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  Evaporator_2, Page 15 of 34  Not logged in ELOG logo
  ID Date Author Target Material Target Oven W.O# Source Status Subjectdown
  201   Thursday, May 28, 2015, 17:50 John WongEndcaps40282-5TARGET BOATDoneSintering TaC coating on Ta endcaps - round 2

Laura Lambert wrote:

 Thursday, May 28, 2015, 11:34

Endcaps were sintered [see elog#199]

A Ta foil is placed in the target boat with separate slots for each endcap [see image]

The target boat is wrapped with 3-layers of Ta-heat shield.

The boat is installed in EVAP2, chamber is currently being pumped down.


 Thursday, May 28, 2015, 14:01

HS water valves opened, no leaks detected.

IGP1 = 1.4e-6 Torr.

Initiating manual tap up.


 Thursday, May 28, 2015, 15:10

Manually tapped up TGHT  to 108A, 1.1V

Initiating auto-ramp at 2.0A/min with a max setpoint of 300A


 Thursday, May 28, 2015, 15:22

Hoping to speed up the process...

IGP1 = 1.0e-6 Torr.

Increasing ramping rate to 4.0A/min with a max setpoint of 500A

Final desired temperature = 1800C


 

 Thursday, May 28, 2015, 17:42

TGHT at 500A. Temp at 1780C.

Increased TGHT to 580A (online operating current),  Temp 1945C, vac 2.9e-6 torr and coming down.  Will remain at that current for the sintering process.

Cooling it down later this evening.


Thursday, May 28, 2015, 21:27  

Temp stabilized at 1960C with TGHT at 580A for almost 4 hours.  Vacuum at 1.8e-7 Torr.

Cooling down initiated at 2A/min.


 

  202   Friday, May 29, 2015, 11:18 Laura LambertEndcaps40282-5TARGET BOATDoneSintering TaC coating on Ta endcaps - round 2

John Wong wrote:

Laura Lambert wrote:

 Thursday, May 28, 2015, 11:34

Endcaps were sintered [see elog#199]

A Ta foil is placed in the target boat with separate slots for each endcap [see image]

The target boat is wrapped with 3-layers of Ta-heat shield.

The boat is installed in EVAP2, chamber is currently being pumped down.


 Thursday, May 28, 2015, 14:01

HS water valves opened, no leaks detected.

IGP1 = 1.4e-6 Torr.

Initiating manual tap up.


 Thursday, May 28, 2015, 15:10

Manually tapped up TGHT  to 108A, 1.1V

Initiating auto-ramp at 2.0A/min with a max setpoint of 300A


 Thursday, May 28, 2015, 15:22

Hoping to speed up the process...

IGP1 = 1.0e-6 Torr.

Increasing ramping rate to 4.0A/min with a max setpoint of 500A

Final desired temperature = 1800C


 

 Thursday, May 28, 2015, 17:42

TGHT at 500A. Temp at 1780C.

Increased TGHT to 580A (online operating current),  Temp 1945C, vac 2.9e-6 torr and coming down.  Will remain at that current for the sintering process.

Cooling it down later this evening.


Thursday, May 28, 2015, 21:27  

Temp stabilized at 1960C with TGHT at 580A for almost 4 hours.  Vacuum at 1.8e-7 Torr.

Cooling down initiated at 2A/min.


 

 Friday, May 29, 2015, 11:16

Vented in air and opened up this morning.

Endcaps look great!  

Sintering was spot on [see pictures]


 

Attachment 1: endcaps_-round2_sintering_(1).jpg
endcaps_-round2_sintering_(1).jpg
Attachment 2: endcaps_-round2_sintering_(2).jpg
endcaps_-round2_sintering_(2).jpg
  199   Thursday, May 28, 2015, 10:23 Laura LambertEndcaps40282-5TARGET BOATProblemsSintering TaC coating on Ta endcaps - not fully sintered

John Wong wrote:

Laura Lambert wrote:

 Tuesday, May 26, 2015, 13:06

Endcaps were sprayed with TaC coating and let dry.

Each endcap is wrapped separately with a sheet of graphite foil and stacked in the target boat [see image]

The target boat is wrapped with 3-layers of Ta-heat shield.

The boat is installed in EVAP2, chamber is currently being pumped down.


 Wednesday, May 27, 2015, 08:50

HS water valves opened, no leaks detected.

Stepped up manually to 35A.

Initiated auto-ramp at 0.2A/min yesterday afternoon.

TGHT = 254A, 3.56V.

IGP1 = 5.9e-7 Torr.

Increasing ramping rate to 1.0A/min with a max setpoint of 400A.


