm from the bottom of the block, as well as removing 10mm of material from the side plates (TSH0246).  He was wondering whether it was also necessary to remove material from the back plate (TSH0253) and weld the back plate to the 6" plate (TSH0252).  I instructed him that it is not necessary to machine and weld the back plate.  This decision is based on weld strength calculations I performed last week which showed that the existing welds are much stronger than what is required to take the load applied when lifting the block (FOS >> 10)

Entry  Friday, November 21, 2014, 13:37, Isaac Earle, 100KW Beam Dump, Development, Destructive Testing of 1" MDC Ceramic Breaks Ceramic_Water_Break_Test_#1.docxCeramic_Water_Break_Test_#2.docxTest_#1_Broken_Sample.JPGTest_#2_Broken_Sample.JPG

Testing was performed on the ceramic water breaks to be used on the beam dump water hose assemblies.  The ceramic breaks are a custom MDC product with the following description:  3kV ceramic break, 1" OD tube 0.083" wall thickness, 2" length, 304SS tube stub each end, 250psi water rating (see TRIUMF PO#  TR199315).

A load was applied perpendicular to the part, 12" away from the center of the ceramic, and increased incrementally until failure.  Two parts were tested, which failed at 125lbf and 170lbf. Equivalent to 125ft*lb and 170ft*lb when converted to torque.  Test data, photos of the failed specimens, and a more detailed description of the test setup are attached.

The purpose of the tests was to gain an understanding of how fragile the ceramic parts are.  The results show that the ceramic breaks should be able to withstand the expected loads caused by the flexible hoses being pulled as the RH water blocks are installed or removed remotely using pole tools, however this operation should still be done cautiously.  The ceramic breaks are at risk of failure if a torque of over 100ft*lb is applied, such as if someone were to stand on the ceramic breaks or the attached hose.

 

Entry  Wednesday, November 26, 2014, 17:50, Isaac Earle, 100KW Beam Dump, Development, Installation of Lower Center Block (TSH0461) Beam_Dump_Lower_Center_Block_Alignment_-_Nov_25_2014_(from_Darren_Blom).txtIMG_1110.JPGIMG_1125.JPGIMG_4297.JPGIMG_4303.JPG

Painting and relabeling of the modified lower center block (TSH0461) was completed on Monday Nov 24.  The height of the modified block was measured at the four corners using a tape measure and found to be approximately 533mm at all corners.

The block was lowered to the E-Hall and aligned on Tuesday Nov 25.   No cantilever lift was required because the catwalk above the hatch had been removed.  During the block installation one of the crane cables was contacting the concrete on the edge of hatch opening.  Future installations should use a long sling or cable to prevent this.  Photos of the installation are attached.  Beamlines Group assisted with alignment using their laser tracker.  Vertical alignment was achieved using 3x3" metal shims of various thicknesses placed at 4 corners of the block.  North-south, east-west alignment was achieved by installing based on marks drawn on the E-Hall floor by Beamlines group.  After initial placement, measurements were taken with the laser tracker, and the position was adjusted.  The nominal positions of the beam dump according to installation drawing TSH0372 are:

East Face: x=-5926.3mm from EHBT CoP
South Face:  y=2223.6mm from EHBT CoP
Top Face: z=-208.0mm from EHBT CoP

The laser tracker measurements of block position after final placement are as follows:

East Face: x = -5926.2 ~ -5926.9mm
South Face: y = 2220.9 ~ 2224.7mm
Top Face: z = -209.6 ~ 211.6mm

The East face is within 0.6mm of nominal position which is excellent (note that the east-west direction cannot be corrected using the alignment rail track).  The south face position is within 2.7mm.  This is fine because adjustment can be made to the north-south position of the rail track.  The top face of the block is a maximum of 3.6mm below the nominal position which is also fine, as the lower lead shield block can be shimmed up to it's nominal position.  Data from Beamlines Group is attached (note that 19.05mm must be added to each measurement to account for the distance from target base to center).  The location of the measurement points on the top face are as follows.

 

                 North Side
--------------------------------------------
| 6                  4                  2 |
|                                           |
| 5                  3                  1 |
--------------------------------------------
 

We will aim to have the bottom of the lower lead shield at z = -204.8mm (this leaves nominal 2mm space to be shimmed under the rail track to bring the BD flange center to beam height).  Therefore the following thickness shims should be placed on the top of the lower center block.

Position 1: 5.8mm (suggest 1/8 + 1/16 + 1/32" shim = 5.6mm)
Position 2: 5.9mm (suggest 1/8 + 1/16 + 1/32" shim = 5.6mm)
Position 3: 6.8mm
Position 4: 6.0mm
Position 5: 5.1mm (suggest 1/8 + 1/16" shim = 4.8mm)
Position 6: 4.8mm (suggest 1/8 + 1/16" shim = 4.8mm)

Position 3 and 4 do not need shims, as the outer four corners should be adequate.

