Logbooks Lab Maintenance Evaporator_1 Evaporator_2 Laser cutter Target Production Test-Stand RH-ISAC RH-Cyclotron RH-Meson Hall RH-Beamlines RH-ARIEL
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Entry  Friday, December 05, 2014, 13:46, Anders Mjos, Conditioning Station, Development, TM2, , Not able to start water system 

 TCS:WPV1 does not open when staging is enabled. Multiple attempts have been made, but the valve remains closed.

Entry  Friday, December 07, 2018, 08:47, chad fisher, North Hot-Cell, Repair, , , North hot cell spare slave repair 20181207_083906.jpg

The tong cable on the spare north hot cell slave has been repaired. Slave came from the factory with the tong cables straddling one of the pulleys they are suppose to run through.

 

 

Entry  Wednesday, August 10, 2016, 14:38, Isaac Earle, North Hot-Cell, Development, , , North Hot Cell Ventilation Test Results 

Testing was performed on August 9th on the ISAC nuclear ventilation system to determine if the existing ventilation system can achieve the required cell depressions for both SHC and NHC under all expected configurations and if a proposed modification to the DDC control system can provide acceptable stability and response time for the system.  The proposed control system observes the lower of the SHC depression or the NHC depression + 10% (to avoid stability issues), and adjusts the dampers to try to achieve 250Pa (1.00" WC) depression in the area it is observing.  With the proposed control system the SHC and NHC dampers are programmed to be at the same position, but can be tuned with a bias between them if required to achieve all ventilation requirements. The NHC and SHC dampers are programmed with a limit at 90% of the fully-open position.  There is a damper in the ducting system in the section of duct after the SHC and NHC legs join together;  this is set at 50% open, and was not adjusted during the the tests.  Test summary and results are listed below:

1.  Prior to switching to SHC+NHC control mode, the flow rate and depression of the SHC was measured with the lid on:  266Pa cell depression, damper 47% open, duct flow 417cfm.  The lid was opened and the measurements repeated:  35Pa, damper 90% open, duct flow 630cfm (results in 83ft/min, 0.42m/s average flow velocity across HC module opening)

2. The control system was switched to the new SHC+NHC single control loop system. Measurements were taken with both hot cell lids closed.  SHC:  246Pa, damper 72% open, 350cfm flow rate.  NHC: 257Pa, damper 72% open, 510cfm flow rate.  The ventilation fan speed was then increased from 53Hz to 57Hz (maximum speed is 60Hz).  Measurements were taken with both hot cell lids closed.  SHC:  257Pa, damper 51% open, 353cfm flow rate.  NHC: 257Pa, damper 51% open, 515cfm flow rate.

3. The SHC module port lid was opened and the NHC lid left closed.  SHC: 37Pa, damper 90% open, 462cfm (results in 61ft/min, 0.31m/s average flow velocity across HC module opening).  NHC: 249Pa, damper 90% open, 551cfm.

4. The NHC module port lid was opened and the SHC lid closed.  SHC: 203Pa, damper 90%, 360cfm.  NHC: 33Pa, damper 90%, 648cfm (results in 85ft/min, 0.44m/s average flow velocity across HC module opening).  The fan speed was then increased to 60Hz (max speed) to see if the depression setpoint for the SHC could be achieved in this configuration.  SHC: 231Pa, damper 90%, 389cfm.  NHC: 29Pa, damper 90%, 705cfm (results in 93ft/min, 0.47m/s average flow velocity across HC module opening)

5. Both SHC and NHC module port lids were opened and the fan was left at 60Hz.  SHC: 31Pa, damper 90%, 448cfm (results in 59ft/min, 0.30m/s average flow velocity across HC module opening).  NHC: 29Pa, 90% damper, 669cfm (results in 88ft/min, 0.45m/s average flow velocity across HC module opening)

 

For all tests the control system arrived at a stable depression value in less than 5 minutes, and thereafter exhibited only minor fluctuations.

It was observed that when the fan speed was increased to 57Hz, and for the duration of the tests, there was negligible change in the depression and damper positions for the mass separator room and target pit area.
 
The HEPA filter in the SHC leg of ducting has not been changed since commissioning of the facility (~15 years), and the SHC charcoal filters have not been changed since installation approximately 5 years ago.  The SHC pre-fitler located inside the cell was changed in January 2016.  When these are changed (which should be done before commissioning of the NHC ventilation system), the difference between SHC and NHC flow rates should decrease, and the SHC depression with NHC open should increase (likely up to the 250Pa setpoint).
 