 

 Wednesday, May 27, 2015, 17:51

TGHT has been at 400A for almost 6 hours.  Temp at 1500C.

Cooling down to 0A at 1A/min.

Chamber will be vented to inspect the caps. 

May have to remove the graphite foil wrapped on the caps and re-sintered the caps to 1800C.


 

 Thursday, May 28, 2015, 08:13

Vented in air and opened up this morning.

Not fully sintered [see pictures]


 

Attachment 1: endcaps_-_round1_sintering_(1).jpg
endcaps_-_round1_sintering_(1).jpg
Attachment 2: endcaps_-_round1_sintering_(2).jpg
endcaps_-_round1_sintering_(2).jpg
  197   Tuesday, May 26, 2015, 13:57 Laura LambertEndcaps40282-5TARGET BOATIn progressSintering TaC coating on Ta endcaps

 Tuesday, May 26, 2015, 13:06

Endcaps were sprayed with TaC coating and let dry.

Each endcap is wrapped separately with a sheet of graphite foil and stacked in the target boat [see image]

The target boat is wrapped with 3-layers of Ta-heat shield.

The boat is installed in EVAP2, chamber is currently being pumped down.


 Wednesday, May 27, 2015, 08:50

HS water valves opened, no leaks detected.

Stepped up manually to 35A.

Initiated auto-ramp at 0.2A/min yesterday afternoon.

TGHT = 254A, 3.56V.

IGP1 = 5.9e-7 Torr.

Increasing ramping rate to 1.0A/min with a max setpoint of 400A.


 

Attachment 1: endcaps_-_may_26.jpg
endcaps_-_may_26.jpg
  198   Wednesday, May 27, 2015, 17:58 John WongEndcaps40282-5TARGET BOATIn progressSintering TaC coating on Ta endcaps

Laura Lambert wrote:

 Tuesday, May 26, 2015, 13:06

Endcaps were sprayed with TaC coating and let dry.

Each endcap is wrapped separately with a sheet of graphite foil and stacked in the target boat [see image]

The target boat is wrapped with 3-layers of Ta-heat shield.

The boat is installed in EVAP2, chamber is currently being pumped down.


 Wednesday, May 27, 2015, 08:50

HS water valves opened, no leaks detected.

Stepped up manually to 35A.

Initiated auto-ramp at 0.2A/min yesterday afternoon.

TGHT = 254A, 3.56V.

IGP1 = 5.9e-7 Torr.

Increasing ramping rate to 1.0A/min with a max setpoint of 400A.


 

 Wednesday, May 27, 2015, 17:51

TGHT has been at 400A for almost 6 hours.  Temp at 1500C.

Cooling down to 0A at 1A/min.

Chamber will be vented to inspect the caps. 

May have to remove the graphite foil wrapped on the caps and re-sintered the caps to 1800C.


 

  230   Monday, July 13, 2015, 11:54 Laura LambertEndcaps40282-5TARGET BOATProblemsSintering TaC coating on Ta endcaps

 Monday, July 13, 2015, 11:53

A Ta foil is placed in the target boat with separate slots for each endcap [same as elog 200]

The target boat is wrapped with 3-layers of Ta-heat shield.

The boat is installed in EVAP2, chamber is currently being pumped down.


 Monday, July 13, 2015, 15:00

Opened HS water valves, no leaks detected.

IGP1 = 2.7e-6 Torr.

Tapping up manually.


 Monday, July 13, 2015, 15:41

Tapped up manually to 30A

TGHT = 30A, 0.05V

IGP1 = 7e-6 Torr.

Initiating auto-ramp at 0.2A/min up to 480A with a final desired temperature of 1800C


 Tuesday, July 14, 2015, 09:12

IGP1 = 7.8e-7 Torr

TGHT = 241A, 3.3V

OMEGA = 1010C

Increasing auto-ramp to 2.0A/min


 Tuesday, July 14, 2015, 11:12

Reached final setpoint of TGHT = 480A, 8.43V

OMEGA = 1667C

IGP1 = 3.3e-6 Torr.

Tapping up manually to reach final desired temperature of 1800C.


 Tuesday, July 14, 2015, 11:33

Reached TGHT = 500A, 8.8V by tapping up manually.

OMEGA = 1714V

IGP1= 3.5e-6 Torr.

Re-initiating auto-ramp at 2.0A/min with a final setpoint of 580A.

New final desired temperature min of 1900C


 Tuesday, July 14, 2015, 13:16

TGHT = 577A, 10.74V

OMEGA = 1938C

IGP1 = 3.2e-6 Torr

Endcaps have been at this temperature for just over an hour.

