ID |
Date |
Author |
Operational Mode |
Subject |
168
|
Thu Oct 12 19:54:10 2006 |
Willy Andersson | Quench Recovery | Energized solenoid. |
Switched to series mode about 6 hours ago. Cooling continued including
power leads until LHe level at about 50% and powerleads appeared stable. |
169
|
Fri Oct 13 00:13:57 2006 |
Experimentor | Quench Recovery | Energized solenoid. |
Hi there,
This is Khashayar (experimenter). Lookin at all different temperatures and
levelson the monitor, it seems everything is stable now. I wonder if you
could let us know what time we can have beam again? Would you please send an
email to kghandi@mta.ca if you know the answer? You can also reach me at my
cell# (506)961-0802 any time.
Thanks
Khashayar
> Switched to series mode about 6 hours ago. Cooling continued including
> power leads until LHe level at about 50% and powerleads appeared stable. |
128
|
Wed Jun 14 16:27:01 2006 |
Willy Andersson | Quench Recovery | Energized solenoid |
Powerleads appear stable. |
130
|
Fri Jun 30 11:13:00 2006 |
Doug Preddy | Normal Running | E-log is back up and running |
I would have made an entry when it died, but----- |
125
|
Tue Jun 13 15:52:46 2006 |
Willy Andersson | Quench Recovery | Doug has reduced and now closed CV155. |
Now in full // cold return mode.
Had just talked with Curtis, He said thta he has already informed the
experimentors that the solenoid will not be ready until tommorow, so he
suggests leaving the system in reduced // cold mode overnight. |
35
|
Wed Jul 28 21:26:19 2004 |
Doug Preddy | Quench Recovery | Double Power bump |
Two power bumps tonight. Everything tripped of. Restarted cooling water
pump, diff. pump under solenoid etc. Computer stayed on! Starting
compressor. |
68
|
Sun Oct 17 05:03:13 2004 |
Other | Start Up | Cycle valve after oscillations begin |
(Sat night/Sun AM) Helium temperature started oscillating, so
powered off magnet (precautionary) and cycled valve 142 (at 04:12).
Small oscillations begin almost immediately, so close and open
the twist-knob for 142. Works better. |
208
|
Thu Jul 5 11:01:47 2007 |
Kevin Trithardt | Other | Current lead warm up |
Due to curent lead temperature occilation Doug recommended warming up the
current leads.
The leads were warmed up this morning then cooled back down. Power supply
is ramping up now.. 2 1/2 hours start to finish. |
143
|
Fri Jul 21 07:39:37 2006 |
Doug Preddy | Quench Recovery | Cool down continues |
Raised PIC229 to 11Bar. Started to close HIC155. Cooling rates improve. |
29
|
Fri Jun 25 12:36:04 2004 |
Willy Andersson | Quench Recovery | Compressor unloaded etc. |
At about 09:30 this morning I noticed the sound coming from the compressor
building seemed louder than usual. After entering the building I noted that
the compressor was unloaded to about 50% and the compressor suction was
running at about 15 psig. Down at the SULZER panel the solenoid vacuum
system was tripped off, the flow was still in series mode but no LHe level,
solenoid temps at over 40 K. Contacted Doug. Cannot figure out why the
compressor was unloaded to 50 %. Solenoid had not tripped on bad vacuum
because jumper was still on PIC901. Doug mentioned there was a power bump
yesterday at about 15:00. May be when the vacuum system tripped but does
not explain the compressor unloading.
Doug restarted vacuum system. I stopped flow to solenoid. Stabilized
pressures. We checked the compressor to try to see what would cause the
Unloaded state. Could not see any oil leaks.
Back at Sulzer panel loaded compressor to 100 %. Stabilize pressures. STart
cooling flow to solenoid, // warm return. Adjusting turbine speeds and
shield heat as required. Switched to // cold return flow after solenoid
temps down to TIC 121 temp of about 20 K. |
40
|
Sat Aug 7 22:37:04 2004 |
Willy Andersson | Quench Recovery | Compressor tripped off. |
Got a call at about 10:00 this morning, the whole system had tripped off.
