02:30 this morning got page from operations.
Looked at system online, appears that there was a powerlead overtemp
that caused the quench. Compressor still running. After arriving to
work set system to // warm return mode to cool down transferlines. Lhe
level starts to boil away. Switch to // cold return mode. Discovered that
seem to get better cooldown rate by not opening supply valves to solenoid
fully. // cold return valves are fully open but both CV143 and CV146 are
only open to 0.55 giving mu1 and mu2 inlet pressures of 2 barA. Getting
good cool down rates and even building LHe level.
04:25 C1 down to 8K, C12 at 7.5K, C6 at 7.5K, 6KS_M at 10.5K |