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New entries since:Wed Dec 31 16:00:00 1969
ID Date Author Category Type Module Target/Number Subject
  1448   Friday, March 10, 2017, 09:19 chad fisherSouth Hot-CellStandard Operation  South Hot Cell Field Measurements

The fields in the hot cell have been measured by means of a pole monitor through the tool port. Field was measured to be 25 uSv/h.

  1447   Wednesday, March 08, 2017, 14:09 David WangITEMaintenanceTM2 ITE IG1S increasing.

By retrieving data further, It has been found no directly relationship between IG1S surging and dump plug water opening. Vacuum surging is 10minutes ahead dump water supply to circuit. SEE attachment 1. Also, The ITE IG1S start to behavior unusual in middle of Feburary. See attachment 2. Today,  ITE IG1S is still slowly climbing up. I decide to leak check ITE vacuum vessel. Before  leak check, for more information and trouble shooting. I closed water supply to ITE to see if vacuum has response on it. I will return water supply to ITE  tomorrow morning.

Water supply to ITE is returned this afternoon at 2: 10 PM.  Everything works fine so far

I leak checked ITE secondary vessel vacuum. A leak have been found in March 09th noon which is located between entrance module and TM2 top tank flange o-ring seal( on tank flange). It could not be confirm on which side of the o-ring the leak is from.

During last night, ITE IG1S reading went back to normal low E-7 range and stays in this range now. So I leak checked same area again this morning. The leak disappeared now. The o-ring works sometime , but not all the time. The plan for this issue: Change ITE target module side o-ring when TM2 is move out., and watch on the ITE IG1s when TM4 is moved back to ITE and pumped down.

Attachment 1: ITE_IGIS_surge.png
ITE_IGIS_surge.png
Attachment 2: ITE_IG1S_and_PNG4.png
ITE_IG1S_and_PNG4.png
Attachment 3: ITE_IG1S_back_to_normal_overnight.png
ITE_IG1S_back_to_normal_overnight.png
Attachment 4: ITE_IG1S_behavior_from_Feb_08th_to_Mar_10th.png
ITE_IG1S_behavior_from_Feb_08th_to_Mar_10th.png
  1446   Tuesday, March 07, 2017, 14:41 David WangITEMaintenance  ITE dump plug water circuit is closed for ITE IG1S small surge.

It is closed @ 2:35PM by closing supply side valve first , the return side valve of ITE dump plug .

Opened ITE dump plug circuit valves @4:28PM. ITE IG1S still at 1XE-6. No change before and after of circuit closing and reopeneing.

  1445   Tuesday, March 07, 2017, 09:25 David WangITWRepair  ITW HALCW 2" return line ball valve seals replacement.

Leaking seals on ITW HALCW 2" return line ball valve have been replaced. 8 liter waters are drained out for this job. Water are drained into a thick plastic bag.  The bag is tie strapped , labeled, and put into a yellow garbage bin in MAA. Water sample is given to RPG. After analyzing, RPG will give instruction on how to deal with it. Since we just refilled NALCW to system before this job, the active level on sample is very low. We may dump them into active sump.  After seals change, The system is refilled . I started pump and set everything back to normal configuration. NO leak has been found on new seals. The HALCW system is operating good so far.

  1444   Monday, March 06, 2017, 08:01 David WangCoolingRepair  HALCW resin tank replacement.

HALCW resin tank has been replaced. The old tank is stored in middle-west silo now. The field on old resin tank bottom is about 3.5 msv/ hr(on contact). By shielding it into silo and putting two lead blankets on the top cover of the silo,The general field 1 feet above this silo is 25usv/hr. And, The field around the silo area are less affected. This old tank will stay there as long as possible.  For the new resin tank during preparation, It was found that on return line side, the 1.25" pipe thread plug with return line tube  was very difficult to be installed onto the female thread adapter which is welded onto to tank body. It was jammed in half way of threading onto tank at manufacturer. This plug was removed out first and inspected. The first and second male threads were galled.  Maico repaired the thread on a lathe. The female thread on the tank was tapped. A tight spot was found during the tap. After that, the return line plug could be installed onto the tank properly.  The new tank was installed into the vessel and connected back to HALCW system. Water are refilled into new tank. During refill air were trapped into the system. This caused  pump restarting problem. By Several times of starting up the pump, stopping the pump and venting,  Most air were breathed out of  system. Finally,The system was restarted by supply water to ITW( without module) only. ITE and resin can circuits were brought back to system after that without problem.