Spikes in vacuum started ~430A - this is due to the green TaC coating reacting with the Ta foil, the carbide is reacting directly with the Ta foil [see picture]

Stopping sintering early before endcaps break -> initiating auto-cool at 2.0A/min.


 Wednesday, July 15, 2015, 11:33

Vented in air and took out this morning.

Endcaps sintered on top side but not fully sintered on inner edge.

Inner edge is peeling off and unsintered green TaC.

The coating peeling off did not shrink, as seen with previous tests done, one would expect a shrinkage in the coating when heated.

The peeling is most likely due to the way to endcaps were placed  in the slots of the Ta foil.

This may have cause the foil to be hotter than the inside of the endcaps and subsequently the Ta foil and TaC coating on the inside reacted - with the Ta foil extracting the carbide from the coating.

This would cause the outer edges of the inside of the endcap to peel/curl inwards as it was heated [like a cast, as the cast dries the outer edges curl inwards].

See photos attached for clarification.

Endcaps will be re-coated and sintered again via a different procedure.


 

Attachment 1: endcaps_july_14_2015.JPG
endcaps_july_14_2015.JPG
Attachment 2: IMG_20150715_102332633.jpg
IMG_20150715_102332633.jpg
Attachment 3: IMG_20150715_102240364_HDR.jpg
IMG_20150715_102240364_HDR.jpg
Attachment 4: IMG_20150715_102631676.jpg
IMG_20150715_102631676.jpg
  235   Thursday, August 06, 2015, 15:45 Laura LambertEndcaps TARGET BOATDoneSintering TaC coating on Ta endcaps

 Thursday, August 06, 2015, 15:36

The endcaps are stacked together with a punched out disc of graphite foil placed in between each endcap for separation so endcaps won't fuse together.

The end caps are further wrapped in a larger piece of graphite foil to hold together as a tube [same method used in elogID # 158]

There are two separate tubes in the target boat:

1) endcaps coated with TaC coating - never been sintered

2) previously sintered [but not fully] endcaps with a second coating done on the one side of each endcap

The boat is wrapped with 3-layers of Ta heatshields.

Chamber is currently being pumped down.


 Friday, August 07, 2015, 08:45

HS water valves opened, no leaks detected.

IGP1 = 3.6e-7 Torr.

Tapped up manually to 30A.


 Friday, August 07, 2015, 11:23

IGP1 = 2.2e-6 Torr.

Vacuum stable.

Initiating auto-ramp at 0.2A/min with a final setpoint of 480A.

Will ramp up over the weekend, confirm temperature readings on monday and tap up to final desired temperature of 1800C manually.


 Friday, August 07, 2015, 13:04

Vacuum climbed quite fast.

IGP1 = 6.3e-6 Torr.

Stopped auto-ramp to allow vacuum to settle.

Waited ~1hr.

IGP1 = 4.3e-6 Torr.

Re-initiating auto-ramp.


 Monday, August 10, 2015, 09:22

TGHT reached 480A, 8.2V on the weekend.

OMEGA = 1708C

IGP1 = 3.8e-7 Torr.

Tapped up manually to 1803C, 520A, 9.0V

IGP1 = 5.9e-7 Torr.


 Monday, August 10, 2015, 14:50

EVAP2 remained at 1800C for 4.5hours.

Internal temperature taken at new window port read 1800C using the mikron.

Initiating auto-cool at 2.0A/min.


 Tuesday, August 11, 2015, 09:23

Vented in air and opened up this morning.

The following observations were noted:

1) single round sintered endcaps:

-Batch of green endcaps, single round of sintering look good. fully sintered.

-however when applying a scratch test, excess TaC scrapes off.

[see single round sintering photos]

2) Re-sintering of batch from july 14th
-Outside of endcap [concave side] was re-coated, Inside of endcap had good first coating - therefore no second coating applied [see photos from elog ID#230]

-A few endcaps almost heated too long and started to appear brittle/ further crystallization on inside of endcap - the side that did not have a second coating applied.

-Outside of endcap looks good/ fully sintered - the side that had a second round of TaC coating

-further tests confirm this batch should still be okay to use

[see round2 batch photos]


 

 

Attachment 1: round2_july_batch_(1).jpg
round2_july_batch_(1).jpg
Attachment 2: round2_july_batch_(2).jpg
round2_july_batch_(2).jpg
Attachment 3: round2_july_batch_(3).jpg
round2_july_batch_(3).jpg
Attachment 4: single_round_sintering_(1).jpg
single_round_sintering_(1).jpg
Attachment 5: single_round_sintering_(2).jpg
single_round_sintering_(2).jpg
  260   Monday, November 09, 2015, 12:56 John Wong 41077-3LP-SISIn progressSintering TaC coating on 'temporary endcaps' springs (Slope changed to 1.04)

Laura Lambert wrote:

 Thursday, November 05, 2015, 16:19

Springs coated with TaC and loaded into container for sintering.