No power bumps or other disturbances. When I arrived the only fault
indications were "ColdBox Trip" light on the compressor panel and on the
QRL panel the red "ColdBox" LED was ON. On the SULZER panel the
yellow "Cryostat Quench" light was ON. On the First Trip logger #1 and #15
LED's were ON. But no indication about what the actual fault was. Cooling
water OK, compressed air OK, compressor ventilation OK. Outside ambient
temperature was cooler than we had last week. BIG1 was off but when I
turned it back on the vacuum looked good but was slowly rising as the
solenoid warmed. I put the jumper on the vacuum controller. Prepared system
for re-start.
Started compressor. Started flow thru coldbox. Raised discharge pressure.
Started turbine flow. Didn't get any freezing but it seemed that T1 speed
wandered slowly +/-0.1k rev/sec when it got up to about 3.6k revs/sec, but
this only lasted for a second or two. Not sure if I was just seeing things.
Got turbines up to speed and started // warm return flow. Solenoid had been
running at 500 Amps and when it quenched and sat warming it had warmed to
about 40 K. Switched it to //cold return too soon and solenoid started to
warm slightly. Back to // warm return mode. Had to throttle flow thru
solenoid with warm return valves to get effective cooling. If had return
valves wide open TI121 would warm up too much. Discovered that if I
throttle the flow out of the solenoid slightly then TI121 would fall and
solenoid would start to cool. Less flow gave more cooling. Don't quite
understand that one. Switched to // cold return mode when solenoid temps
falling below 20K.
About 15:00 stable // cold return cooling. Going home for a while.
19:30 solenoid temps bottomed out at about 11K. Switch to series mode.
Something strange about the first trip detect. I reset it once and when I
checked it an hour or two later it showed a trip on #1 and #15 LED's even
though nothing had happened. Something must be causing false indications.
20:15 series cooling, solenoid temps at about 6K, LHe level rising slowly
at about 10%. Removed jumper on vacuum controller. |
124
|
Tue Jun 13 10:54:27 2006 |
Doug Preddy | Quench Recovery | Compressor tripped off |
No indicator lights etc as to why the compressor tripped. The only light
was a cold box fault. I had to shut off the main breaker before the
compressor would come back on.
Started cooling in parallel cold return. |
181
|
Wed Nov 15 11:09:28 2006 |
Doug Preddy | Quench Recovery | Compressor tripped off |
Compressor tripped this morning at ~8:45. I restarted the compressor, but
turbine 1 would not spin up. I let it warm for an hour and it started. I
started flow to the solenoind in parallel cold return. |
167
|
Thu Oct 12 11:53:04 2006 |
Willy Andersson | Quench Recovery | Compressor trip, 09:50 this morning. |
Main compressor tripped, refrigerator shutdown. Checked with experimentors
and main control room, no indications of power bump etc.
Restarted compressor, // warm then // cold return. One of the MV5x valves
frozen open, had to de-power valve a couple of times to get it to seal. |
106
|
Mon Jul 18 15:51:17 2005 |
Doug Preddy | Quench Recovery | Compressor restarted, flow to solenoid |
Recovered the vacuum in the solenoid, then started the compressor.
Started flow to solenoid in parallel warm return. |
213
|
Mon Aug 6 08:41:31 2007 |
Doug Preddy | Quench Recovery | Cold box trip at 6:00 |
compressor off due to cold box trip at 6:00 this morning. Restarted system
and started flow to solenoid in parallel cold return. |
4
|
Fri Apr 16 10:15:26 2004 |
Doug Preddy | Start Up | Changes to M9sol Vacuum PC |
Yesterday and today there have been a number of changes made to the M9
Vacuum control computer. The computer now automatically boots up to the
Epics control page. This logbook is also automatically started. |
120
|
Fri May 26 08:45:38 2006 |
Doug Preddy | Start Up | Changed to series mode |
Changed to series mode.
Liquid level building. |
13
|
Fri Apr 23 09:19:30 2004 |
Doug Preddy | Normal Running | CV211 |
PIC 229 was down to 10.8 bar this morning. PIC 229 was trying to open CV211
to charge the system. I realized that in restoring the control to CV211 I
did not get the wire into the connector properly. Went back up to the
compressor building and reconnected the control wire to CV211. pressure is
back to 11 bar. TI121, LHE in and liquid level ripples are now all reduced.
System was ramped up to 500 amps yesterday at 14:00 |
119
|
Fri May 26 07:29:54 2006 |
Doug Preddy | Start Up | CV155 closed |
CV155 closed.
Temps about 15K |