 Before removing the old tank, We drained water out of old tank to decay tank. Since the resin tank is largely filled with  resin, and water are soaked into resin, we only can drain out less than 10 liters water out of tank. Also, The drain caused some part of return line on pumps have to been drained. This is the main reason air was trapped in system during the new resin tank water refilling. For the future replacement, we should not drain water in old tank. It does not worth to do it. 

Attach TH HALCW resin tank replacement procedure here.

2022-02-17 reload replacement procedure and draining schematic.

Attachment 1: new_resin_tank_installation_004.JPG
new_resin_tank_installation_004.JPG
Attachment 2: new_resin_tank_installation_005.JPG
new_resin_tank_installation_005.JPG
Attachment 3: new_resin_tank_installation_006.JPG
new_resin_tank_installation_006.JPG
Attachment 4: new_resin_tank_installation_008.JPG
new_resin_tank_installation_008.JPG
Attachment 5: new_resin_tank_installation_010.JPG
new_resin_tank_installation_010.JPG
Attachment 6: new_resin_tank_installation_012.JPG
new_resin_tank_installation_012.JPG
Attachment 7: new_resin_tank_installation_013.JPG
new_resin_tank_installation_013.JPG
Attachment 8: HALCW_Resin_Tank_Replacement_Procedure..docx
Attachment 9: HALCW_Resin_Tank_Replacement_Procedure..pdf
HALCW_Resin_Tank_Replacement_Procedure..pdf HALCW_Resin_Tank_Replacement_Procedure..pdf HALCW_Resin_Tank_Replacement_Procedure..pdf
Attachment 10: HALCW_resin_can_replacement__procedure..pdf
HALCW_resin_can_replacement__procedure..pdf
Attachment 11: resin_tank_draining.pdf
resin_tank_draining.pdf
  1443   Thursday, March 02, 2017, 15:02 Isaac EarleNorth Hot-CellDevelopment  NHC roughing filter installed

 The roughing filter assembly (RFM0001D) has been installed at the ventilation exhaust hole on the NHC partition wall.  The filter used is Model # 332-528-002 supplied by BGE Service & Supply Ltd (see PO # TR123998).  Installation and removal of the filter using the manipulators will be tested after they have been installed.

 

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  1442   Tuesday, February 28, 2017, 17:51 Isaac EarleNorth Hot-CellDevelopment  NHC flanged ducting connection sealed

 The North Hot Cell ducting (IRH1617) has been sealed with a bead of Sikaflex 1a polyurethane construction sealant where the flanged connection bolts to the NHC/TCS partition wall.  When this sealant shows signs of aging it may be cut away and re-applied without unbolting the flange.

 

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  1441   Monday, February 27, 2017, 14:23 chad fisherSouth Hot-CellRepair  Manip. 'Z' motion cable run through

Aaron and I successfully completed a run through on the procedure to replace the 'Z' motion cable. I will be writing up the procedure for review and we will be performing more run through-s for practice before the actual job.