Conclusion: The new SHC+NHC single control loop system effectively controls the system under all conditions tested.  The existing ventilation system achieved the required NHC depression (250Pa, from RS 50, Document #131915) with both cells closed, and with SHC open only.  The same depression for SHC with both cells closed was achieved with both cells closed, but only reached 231Pa w/ NHC open (203Pa at 57Hz fan speed).  It is expected that 250Pa can be easily achieved in the final system because the NHC will be better sealed than in its current condition, the damper in the shared SHC/NHC leg can be opened further, there will be greater flow through the SHC leg after changing the HEPA and charcoal filters, and the system can be tuned to better balance the SHC and NHC flow rates.  RS51 states "the ventilation system should maintain an average air flow velocity of 0.5m/s across the opening into the hot cell".  This is almost achieved with the NHC open, but SHC only had 0.3m/s average flow velocity.  It should be possible to increase both to > 0.5m/s by further opening the shared leg damper and tuning the system to have more balanced flow rates.  At the very least, both SHC and NHC should have > 0.42m/s average flow velocity to match what is currently achieved in SHC only mode (measured in test step #1), which to date has not allowed contamination to escape out the top of the hot cell.  Depending on what flow velocity is deemed acceptable, after commissioning it may be possible to have both the SHC and NHC open concurrently based on the results of Test 5.  At the time of commissioning, the SHC/NHC damper bias and NHC air inlet damper should both be tuned to achieve as similar depression and flow rate conditions as possible for both cells, and to meet all requirements in the RS document.

 

Notes:

Duct flow rate was calculated assuming that measured flow velocity at the center of the duct is 90% of average duct velocity.  The duct ID at the sample location is 7.75", the hot cell opening size used for SHC and NHC module opening flow velocity calculations was 33" x 33".

Duct flow velocity measurements were taken using a thermal anemometer (Model number: 9555-P, Serial number: 9555:1108059 Rev. 2.11.0, Last calibrated by Rob Walker on April 29, 2016).

After completion of the tests the system was restored to it's original configuration and the ISAC target hall was swiped for contamination: none found.  No EF12 trips occurred during these tests.

Entry  Thursday, February 09, 2017, 14:07, Isaac Earle, North Hot-Cell, Development, , , North Hot Cell Shielding Window Gaskets Changed 23x

 The North Hot Cell shielding window gaskets have been changed and the window has been filled with new oil.  Although there was no noticeable oil leaks before starting the job, the gaskets had not been changed since initial installation approximately 15 years ago, so they were done now as part of construction of the new  cell.  The work took place between January 26 – Feb 8, 2017 following the attached PDF “Full procedure for NHC shielding window gasket change” which references “Gasket change procedure from Hot Cell Services” (also attached).

To drain the window a 1/2”polyethylene hose was attached to the drain line using  a Swagelok fitting and routed into a 55 gallon drum.  A vent valve on the expansion tank was opened to allow air to enter  the window.  It took approximately 5 hours to drain the window using this method.  Approximately 50 US gallons were drained from the window, agreeing with the amount specified on Hot Cell Services drawing #96173-100 (attached).

After draining, the window was purged with helium then pressurized to approximately 13” WC with helium.  A pressure drop of 0.6” WC was observed over a 2 hour period.  While pressurized, a Varian G8601-60001 leak detector was  used to sniff for helium around the perimeter of the gaskets on both the hot and cold  sides – no helium leaks detected.  A small leak was found on the pressure gauge used to monitor helium pressure.

The cold side cover panel assembly was  then removed  following the HCS procedure.  From HCS Drawing #96173-100, the weight  of the cold side glass cover panel was estimated to be  approximately 50lbs.  The guide  pins used were McMaster-Carr PN# 93460A385.  The trim frame could be easily removed, however the glass panel was stuck to the window housing.  A putty knife and isopropyl alcohol were used to cut through the gasket to separate the window from the housing.  The alcohol did not damage the paint of the housing – acetone was also tested on a small area and did not cause damage  to the paint.  Two suction cup handles were used to transport the glass panel, and it was easily lifted by two people.  Various methods were attempted to remove old gasket material and gasket adhesive  from the trim frame and housing surfaces – the most successful was using a razor blade scraper to remove the majority of the material, followed by an acetone wipe to remove the remainder of the stuck-on gasket adhesive.  The panel was reinstalled with new gaskets following the attached  procedures - no issues encountered.  After torqueing the trim frame bolts the window was leak checked as before.  A drop of 0.8” WC was observed over two hours, and no helium could be detected around  the perimeter of the new cold side gasket.

The hot side cover panel assembly was changed using the same method as for the cold side.  The glass panel was estimated to be 150lbs.  A small amount of oil (< 0.5 L) remained behind the hot side glass panel after draining which spilled out after removal of the glass. Four suction cup handles were used, and four people were required to remove and reinstall the panel.  After installation the leak check was repeated with a drop of 0.3” WC observed over two hours, and no helium detectable around the perimeter of the hot side gasket.

