Logbooks Lab Maintenance Evaporator_1 Evaporator_2 Laser cutter Target Production Test-Stand RH-ISAC RH-Cyclotron RH-Meson Hall RH-Beamlines RH-ARIEL
  RH-ISAC, Page 9 of 138  Not logged in ELOG logo
  ID Date Authordown Category Type Module Target/Number Subject
  997   Wednesday, July 15, 2015, 11:02 chad fisherSouth Hot-CellRepairTM2 TM2 Coil Line Vacuum Leak Check

TM2 coil line R,U has been vacuum leaked check at the hot cell and has passed with no response from the leak detector.

  1000   Thursday, July 16, 2015, 14:36 chad fisherSouth Hot-CellRepairTM2 TM2 Status

IMG gauge, clip for ground to window lines and gas line extensions were installed today.

David and I also tried to locate the short between the coil line and MSP/Heat Shield...it went away for a bit...but is back.

Attachment 1: 20150716_110247.jpg
20150716_110247.jpg
Attachment 2: 20150716_142818.jpg
20150716_142818.jpg
  1001   Friday, July 17, 2015, 13:51 chad fisherSouth Hot-CellRepairTM2 TM2 Status

Gas lines extensions installed yesterday were too long and gas lines touched top inside of containment box. They have been removed and the gas lines re-installed in their original manner. Gas lines have been "adjusted" as to clear the tube heater lines, which was the original issue.

Attachment 1: 20150717_134123.jpg
20150717_134123.jpg
  1002   Monday, July 20, 2015, 14:12 chad fisherSouth Hot-CellRepairTM2 TM2 Status

Ultem high voltage spacer installed and 9 pin banana plug plugged in. Target has been inserted into the hot cell and will be installed after base-line electrical checks...probably first thing in the morning.

Attachment 1: 20150720_134819.jpg
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Attachment 2: 20150720_135747.jpg
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Attachment 3: 20150720_140100.jpg
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  1009   Wednesday, July 22, 2015, 12:13 chad fisherSouth Hot-CellRepairTM2 TM2 Short Findings

Pin X was unplugged, short remained, however any slight pressure on the block towards the source tray makes the short go away.

Confirmed clearance between the EE and thr R / U coil lines as well as MSP of coil line.

Camera inspection would seem to indicate that ALL issues stem from a common location...there is a spot where both the pin X waterline and the one of the R / U waterline  contact the heat shield waterline...one on one side of the heat shield line and the other on the other side.

 

 

Attachment 1: TM2_Short_July_22.jpg
TM2_Short_July_22.jpg
  1022   Tuesday, July 28, 2015, 14:36 chad fisherSouth Hot-CellStandard OperationTM4SiC#31SiC#31 Autopsy

Extraction electrode was removed from SiC#31 and target inspected.

Pictures of findings can be found at          https://documents.triumf.ca/docushare/dsweb/View/Collection-15131

 

 

 

  1023   Tuesday, July 28, 2015, 14:40 chad fisherSouth Hot-CellStandard OperationTM4SiC#31 UCx#13SiC#31 removed UCx#13 installed

SiC#31 has been removed from TM4 and UCx#13 installed. UCx#13 connection to the 9 pin connector was VERY VERY tight to the tube heater insulator on both the test jig and module.

 

 

Attachment 1: 20150727_115314.jpg
20150727_115314.jpg
  1033   Thursday, August 13, 2015, 09:17 chad fisherSouth Hot-CellRepairTM2 TM2 status

Tuesday, August 11,  insulator ITA6272 was installed onto the "pin x" line (unused plasma electrode) and tested; it seems to have successfully eliminated the shorts on that line.

Wednesday, August 12  "shunts" installed on tube heater and oven circuit and electrically  tested.

Thursday , August 13, dummy target installed.

 

Attachment 1: 20150811_132709.jpg
20150811_132709.jpg
Attachment 2: 20150813_083255.jpg
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Attachment 3: 20150813_090814.jpg
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  1035   Thursday, August 13, 2015, 13:46 chad fisherSouth Hot-CellRepairTM2 TM2 Status

As previously mentioned, dump target installed with new mounting and high current fasteners.

Leak Check complete and ready to move to CS at 1:30

  1049   Wednesday, August 26, 2015, 10:55 chad fisherSouth Hot-CellRepairTM2ZrC#7New wiring and target

New wiring was installed yesterday as well as ZrC#7 which had its high current fasteners torqued to 130 in lbs.

 

Attachment 1: 20150826_090047.jpg
20150826_090047.jpg
  1065   Thursday, September 10, 2015, 08:55 chad fisherSouth Hot-CellRepairTM1 TM1 Window Leak Diag.