  1440   Friday, February 24, 2017, 15:12 Isaac EarleNorth Hot-CellDevelopment  NHC interior walls/floor/ceiling re-finished, sealed, and painted

The North Hot Cell interior walls, floor, and ceiling were re-finished, sealed, and painted by Omni Coating from Feb 6 - 17 under PO #3036471.  This job required 2-3 people for 4-6 hours per day over the 2 week period.  First the existing surfaces were ground and/or sanded to remove existing coatings and protrusions/sharp edges.  This was followed by a coat of primer to highlight uneven surfaces and improve adhesion of following fillers and coatings.  Metal shims between the cell walls and roof were cut away where they protruded into the cell.  Loose steel cylinders between SHC and NHC spaces were fixed in place using epoxy filler. Epoxy or polyurethane fillers were used to fill all gaps, cracks, holes, etc, as detailed below.  Foam backer rod and polyurethane filler were used to seal all large wall-to-wall and ceiling-to-wall gaps.  An approximate 2cm radius rounded corner was formed at all wall-to-wall and floor-to-wall corners using polyurethane sealant.  The interior of the tool-port, personnel access hatch, as well as the north roof hatch were also re-finished with the same procedure.  After all sealing and finishing work the surfaces were coated with "Mill White"  Macropoxy 646 Fast Cure Epoxy Paint as per manufacturer instructions.  Note:  this paint is recommended by the manufacturer for nuclear applications and has been tested for decontaminability:  99% water wash; 95% overall as per ASTM D4256/ANSI N 5.12 as well as for radiation tolerance:  Passed ASTM D4082 / ANSI 5.12 with a 525 micron thick coating.

 

The following products were used as described (data sheets attached):

Sanitile 120 Universal Acrylic Primer - 50-75 micron dry film thickness coat applied over all existing ceiling, walls, and floor surfaces after preparation by sanding

Sika Duochem 8107 Epoxy Paste - Used for filling voids and cracks in concrete surfaces

Sikaflex 291 Polyurethane Elastomeric Adhesive and Sealant - used for caulking joints and cracks in the concrete walls and aluminum panel wall and for creating radiused corners in wall-to-wall and wall-to-floor corners

Macropoxy 646 Fast Cure Epoxy Paint - 4 coats applied on all surfaces using rollers or brushes to create a total thickness of 525 microns as per data sheet

 

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Attachment 1: ind-pds-sikaflex-291lot.pdf
ind-pds-sikaflex-291lot.pdf ind-pds-sikaflex-291lot.pdf
Attachment 2: MACROPOXY®_646_FAST_CURE_EPOXY.pdf
MACROPOXY®_646_FAST_CURE_EPOXY.pdf MACROPOXY®_646_FAST_CURE_EPOXY.pdf MACROPOXY®_646_FAST_CURE_EPOXY.pdf MACROPOXY®_646_FAST_CURE_EPOXY.pdf
Attachment 3: Sanitile_120_PDS.pdf
Sanitile_120_PDS.pdf Sanitile_120_PDS.pdf
Attachment 4: Sika_Duochem_8107_Fpds.pdf
Sika_Duochem_8107_Fpds.pdf Sika_Duochem_8107_Fpds.pdf Sika_Duochem_8107_Fpds.pdf Sika_Duochem_8107_Fpds.pdf
  1439   Wednesday, February 15, 2017, 12:07 chad fisherSouth Hot-CellMaintenance  Manipulator 'Z' motion cable replacement preparation status

Aaron and I completed assembling (re-assembling) the clean spare on Tuesday, February 14th to assist in determining a procedure for replacement of the 'Z' motion cable on the south hot cell manipulators.

 

The anchor point in the slave end of the clean manipulator could not be found as the manipulator stand is too low and does not allow full extension of the slave end.

 

Did some poking around on the in-situ manipulator in the south cell and was able to find the anchor point viewing it with the in cell camera (see blurry attached photo).

 

Was able to then find reference to the "cable clamp" in the parts list and drawing for the slave end. Also, confirmed there is not a procedure in the manual for a CABLE 'Z' motion system as we have, only a tape driven system. The procedure should however be very similar safe this mystery anchor point I discovered today and how readily this anchor point can be worked in.

Attachment 1: 20170215_113609.jpg
20170215_113609.jpg
  1438   Friday, February 10, 2017, 09:56 David WangConditioning StationStandard Operation  water has been refilled to TCS:TK2

TCS:TK2 , Water has been refilled to 28.5" level. It was 15.1". Fall protection equipment  are used during the job.