The replacement gaskets were ordered from Hot Cell Services under PO# 3033973 matching the material and sizes specified on  HCS drawing #96173-100.

The window was filled with Drakeol 10B LT MIN OIL NF, Product  code: PEN1550-00-C-DR, PO #3034657.  The window was filled by lifting the drum onto the walkway leading  to the target hall entrance, and siphoning the oil out of the drum with a 1/2” polyethylene tube connected to the drain fitting, and an air vent open on the expansion tank.  Oil was added until the expansion tank was approximately 80% full.

After filling was complete, the cold side housing was repainted using Macropoxy 646 epoxy paint, 4019 Flint Gray.  When the inside of the NHC is next accessible the hot side trim frame bolts will be re-painted to protect the bare metal exposed from removing and reinstalling them.

Note that a quote for $74,313 ($56,823 USD) (PDF attached) was received from Hot Cell Services for them to do this job.  We were able to  successfully complete this ourselves with approximately $4500 required for the gaskets, $200 for other materials, and roughly 8 FTE days of work.

 

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Entry  Wednesday, May 04, 2016, 11:14, Isaac Earle, North Hot-Cell, Development, , , North Hot Cell Scope Decision 

A meeting was held on May 4, 2016 to determine the scope of the North Hot Cell project.  The following was agreed upon by those in attendance:

The NHC will be a designated target change hot cell.  It will be capable of performing all routine target operations (target removal/installation, leak check, electrical check, video inspection, post irradiation examination, target waste packaging and removal) using the same method currently used in the south hot cell.  Provisions will be included for the ability to perform target waste separation in the future unless a significant obstacle is encountered in which case the meeting attendees will be consulted.  Target waste separation involves separating the internal target heater from the target heat shield, then combining multiple target heaters in a single F-308 shipment.  Neither an inert gas atmosphere nor a double-door waste transfer system will be part of the NHC scope.

 

The following people were in attendance:  Bob Laxdal, Anders Mjos, Don Jackson, Joe Mildenberger, Friedhelm Ames, Alex Gottberg, Grant Minor, Yasmine Saboui, Peter Kunz

The following people were invited, but were unable to attend:  Chad Fisher, Pierre Bricault

The project will begin immediately, with Isaac Earle as the project leader.  The first steps will be to submit a Project Initiation Sheet, then to write and release the Requirements Specification document.

Entry  Friday, July 29, 2016, 14:27, Isaac Earle, North Hot-Cell, Development, , , North Hot Cell Measurements & Cleanup 

 The North Hot Cell was accessed today via the Ante Room for inspection, measurements, and clean-up.  There were no modules in the SHC or TCS, and no spent targets in the SHC.  Under these conditions the maximum field in the NHC was approximately 2μSv/hr.  The inside of the cell was cleaned and swept, followed by a floor swipe to check for contamination (none found).  All areas of the ante room floor were also swiped:  no contamination found.

 


The following measurements were taken in the NHC for comparison with the Soldiworks model:

SHC/NHC feedthrough panel fastener size:  1/4"-20,  1/2" long
NHC west wall to east edge of SEG block:  33-1/4" on south side, 33" on north side
NHC west wall to furthest extent of TCS (IRH1170): 40"
NHC west wall to wall indentation for viewing window: 46-7/8"
NHC west wall to end of existing ventilation duct: 4-1/8"

 

Entry  Wednesday, June 30, 2021, 14:11, Matthew Gareau, North Hot-Cell, Standard Operation, , , North Hot Cell Commemorative Opening 

 Yesterday a bottle of Cava (sparkling wine) was place, opened, and poured in the NHC, to commemorate its new operational status.

The NHC is now a functional hot cell and is ready for many years of target exchanges to come.

Entry  Wednesday, November 20, 2013, 08:50, chad fisher, South Hot-Cell, Standard Operation, TM3, NiO#2, NiO#2 removed TM3_20131120.jpgTM3_20131120_2.jpg

NiO#2 has been removed from TM3

Entry  Tuesday, October 09, 2012, 13:44, chad fisher, South Hot-Cell, Standard Operation, TM4, UCx#5, NiO#1 removal UCx#5 installation IMG_0780[1].JPG

NiO#1 was removed this morning.

UCx#5 was inserted into the hot cell around 1 pm, installed and leak checked and ready to go to the conditioning station 1:40pm

did have a little trouble with the 9 pin connector. It had to be lossened to get it to mate properly. It was le-tightened once the proper fit was achieved.

Entry  Wednesday, August 26, 2015, 10:55, chad fisher, South Hot-Cell, Repair, TM2, ZrC#7, New wiring and target 20150826_090047.jpg

New wiring was installed yesterday as well as ZrC#7 which had its high current fasteners torqued to 130 in lbs.