3x Ta heat shield.

EVAP2 currently pumping down.


 Friday, November 06, 2015, 08:39

Opened HS water valves, no leaks detected.

Tapped up manually to 35A.

IGP1 = 5.5e-7 Torr.


 Friday, November 06, 2015, 10:08

IGP1 = 5.8e-7 Torr.

Vacuum stable.

Initiating auto-ramp at 0.2A/min and 0.1A/min with final setpoints of 450A and 230A for the TGHT and TBHT respectively.

See photos attached to view how springs were coated and loaded into container.


 Monday, November 09, 2015, 09:07

TGHT reached 450A, 7.2V ~8pm sat, nov 7th.

OMEGA = 1775C

IGP1 = 3.2e-7 Torr.

Tapping up manually to 1900C.


 

 Monday, November 09, 2015, 12:30

Checked the temp on the inner surface (not at the spring) of the container was around 2050C at 500A. 

The TaC coated spring is reading at 1900C; that's what the OMEGA is reading with the setting for 2-colors and slope at 0.98.

Lower TGHT to 450A/ 7.12V.

By comparing the data from the previous temp curve (OMEGA slope at 0.98) with no material inside the container,  the voltage and current plot is aligned with the curve.

Changed OMEGA setting slope to 1.04.  Current temp is reading at 1917C at 450A.

For 2-Color setting, the emissivity should be negligible.  That makes me believe that different materials has different slope setting for the temp reading.  

One thing to note is that, the sintering temp of TaC is around 1900-2000C.  It was clear that the container was fully sintered with TGHT at 450A.

Will need to gather more data with different material to understand the slope setting better. 

Try: 

SiC at 1700C, slope at 1.04

ZrC at 1900C, slope at 104

Ta at 1900C, slope at 0.98.

Compare the data...


 

  261   Monday, November 09, 2015, 14:22 Laura Lambert 41077-3LP-SISDoneSintering TaC coating on 'temporary endcaps' springs (Slope changed to 1.04)

John Wong wrote:

Laura Lambert wrote:

 Thursday, November 05, 2015, 16:19

Springs coated with TaC and loaded into container for sintering.

3x Ta heat shield.

EVAP2 currently pumping down.


 Friday, November 06, 2015, 08:39

Opened HS water valves, no leaks detected.

Tapped up manually to 35A.

IGP1 = 5.5e-7 Torr.


 Friday, November 06, 2015, 10:08

IGP1 = 5.8e-7 Torr.

Vacuum stable.

Initiating auto-ramp at 0.2A/min and 0.1A/min with final setpoints of 450A and 230A for the TGHT and TBHT respectively.

See photos attached to view how springs were coated and loaded into container.


 Monday, November 09, 2015, 09:07

TGHT reached 450A, 7.2V ~8pm sat, nov 7th.

OMEGA = 1775C

IGP1 = 3.2e-7 Torr.

Tapping up manually to 1900C.


 

 Monday, November 09, 2015, 12:30

Checked the temp on the inner surface (not at the spring) of the container was around 2050C at 500A. 

The TaC coated spring is reading at 1900C; that's what the OMEGA is reading with the setting for 2-colors and slope at 0.98.

Lower TGHT to 450A/ 7.12V.

By comparing the data from the previous temp curve (OMEGA slope at 0.98) with no material inside the container,  the voltage and current plot is aligned with the curve.

Changed OMEGA setting slope to 1.04.  Current temp is reading at 1917C at 450A.

For 2-Color setting, the emissivity should be negligible.  That makes me believe that different materials has different slope setting for the temp reading.  

One thing to note is that, the sintering temp of TaC is around 1900-2000C.  It was clear that the container was fully sintered with TGHT at 450A.

Will need to gather more data with different material to understand the slope setting better. 

Try: 

SiC at 1700C, slope at 1.04

ZrC at 1900C, slope at 104

Ta at 1900C, slope at 0.98.

Compare the data...


 

 Monday, November 09, 2015, 14:20

IGP1 = 3.3e-7 Torr.

TGHT = 450A, 7.12V

OMEGA = 1915C

Initiating auto-cool at 2.0A/min and 1.0A/min for the TGHT and TBHT respectively.


 Tuesday, November 10, 2015, 13:23

Vented and opened this morning.

springs look [mostly] sintered.

see photo attached.