  1437   Thursday, February 09, 2017, 14:07 Isaac EarleNorth Hot-CellDevelopment  North Hot Cell Shielding Window Gaskets Changed

 The North Hot Cell shielding window gaskets have been changed and the window has been filled with new oil.  Although there was no noticeable oil leaks before starting the job, the gaskets had not been changed since initial installation approximately 15 years ago, so they were done now as part of construction of the new  cell.  The work took place between January 26 – Feb 8, 2017 following the attached PDF “Full procedure for NHC shielding window gasket change” which references “Gasket change procedure from Hot Cell Services” (also attached).

To drain the window a 1/2”polyethylene hose was attached to the drain line using  a Swagelok fitting and routed into a 55 gallon drum.  A vent valve on the expansion tank was opened to allow air to enter  the window.  It took approximately 5 hours to drain the window using this method.  Approximately 50 US gallons were drained from the window, agreeing with the amount specified on Hot Cell Services drawing #96173-100 (attached).

After draining, the window was purged with helium then pressurized to approximately 13” WC with helium.  A pressure drop of 0.6” WC was observed over a 2 hour period.  While pressurized, a Varian G8601-60001 leak detector was  used to sniff for helium around the perimeter of the gaskets on both the hot and cold  sides – no helium leaks detected.  A small leak was found on the pressure gauge used to monitor helium pressure.

The cold side cover panel assembly was  then removed  following the HCS procedure.  From HCS Drawing #96173-100, the weight  of the cold side glass cover panel was estimated to be  approximately 50lbs.  The guide  pins used were McMaster-Carr PN# 93460A385.  The trim frame could be easily removed, however the glass panel was stuck to the window housing.  A putty knife and isopropyl alcohol were used to cut through the gasket to separate the window from the housing.  The alcohol did not damage the paint of the housing – acetone was also tested on a small area and did not cause damage  to the paint.  Two suction cup handles were used to transport the glass panel, and it was easily lifted by two people.  Various methods were attempted to remove old gasket material and gasket adhesive  from the trim frame and housing surfaces – the most successful was using a razor blade scraper to remove the majority of the material, followed by an acetone wipe to remove the remainder of the stuck-on gasket adhesive.  The panel was reinstalled with new gaskets following the attached  procedures - no issues encountered.  After torqueing the trim frame bolts the window was leak checked as before.  A drop of 0.8” WC was observed over two hours, and no helium could be detected around  the perimeter of the new cold side gasket.

The hot side cover panel assembly was changed using the same method as for the cold side.  The glass panel was estimated to be 150lbs.  A small amount of oil (< 0.5 L) remained behind the hot side glass panel after draining which spilled out after removal of the glass. Four suction cup handles were used, and four people were required to remove and reinstall the panel.  After installation the leak check was repeated with a drop of 0.3” WC observed over two hours, and no helium detectable around the perimeter of the hot side gasket.

The replacement gaskets were ordered from Hot Cell Services under PO# 3033973 matching the material and sizes specified on  HCS drawing #96173-100.

The window was filled with Drakeol 10B LT MIN OIL NF, Product  code: PEN1550-00-C-DR, PO #3034657.  The window was filled by lifting the drum onto the walkway leading  to the target hall entrance, and siphoning the oil out of the drum with a 1/2” polyethylene tube connected to the drain fitting, and an air vent open on the expansion tank.  Oil was added until the expansion tank was approximately 80% full.

After filling was complete, the cold side housing was repainted using Macropoxy 646 epoxy paint, 4019 Flint Gray.  When the inside of the NHC is next accessible the hot side trim frame bolts will be re-painted to protect the bare metal exposed from removing and reinstalling them.

Note that a quote for $74,313 ($56,823 USD) (PDF attached) was received from Hot Cell Services for them to do this job.  We were able to  successfully complete this ourselves with approximately $4500 required for the gaskets, $200 for other materials, and roughly 8 FTE days of work.