Entry  Wednesday, December 03, 2014, 10:16, Isaac Earle, 100KW Beam Dump, Development, Installation of Lower Lead Block and Beam Dump Insert 

On November 28th the lower lead shield was installed with 3/8" shimming at the front end, and 11/32" shimming at the rear end.  The south and east faces were aligned as flush as possible with the lower center block.  The beam dump insert was then placed on the rails in the lower lead shield.

Laser tracker measurements were performed by Michael Vogel, and he reported that the beam dump was 1.7mm high at the rear, and 0.8mm high at the front.

The lower lead shield was lifted, and 1/32" shimming was removed from the front, and 3/32" from the rear.  The block was then placed precisely using the laser tracker with targets on the beam dump insert.

After placing the lower lead shield, Michael aligned the beam dump by shimming and adjusting the rail track, and was able to get all fiducial points within 0.2mm of the nominal position.

Entry  Wednesday, December 03, 2014, 10:36, Isaac Earle, 100KW Beam Dump, Development, Upper half of BD water blocks installed; Bypass loops installed IMG_4381.JPG

On December 2 the upper half of the RH water blocks were installed (4 total) using a 0.030" thick 6061-T6 Al shim torqued to 60ft*lbs as was tested in Document-114260.

Bypass loops for testing the cooling system piping were installed as shown in the attached photo.

 

IMG_4381.JPG

Entry  Wednesday, December 03, 2014, 10:45, Isaac Earle, 100KW Beam Dump, Development, BD Signals Traced from Service Stand to Junction Box 

On Dec 2 the cables from the BD service stand area to the junction box were traced to establish which sensors correspond to which cable number in the junction box.

 

The beam dump thermocouple probe cable numbers are as follows (as labeled on the beam dump and the TC block upper half):
TC#1: T44,  TC#2: T55,  TC#3: T11,  TC#4:  T22,  TC#5: T66,  TC#6: T77
 

The service stand water sensor cable numbers are as follows:
Inside Tray, East Side: 44
Inside Tray, West Side: 22
Under Tray, East Side: 33
Under Tray, West Side: 11

Entry  Friday, December 05, 2014, 10:43, Isaac Earle, 100KW Beam Dump, Development, Lower Lead Shield Drain Line Installed IMG_4383.JPGIMG_4384.JPGIMG_4385.JPG

A 1/8" SS tube was routed from the Swagelok fitting on the front of the lower lead shield to the service stand water catch tray as shown in the attached photos.

The tube was routed to fit in the cut-out and chamfered corner gaps of block TSH0387 in the de-rated EHDT shielding assembly TSH0293.

Entry  Tuesday, December 16, 2014, 16:36, Isaac Earle, 100KW Beam Dump, Development, Upper Pb Shield and Water Hoses Installed BD_Hose_Install_Notes.pdfIMG_4407.JPGIMG_4408.JPGIMG_4410.JPG

 The upper lead shield was installed this morning.  Also the water hoses for lower lead shield, beam dump, and upper lead shield were all installed.  See attached photos and hose installation information PDF.

Entry  Friday, December 19, 2014, 14:05, Isaac Earle, 100KW Beam Dump, Development, Beam Dump & Lead Shielding Design Documentation Cooled_Lead_Shielding_Scanned_Design_Notes_(Isaac_Earle).pdf

 As there likely won't be an opportunity to properly document the design of the beam dump insert and cooled lead shielding in design notes, a list of design reviews, released on Docushare is provided below.  These provide a reasonable overview of the design process for each item.  In addition the attached PDF of scanned notes provides detailed information on the lead shielding design.  Further notes, ANSYS documents, meeting minutes, concept reviews, etc, can be be found on Isaac Earle's hard drive.  Released drawings for each completed design are available on the PDM Works Vault.

 

DR-P0104-35 (Document-110856):   Design Review for the e-Linac 100kW Tuning Dump Pb Shielding

DR.P0104-23  (Document-104081):   E-Linac 100kW Tuning Dump Water Cooling Package Concept Design Review

DR-P0104-41:   Design Review for the Tuning Dump Local Shielding (10kW De-Rated)

DR.P0104-24 (Document-104082):   E-Linac 100kW Beam Dump Insert Design Review

DR.P0104-32  (Document-109104):   E-Linac 100kW Beam Dump Shielding Design Review

Entry  Monday, December 22, 2014, 14:21, Isaac Earle, 100KW Beam Dump, Development, Water System Leak Checked 

This morning Bill Richert pressurized the beam dump water cooling system with 30psi air and held for 2 hours.  He reported no change in pressure which indicates the flexible hose connections installed last week are leak tight.

ELOG V2.9.2-2455