 

Attachment 1: Evernote_Camera_Roll_20151110_113123.jpg
Evernote_Camera_Roll_20151110_113123.jpg
  259   Thursday, November 05, 2015, 16:20 Laura Lambert 41077-3LP-SISIn progressSintering TaC coating on 'temporary endcaps' springs

 Thursday, November 05, 2015, 16:19

Springs coated with TaC and loaded into container for sintering.

3x Ta heat shield.

EVAP2 currently pumping down.


 Friday, November 06, 2015, 08:39

Opened HS water valves, no leaks detected.

Tapped up manually to 35A.

IGP1 = 5.5e-7 Torr.


 Friday, November 06, 2015, 10:08

IGP1 = 5.8e-7 Torr.

Vacuum stable.

Initiating auto-ramp at 0.2A/min and 0.1A/min with final setpoints of 450A and 230A for the TGHT and TBHT respectively.

See photos attached to view how springs were coated and loaded into container.


 Monday, November 09, 2015, 09:07

TGHT reached 450A, 7.2V ~8pm sat, nov 7th.

OMEGA = 1775C

IGP1 = 3.2e-7 Torr.

Tapping up manually to 1900C.


 

Attachment 1: 2015-11-02_16.03.10.jpg
2015-11-02_16.03.10.jpg
Attachment 2: 'temporary_endcap'_springs_nov.3_2015.jpg
'temporary_endcap'_springs_nov.3_2015.jpg
Attachment 3: IMG_20151105_141239627_HDR.jpg
IMG_20151105_141239627_HDR.jpg
Attachment 4: IMG_20151105_141248901_HDR.jpg
IMG_20151105_141248901_HDR.jpg
  210   Tuesday, June 09, 2015, 10:44 Laura LambertEmpty41177-2LP-SISIn progressSintering TaC coating container for ZrC back-up

 Tuesday, June 09, 2015, 9:16

Target container is coated with TaC. No Ta-heat shields are used.

TGHT will be ramped up to 580A at 0.2A/min.

TBHT will be ramped up to 230A at 01A/min.

Chamber is currently being pumped down.


 Tuesday, June 09, 2015, 15:37

HS water valves were opened. no leaks detected.

Tapped up manually to 35A.

Once vacuum stabilized after ~45min, initiated auto-ramp.


 Wednesday, June 10, 2015, 08:02

IGP1 = 5.3e-7 Torr.

TGHT = 250A and TBHT = 140A.

Increasing auto ramp to 2.0A/min and 1.0A/min for the TGHT and TBHT respectively.


 

  212   Wednesday, June 10, 2015, 16:35 John WongEmpty41177-2LP-SISIn progressSintering TaC coating container for ZrC back-up

Laura Lambert wrote:

 Tuesday, June 09, 2015, 9:16

Target container is coated with TaC. No Ta-heat shields are used.

TGHT will be ramped up to 580A at 0.2A/min.

TBHT will be ramped up to 230A at 01A/min.

Chamber is currently being pumped down.


 Tuesday, June 09, 2015, 15:37

HS water valves were opened. no leaks detected.

Tapped up manually to 35A.

Once vacuum stabilized after ~45min, initiated auto-ramp.


 Wednesday, June 10, 2015, 08:02

IGP1 = 5.3e-7 Torr.

TGHT = 250A and TBHT = 140A.

Increasing auto ramp to 2.0A/min and 1.0A/min for the TGHT and TBHT respectively.


 

 Wednesday, June 10, 2015, 16:32

TGHT/TBHT are at 580A/230A for almost 6 hours, temp at 1728C.

Vac at 8.5e-7 Torr. 

Cooling down initiated at 1A/min.

Target container should be inspected once the chamber is vented.


 

  213   Thursday, June 11, 2015, 16:10 Laura LambertEmpty41177-2LP-SISIn progressSintering TaC coating container for ZrC back-up

John Wong wrote:

Laura Lambert wrote:

 Tuesday, June 09, 2015, 9:16

Target container is coated with TaC. No Ta-heat shields are used.

TGHT will be ramped up to 580A at 0.2A/min.

TBHT will be ramped up to 230A at 01A/min.

Chamber is currently being pumped down.


 Tuesday, June 09, 2015, 15:37

HS water valves were opened. no leaks detected.

Tapped up manually to 35A.

Once vacuum stabilized after ~45min, initiated auto-ramp.


 Wednesday, June 10, 2015, 08:02

IGP1 = 5.3e-7 Torr.

TGHT = 250A and TBHT = 140A.

Increasing auto ramp to 2.0A/min and 1.0A/min for the TGHT and TBHT respectively.