Vacuum leak check on the window line circuit of TM1 took place yesterday and again to confirm this morning. Both days the response to helium is in the area of a soldered reduction fitting at the top of the containment box above and to the shutter side of the extraction column (see attached picture). To verify this morning each joint in the system had a 1 second shot of helium and then timed for 1 minute to wait for a response. This area responded both times tested at about 40 seconds...no response at any of the other locations.

Attachment 1: P0000122.JPG
P0000122.JPG
  1066   Thursday, September 10, 2015, 08:59 chad fisherSouth Hot-CellRepair  Manipulator Mait. and field check Sept. 4

Hot cell was entered for preventative mait. on left manip. field measurements around the cell were taken in prep. for window removal in January and left/south light bulb changed.

Hottest item in the cell was the conductor block end of the TM4 febiad coil line. It was 70 mSv/H on contact and seemed to be the major source of field in the hot cell. The waterblock end of this line did not apper to be hot.

  1069   Tuesday, September 15, 2015, 11:06 chad fisherSouth Hot-CellRepairTM1 TM1 Window Gasket Replacement

Replaced the custom silver gaskets on the entrance window panel of TM1 this morning...this has eliminated an sign of leak at this joint, however there appears to still be a leak somewhere...a good distance from the vcr joints of the window as we are getting a drift response.

Chad sprayed helium to soldering stems in containment box which we suspected with leak last week. With 1second click  on helium, after 80 seconds waiting time , the LD started to show leak up to 3xe-9atm.cc/sec.

Chad sprayed helium close to service tray and vacuum chase. with 1second click on helium , after 30 seconds waiting time, the LD started to show leak up to 2Xe-8 atm.cc/sec.

After this test, we knew the leak is somewhere in service tray or service cap, but not the soldering stems in containment box we suspected before.The further investigation is needed.

  1101   Wednesday, October 14, 2015, 14:03 chad fisherSouth Hot-CellStandard OperationTM2ZrC#7ZrC#7 removed

ZrC#7 has been removed from TM2. Everything looks good.

Attachment 1: 20151014_134022.jpg
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Attachment 2: 20151014_135127.jpg
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  1104   Thursday, October 15, 2015, 14:17 chad fisherSouth Hot-CellRepairTM2 Anode Connector Install and adjustment

The TM2 containment box was removed this morning for installation of the 9 pin connector...connection.

The 9 pin connector copper tube connection was made and Anders advised on routing of the cable to the banana plug water block connection.

Short was diagnosed (short disappeared when water block was pushed slightly towards center of module) and thicker Ultem spacer installed and tested again. All good.

Attachment 1: 20151015_085914.jpg
20151015_085914.jpg
  1105   Monday, October 19, 2015, 11:53 chad fisherSouth Hot-CellStandard OperationTM2SiC#32SiC#32 installed on TM2

SiC#32 has been installed on TM2. High current fasteners torqued to 130 in lbs.

  1109   Tuesday, October 20, 2015, 13:52 chad fisherSouth Hot-CellMaintenance  TM4 Febiad coil line disposal

The febiad coil line removed from TM4 has been cut into pieces small enough to be disposed of in a 5 gal pal. The line was cut with a Ridgid Model 104 manual pipe cutter (using the manipulators of course).

This pieces constitute the bulk of the field in the hot cell and will be disposed of with the next spent target.

Attachment 1: 20151020_133045.jpg
20151020_133045.jpg
Attachment 2: 20151020_134303.jpg
20151020_134303.jpg
  1110   Wednesday, October 21, 2015, 09:49 chad fisherSouth Hot-CellRepair  Manipulator handle repair

Rebuild handle of manipulator serial 7986 (currently in the east position) and replaced broken snap ring 5555-18h on west side of the handle underneath motion switch.

  1113   Friday, October 23, 2015, 11:30 chad fisherSouth Hot-CellStandard Operation ZrC#7ZrC#7 Spent Move and Febiad Coil

ZrC#7 was transfered to a spent target disposal pail today and removed from the hot cell. The "hot" end of the TM4 coil end was also disposed of in the same pail (#129)

  1129   Tuesday, November 24, 2015, 13:54 chad fisherSouth Hot-CellRepair  Cell Decon

Decon/removal of large solid waste was performed on Wednesday November 18th."Hot" activated items included containment box cover from TM2, Febiad coil line remnants from TM4 (the hottest ends were previously cut off and disposed of), some target conductor bolts, steerer plugs from TM2, target material remn.

Drum containing these solid items is 2.5mSv/hr at 1/2m.

Drum is stored in the north hot cell temp.

Compressible waste will require another drum.

Swipes were taken of the window... 170k counts per minute of cont.

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