 

Entry  Wednesday, April 24, 2013, 09:00, Bevan Moss, Conditioning Station, Development, , , New user testing 

 Controls has created a new user group that can operate the conditioning station but cannot use any of the bypasses or forces. The cooling package will be used to test this new profile. The main loop bypass has been opened to allow this testing to happen without the risk of over pressure.

Entry  Tuesday, July 19, 2011, 11:52, chad fisher, South Hot-Cell, Standard Operation, TM4, Ta#36, New target Ta#36 Installed on TM4 DSC_0897.JPGDSC_0899.JPGDSC_0901.JPGDSC_0905.JPG

Ta#36 has been installed on TM4 and is awaiting leak and electrical check.

A small piece of the standard top insulator ITA3376 broke off during removal of Ta#35 (indicated with a blue circle on attached pictures).

"JP's connector, ITA2493 showed the usual and as yet undiagnosed "arc" mark (picture to follow).

The plastic retainers on the new torqtite gaskets showed rad damage.

Entry  Monday, July 29, 2019, 16:17, Carla Babcock, Conditioning Station, Repair, TM4, Dummy LP SIS, New leak on EE water line while testing new In seals 13_PM.png15_PM.png

Original Problem:

Leaks on the B and D copper blocks, probably due to corrosion between the blocks and the inserts. Final solution, after many tries, was to make an indium sheet the size of the copper blocks and use that to seal the entire surface.

So far offline tests seem to show these seals working, though long term tests are needed to say for sure.

 

New Problem:

TM4 was in the conditioning station, running water and under vacuum. 50A on the target and tube heaters from Friday evening to Saturday afternoon.

Sunday morning 9:30am target heating increased to 200A, 100A on the tube heater, ramp finishing around 1:30pm.

At around 3pm, the vacuum stops dropping and begins to climb very slowly, continuing until Monday morning (see first attachment).

Tests on the individual water lines show an immediate vacuum response only to the EE lines, the other lines show no response (note the window line is blanked off since the containment box is not on).

With water in the EE lines, the vacuum sits around 1e-6 near the target.

 

Testing:

Ramped target to 400A and tube to 200A. Sitting there for several hours shows no change in the vacuum response, though there is a variation that corresponds to the chiller turning on and off (see second attachment).

Ramped target to 450A and tube stayed at 200A. Vacuum staying in the low 10^-6 range, seems to be entirely due to EE leak, other seals are holding well.

 

Entry  Wednesday, November 28, 2018, 07:04, David Wang, ITE, Development, TM4, LpTa 56, New high current flexible cables inspection after LpTa#56 beam run. new_flexibble_cable_in_ITE_after_Ta#56_run_001.JPGnew_flexibble_cable_in_ITE_after_Ta#56_run_004.JPG

Inspected new high current flexible cables during TM4 disconnection. The new cables and adapters work fine.

Entry  Wednesday, February 11, 2015, 13:13, chad fisher, South Hot-Cell, Maintenance, , , New gas bottle storage rack 20150211_115656.jpg

The new gas bottle storage rack has been installed by/for the south hot cell.

 

Entry  Wednesday, December 04, 2013, 11:15, David Wang, ITE, Repair, TM4, , New bolts are installed on ITE TP3. 

I installed 8 new bolts(3/8-16 UNC x1.25  STL) on the ITE TP3. The ITE TP3 replacement job is done. Everything is connected back to the pump. and it is ready for starting.

Entry  Friday, June 12, 2015, 07:49, chad fisher, Assembly/Bench Test, Repair, TM2, , New TM2 Source Tray Ground to HV Measurements 

After bending and leak checking the new measurements from ground to HV on the TM2 source tray are:

Ground to C1+ 0.6645"

ground to heat shield 0.506

Window to mounting support plate - unchanged - over 0.80"

Entry  Monday, April 12, 2021, 13:45, Anders Mjos, Cooling, Maintenance, , , New T installed for instrumentation loop on HALCW system MicrosoftTeams-image_(9).png

Adrian and co installed a new T to be able to add an instrument loop for O2 and pH monitoring on the low conductivity water systtem (photo). See WP I2021-04-09-4

Entry  Thursday, August 27, 2020, 13:18, Anders Mjos, Conditioning Station, Maintenance, TM2, , New Power Supply installed for TGHT 

Arthur installed a new Magna Power PS for the TGHT yesterday. The old power supply has been moved to Evaporator 2. The power supply was configured for remote operation and tested successfully with low current (30 A).

Entry  Thursday, July 19, 2018, 09:17, chad fisher, South Hot-Cell, Repair, TM4, , New Optics Tray Modification 20180719_TM4_2.jpg20180709_TM4.jpg

The waterline loop bracket has been installed onto the new loop holding bracket and both installed onto the new source tray.

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