 

 Wednesday, June 10, 2015, 16:32

TGHT/TBHT are at 580A/230A for almost 6 hours, temp at 1728C.

Vac at 8.5e-7 Torr. 

Cooling down initiated at 1A/min.

Target container should be inspected once the chamber is vented.


 

 Thursday, June 11, 2015, 10:55

Vented in air and opened up this morning.

Same as last container sintered in evap2 [IG-LIS for UCx#13] - ends not quite fully sintered and coating not very good.

most likely due to old TaC spray.

See link for photos.

https://www.dropbox.com/sh/75o43x8y2z16e7j/AABc8Z1fTTaTRtJ5_Jr1eacWa?dl=0


 

  193   Tuesday, May 19, 2015, 13:54 Laura LambertEmpty41177-1LP-SISDoneSintering TaC coating container for ZrC

 Tuesday, May 19, 2015, 13:33

Target container is coated with TaC.  No Ta-heat shields are used.

TGHT will be ramped up to 580A at 0.2A/min.

TBHT will be ramped up to 230A at 0.1A/min.

Chamber is currently being pumped down


 Tuesday, May 19, 2015, 15:04

Opened up HS water, no leaks detected.

Stepped up to 35A.

Waited ~35min, vacuum stable.

IGP1 = 1.7e-6 Torr.

Initiating auto-ramp.


 Wednesday, May 20, 2015, 11:43

IGP1 = 3e-7 Torr.

TGHT = 282A, 3.8V

TBHT = 156A, 2.2V

Increasing ramping rate to 1.0A/min and 0.5A/min for the TGHT and TBHT respectively.


 Thursday, May 21, 2015, 10:42

IGP1 = 2.9e-7

Direct voltage = 5.48V

OMEGA = 1703C.

Initiating auto-cool at 2.0A/min  and 1.0A/min for the TGHT and TBHT.


 Friday, May 22, 2015, 11:41

Vented in air and opened up this morning.

TaC coating fully sintered, looks good! 


 

  410   Wednesday, May 23, 2018, 15:21 Laura LambertEmpty HP-FEBIAD-CTLDoneSintering TaC coating container for UCx#23

Wednesday, May 16, 2018, 09:56

Container coated with TaC using 'flushing technique' and let dry over weekend.

Cleaned ionizer tube with acetone, no coating inside ionizer tube.

Wrapped with 3 x Ta heat shields, not incl center block

OMEGA slope = 0.98

*NOTE: realized after pumping down, filament on IGP2 is burnt out and needs replacing, will order a new one and use IGP1 for this process


Thursday, May 17, 2018, 13:15 

HS water valves remained open since the last time evap2 was used, no leak check done.

Tapped up manually to 50A.

Waited ~1hr

Vacuum stable.

IGP1 = 1e-6 Torr

Initiating auto ramp for TGHT @ 0.2A/min to a max setpoint of 350A

Initiating auto ramp for TBHT @ 0.1A/min to a max setpoint of 230A

Once max setpoints achieved, will tap up manually to final desired temperature of 1900C


Friday, May 18, 2018, 13:00 

Tapped up manually.

TGHT = 495A, 8.84V

TBHT = 230A, 3.26V

MIKRON = 2000C

Filament = 1910C

OMEGA = 1910C

Will remain at max setpoints over weekend.


Tuesday, May 22, 2018, 10:04 

Remained at max setpoints over long wknd.

TGHT = 495A, 8.85V

TBHT = 230A, 3.26V

IGP1 = 2.47e-7 Torr

Initiating auto-cool at 2.0A/min and 1.0A/min for the TGHT and TBHT respectively.


Wednesday, May 23, 2018, 10:08 

Vented in air this morning.

Container looks good!

Transferred into glove box.


 

 

  182   Thursday, February 19, 2015, 15:21 Laura LambertEmpty41177-2LP-SISDoneSintering TaC coating container for UCx#12

 Thursday, February 19, 2015, 15:19

Target container coated with TaC, loaded in EVAP2.

No Ta heat shields.

Will pump down over the weekend.


 Monday, February 23, 2015, 10:22

IGP1  = 1.75e-7 Torr

TGHT will be ramped up to 580A at 0.2A/min

TBHT will be ramped up to 230A at 0.2A/min

evap2 power supply not responding to epics controls...waiting on fix


 Wednesday, February 25, 2015, 16:05

controls now fixed.

danceioc1 involving evap ioc will be updated tomorrow by controls.

once ioc update complete will ramp up.


 Friday, February 27, 2015, 09:34

ioc update complete yesterday afternoon.

IGP1 = 1.1e-7

initiating ramp up...