 

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Attachment 1: Full_Procedure_for_NHC_shielding_window_gasket_change.pdf
Full_Procedure_for_NHC_shielding_window_gasket_change.pdf
Attachment 2: Gasket_Change_Procedure_from_Hot_Cell_Services.pdf
Gasket_Change_Procedure_from_Hot_Cell_Services.pdf Gasket_Change_Procedure_from_Hot_Cell_Services.pdf Gasket_Change_Procedure_from_Hot_Cell_Services.pdf Gasket_Change_Procedure_from_Hot_Cell_Services.pdf Gasket_Change_Procedure_from_Hot_Cell_Services.pdf Gasket_Change_Procedure_from_Hot_Cell_Services.pdf Gasket_Change_Procedure_from_Hot_Cell_Services.pdf Gasket_Change_Procedure_from_Hot_Cell_Services.pdf
Attachment 21: 15199-1.PDF
15199-1.PDF
Attachment 22: 96173-100.pdf
96173-100.pdf
Attachment 23: 36007.1_quote_Triumf_oil-gasket_change.pdf
36007.1_quote_Triumf_oil-gasket_change.pdf 36007.1_quote_Triumf_oil-gasket_change.pdf 36007.1_quote_Triumf_oil-gasket_change.pdf 36007.1_quote_Triumf_oil-gasket_change.pdf
  1436   Thursday, February 09, 2017, 09:24 David WangConditioning StationDevelopment  Target module window cooling lines at TCS.

Target module window  cooling lines at TCS has been modified to use spare 2 channel in TCS: WFB1. The old cooling lines used a spare channel in TCS WFB2(HVC channel) are removed and capped. After change, TCS window cooling lines will be interlocked with heaters. The test run on new lines are good. No leak  on all fittings, and signals on flow and temperature are good.   Control people will be noticed on this change for their following up job.

  1435   Tuesday, February 07, 2017, 15:57 Isaac EarleNorth Hot-CellDevelopment  Ventilation Ducting Gasket Installed

 Lead gasket IRH1633 was installed today according to assembly drawing IRH1618 Rev B.

  1434   Tuesday, February 07, 2017, 10:34 David WangITWMaintenance  ITW clean up

ITW has been cleaned up today.  All station are vacuum cleaned. I wiped all HV cover and HV area including conductors and insulators. The black foams which are used to wrap around TP back up line are degrading now. I removed most of these foams. Also, Some obsolete  water lines  are moved our of station. All waste are bagged . they will be surveyed and  stored(or disposed) according to radio-active level.

  1433   Friday, February 03, 2017, 11:49 David WangConditioning StationStandard Operation  Update 2017 winter shutdown TH schedule.

Update 2017 winter shut down target hall schedule. See attachments

Attachment 1: 2017_Winter_Shut_Down_Target_Hall_Schedule.mpp
Attachment 2: 2017_Winter_Shut_Down_Target_Hall_Schedule.pdf
2017_Winter_Shut_Down_Target_Hall_Schedule.pdf
  1432   Wednesday, February 01, 2017, 12:23 David WangITEStandard OperationTM2 TM2 has been connected in ITE.

TM2 has been connected in ITE. The SST window water lines in ITE can not be connected properly to TM2. The water line connector on TM2 window is 90 degree CCW installed in direction comparing to TM4.This caused the problem. Solution: Two piece of flexible lines and extra male QC adapters have been used to fix this issue.  HV cover and HV fence in ITE work  with TM2. Other connections are good as well.

  1431   Friday, January 27, 2017, 10:52 David WangConditioning StationStandard OperationTM2 TM2 has been moved from TCS to ITE

The move is successful.

  1430   Friday, January 27, 2017, 08:50 chad fisherSouth Hot-CellStandard Operation  UCx#18 and Ta#50 autopsy and spent target move

On Thursday, January 26th UCx#18 and Ta#50 were inspected and packaged into spent target pails, move to storage vault.

  1429   Friday, January 27, 2017, 08:46 chad fisherSouth Hot-CellStandard OperationTM4Ta#50 Ta#50 Removed

Ta#50 has been was removed from TM4 on Wednesday, January 25th.

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