Parameter setup: 5.0e-5 good vac, 6.0e-5 bad vac.


 Monday, March 02, 2015, 09:01

IGP1 = 2.5e-7 Torr

TGHT = 578A

TBHT = 232A

OMEGA = 1750C

Increasing to 1800C


 Monday, March 02, 2015, 10:42

Reached 1800C at 10:30

TGHT = 603A

TBHT = 232A

IGP1 = 2.8e-7 Torr


 Monday, March 02, 2015, 14:26

Sat at max set point for 4hrs.

IGP1 = 2.7e-7 Torr.

Initiating auto-cool, TGHT @ 2A/min, TBHT @ 1A/min.


 Tuesday, March 03, 2015, 09:17

vented and opened this a.m.

target container looks good, TaC coating fully sintered.


 

  170   Monday, November 10, 2014, 13:55 Laura LambertEmpty LP-SISDoneSintering TaC coating container for UCx#11 [2nd container]

Monday, November 10, 2014, 13:51

target container was sprayed with TaC on friday and sintered over the weekend.
vented and removed from evap2 this morning, looks good.

this container will be used as a round2 for UCx #11 since the last container broke as it was being assembled.

hopefully all the materials can be recovered and re-used/re-loaded into the new container...


 

  162   Monday, October 06, 2014, 12:17 John WongEmpty40282-5LP-SISIn progressSintering TaC coating container for UCx#11 (temp measured with OMEGA 2IR)

Laura Lambert wrote:

 Thursday, October 02, 2014, 11:51

Target container sprayed with TaC, currently drying in fume hood


 Monday, October 06, 2014, 12:11

Target container & back block is wrapped with 3 layers of Ta-heat shield.  The chamber has been pumped down over the weekend. 

Pressure currently at 2.23e-7 Torr. 

HS water valves open; no leaks detected.

TGHT will be ramped up to 580A at 0.2A/min

TBHT will be ramped up to 230A at 0.2A/min.


 

 Monday, October 06, 2014, 12:16

Stepped up both TGHT/TBHT to 35A. 


Tuesday, October 07, 2014, 12:54

TBHT reached to 230A/3.7V and TGHT is still ramping up, currently at 303A/4.5V. Temp measured with Omega-IR2 = 1165C with e'=0.85

Pressure @ 5.2e-7 Torr. 

Increase ramping rate to 2A/min.


 Tuesday, October 07, 2014, 16:21

TGHT is now at 580A and TGHT at 230A.

Temperature is measured with OMEGA-IR2, MIKRON, and analog pyrometer - All the measurements are agreed at 1700C (without the tantalum emissivity correction of 250C)

The OMEGA-IR2 slope has changed to 0.97 for the correction - The real temperature reading from the display is showing 1935C.

Now... attempting to low TBHT to see any temperature change.


 Tuesday, October 07, 2014, 17:01

TGHT @ 580A.

TBHT = 180C, Temp = 1925C

TBHT = 130C, Temp = 1920C

Not much of change in the temperature on the target tube...


Tuesday, October 07, 2014, 17:07

Attempting to increase the temperature to 2000C

TGHT = 600A, Temp = 1955C

TGHT = 620A, Temp = 2000C

Target will continue heating at this temperature overnight... Will continue to monitor.


 Tuesday, October 07, 2014, 20:59

After almost 4 hours of heating at 620A on TGHT, the temperature has dropped to 1980C.  

Pressure is coming down to 1.17e-6 Torr.  

Increased TGHT to 630A to maintain temp @ 2000C


 

  163   Wednesday, October 08, 2014, 11:51 Laura LambertEmpty40282-5LP-SISDoneSintering TaC coating container for UCx#11 (temp measured with OMEGA 2IR)

John Wong wrote:

Laura Lambert wrote:

 Thursday, October 02, 2014, 11:51

Target container sprayed with TaC, currently drying in fume hood


 Monday, October 06, 2014, 12:11

Target container & back block is wrapped with 3 layers of Ta-heat shield.  The chamber has been pumped down over the weekend. 

Pressure currently at 2.23e-7 Torr. 

HS water valves open; no leaks detected.

TGHT will be ramped up to 580A at 0.2A/min

TBHT will be ramped up to 230A at 0.2A/min.


 

 Monday, October 06, 2014, 12:16

Stepped up both TGHT/TBHT to 35A. 


Tuesday, October 07, 2014, 12:54

TBHT reached to 230A/3.7V and TGHT is still ramping up, currently at 303A/4.5V. Temp measured with Omega-IR2 = 1165C with e'=0.85

Pressure @ 5.2e-7 Torr. 

Increase ramping rate to 2A/min.


 Tuesday, October 07, 2014, 16:21

TGHT is now at 580A and TGHT at 230A.

Temperature is measured with OMEGA-IR2, MIKRON, and analog pyrometer - All the measurements are agreed at 1700C (without the tantalum emissivity correction of 250C)

The OMEGA-IR2 slope has changed to 0.97 for the correction - The real temperature reading from the display is showing 1935C.

Now... attempting to low TBHT to see any temperature change.


 Tuesday, October 07, 2014, 17:01

TGHT @ 580A.

TBHT = 180C, Temp = 1925C

TBHT = 130C, Temp = 1920C

Not much of change in the temperature on the target tube...


Tuesday, October 07, 2014, 17:07

Attempting to increase the temperature to 2000C

TGHT = 600A, Temp = 1955C

TGHT = 620A, Temp = 2000C

Target will continue heating at this temperature overnight... Will continue to monitor.


 Tuesday, October 07, 2014, 20:59

After almost 4 hours of heating at 620A on TGHT, the temperature has dropped to 1980C.  

Pressure is coming down to 1.17e-6 Torr.  

Increased TGHT to 630A to maintain temp @ 2000C


 

 Wednesday, October 08, 2014, 11:46

Temperature readout from omega-IR2C = 2054C

TGHT = 11.14V, 628.0A

TBHT = 2.01V, 129.8A

IGP1 = 8.2e-7Torr

Initiating auto-cool for TGHT @ 2A/min, TBHT @ 1A/min


 Thursday, October 09, 2014, 16:00

vented in air and opened up this morning

target container looks good!


 

  165   Thursday, October 09, 2014, 16:37 John WongEmpty40282-5LP-SISDoneSintering TaC coating container for UCx#11 (temp measured with OMEGA 2IR)

Laura Lambert wrote:

John Wong wrote:

Laura Lambert wrote:

 Thursday, October 02, 2014, 11:51

Target container sprayed with TaC, currently drying in fume hood


 Monday, October 06, 2014, 12:11

Target container & back block is wrapped with 3 layers of Ta-heat shield.  The chamber has been pumped down over the weekend. 

Pressure currently at 2.23e-7 Torr. 

HS water valves open; no leaks detected.

TGHT will be ramped up to 580A at 0.2A/min

TBHT will be ramped up to 230A at 0.2A/min.


 

 Monday, October 06, 2014, 12:16

Stepped up both TGHT/TBHT to 35A. 


Tuesday, October 07, 2014, 12:54

TBHT reached to 230A/3.7V and TGHT is still ramping up, currently at 303A/4.5V. Temp measured with Omega-IR2 = 1165C with e'=0.85

Pressure @ 5.2e-7 Torr. 

Increase ramping rate to 2A/min.


 Tuesday, October 07, 2014, 16:21

TGHT is now at 580A and TGHT at 230A.

Temperature is measured with OMEGA-IR2, MIKRON, and analog pyrometer - All the measurements are agreed at 1700C (without the tantalum emissivity correction of 250C)

The OMEGA-IR2 slope has changed to 0.97 for the correction - The real temperature reading from the display is showing 1935C.

Now... attempting to low TBHT to see any temperature change.


 Tuesday, October 07, 2014, 17:01

TGHT @ 580A.

TBHT = 180C, Temp = 1925C

TBHT = 130C, Temp = 1920C

Not much of change in the temperature on the target tube...


Tuesday, October 07, 2014, 17:07

Attempting to increase the temperature to 2000C

TGHT = 600A, Temp = 1955C

TGHT = 620A, Temp = 2000C

Target will continue heating at this temperature overnight... Will continue to monitor.


 Tuesday, October 07, 2014, 20:59

After almost 4 hours of heating at 620A on TGHT, the temperature has dropped to 1980C.  

Pressure is coming down to 1.17e-6 Torr.  

Increased TGHT to 630A to maintain temp @ 2000C


 

 Wednesday, October 08, 2014, 11:46

Temperature readout from omega-IR2C = 2054C

TGHT = 11.14V, 628.0A

TBHT = 2.01V, 129.8A

IGP1 = 8.2e-7Torr

Initiating auto-cool for TGHT @ 2A/min, TBHT @ 1A/min


 Thursday, October 09, 2014, 16:00

vented in air and opened up this morning

target container looks good!


 

 Thursday, October 09, 2014, 16:36

Photos for the OMEGA-IR2C temp measurement can be found on this link (see also the subfolder for the heating process):

https://www.dropbox.com/sh/n5sxcepg7e847xw/AACMubuKW1idd49D1Nz_0diNa?dl=0

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